LER-1978-035, /01T-0 on 781227:torus Water Temp in Excess of Tech Specs.Caused by Failure of Operations Personnel to Recognize Torus Water Temp Nearing Tech Spec Limit |
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| 2191978035R01 - NRC Website |
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61 COCKET NUMB ER 68 6fr EVE NT DATE 74 76 REPORT D ATE 80 EVENT DESCRVTION AND PROSABLE CONSEQUENCES h o
2 l During normal operation, the torus water temperature was found to be in l
ggi excess of the Tech Spec limits.
The average value for the four suppres-l sion pool thermocouolas at the time of the incident was 95.35'F.
The i
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Safety significance of this event I
o is is considered minimal sincu 15'F. marcin exists between the Tech SOec.
I o17 I limit and the reactor scram recuirement of 110'F, l
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CAUSE
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40 41 42 43 44 47 cAUSE OEsORIPTION AND CORRECTIVE ACTIONS i it l The cause of the occurrence is attributed to the failure 'f operations l
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personnel to recognize that the torus water temperature was nearinc the i
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Tne water temperature was reduced by operating the contain-l 3 ;3 I
ment spray system.
Procedure changes will be made to insure that this I
system is operated as recuired to keep the temperature below the limit.
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,$$g g "@lOESC RirTION Veekly press release - January 9, 1979 l lltl1lll l t j i [f y
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112016 201-455-8764 e
Donald A. Ross 8"ONE.
,g NAVEOrpAEpApEp
Reportable Occurrence No. 50-219/78-35/IT-0 Page 2 January 5, 1979 Analysis of Occurrence The suppression pool water temperature limits were established to reduce the affects of the steam quenching vibration phenomenon which may occur at elevated suppression pool water temperature during a loss-of-coolant accident.
The requirement for reactor scram for suppression pool water temperature in excess of 110*F. was developed to prevent exceeding 160*F.
during relief valve operation.
The 95'F. limit for power operation is intended to provide a 10*F. allowance for testing which adds heat to the suppression pool and still provide a 5'F. margin below the scram requirement.
Since the suppression pool water temperature did not exceed the IIO*F.
limit during this incident, there appears to be minimal safety significance.
Additionally, the time the suppression pool temperature exceeded the 95'F.
limit was minimal.
Corrective Action
The torus water temperature was reduced to less than 95'F. by operation of the containment spray system.
The appropriate procedure changes will be made to insure that the containment spray system is operated as required to maintain torus water temperature to less than 90*F.
The PORC recognizes that there is an increasing frequency of administrative related problems and will formally address these problems in the near future.
Failure Data None.
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| 05000219/LER-1978-001-03, /03L-0:on 780103,during Operability Test,Emergency Diesel Generator 1 Trouble Alarm Received & Unit Tripped. Caused by Temp Switch Being Erratic Re Setpoint.Switch Replaced.Louver Control Mod Being Installed | /03L-0:on 780103,during Operability Test,Emergency Diesel Generator 1 Trouble Alarm Received & Unit Tripped. Caused by Temp Switch Being Erratic Re Setpoint.Switch Replaced.Louver Control Mod Being Installed | | | 05000219/LER-1978-017-03, /03L-0:on 780914,circuit Breaker for motor- Operated Valve Tripped When Valve Closed by Isolation Signal.Caused by Component Failure Allowing Switch Setting to Shift.Setting Corrected & Set Screw Tightened | /03L-0:on 780914,circuit Breaker for motor- Operated Valve Tripped When Valve Closed by Isolation Signal.Caused by Component Failure Allowing Switch Setting to Shift.Setting Corrected & Set Screw Tightened | | | 05000219/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000219/LER-1978-018-01, /01T-0 on 780916:3 MSIVs(NS03A,NS04A,NS04B) Had Leakage Rates in Excess of Maximum Allowable Due to Stem Packing,Cracked Stellite Weld & Failure of Main Poppet to Seat Properly.Msiv Failures Being Investigated | /01T-0 on 780916:3 MSIVs(NS03A,NS04A,NS04B) Had Leakage Rates in Excess of Maximum Allowable Due to Stem Packing,Cracked 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/01T-0 on 781010:while Performing Inservice Insp, Discovered Through Wall Crack on Sparger Pipe.Caused by Methods Used to Install Sparger Pipe.Corrective Action Will Be Determined After Full Investigation | | | 05000219/LER-1978-022-03, /03L-0 on 781017:during Routine Surveillance Test of Standby Gas Treatment Sys,The Sys II Discharge Valve Failed to Open,Due to Stuck Solenoid in Control Air Supply to Operator for V-28-30 | /03L-0 on 781017:during Routine Surveillance Test of Standby Gas Treatment Sys,The Sys II Discharge Valve Failed to Open,Due to Stuck Solenoid in Control Air Supply to Operator for V-28-30 | | | 05000219/LER-1978-023, Forwards LER 78-023/03L-0 | Forwards LER 78-023/03L-0 | | | 05000219/LER-1978-023-03, /03L-0 on 781019:IRM 12 Became Inoperative While Cable to IRM 14 Was Disconnected.Irm 12 Failure Attributed to Maint Activities Under Vessel.Subesquent Inspec Showed IRM 12 Cable Damaged | /03L-0 on 781019:IRM 12 Became Inoperative While Cable to IRM 14 Was Disconnected.Irm 12 Failure Attributed to Maint Activities Under Vessel.Subesquent Inspec Showed IRM 12 Cable Damaged | | | 05000219/LER-1978-024-03, /03L-0 on 781018:isolation Valve V-7-31 Had Damaged Rubber Seat & Drain Valve V-7-29 Obstructed by Piece of Cork & Filter F-1-58 Medium Disintegrated.Cause of V-7-31 & F-7-58 Degradations Due to Detonations in Sys | /03L-0 on 781018:isolation Valve V-7-31 Had Damaged Rubber Seat & Drain Valve V-7-29 Obstructed by Piece of Cork & Filter F-1-58 Medium Disintegrated.Cause of V-7-31 & F-7-58 Degradations Due to Detonations in Sys | | | 05000219/LER-1978-024, Forwards LER 78-024/03L-0 | Forwards LER 78-024/03L-0 | | | 05000219/LER-1978-025-03, /03L-0 on 781031:condensate Storage Tank Was Leaking Due to Galvanic Corrosion.Leak & Other Weak Spots Were Patch Welded | /03L-0 on 781031:condensate Storage Tank Was Leaking Due to Galvanic Corrosion.Leak & Other Weak Spots Were Patch Welded | | | 05000219/LER-1978-025, Forwards LER 78-025/03L-0 | Forwards LER 78-025/03L-0 | | | 05000219/LER-1978-026, Forwards LER 78-026/01T-0 | Forwards LER 78-026/01T-0 | | | 05000219/LER-1978-026-01, /01T-0:on 781121 torus-to-reactor Bldg Differential Pressure Switches DPS-66A & B Had Ruptured Diaphragms.Caused by Excessive Differential Pressure | /01T-0:on 781121 torus-to-reactor Bldg Differential Pressure Switches DPS-66A & B Had Ruptured Diaphragms.Caused by Excessive Differential Pressure | | | 05000219/LER-1978-027, Forwards LER 78-027/03L-0 | Forwards LER 78-027/03L-0 | | | 05000219/LER-1978-027-03, /03L-0 on 781125:switch RE03C Was Found to Trip at Pressure Less conservative(1075 Psig)Than Specified in Tech Specs 2.3.3.Cause of Pressure Switch Tripping Is Attributed to Sensor Repeatability | /03L-0 on 781125:switch RE03C Was Found to Trip at Pressure Less conservative(1075 Psig)Than Specified in Tech Specs 2.3.3.Cause of Pressure Switch Tripping Is Attributed to Sensor Repeatability | | | 05000219/LER-1978-028, Forwards LER 78-028/01T-0 | Forwards LER 78-028/01T-0 | | | 05000219/LER-1978-028-01, /01T-0 on 781129:during Test,Main Steam Line Drain Valve V-1-106 Did Not Close 2 Incore Probes,Did Not Fully W/Draw & Reactor Coolant Valve Did Not Indicate Closed.Due to Jammed Armature,Faulty Fuse Holder & Incorrect Settin | /01T-0 on 781129:during Test,Main Steam Line Drain Valve V-1-106 Did Not Close 2 Incore Probes,Did Not Fully W/Draw & Reactor Coolant Valve Did Not Indicate Closed.Due to Jammed Armature,Faulty Fuse Holder & Incorrect Settings | | | 05000219/LER-1978-029-01, /01T-0 on 781129:during Test,Noted That Containment Leakage Rate Greater than Allowable.Discovered That Vent Valves Were Leaking.Caused by Leakage Past the Seating Surfaces | /01T-0 on 781129:during Test,Noted That Containment Leakage Rate Greater than Allowable.Discovered That Vent Valves Were Leaking.Caused by Leakage Past the Seating Surfaces | | | 05000219/LER-1978-029, Forwards LER 78-029/01T-0 | Forwards LER 78-029/01T-0 | | | 05000219/LER-1978-030, Forwards LER 78-030/03L-0 | Forwards LER 78-030/03L-0 | | | 05000219/LER-1978-030-03, /03L-0 on 781126:during Testing Containment Spray Pumps 51C & 51A Failed to Start on Signal Due to Excess Friction in Circuit Breaker Trip Bar Bearings.Bearings Were Cleaned & Lubricated | /03L-0 on 781126:during Testing Containment Spray Pumps 51C & 51A Failed to Start on Signal Due to Excess Friction in Circuit Breaker Trip Bar Bearings.Bearings Were Cleaned & Lubricated | | | 05000219/LER-1978-031, Forwards LER 78-031/03L-0 | Forwards LER 78-031/03L-0 | | | 05000219/LER-1978-031-03, /03L-0 on 781130:during Diesel Generator Automatic Actuation Test,Generator Failed to Excite Due to Unused Target Mechanical Linkage Binding.Svc Water Pumps 1 & 2 Did Not Start Due to Binding in Trip Mechanism | /03L-0 on 781130:during Diesel Generator Automatic Actuation Test,Generator Failed to Excite Due to Unused Target Mechanical Linkage Binding.Svc Water Pumps 1 & 2 Did Not Start Due to Binding in Trip Mechanism | | | 05000219/LER-1978-032-03, /03L-0 on 781204:during Refueling Operations & Containment Spray Sys 1 Automatic Actuation Test,Valve V-21-78 Failed to Open.Caused by Valve Motor Breaker Not Racked Properly & Overload in Trip Position | /03L-0 on 781204:during Refueling Operations & Containment Spray Sys 1 Automatic Actuation Test,Valve V-21-78 Failed to Open.Caused by Valve Motor Breaker Not Racked Properly & Overload in Trip Position | | | 05000219/LER-1978-032, Forwards LER 78-032/03L-0 | Forwards LER 78-032/03L-0 | | | 05000219/LER-1978-033-01, /01T-2 on 781214:reactor Scram Occurred in Range 1 of Intermediate Range Monitors Due to Failure of Emergency Rod in Control Switch.Caused by Bent Switch Stop.Stop Plate Replaced | /01T-2 on 781214:reactor Scram Occurred in Range 1 of Intermediate Range Monitors Due to Failure of Emergency Rod in Control Switch.Caused by Bent Switch Stop.Stop Plate Replaced | | | 05000219/LER-1978-033, Forwards LER 78-033/01T-2 | Forwards LER 78-033/01T-2 | | | 05000219/LER-1978-034-03, /03L-0 781213:both Diesel Generator & Station Batteries Were Not Tested & Monitored within Specified Time Interval.Caused by Failure to Adhere to Surveillance Schedule | /03L-0 781213:both Diesel Generator & Station Batteries Were Not Tested & Monitored within Specified Time Interval.Caused by Failure to Adhere to Surveillance Schedule | | | 05000219/LER-1978-034, Forwards LER 78-034/03L-0 | Forwards LER 78-034/03L-0 | | | 05000219/LER-1978-035-01, /01T-0 on 781227:torus Water Temp in Excess of Tech Specs.Caused by Failure of Operations Personnel to Recognize Torus Water Temp Nearing Tech Spec Limit | /01T-0 on 781227:torus Water Temp in Excess of Tech Specs.Caused by Failure of Operations Personnel to Recognize Torus Water Temp Nearing Tech Spec Limit | | | 05000219/LER-1978-035, Forwards LER 78-035/01T-0 | Forwards LER 78-035/01T-0 | | | 05000219/LER-1978-036-03, /03L-0 on 781212:during Routine Tests,Standby Gas Treatment Sys II Discharge Valve V-28-30 Failed to Close. Caused by Buildup of Dirt & Corrosion in Piston Cylinder of Valve Operator | /03L-0 on 781212:during Routine Tests,Standby Gas Treatment Sys II Discharge Valve V-28-30 Failed to Close. Caused by Buildup of Dirt & Corrosion in Piston Cylinder of Valve Operator | | | 05000219/LER-1978-036, Forwards LER 78-036/03L-0 | Forwards LER 78-036/03L-0 | |
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