ML19249E823
| ML19249E823 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 09/13/1979 |
| From: | Grier B NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Woolever E DUQUESNE LIGHT CO. |
| References | |
| NUDOCS 7910020519 | |
| Download: ML19249E823 (1) | |
Text
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,o UNITED STATES y y 'ss(/( g NUCLEAR REGULATORY COMMISSION g
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Docket No. 50-412 SEP 1 3 m Duquesne Light Company ATTN:
Mr. E. J. Woolever Vice President 435 Sixth Avenue Pittsburgh, PA 15219 Gentlemen:
The enclosed IE Circular No. 79-19, is forwarded to you for information.
No written response is required.
Should you have any questions related to your understanding of this matter, please contact this office.
Sincerely,
/ bW,
/,z oyce H. Grier Director
Enclosures:
1.
IE Circular No. 79-19 2.
List of IE Circulars Issued in the Last Six Months cc w/encls:
R. J. Washabaugh, Quality Assurance Manager 1072 116 7910020
ENCLOSURE 1 SSINS:
6830 Accession No: 7908220111 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D. C.
20555 IE Circular No. 79-19 Date:
September 13, 1979 Page 1 of 2 LOOSE LOCKING DEVICES Gh INGERSOLL-RAND PUMP IMPELLERS Description of Circumstances:
Three reports have been submitted to the NRC regarding the loosening of locking devices on the impellers of pumps manufactured by the Ingersoll-Rand Company.
The first report was submitted as a significant deficiency (10 CFR 50.55[e])
by Arkansas Power and Light Company in letters of March 17, 1978 and May 9, 1978.
The licensee reported excessive noise and vibrations in both Low Pressure Safety Injection (LPSI) pumps during the preoperational test program on Unit 2 of Arkansas Nuclear One (AN0).
It was discovered that the washers, jam nut and cap nut used to retain the impellers were missing on both pumps (Ingersoll-Rand Type 8X20WD).
The licensee's corrective action involved the installation of a tab washer.
This corrective action was also taken on the containment spray pumps (Ingersoll-Rand Type 6X23WD) because of similarity of design.
The second report was submitted by Duke Pcwer Company in a licensee event report (LER 50-287/78-23) dated January 24, 1979.
The symptoms were similar to those observed at ANO Unit 2 in that high vibration was detected in a reactor building spray pump (Ingersoll-Rand Type 4X11A) for Oconee Unit No. 3.
The licensee found that the impeller had worked loose.
The corrective action included a revision to the mainteinance procedure to specify torque requirements.
The third report was 10 CFR 21 Report No. 79-01 submitted by Portland General Electric Co. on April 16, 1979.
This report identified a deficiency that may exist in the Trojan Nuclear Plant containment spray pumps (Ingersoll-Rand T/pe 6X23WD) in that there is a potential for the impeller lock nut tn loosen.
The potential deficiency was identified because of the similar;ty of the ccatainment spray pumps design to the residual heat removal (RHR) pumps (Ingersoll-Rand
^/pe 8X20WD) and the discovery of a loose lock nut on an RHR pump during pump intenance. The corrective action was to provide a positive mechanical lock c; the impeller nut.
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Westinghouse Nuclear Service Division I"
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Westinghouse plant owners on loose loc DUPLICATE DOCUMENT and WDF pumps.
Excerpts from that Tec Combustion Engineering, Inc. has also Entire document previously entered to the same problem in a letter dated into system under:
letter are in Attachment No. 2.
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