ML19225A099

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IE Insp Repts 50-295/79-08 & 50-304/79-09 on 790406,10,11 & 23-27.Noncompliance Noted:Tech Specs for Unit 1 Violated When Cross Tie Breaker from Unit 2 Auxiliary Transformer Was Taken Out of Svc
ML19225A099
Person / Time
Site: Zion  File:ZionSolutions icon.png
Issue date: 05/14/1979
From: Boyd D, Kohler J, Spessard R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19225A087 List:
References
50-295-79-08, 50-295-79-8, 50-304-79-09, 50-304-79-9, NUDOCS 7907180323
Download: ML19225A099 (4)


See also: IR 05000295/1979008

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U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

REGION III

Report No. 50-295/79-08; 50-304/79-09

Docket No. 50-295; 50-304

License No. DPR-39; DPR-48

Licensee:

Commonwealth Edison Company

Post Office Box 767

Chicago, IL 60690

Facility Name:

Zion Nuclear Fower Station, Units 1 and 2

Inspection At:

Zion Site, Zion IL

Inspection Conducted: April 6, 10, 11 and 23-27, 1979

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Inspectors:

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Approved By:

R. L. Spbssard, Chief

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Reactor Projects Section 1

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Inspection Summary

Inspection on April 6,10,11 and 23-27, 1979 (Report No.

50-295/79-08; 50-304/79-09)

Areas Inspected:

Three Mile Island event training, Unit I reactor

startup, plant operations, compliance with IE Bulletin to trip

pressurizer level channels, and licensee event reports.

The inspec-

tion consisted of 71 inspector-hours onsite by two NRC inspectors.

Results: One item of noncompliance (infraction - violation of a

limiting condition for operation

paragraph 7) was identified.

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DETAILS

1.

Persons Contacted

N. Wandke, Plant Superintendent

C. Schumann, Operating Assistant Superintendent

E. Fuerst, Operating Engineer, Unit 1

B. Ward, Operating Engineer, Unit 2

C. Schultz, Training Supervisor

J. Harbin, Shift Engineer

J. Flowers, Shift Engineer

N. Valos, Shift Foreman

L. Soth, Assistant Superintendent, Administrative and Support

J. Johnson, Lead Operator

2.

Three Mile Island Training

The inspector audited a training courre offered to station

personnel regarding the events which took place at Three Mile

Island. The TMI training courses reflect the requirement in IE

Bulletin 79-06 that licensee management brief its personnel as

completely as possible on the TMI incident.

The inspector has

no further questions regarding this item.

3.

Unit 1 Reactor Startup

On April 27, 1979, the inspector reviewed the Unit I startup

associated with the Unit I reactor trip caused by steam gener-

ator low low level on April 26, 1979. The startup was orderly

and procedures were followed.

At about a power level of 150 MWe into the startup while trans-

itioning f om the feedwater bypass valve to the main feed

regulating ;alve, the reactor tripped on low low steam generator

level.

The cause of the trip was traced to a failed solenoid

in the feedwatt reg valve.

The soletoid failure inhibited the

regulat ing valve fi am opening and starved the steam generator.

The soleno)d in both Unit 1 feedwater reg valves was changed

out, and a reactor startup took place shortly thereafter.

D'u.ng the review of the Unit I reactor trip on April 26, 1979,

one electric auxiliary feed pump failed to start.

Tbn two

redundant pumps func'ioned properly.

Caure of the pump start

failure was traced to the pressure switch in the lube oil pump

which had drifted high.

These pressure switches were being

calibrated under a Work Request issued on April 26, 1979.

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The inspector has no further questions regarding the Unit 1

startup after the reactor trip of April 26, 1979.

4.

Plant Tour,

The inspector toured the turbine building, the auxiliary

building, and the control room with a D-operator who was making

normal rounds.

The tour was routine and no concerns resulted.

5.

Pressurizer Level Trips

Based on requirements in IE Bulletin 79-06A, the inspector

verified that the low pressurizer level trip bistables which

act in coincidence with low pressurizer pressure to cause a

safety injection were placed in the trip condition for both

Units 1 and 2.

6.

Review of Plant Operations

The inspector spent time in the control room and reviewed the

tagging out log, the shift logs, and the surveillance required

to be parf- ied due to limiting conditions for operation (LCO).

The inspector found that the required surveillance was being

performed for LCO's and has no further questions in this area.

7.

Review of Licensee Event Report (50-295/79-16)

The licensee notified RIII on March 12, 1979, that Technical Specification 3.15.2.c for Unit 1 was violated when the cross

tie breaker from Unit 2 system auxiliary transformer to Unit 1

essential service feature bus was taken out of service coinci-

dentally with the IB diesel generator out of service.

The

inspector reviewed the event associated with taking the cross

tie breaker out of service. The cause of event was classified

as personnnl error.

Corrective action cor.sisted of shift

reinstruction as well as the procedure change in periodic test

14.

This item is considered an item of noncompliance against Tech-

nical Specification 3.15.2.c and is classified as an infraction.

During the management exit, the inspector stated that the cross

tie breaker noncompliance was the second this year in the

auxiliary electrical area.

The first noncompliance was docu-

mented in RIII Inspection Report 50-295/79-01.

There was.

agreement that additional licensee action must be taken to

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insure that Technical Specification 3.15 is not violated.

Consequently, the licensee will be requested to submit, as an

additional response to this item, plans to augment surveillance

in the auxiliary electrical area with particular attention to

insuring that all essential service features buses are aligned

to their proper power sources.

8.

Management Exit

A management exit was held on April 27, 1979 in which the

following items were discussed:

a.

Unit 1 reactor trip due to the feedwater transient.

b.

Unit 1, Unit 2 compliance with tripping pressurizer level

channels and safety injection logic.

Licensee deficiency in the auxiliary electrical area, and

c.

the noncompliance associated with Technical Specification 3.15.

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