05000277/LER-1979-045-03, /03L-0:on 790924,E-2 Diesel Tripped,Causing Half Scram & Half Isolation.Caused by Erroneous Shutdown of Emergency Svc Water Sys & Subsequent Rise in Lube Oil Temp in Generator.Control Switch Tagged

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/03L-0:on 790924,E-2 Diesel Tripped,Causing Half Scram & Half Isolation.Caused by Erroneous Shutdown of Emergency Svc Water Sys & Subsequent Rise in Lube Oil Temp in Generator.Control Switch Tagged
ML19254E541
Person / Time
Site: Peach Bottom 
Issue date: 10/24/1979
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19254E537 List:
References
LER-79-045-03L, LER-79-45-3L, NUDOCS 7911010449
Download: ML19254E541 (1)


LER-1979-045, /03L-0:on 790924,E-2 Diesel Tripped,Causing Half Scram & Half Isolation.Caused by Erroneous Shutdown of Emergency Svc Water Sys & Subsequent Rise in Lube Oil Temp in Generator.Control Switch Tagged
Event date:
Report date:
2771979045R03 - NRC Website

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