ML19224D828

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LER 79-015/03L-0 on 790610:leak Identified in RCS & Traced to Isolation Valve.Cause Unknown.Isolation Valve Repaired & power-operated Relief Valve Declared Operable
ML19224D828
Person / Time
Site: Millstone Dominion icon.png
Issue date: 07/09/1979
From:
NORTHEAST UTILITIES
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19224D824 List:
References
LER-79-015-03L-01, LER-79-15-3L-1, NUDOCS 7907170092
Download: ML19224D828 (1)


Text

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  1. 3 CJ L1 U DC t, E T f;U'.' _ , H tvenT oEScHmllON AND PhOa AM CONSf uuCNCLS @

O 2 During steady state power operation, a leak of unknown origin in the Reactor _i

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Coolant Systeu in excess of 1 Gril was identified in containment. The plant was l

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plcted in cold shutdown in accordance with the Action Statement of Technical F5TC) 1 Specificction 3.4.6.2 and the leak traced to an isoletion valve, 2-RC-405, for one j

[Tpq l of two po'.;er operated pressurizer relief valves. As a result the power operate ' ]

gl relief valve, 2-RC-404, was declared inoperable in accordance with Technicul Speci- l griq L fication 3.4.9.3.G. The isolation valve, 2-RC-405, was then repaired. l CAUS C O Y P. VAlVF SYSTE'A CAU5L SU0 CODE SueCocE COCL CODE .UacoDF COYr0*.LN1 COD 1019t: I C ] B l@ [E]@ l B j @ [V l A l L l V l E l X j@ lE @ [D _

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[V 44 0 l8 lS l@ 4p CAUSE DESCHWHON AND COHHECTIVE ACTIONS h i o l The valve leakage issued frerL th e body to bonnet seal. The valve,2-RC /0S, is a [

ggl 21/2 inch pressure seal gate valve with a notor operator, rated at 2500 PSI, ASME [

Ill, Class 1, SA-182 stainless steel. The valve gasket end spacer ring were replaced; g , ; ;,g i and the valveput igck into service. The power operated relief valve was then also j

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i i j g, j ] declared operable, 7 8 9 , P.'E T HOD OF F /+ Cit iTY OTHF R ST AT US DitCOV 5. H Y DISCOVUtY DESCHIPTION 32

$TATUS %FOWEH

[A,j@l Leakacie Calculated l

[_i_lij I F l@ l O l 91 5 @l NA l Atie v !Y CO IlNT LOCATION 0F HELE ASE Ftl LE ASE D OF Hlli > J A'.900N T OF ACTIVITY HA l liIcl Z l @ Llj@l NA I I _

FEf tSON*1E t f XPC (E S NUYa C Ft TYPE DE SChiP flON NA l i i l 0 l 0 l 0 l@l z l@l 00 Pt n%ONNE L IN JU IES b uY Lii H O L SCH tP f lON l

7 i a 8 9 l0l0 0l@] 11 12 UA LOis or 04 U A*.' AGE T O F ACill T Y -

TYPE DL5CalP r ION NA m 0 %r 7907170 l li l H UI I U !@lto C' CO 1

12iol 15SUt HIPilON Yl r@I Ll press telea y _1100. .lun, 10. 1071 1 o ce IIIIIIIIIIII}{^ u.-

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