ML19253C387
| ML19253C387 | |
| Person / Time | |
|---|---|
| Site: | Sterling |
| Issue date: | 11/16/1979 |
| From: | Grier B NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Arthur J ROCHESTER GAS & ELECTRIC CORP. |
| References | |
| NUDOCS 7912050306 | |
| Download: ML19253C387 (1) | |
Text
N 7g ya nuco UNITED STATES
,o,j NUCLEAR REGULATORY COMMISSION y *)
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,e KING OF PRUSSIA, PENNSYLVANIA 19406 NOV 1 g 7973 Docket No. 50-485 Rochester Gas & Electric Corporation ATTN:
Mr. J. E. Arthur Chief Engineer 89 East Avenue Rochester, New York 14649 Gentlemen:
The enclosed IE information Notice No. 79-27 provides information with regard to the sequence cf events that followed incidents involving steam generator tube reptures at two PWR units.
If you have any questions regarding this matter, please contact this office.
Sincerely, n
f;_CW4Yl.
kb;-
f v Boyce H. Grier f--d. Director
/
Enclosures:
1.
IE Information Notice No. 79-27 2.
List of Recently Issued Information Notices CONTACT:
W. H. Baunack (215-337-5334) cc w/encls:
C. R. Anderson, Manager, QA Lex K. Larson, Esquire N. A. Petrick, Executive Director, SNUPPS Gerald Charnoff, Esquire 1503 359 o so 3c) 6 yom G) i
ENCLOSURE 1 SSINS No.:
6870 Accession No.:
7910250488 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON D.C.
20555 IE Information Notice No. 79-27 Date:
November 16, 1979 Page 1 of 9 STEAM GENERATOR TUBE RUPTURES AT TWO PWR PLANTS Description of Circumstances:
In recent months two incidents involving steam generator tube ruptures have occurred.
In both instances, the units were cooled down and placed in the residual heat removal mode with existing procedures.
Event of June 25, 1979 at the Doel 2 Nuclear Power Plant in Belgium The first event occurred on June 25, 1979, at the Doel 2 nuclear power plant in Belgium.
The Doel unit is a 390 Mwe Westinghouse two-loop reactor.
The event consisted of a rupture of several tubes in the loop B steam generator.
The resultant leakage between the primary ar.d secondary systems was estimated to be 125 gpm.
The event started when the plant was heated up after a shutdown caused by a malfunction of the main steam isolation valve.
At the time of the incident the primary coolant pressure was:
2233 psi and the temperature:
491 F.
The reactor remained subcritical throughout the event.
The first indication of abnormal behavior was a rapid decrease of the primary system pressyre (approximately:
28 psi / min.).
This was followed by the sequence of events listed below:
Time, min.
1.
Increase of charging flow demar.d, requiring startup of a second 1.8 charging pump.
2.
Automatic isolation of the CVCS letdown line.
2.4 3.
Shut off of the pressurizer heaters due to low liquid level in the 2.4 pressurizer.
1503 560 DUPLICATE DOCUMENT Entire document previously entered into system under:
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