05000324/LER-1980-014-03, /03L-0:on 800116,during Evolutions,Torus Filled to -25.5 Inches Exceeding -27 Inch Limit.Caused by Operator Error.Operation Procedure OP-17 Revised to Require Second Operator to Monitor Torus

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/03L-0:on 800116,during Evolutions,Torus Filled to -25.5 Inches Exceeding -27 Inch Limit.Caused by Operator Error.Operation Procedure OP-17 Revised to Require Second Operator to Monitor Torus
ML19296B351
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 02/11/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19296B349 List:
References
LER-80-014-03L, LER-80-14-3L, NUDOCS 8002200441
Download: ML19296B351 (1)


LER-1980-014, /03L-0:on 800116,during Evolutions,Torus Filled to -25.5 Inches Exceeding -27 Inch Limit.Caused by Operator Error.Operation Procedure OP-17 Revised to Require Second Operator to Monitor Torus
Event date:
Report date:
3241980014R03 - NRC Website

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jolsjq to Radwaste. During one of these evolutions, the torus was filled to -25.5 inches.

I l exceeding the -27 inch limit. Technical Specifications 3.6.2, 6.9.1.95 c

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3 [,j ; torus was in progress, the Operator's attention was diverted for approximate 1v one i

minute on another problem, and when he returned, the level was high. Operation Pro-cedure OP-17 will be revised to require a second Operator to monitor torus level when-l

ever the level is being changed. All Operations personnel will review this LER.

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