05000324/LER-1979-104-03, /03L-0:on 791226,while Performing Main Steam Line High Radiation Functional Check,Drawer 2-D12-K603D Found Out of Calibr.Caused by Instrument Drift.Drawer Recalibr & Returned to Svc

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/03L-0:on 791226,while Performing Main Steam Line High Radiation Functional Check,Drawer 2-D12-K603D Found Out of Calibr.Caused by Instrument Drift.Drawer Recalibr & Returned to Svc
ML19257C653
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/18/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19257C650 List:
References
LER-79-104-03L-01, LER-79-104-3L-1, NUDOCS 8001290550
Download: ML19257C653 (1)


LER-1979-104, /03L-0:on 791226,while Performing Main Steam Line High Radiation Functional Check,Drawer 2-D12-K603D Found Out of Calibr.Caused by Instrument Drift.Drawer Recalibr & Returned to Svc
Event date:
Report date:
3241979104R03 - NRC Website

text

NltC F ORM 364 U. S. NUCLE AH HEGUL ATOHY COf.1 MISSION (7 77)

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HE POf tT D ATE 40 E'/ENT DESCRIPTION AND PROH AdLE CON'd v;E'.CE. h k'h i l e performing PT 1.1.12PC, Main Steam Line liigh Radiat ion Func tional Check,_

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Drawer 2-D12-K603D was found out of calibration.

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C AUSE DESC AiPTICN AND CO ::ECTivE ACTIONS I,

The drawer was recalibrated and returned to se vice.

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the 1980 refueling outage to help determine the cause of this problem. A new drawer.

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