LER-1980-010, /01T-0:on 800214,reanalysis of RCS Pipe Restraints Per IE Insp Rept 50-346/79-23 Revealed Design Deficiency on Two Reactor Coolant Hot Leg Pipe Whip Restraints at Top of Each RCS Hot Leg.Caused by Design Error |
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b3 El Dh E T V'9En b3 t' 3 EVENT DATE 14 75 REPORT DATE cJ EVENT DESCRIPTICU AND PROSASLE CONSECUENtES h l An extensive re-analysis of the reactor coolant system pipe restraints in compliance t
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This became immediately reportable under Technical Specification O c 1 6.9.1.8.1.
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{iO IThe cause of the occurrence was a design error by the architect / engineer, Bechtel.
A jijill bolted connection between two pipe whip restraints and their support beams on each hot;
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TOLEDO EDISON COMPANY
' DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-32-80-02 DATE OF EVENT:
February 14, 1980 FACILITY:
Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: The design of two Reactor Coolant System (RCS) pipe whip restraints on each coolant loop did not meet the acceptance criteria Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2772, and Load (Gross MWE) = 923.
Description of Occurrence: While performing the analysis to verify the design of the RCS pipe whip restraints in compliance with Item 6.a of OISE Inspection Report No. 50-346/79-23 it was discovered that four RCS pipe whip restraints, designated HLR-5 and HLR-6, two on each hot leg did not meet the acceptance criteria set forth in Section II, Paragraph 1.1 of the " Davis-Besse Nuclear Power Station Unit 1 Veri-fication Study of Pipe Whip Restraints on the Reactor Coolant System", dated Decem-ber 7, 1979. The analysis showed that the bolts connecting restraints HLR-5 and HLR-6 to their supporting beams did not remain clastic as required in Section II, Paragraph 1.1.L of our December 7, 1979 report, and thus limited the capacity of the restraints.
Designation of Apparent Cause of Occurrence: The cause of the occurrence was a design error by the architect / engineer, Bechtel Power Corporation. The designer failed to take into account the eccentricity in the bolted connection between res-traints HLR-5 and HLR-6 and their support beams. This eccentricity caused a non-uniform load distribution to the bolts, which was not originally considered, thus underpredicting the load to the maximum stressed bolt, with the result being the connection not meeting acceptance criteria.
Bechtel has reviewed all other pipe whip restraints to see if any contain bolted connections which could have a simi-lar design error. This review ver'ified that no other pipe whip restraints have sinilar bolted eccentric connections.
Based on this review, there is no reason to believe that this design error was a result of a generic deficiency in the original design method.
Analysis of Occurrence:
Pipe whip restraints are not required for normal operation.
The analysis performed thus far indicates that the bolted connection between pipe whip restraints ifLR-5 and HLR-6 and their support beams fails to meet the acceptance criteria when subjected to a double ended hot leg pipe rupture at the steam genera-tor inlet nozzle or at restraint HLR-6.
A review of the RCS pipe stress analysis shows that the pipe stress levels at these two locations are 46 and 57 percent of the stress levels required by NRC Branch Technical Position MEB 3-1 for postulating a pipe break. These non-mechanistic pipe breaks are postulated, in accordance with NRC criteria even though not justified by calculated pipe stress levels, because they are at either a terminal pipe end or one of the two highest stressed intermedia' e t
locations.
LER #80-010
TOLEDO EDISON C0:qANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE PAGE 2 SUPPLEMENTAL INFORMATION FOR LER NP-32-80-02 The analysis which indicated the bolted connection would not meet acceptance criteria was a single degree of freedom dynamic analysis. The analysis modeled the bolts us-ing a tension and shear spring for each bolt.
Finite element models were developed for restraints HLR-5 and HLR-6 and their supporting beams. These models were then An RCS blow-coupled and analyzed using time-history and energy balance techniques.
down time-history, developed by Babcock and Wilcox was used as the forcing function.
An allowable stress of 0.9 of the dynamic yield stress was established for the bolts in the connection between HLR-5 and HLR-6 and their support beams. The criteria was-also established that if any one bolt were stressed to the allowable it would constitute a failure of all the bolts in the connection. The connection was shown to be unacceptable under these criteria. However, there are several factors which have not been considered which make the above analysis conservative; they are:
1.
The analysis used a single degree of freedom model instead of a multi-degree of freedom model.
2.
The analysis assumed that the load resulting from the pipe break was totally applied at the point of the pipe break instead of at multiple locations along the pipe, (i.e. pipe bends).
3.
No inelastic load redistribution of the bolt loads was considered.
4.
No damping of the system was assumed at impact.
5.
The energy absorbing capacity of other structures, such as the secondary shield walls, was not considered.
6.
No loss of energy was considered to occur at impact between the RCS hot leg and the restraint.
Considering the above factors of conservatism the capacity of the bolted connection between restraints HLR-5 and HLR-6 and their support beams will increase by a mini-mum of 70 percent to a maximum of 220 percent.
In the current analysis the bolted connection falls short of our acceptance criteria by 60 percent. This demonstrates there is a high probability that the restraints will perform their intended function.
Based on the conservatisms in establishing the acceptance criteria, the conserva-tive analytical methodology and the low calculated stress levels in the RCS piping, continued operation of the facility until the refueling outage, currently scheduled to begin April 10, 1980, will pose no danger to the health and safety of the public or station personnel.
The Company Nuclear Review Board has reviewed this occurrence, in particular the low stress levels in the RCS piping and the low probability of the occurrence of a design basis accident which would require restraints HLR-5 and HLR-6 to perform their intended design function. The Company Nuclear Review Board has determined that continued operation until shutdown for the scheduled refueling outage does not compromise the health and safety of the public.
LER #80-010
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE PAGE 3 SUPPLEMENTAL INFORMATION FOR LER NP-32-80-02
Corrective Action
Under Facility Change Request 80-047, pipe whip restraints llLR-5 and HLR-6 and their support beams will be modified during the refueling outage currently scheduled to begin /.pril 10, 1930. The modifications will either increase the capacity of the connection between restraints ELR-5 and HLR-6 and their support beams or reduce the load transmitted to the connection by the addi-tion of shear plates and reducing the gap between the restraints and the hot leg pipe. The facility will not be returned to operation, after the refueling outage, until these modifications are completed.
Failure Data: There are no previous reported instances where these pipe ' hip res-traints have not met acceptance criteria.
LER #80-010
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| 05000346/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000346/LER-1980-001-01, /01T-0:on 800103,during Plant Heatup,Safety Features Actuation Sys Channels 1 & 3 Tripped at 1,600 Psig, Causing Level 2 Actuation.Operators Correctly Tripped Reactor Coolant Pumps.Caused by Procedural Deficiency | /01T-0:on 800103,during Plant Heatup,Safety Features Actuation Sys Channels 1 & 3 Tripped at 1,600 Psig, Causing Level 2 Actuation.Operators Correctly Tripped Reactor Coolant Pumps.Caused by Procedural Deficiency | | | 05000346/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000346/LER-1980-002-03, /03L-0:on 800103,after Actuating of Safety Features Actuation Sys Level 2,demin Water Valve DW68318 Did Not Indicate Closed & Monitor Light Did Not Indicate Properly.Caused by Maladjusted Position Indicator Switch | /03L-0:on 800103,after Actuating of Safety Features Actuation Sys Level 2,demin Water Valve DW68318 Did Not Indicate Closed & Monitor Light Did Not Indicate Properly.Caused by Maladjusted Position Indicator Switch | | | 05000346/LER-1980-003-03, /03L-0:on 800103,during Auxiliary Feedwater Pump Test,Pump l-1 Was Declared Inoperable.Caused by Improperly Adjusted Slip Clutch Between Governor Manual Speed Adjustment Shaft & Remotely Controlled Speed Changer Motion | /03L-0:on 800103,during Auxiliary Feedwater Pump Test,Pump l-1 Was Declared Inoperable.Caused by Improperly Adjusted Slip Clutch Between Governor Manual Speed Adjustment Shaft & Remotely Controlled Speed Changer Motion | | | 05000346/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000346/LER-1980-004-03, /03L-0:on 800107,control Rod 5-11 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals.Possibly Caused by Isolation of Position Indication Cabling & Electrical Penetration | /03L-0:on 800107,control Rod 5-11 Absolute Position Indication Declared Inoperable Due to Fluctuating Signals.Possibly Caused by Isolation of Position Indication Cabling & Electrical Penetration | | | 05000346/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000346/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000346/LER-1980-005-03, /03L-0:on 800110,Tech Spec Late Date Passed W/O Performance of Boric Acid Flowpath Heat Tracing Weekly Test. Caused by Known Deficiency in Design of Sys Resulting in Inability to Maintain Min Temp Necessary During Startup | /03L-0:on 800110,Tech Spec Late Date Passed W/O Performance of Boric Acid Flowpath Heat Tracing Weekly Test. Caused by Known Deficiency in Design of Sys Resulting in Inability to Maintain Min Temp Necessary During Startup | | | 05000346/LER-1980-006-03, /03L-0:on 800112,found Fiberglass Insulation Stuffed Into Open Wall Ventilator Between Water Treatment Bldg & Svc Water Valve Room,Causing Fire Damper to Be Inoperable.Figerglass Removed | /03L-0:on 800112,found Fiberglass Insulation Stuffed Into Open Wall Ventilator Between Water Treatment Bldg & Svc Water Valve Room,Causing Fire Damper to Be Inoperable.Figerglass Removed | | | 05000346/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000346/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000346/LER-1980-007-03, /03L-0:on 800116,ref Position Verification for Group 5,rod 11,was Made 1-h & 40 Minutes Late.Caused by Operator Oversight Due to Lack of Adequate Reminder Sys. Multiple Timer Sys Will Prevent Recurrence | /03L-0:on 800116,ref Position Verification for Group 5,rod 11,was Made 1-h & 40 Minutes Late.Caused by Operator Oversight Due to Lack of Adequate Reminder Sys. Multiple Timer Sys Will Prevent Recurrence | | | 05000346/LER-1980-008-03, Gap Discovered in Wall Where Five two-inch Conduits Go from Electrical Penetration Room 2 to Cable room.Six-inch Gap Around Ventilation Duct Also Found.Caused by Improper Initial Installation | Gap Discovered in Wall Where Five two-inch Conduits Go from Electrical Penetration Room 2 to Cable room.Six-inch Gap Around Ventilation Duct Also Found.Caused by Improper Initial Installation | | | 05000346/LER-1980-008, Forwards Revised LER 80-008/03L-1 | Forwards Revised LER 80-008/03L-1 | | | 05000346/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000346/LER-1980-009-03, /03L-0:on 800122,discovered That NI-7 Indication on Computer Group 38 Was Reading Less than Heat Balance Power,Putting NI-7 Below Instrumentation Operability Limit Line.Caused by Extremely Tight Calibr Band at 100% Power | /03L-0:on 800122,discovered That NI-7 Indication on Computer Group 38 Was Reading Less than Heat Balance Power,Putting NI-7 Below Instrumentation Operability Limit Line.Caused by Extremely Tight Calibr Band at 100% Power | | | 05000346/LER-1980-010-01, /01T-0:on 800214,reanalysis of RCS Pipe Restraints Per IE Insp Rept 50-346/79-23 Revealed Design Deficiency on Two Reactor Coolant Hot Leg Pipe Whip Restraints at Top of Each RCS Hot Leg.Caused by Design Error | /01T-0:on 800214,reanalysis of RCS Pipe Restraints Per IE Insp Rept 50-346/79-23 Revealed Design Deficiency on Two Reactor Coolant Hot Leg Pipe Whip Restraints at Top of Each RCS Hot Leg.Caused by Design Error | | | 05000346/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000346/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000346/LER-1980-011-03, /03L-0:on 800131,during Normal Operation, Operations Personnel Received Half Trip on Steam & Feedwater Rupture Control Sys Channels 1/3.Caused by Spurious Trip from +25 Volt Dc Power Supply PS03 in Sglic Channel 1 | /03L-0:on 800131,during Normal Operation, Operations Personnel Received Half Trip on Steam & Feedwater Rupture Control Sys Channels 1/3.Caused by Spurious Trip from +25 Volt Dc Power Supply PS03 in Sglic Channel 1 | | | 05000346/LER-1980-012-03, /03L-0:on 800201,operator Noticed Loss of Control Room Position Indication for Letdown Cooler Isolation Valve MU2A.Caused by Design Deficiency.Apparently,Someone Brushed Up Against Disconnect Breaker Switch.Switch Reposition | /03L-0:on 800201,operator Noticed Loss of Control Room Position Indication for Letdown Cooler Isolation Valve MU2A.Caused by Design Deficiency.Apparently,Someone Brushed Up Against Disconnect Breaker Switch.Switch Repositioned | | | 05000346/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000346/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000346/LER-1980-013-03, /03L-0:on 800208,w/reactor Startup in Progress, Personnel Noted Control Rod 5-11 Absolute Position Indication Was Not Responding.Caused by Blown Fuse F14 in Position Ref Panel | /03L-0:on 800208,w/reactor Startup in Progress, Personnel Noted Control Rod 5-11 Absolute Position Indication Was Not Responding.Caused by Blown Fuse F14 in Position Ref Panel | | | 05000346/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000346/LER-1980-014-03, /03L-0:on 800208,pressurizer Sample Sys Containment Isolation Valve RC240B Failed to Close Twice. Caused by Improper Torque Switch Setting & Stripped Screw on Closing Contactor.Settings Readjusted & Switch Replaced | /03L-0:on 800208,pressurizer Sample Sys Containment Isolation Valve RC240B Failed to Close Twice. Caused by Improper Torque Switch Setting & Stripped Screw on Closing Contactor.Settings Readjusted & Switch Replaced | | | 05000346/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000346/LER-1980-015-03, /03L-0:on 800210,during Normal Startup,Control Rod 5-11 Absolute Position Indication Declared Inoperable.Caused by Numerous Asymmetric Rod Alarms.Data from Current Failure Evaluated | /03L-0:on 800210,during Normal Startup,Control Rod 5-11 Absolute Position Indication Declared Inoperable.Caused by Numerous Asymmetric Rod Alarms.Data from Current Failure Evaluated | | | 05000346/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000346/LER-1980-016-03, /03L-0:on 800213,while Reviewing Station Log,Shift Foreman Discovered That Containment Airlock Seal Leakage Test Had Not Been Performed After Last Entry Into Containment During Startup.Caused by Procedural Inadequacy | /03L-0:on 800213,while Reviewing Station Log,Shift Foreman Discovered That Containment Airlock Seal Leakage Test Had Not Been Performed After Last Entry Into Containment During Startup.Caused by Procedural Inadequacy | | | 05000346/LER-1980-017-03, /03L-0:on 800217,operations Personnel Noted That Safety Features Actuation Sys Channel 3 Borated Water Storage Tank Level Indication Was Six Feet Higher than Other Meters.Caused by Freezing of Transmitter Sensing Line | /03L-0:on 800217,operations Personnel Noted That Safety Features Actuation Sys Channel 3 Borated Water Storage Tank Level Indication Was Six Feet Higher than Other Meters.Caused by Freezing of Transmitter Sensing Line | | | 05000346/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000346/LER-1980-018-03, /03L-0:on 800226,safety Features Actuation Sys Channel 3 Borated Water Storatge Tank Level Indication Was Discovered Reading Four Feet Higher than Other Three Channels.Caused by Inadequate Design of Freeze Protection | /03L-0:on 800226,safety Features Actuation Sys Channel 3 Borated Water Storatge Tank Level Indication Was Discovered Reading Four Feet Higher than Other Three Channels.Caused by Inadequate Design of Freeze Protection | | | 05000346/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000346/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000346/LER-1980-019-01, /01T-0:on 800325 Reactor Flux/Flow Trip Setpoints Were Not Verified to Be Properly Reset within 4-h of Manual Shutdown of Rcp.Caused by Attention Given to Feedwater Swings.Trip Setpoints Verified Later | /01T-0:on 800325 Reactor Flux/Flow Trip Setpoints Were Not Verified to Be Properly Reset within 4-h of Manual Shutdown of Rcp.Caused by Attention Given to Feedwater Swings.Trip Setpoints Verified Later | | | 05000346/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000346/LER-1980-020-03, /03L-0:on 800306,control Operator Noted No Control Room Indication for Containment Vacuum Relief Isolation Valve CV5072.Caused by Breaker BE1139 Being Closed,Probably Resulting from Someone Bumping Into Breaker | /03L-0:on 800306,control Operator Noted No Control Room Indication for Containment Vacuum Relief Isolation Valve CV5072.Caused by Breaker BE1139 Being Closed,Probably Resulting from Someone Bumping Into Breaker | | | 05000346/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000346/LER-1980-021-03, /03L-0:on 800313,during Diesel Fire Protection Pump Weekly Test,Pump Could Not Be Stopped W/Control Button. Once Stopped,Pump Could Not Be Started.Cause Not Determined by Scheme Check.Retrial of Pump Proved Successful | /03L-0:on 800313,during Diesel Fire Protection Pump Weekly Test,Pump Could Not Be Stopped W/Control Button. Once Stopped,Pump Could Not Be Started.Cause Not Determined by Scheme Check.Retrial of Pump Proved Successful | | | 05000346/LER-1980-022-03, /03L-0:on 800317,operations Personnel Noticed Loss of Control Room Indication for Containment Dihydrogen Analyzer 2 Discharge Line Valve CV5010E.Caused by Const Personnel Accidentally Opening Breaker | /03L-0:on 800317,operations Personnel Noticed Loss of Control Room Indication for Containment Dihydrogen Analyzer 2 Discharge Line Valve CV5010E.Caused by Const Personnel Accidentally Opening Breaker | | | 05000346/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000346/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000346/LER-1980-023-03, /03L-0:on 800327,discovered That Control Rod Groups 3 & 4 Were Moving in on Their Own.Group 3 Was 0% Withdrawn.Group 4 Was 90% Withdrawn.Caused by Component Failure.Component Replaced | /03L-0:on 800327,discovered That Control Rod Groups 3 & 4 Were Moving in on Their Own.Group 3 Was 0% Withdrawn.Group 4 Was 90% Withdrawn.Caused by Component Failure.Component Replaced | | | 05000346/LER-1980-024-03, /03L-0:on 800327,following Normally Initiated Reactor Trip,Auxiliary Feed Pump Turbine 1-2 Main Steam Isolation Valve MS-107 Closed.Cause Unknown.Further Investigation of Valve & Operator Will Be Pursued | /03L-0:on 800327,following Normally Initiated Reactor Trip,Auxiliary Feed Pump Turbine 1-2 Main Steam Isolation Valve MS-107 Closed.Cause Unknown.Further Investigation of Valve & Operator Will Be Pursued | | | 05000346/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000346/LER-1980-025-03, /03X-1:on 800330,control Rod Group 5,rod 11 Absolute Position Indication Declared Inoperable.Caused by Fluctuating Signals Resulting in Numerous Asymmetric Rod Alarms Due to Defective Reed Switch Assemblies | /03X-1:on 800330,control Rod Group 5,rod 11 Absolute Position Indication Declared Inoperable.Caused by Fluctuating Signals Resulting in Numerous Asymmetric Rod Alarms Due to Defective Reed Switch Assemblies | | | 05000346/LER-1980-025, Forwards LER 80-025/03X-1 | Forwards LER 80-025/03X-1 | |
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