ML19256F351

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LER 79-038/01T-0:on 791120,during Review of Surveillance Test,Two MSIVs in a Steamline Closed in Times Shorter than Specified in Tech Specs.Caused by Operator Not Recognizing Fast MSIV Closure Time.Operator Procedure Revised
ML19256F351
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 12/06/1979
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19256F347 List:
References
LER-79-038-01T, LER-79-38-1T, NUDOCS 7912180591
Download: ML19256F351 (1)


Text

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