ML19241C245

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Discusses Actions Taken in Response to NRC 790507 Shutdown Order.Licensee Has Complied W/Requirements Specified in Order
ML19241C245
Person / Time
Site: Rancho Seco
Issue date: 06/18/1979
From: Crews J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Moseley N
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
Shared Package
ML19241C242 List:
References
FOIA-79-98 NUDOCS 7907300450
Download: ML19241C245 (2)


Text

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MaiORANDUM FOR:

N. C. Moseley, Director, Division of Reactor Operations Inspection, IE:HQ FROM:

J. L. Crews, Chief, Reactor Operations and fluclear Support Branch, Region V SU3 JECT:

COMMISSION ORDER 7590-01 DATED MAY 7,1979 SACRMENTO l'UNICIPAL UTILITY DISTRICT RANCHO SEC0 NUCLEAR POWER PLANT (DOCKET NO. 50-312)

The sub.iect Co=11ssion Order required certain actions to be completed by the licensee prior to startup of the Rancho Seco Nuclear Power Plant. This fa:ility was shutdown on April 28, 1979.

Region V inspection activities, subsequent to the facility shutdown, have confirmed as indicated below that the licensee has complied with requirements specified in the Comission Order. These inspection activities also confimed the accuracy of the information contained in the licensee's letters to the NRC dated April 11, April 16, April 19, April 22, May 2, May 11, May 14, and May 21, 1979. These letters are responses to IEB 79-05A and IEB 79-053.

The specific inspection activities performed by Region V for purposes of confirming licensee compliance with the Co=1ission Order included the following:

1.

Verification of the installation and testing of hard-wiring control-grade reactor trips that are actuated by loss of both main feedwater pumps or an autcmatic turbine trip.

2.

A review of the revised procedures for responding to small reactor coolant system breaks and for initiating and controlling auxiliary feedwater independent of the Integrated Control System. Comments on these procedures were provided to the NRR B&W task force.

3.

Verification that an evaluation of transient behavior and small reactor coolant system breaks was prepared and submitted to flRR for their review and evaluation.

4.

Verification that a sufficient nuner of plant operators have been trained at the B&W simulator, on the TMI incident, to assign at lee.st one such operator to the control room and two such operators on each work shift.

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N. C. f'oseley DUN 18 679 5.

Verification that Auxiliary Feedwater System (AFS) flow indicators were installed, calibrated, and successfully tested to demonstate flow indication in the control room of AFS flow to each steam generator.

6.

Verification that licensed operators are knowledgeable of facility modifications, procedure changes, and system and equipment operation requirements resulting from the TMI incident. This verification was obtained oy conducting oral interviews with plant operators on June 1-2, 1979 and again on June 17-18, 1979, after additional training was provided by a licensee contractor. Written operator examinations given by the licensee were also reviewed.

A representative of the Operator Licensing Branch of NRR assisted with the operator interviews on June 1-2 and with review of the written examinations.

7.

Verification that facility operating procedures were revised and/or developed to address the applicable items identified in Enclosure (1) of the licensee's letter to H. R. Denton, dated April 27, 1979. The NRR B&W task force reviewed and evaluated these procedures and procedure revisions for acceptability.

8.

Verification that tests were performed to assure AFS air-operated control valves fail to the 50% open position upon loss of electrical power to the electric-to-pneumatic converter and fail to the 100% open position upon loss of air.

9.

Verification that a test was conducted to assure AFS flow capacity is in accordance with Technical Specification requirements.

10.

Verification that necessary modifications have been satisfactorily completed to provide annunciation in the control room of all auto start conditions of the Auxiliary Feedwater System.

With regard to Item 2 above, it is our understanding that discussions are continuing between NRR and the licensee regarding the use of high pressure injection as it relates to the temperature-pressure limits contained within the Technical Specifications.

(Y?0W rews, Chief Reaitor Operations and Nuclear Support Branch cc:

E. L. Jordan, IE:HQ 5782.77

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