ML19290C917

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IE Insp Repts 50-338/79-45 & 50-339/79-54 on 791004-1102. Noncompliance Noted:Inoperable Steam Pressure Transmitters Due to Swapped Sensing Lines & Failure to Properly Retain Personnel Training & Qualification Records
ML19290C917
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 12/04/1979
From: Kellogg P, Kidd M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19290C906 List:
References
50-338-79-45, 50-339-79-54, NUDOCS 8002150061
Download: ML19290C917 (10)


See also: IR 05000338/1979045

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA ST

N.W.. SulTE 3100

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ATLANTA, GEORGIA 30303

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Report Nos. 50-338/79-45 and 50-339/79-54

Licensee: Virginia Electric and Power Company

P. O. Box 26666

Richmond, Virginia 23261

Facility Name: North Anna Units 1 and 2

Docket Nos. 50-338 and 50-339

License Nos. NPR-4 and CPPR-78

Inspected at North Anna- Site,Ci /near Mineral, Virginia

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Inspected by:

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,[c , M. S. Kidd, Resident Inspector

Date Signed

Approved by:

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P. J. Kellogg, QRction Chief, R6NS Branch

Date Signed

SUMMARY

inspection on October 9 - November 2, 1979

Unit 1 Areas Inspected

This routine inspection by the resident inspector involved thirty seven hours

onsite in the areas of licensee event reports, maintenance procedures and activ-

ities, previously identified open and unresolved items, and plant tours.

Unit 1 Findings

Within the four areas inspected, no items of noncompliance or deviations were

identified in two areas. Two apparent items of noncompliance were identified in

two areas (Infraction - Failure to operate within the Limiting Condition for

Operation for main steam channels for loops A and C

paragraph 11.b; Deficiency -

Failure to maintain mechanical and electrical maintenance training records in

accordance with requirements

paragraph 6.c).

Unit 2 Areas Inspected

This routine inspection by the resident inspector involved seventeen hours

onsite in the areas of IE Bulletin followup, reports per 10CFR 50.55(e) and 10 CFR 21, previously identified open items, and plant tours.

Unit 2 Findings

No items of noncompliance or deviaitions were identified.

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DETAILS

1.

Persons Contacted

Licensee Employees

R. A. Berquist, Assistant Instrument Supervisor

  • W. R. Cartwright, Station Manager

L. O. Goodrich, Supervisor - Mechanical Maintenance

  • E. W. Harrell, Superintendent of Maintenance

J. R. Harper, Instrument Supervisor

S. L. Harvey, Operating Supervisor

D. M. Hopper, Health Physics Supervisor

H. T. Hyer, Mechanical Foreman

Other licensee employees contacted included operators, three mechanics, and

three office personnel.

Other Organizations

Stone and Webster Engineering Corporation (S&W)

W. L. Lehmbeck, Assistant Lead Advisory Engineer

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized on October 19, and 26 and

November 2, 1979 for those persons indicated in Paragraph I above. The

apparent infraction defined in paragraph 11.b and the apparent Deficiency

described in paragraph 6.c were discussed in detail on November 2, 1979.

3.

Licensee Action on Previous Inspection Findings

(Closed) Unresolved Item 338/79-13-01:

Piezometer Trend Analysis.

Discussions by the Resident Inspector and a Regional Specialist Inspector

on September 21, 1979, revealed that the specialist had reviewed the vendor's

analysis provided to VEPCO on April 4, 1979, and had no further questions.

This item is resolved.

4.

Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve noncompliance or

deviations. New unresolved items identified during this inspection are

discussed in paragraph 11.f.

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5.

Plant Status

The first Unit I refueling fuel shuffle was completed October 30, 1979.

The shutdown is expected to continue through early to mid December, 1979.

Unit 2 was in the final stages of preoperational testing at the conclusion

of the inspection period.

6.

Maintenance Procedures and Activities - Unit 1

During the inspection period, the inspector reviewed selected maintenance

procedures for activities to be performed during the current refueling

shutdown, witnessed portions of one maintenance activity, and reviewed

qualifications of certain maintenance personnel as defined below:

a.

Procedure Reviews

The following procedures were reviewed and compared to the provisions

of ANSI N 18.7-1972, " Standard for Administrative Controls for Nuclear

Power Plants"; VEPCO's Nuclear Power Station Quality Assurance Manual

(NPSQAM), sections 7, " Control of Purchased Material, Equipment and

Services" and 16, " Corrective Action"; station administrative procedures

8.0, " Fire Prevention" and 45.0, " Housekeeping"; and Mechanical

Maintenance administrative procedure 6.0, " Cleanliness Control".

1-M0P-5.94, " Removing C Reactor Coolant Loop From Service for

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Maintenance"

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1-M0P-32.3, " Pumping Water From a Steam Generator to Clarifier

Using Steam Generator Transfer Pump (1-WT-P-35)"

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MMP-C-MISC-3, " Mechanical Maintenance Procedure for Steam

Generator Explosive Tube Plugging"

1-M0P-5.32, " Steam Generator 1-RC-E-IC"

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1-M0P-8.02, " Charging Pump 1-CH-P-1B"

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MMP-C-CH-2, " Mechanical Maintenance Procedure for Seals on

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Charging and Safety Injection Pumps"

MMP-P-CH-1, " Mechanical Maintenance Procedure for Charging

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Pumps /High Head Safety Injection".

The above procedures, covering two maintenance activities, were

reviewed along with other maintenance controls, such as the

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Maintenance Report and Tagging Record, defined in sections 16 and 14

of the NPSQAM, to determine whether the following functions had been

properly addressed:

(1) Administrative approvals for removing the system from service and

returning it to service.

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(2) Hold Points for inspection / audit and signoff by QA or other

licensee personnel.

(3) Provisions for operational readiness testing following maintenance.

(4) Requirements to obtain special authorization for activities

involving welding, open flame, or other ignition sources, and

posting of a firewatch as needed.

(5) Provisions for review of materials certifications data, if

applicable.

(6) Provisions for assuring that LC0 requirements of the Technical

Specifications were satisfied during the repair period.

(7) Provisions for the control of housekeeping during the maintenance

effort.

(8) Provisions for cleaning safety related systems / components

following Maintenance.

(9) Provisions for assuring that system valves, breakers, etc.

are

aligned for normal service.

(10) Provisions for removal of jumpers which may be required for

maintenance / testing activities.

(11) Respvasibility for reporting to licensee management details

concerning design or construction related deficiencies identified

during maintenance.

The inspector had comments on MMP-C-CH-2, relating to maintenance of

system and component cleanliness, and on MMP-C-MISC-3 regarding the

sequence and adequacy of certain steps involving tube plugging opera-

tions. Licensee personnel had initiated changes to the procedures to

address the inspector's concerns, thus there were no further questions.

No items of noncompliance or deviations were identified.

b.

Maintenance Activity Witnessing

On October 25 and 26, 1979, the inspector observed portions of the

disassembly and inspection of the out board seal for charging / safety

injection pump 1-CH-P-1B. This activity was conducted by use of pro-

cedures 1-M0P-8.02 and MMP-C-CH-02, Maintenance Report (MR)

N1-78-12040635, Tagging Record (TR) N1-6287, and Radiation Work

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Permits (RWP) 79-SP-317 and 79-SP-320.

Observations included the

following:

(1) A sampling of valves and breakers found them to be properly

tagged and positioned as requied by 1-M0P-8.02 and the TR.

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(2) Copies of the procedure were available and in use in the pump

cubicle and the auxiliary building " hot shop", where the seal

inspection and repair was conducted.

Also, RWP's were posted at

both locations.

(3) A Quality Control inspector was present and observing hold points.

(4) Necessary deviations to procedures were processed in accordance

with the NPSQAM and Technical Specifications.

(5) System and pump internals cleanliness was being maintained.

Housekeeping was in order.

Within the areas observed, no items of noncompliance or deviations

were observed.

c.

Personnel Qualifications

Records of training, education, and previous work experiences for two

mechanics and one mechanic trainee involved in the charging pump seal

replacement discussed in 6.b were reviewed to ascertain their qualifi-

cations for this activity. Available records demonstrated that the

mechanics were qualified for this function.

The trainee, working in

an assisting capacity, is in step 3 of the 10 step Mechanic Development

Program. The inspector had no questions regarding training / qualifications.

During the review and discussions with station personnel, it was noted

that records of training for mechanical and electrical maintenance

personnel via the Mechanic Development Program (see FSAR section

13.2.1.6) are not maintained at the station, but are maintained in

VEPCO's corporate offices. The inspector stated that this appeared to

be in noncompliance with Unit 1 Technical Specification 6.10.2 b as

implemented by section 17, " Records," of the NPSQAM. The Specification

requires that records of training and qualification for current plant

staff members be maintained as lifetime records. NPSQAM section 17

and VEPCO's Topical Report Quality Assurance Program - Operations

Phase (VEP-1-3A) section 17.2.17 commit to retention of such records

in accordance with ANS1 N-45.2.9, 1974, which requires a special

storage repository or duplicate records systems. This apparent non-

compliance (Deficieny) is designated as 338/79-45-01.

7.

Plant Tours

Tours of selected plant areas were conducted on October 19, 22, 24, and 25,

1979. The following items, as available were observed:

a.

Fire Equipment

Operability and evidence of periodic inspection of fire suppression

equipment.

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b.

Housekeeping

Minimal accumulations of debris and maintenance of required cleanliness

levels in systems under or following testing.

Observation regarding

certain areas were given to station management who acknowledged the

inspector's comments.

c.

Equipment Preservation

Maintenance of special preservative measures for installed equipment

as applicable.

d.

Component Tagging

Implementation and observance of equipment tagging for safety or

equipment protection.

e.

Communication

Ef fectiveness of public address system in all areas toured.

f.

Equipment Controls

Ef fectiveness of jurisdictional controls in precluding unauthorized

work on systems turned over for initial operations or preoperational

testing.

g.

Foreign Material Exclusion

Maintenance of controls to assure systems which have been cleaned and

flushed are not reopened to admit foreign material.

h.

Security

Implementation of security provisions for both Units.

Within the above areas, no items of noncompliance or deviations were observed

when compared to the applicable station programs and procedures.

8.

IE Bulletin 79-02, Unit 2

Inspection of the Unit 2 program, procedures, and installation for pipe

support base plates using expansion anchor bolts was documented in IE

Report 50-339/79-37 with no adverse findings. Following receipt of an

internal NRR memorandum stating that the Mechanical Engineering Branch of

the Division of System Safety had no further questions on this IEB for

North Anna 2, the inspector informed station management that the IEB was

considered closed for that unit (339/79-28-06).

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9.

Followup on Reactor Trip and Safety Injection - Unit 1

Compilation of the inspection / investigation report for this event, 50-338/

79-39, and confirmation of data and information gathered during that inspec-

tion period were discussed with Region II and/or station management on

October 9, 11, and 15-13, 1979. Details of the event and inspection findings

are given in the referenced report.

10.

Followup on Previously Identified Open Items

Fuel Transfer Tube Surveys (338/78-28-06)

a.

This item resulted from IE Bulletin 78-08 and was used to track the

conduct of radiation surveys of the fuel transfer tube and surrounding

plant areas during the first refueling.

0n October 18, 1979, surveys were conducted on two spent fuel assem-

blies as they were transporeted to the fuel building.

Readings as

high as 400 R per hour were seen on the fuel tube shield block.

Levels around the operator's fuel handling machinery control panel in

containment were about 200 mr per hour.

Considerable streaming was

evident on all levels of containment.

Station management administra-

tively controlled access to containment during fuel movement, allowing

only operators and health physics personnel to be present on the 291

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foot elevation (operating deck) during spent fuel movement. Also,

operators were instructed to move to a more shielded area after

initiating fuel transfer at the control panel.

In certain instances,

other workers were allowed in containment if their work stations were

not near the fuel tube and constant health physics coverage provided.

These administrative controls appeared successful, but station manage-

ment was informed that consideration should be given to installation

of shiciding around the transfer tube prior to the second refueling on

Unit 1 and the first refueling on Unit 2.

Management stated that

studies would be conducted to determine what shielding measures could

be taken.

Item 338/78-28-06 remains open and item 339/79-54-01 is

identified for Unit 2.

b.

Unit 2 Radiation Monitoring Systems Testing (339/78-31-02)

This item was identified to track completion of preoperational test

2-P0-10.

This completed test was reviewed and findings discussed in

IE Reports 50-339/79-45 and 50-339/79-48.

This item is closed.

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11.

Licensee Event Reports - Units 1 and/or 2

The following events or problems were reported as prompt (24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) LER's

per Unit 1 Technical Specifications and/or under the provisions of 10 CFR 50.55(e) and 10 CFR 21 for Unit 2 during the inspection period:

Service Water Radiation Monitoring Pumps (LER 79-133)

a.

On October 5,1979, licensee personnel reported that the Unit 1 Service

Water (SW) radiation monitoring pumps, 1-SP-5, 6, 7, and 8 all failed

to start on a test containment depressurization actuation (CDA) signal

as they are designed to do.

The motor overloads were found to be

tripped. This will be reviewed in more detail at a later date (0 pen

item 338/79-45-02).

b.

Main Steam Pressure Transmitter Tubing Reversed (LER 79-142)

On October 16, 1979, station management reported that while pressurizing

Unit 1 "C" steam generator to check for tube leaks, it was observed

that the Channel IV steamline pressure indicator for "A" steam generator

gave an indication while the channel IV steamline pressure indicator

for "C" steam generator was unaffected. This signified that the two

indications were swapped.

It was found that the sensor tubing from

the transmitter root valves were swapped. A test procedure was devel-

oped that same date and other main steam pressure sensing lines check

to assure proper alignment. No other discrepancies were found.

Station man gement stated that this test procedure (IMP-P-PROC-4)

would be used to verify proper alignment of all fluid sensing lines

for Units 1 and 2.

This effort was continuing at the conclusion of

the inspection, having been slowed down due to containment accessibility

problems during fuel shuffle in Unit 1.

This verification process

will be reviewed prior to Unit I restart and Unit 2 fuel load (items

338/79-45-03 and 339/79-54-02).

In researching the cause of the sensing line swap for transmitters

PT-1476 and PT-1496, S&W discovered that the lines had been properly

installed at the time of reletse to VEPC0 by documentation required by

1-TIP-2, an installation test procedure which checks continuity of

sensing lines, along with other construction checkout tests.

In

July of 1977, a rework control form (RCF) I-350 was issued to cut

these two lines to allow modification of piping hanger supports in the

The retest requirement specified on the RCF was only for a leak

area.

test of the lines after rewelding.

S&W Field Quality Control (FQC)

procedure QC-15.4, paragraph 4.2.7 states that during rework and prior

to any retesting, the Advisory Engineer or his designee shall record

any retest requirements on the original RCF. The procedure does not

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provide any guidelines for determining what retest requirements should

be specified for a given job. Licensee personnel were informed that

this weakness should be evaluated and rectified unless adequately

covered otherwise by the FQC Manual (Unit 2 open item 339/79-54-03).

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The inspector stated that the swapped sensing lines had created a

situation wherein the minimum required operable channels for steam

generators "A" and "C" given in Technical Specification Table 3.3-3,

item 1.e were not met.

In that the parameter being compared is dif-

ferential pressure between steam lines, the swap negated the ability

of the affected channels to be used in such a comparison. He further

stated that this appeared to be in noncompliance (Infraction) with

Action Statement 14 of Table 3.3-3 which permits operation with the

number of operable channels being one less than the total number of

channels until the next required Channel Functional Test (monthly),

provided the inoperable channel is placed in the trip condition within

one hour.

In that station personnel were not aware of the inoperable

channels because of the swap, the Action Statement was not adhered to.

This apparent Infraction is also designated as 338/79-45-03.

c.

Cracked Valve Disk - Unit 2

On September 28, 1979, licensee personnel reported that a crack had

been found in the disk of MOV-2380, a Unit 2 containment isolation

valve. This was reported per 10 CFR 50.55 (e) and 10 CFR 21 and will

be reviewed in more detail at a later date (open item 339/79-54-04).

d.

Insulation in Diesel Generator 2-H Turbocharger

On October 12, 1979, licensee personnel reported per 10 CFR 50.55(e)

and 10 CFR 21 that insulation material had been found in the turbo-

charger for Unit 2 emergency diesel generator (DG) 2 H. This had the

potential for rendering the DG inoperable. Circumstances of this

event will be reviewed in more detail at a later date (open item

339/79-54-05).

Safeguards Building Ventilation Seismic Qualification - Units 1 and 2

e.

On October 31, 1979, the inspector was informed that S&W had discovered

that the discharge ductwork of the Unit 2 safeguards area ventilation

exhaust system was not built to Seismic Class 1 standards as stated in

FSAR section 9.4.6.1.

This was reported per 10 CFR 50.55(e) and 10 CFR 21 for Unit 2 and as a prompt LER per Technical Specifications for

Unit 1.

Requirements for design of the discharge ductwork from the

fans out to the vent stack were questionable in that FSAR Table 3.2.1-1

and supplementary section S9.68 state that only the suction ductwork

for these exhaust fans is Class 1.

The office of Nuclear Reactor

Regulations (NRR) Safety Evaluation Report for Units 1 and 2 states in

section 9.4.2 that the exhaust system is designed to Class I require-

ments making no distinction between suction and discharge ductworks.

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Evaluation of this potential problem by VEPC0 and S&W was continuing

at the conclusion of the inspection period. NRR representatives were

apprised of this matter on October 31, 1979. Licensee personnel were

informed that this system as well as others shown on FSAR Figure

S9.86-1 as not being seismic Class 1 should be evaluated for adequacy.

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This is designated as unresolved items 50-338/79-45-04 and 50-339/

79-54-06.

Station management stated that these systems would be

evaluated further.

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f.

Defective Electrical Cable - Unit 1

On October 23, 1979, station management reported that s defective

cable had been identified during installation in Unit 1.

A partially

exposed wire was discovered in the area of an apparent insulation

splice in a twelve conductor control cable being installed in the

control circuitry of a Unit 1 emergency DG. This cable had been part

of an order of four reels, with this one cable being the first appli-

cation in safety related circuits for Unit I none of which had been

used in Unit 2.

The cable and unused /used reels were returned to the

vendor, Cerro-Rockbestos, except for one reel, which had been sent to

the Surry Power Station (later notified of potential problem). At the

conclusion of the inspect ion, the cable vendor, S&W and VEPCO were

involved in analyzing the defect and evaluating its possible generic

implications. This matter will be reviewed further and is designated

as open item 338/79-45-05.