LER-1979-020, /01T-0 on 790621:radioactive Release Rate at Main Stack During Plant Startup Exceeded Tech Specs.Caused by Deficiency in Procedure for Depressurization Following Shutdown.Investigation Underway to Improve Procedure |
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text
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Mr. Boyce H.
Grier Page 2 July 6,
1979 LER 3-79-20/Ir shutdown immediately.
Main stack release, however, continued to increase due to transport time between the vacuum pump and the main stack.
This release continued over approxinately 50 minutes.
The maximum release rate was 106 % of Technical Specification limits.
Technical Specification release limits were exceeded for less than 10 minutes during this transient.
Simultaneoualy with this release, the two reactor building roof vents were releasing at a.value of 11 % of Technical Specification limits.
The maximum site gaseous release rate was therefore approximately 117 % of the Technical Specification limit.
Approximately 1000 Ci of m
,od noble gases were released during this event.
Consequences of Event:
Analysis of the roof vent iodine and particulate samples indicated no significant increase in the iodine or particulate release rates during the period of high gaseous activity releases.
Analysis of the main stack effluent, sampled 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> later when the startup vacuum pump was placed back in service, indicated that the majority of the activity was XE-133 and XE-135 (long lived noble gases).
The release was terminated as soon as the increase in radiation levels on the off-gas stack radiation monitor was observed.
For these reasons, no environmental impact is anticipated.
Plant personnel received no radiation exposure as a result of this event.
Cause of Event
Depressurization of the p rima ry coolant system following reactor shutdcwn introduced non-condensible fission product gases into the condenser.
Transfer of this inventory to the main stack in accordance with normal startup procedures resulted in a gaseous release rate in excess of Technical Specification linits.
The appropriate procedures were deficient in that they did not adequately address the special case of significant fission product inventory in the main condenser with respect to operation of the startup vacuum pump.
Corrective Action
When the increase in the radiation monitor reac ~ ng was noticed, the startup vacuum pump was tripped to terminate the rele se.
Following the initial high release rate, air was pulled through the condenser to provide dilution flow to the vacuum pump during the evacuation of the condenser air space.
This eventually get.dtted establishing a condenser vacuum sufficient to permit return of the unit to service.
No additional releases scc JJ L')
s 79071267
Mr. Boyce 11. Grier Page 3 July 6,
1973 LER 3-79-20/IT in excess of T'chnical Specification limits occurred during the condenser evacuation operation.
An investigation of tnis occurrence is being performed by the Electric Production Department and the Mechanical Engince-ing Division to determine acceptable procedural or equipment modifications to prevent a recurrence.
Yours truly,
/
/ f cf.
Cooney St erintende t Generation Division-Nucle Attachment ec:
Director, NRC - Office cf Inspection and Enforcement Mr. Norman M.
Haller, NRC - Office of Management &
Program Analysis 9
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During plant startup, the radioactive release rate at the in stack I
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pump.
The release rate exceeded Tech Spec li=its for less than 10 lo s I cinutes. The cannum releaca rate was 106% of Tech Spec limits. The off-
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o l Reactor depressurization introd2ced fission gas into condenser. This ans j
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| 05000277/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000277/LER-1979-001-01, /01T-0 on 790104:design Errors in Cable Designations Were Identified.Ten Cables Found to Be Designated Nonsafeguard.Caused by Improper Designation of Cables During Design Phase.New Cable Routing Completed | /01T-0 on 790104:design Errors in Cable Designations Were Identified.Ten Cables Found to Be Designated Nonsafeguard.Caused by Improper Designation of Cables During Design Phase.New Cable Routing Completed | | | 05000278/LER-1979-001-03, /03L-0 on 790111:discovered That Recorded hi-hi Trip Valve for Steam Line Radiation Monitor Was 50 man-rem/h Greater than Tech Spec Limit & No Corrective Action Taken. Caused by Procedural Deficiency | /03L-0 on 790111:discovered That Recorded hi-hi Trip Valve for Steam Line Radiation Monitor Was 50 man-rem/h Greater than Tech Spec Limit & No Corrective Action Taken. Caused by Procedural Deficiency | | | 05000277/LER-1979-002-01, /01T-0 on 790108:cable Spreading Room Cardox Sys Disabled W/O Firewatch Present.Absence Due to Failure of Personnel to Notify Shift Supervisor Upon Work Completion | /01T-0 on 790108:cable Spreading Room Cardox Sys Disabled W/O Firewatch Present.Absence Due to Failure of Personnel to Notify Shift Supervisor Upon Work Completion | | | 05000277/LER-1979-002, Forwards LER 79-002/01T-0 | Forwards LER 79-002/01T-0 | | | 05000278/LER-1979-002-01, /01T-0 on 790108:roof Vent Stack Instantaneous Gas Release Rate Above Tech Spec Limit Due to Valve Operator Failure,Causing Loss of Inservice RHR Loop,Rise in Coolant Temp & Gaseous Release Via Core Isolation Cooling Valves | /01T-0 on 790108:roof Vent Stack Instantaneous Gas Release Rate Above Tech Spec Limit Due to Valve Operator Failure,Causing Loss of Inservice RHR Loop,Rise in Coolant Temp & Gaseous Release Via Core Isolation Cooling Valves | | | 05000278/LER-1979-002, Forwards LER 79-002/01T-0 | Forwards LER 79-002/01T-0 | | | 05000277/LER-1979-003-03, /03L-0 on 790109:2A Offgas Radiation Monitor Failed Downscale.Dirt on Contacts of Trip Test/Zero Calibr Switch Caused Input Key to Remain Deenergized Upon Release of Switch.Contacts Were Cleaned & Monitor Returned to Svc | /03L-0 on 790109:2A Offgas Radiation Monitor Failed Downscale.Dirt on Contacts of Trip Test/Zero Calibr Switch Caused Input Key to Remain Deenergized Upon Release of Switch.Contacts Were Cleaned & Monitor Returned to Svc | | | 05000278/LER-1979-003-03, /03L-0 on 790111:during Unit Shutdown for Maint an Instrument Shutoff Valve to Pressure Switch Found Closed Due to Personnel Error.Unit Operated 9 Days W/Instrument Out of Svc.Appropriate Disciplinary Action Taken | /03L-0 on 790111:during Unit Shutdown for Maint an Instrument Shutoff Valve to Pressure Switch Found Closed Due to Personnel Error.Unit Operated 9 Days W/Instrument Out of Svc.Appropriate Disciplinary Action Taken | | | 05000277/LER-1979-004-03, /04L-0 on 790112:during Surveillance Test of Cable Spreading Room Smoke Detector,Annunciator Could Not Be Reset Because It Was Not Properly Reset Previously.Detector Lead Disconnected to Reset Annunciator | /04L-0 on 790112:during Surveillance Test of Cable Spreading Room Smoke Detector,Annunciator Could Not Be Reset Because It Was Not Properly Reset Previously.Detector Lead Disconnected to Reset Annunciator | | | 05000278/LER-1979-004-03, /03L-0 on 790117:during Surveillance Test,Setpoint of PS-3-14-44D Found to Be Greater than Tech Spec Max.Caused by Setpoint Drift on static-o-ring Model 5N-AA3 Pressure Switch.Instrument Recalibrated | /03L-0 on 790117:during Surveillance Test,Setpoint of PS-3-14-44D Found to Be Greater than Tech Spec Max.Caused by Setpoint Drift on static-o-ring Model 5N-AA3 Pressure Switch.Instrument Recalibrated | | | 05000277/LER-1979-005-03, /03L-0 on 790118:at Power,Routine Surveillance Test Revealed Setpoint of DPIS-2-14-43B Was Below Tech Spec Min.Caused by Instrument DPIS-2-14-43B Being Out of Calibr Due to Setpoint Drift | /03L-0 on 790118:at Power,Routine Surveillance Test Revealed Setpoint of DPIS-2-14-43B Was Below Tech Spec Min.Caused by Instrument DPIS-2-14-43B Being Out of Calibr Due to Setpoint Drift | | | 05000278/LER-1979-005-03, /03L-0 on 790208:setpoint of Reactor Core Isolation Cooling Turbine Steam Supply Flow Sensor Was Above Tech Specs Max.Caused by Setpoint Drift on Barton Model 288 Differential Pressure Switch.Switch Recalibrated | /03L-0 on 790208:setpoint of Reactor Core Isolation Cooling Turbine Steam Supply Flow Sensor Was Above Tech Specs Max.Caused by Setpoint Drift on Barton Model 288 Differential Pressure Switch.Switch Recalibrated | | | 05000277/LER-1979-006-01, /01T-0 on 790130:recirculation Motor Generator Set Room Fire Detection Sys (Smoke Detectors) Disabled for Mod Work & Not Restored When Work Completed.Caused by Personnel Error.Sys Restored to Svc Upon Discovery | /01T-0 on 790130:recirculation Motor Generator Set Room Fire Detection Sys (Smoke Detectors) Disabled for Mod Work & Not Restored When Work Completed.Caused by Personnel Error.Sys Restored to Svc Upon Discovery | | | 05000277/LER-1979-006, Forwards LER 79-006/01T-0 | Forwards LER 79-006/01T-0 | | | 05000278/LER-1979-006-03, /03L-1 on 790212:at Power & During Surveillance Test,Setpoint of B Core Spray Pump Start Timer Was Less than Tech Spec Min.Caused by Setpoint Drift on GE Model CR-2820 Time Delay Relay.Relay Readjusted & Tested | /03L-1 on 790212:at Power & During Surveillance Test,Setpoint of B Core Spray Pump Start Timer Was Less than Tech Spec Min.Caused by Setpoint Drift on GE Model CR-2820 Time Delay Relay.Relay Readjusted & Tested | | | 05000278/LER-1979-007-03, /03L-0 on 790212:during Surveillance,Setpoint of a Logic Automatic Depressurization Sys Time Delay Relay Was Greater than Tech Spec Limit.Caused by Setpoint Drift on GE Model CR-2820 Time Delay.Relay Readjusted & Tested | /03L-0 on 790212:during Surveillance,Setpoint of a Logic Automatic Depressurization Sys Time Delay Relay Was Greater than Tech Spec Limit.Caused by Setpoint Drift on GE Model CR-2820 Time Delay.Relay Readjusted & Tested | | | 05000277/LER-1979-008-03, /03L-0 on 790225:fuses Were Blown in Control Circuit of Main Steam Relief Valve RV-71L.Replacements Blew Immediately.Caused by Failed Solenoid & Short Circuit.Leads to Solenoid Lifted;Fuses & Solenoid Replaced | /03L-0 on 790225:fuses Were Blown in Control Circuit of Main Steam Relief Valve RV-71L.Replacements Blew Immediately.Caused by Failed Solenoid & Short Circuit.Leads to Solenoid Lifted;Fuses & Solenoid Replaced | | | 05000277/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000277/LER-1979-008-01, /01T-0 on 790219:steady State Power Level Exceeded License Limit by Less than 2% for About 6-h.Caused by Error Calculating Scanned Feedwater Flow.Power Reduced to License Limit | /01T-0 on 790219:steady State Power Level Exceeded License Limit by Less than 2% for About 6-h.Caused by Error Calculating Scanned Feedwater Flow.Power Reduced to License Limit | | | 05000277/LER-1979-009-03, /03L-0 on 790213:fire Alarm Sys Malfunctioned, Causing Audible Signal to Alarm W/O Coding.Caused by Mechanical Binding of Cam in Alarm Box.Binding Problem Corrected & Sys Returned to Svc | /03L-0 on 790213:fire Alarm Sys Malfunctioned, Causing Audible Signal to Alarm W/O Coding.Caused by Mechanical Binding of Cam in Alarm Box.Binding Problem Corrected & Sys Returned to Svc | | | 05000278/LER-1979-009-03, /03L-0 on 790307:calculated Torus Water Level Did Not Provide Proper Torus Water Vol Per Tech Spec.Caused by Failure to See Pressure Differential Between Drywell & Torus Holds Level in Downcomers Was Below Torus Level | /03L-0 on 790307:calculated Torus Water Level Did Not Provide Proper Torus Water Vol Per Tech Spec.Caused by Failure to See Pressure Differential Between Drywell & Torus Holds Level in Downcomers Was Below Torus Level | | | 05000277/LER-1979-010-01, /01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase | /01T-0 on 790226:power & Control Cables Associated W/Recirculation Pump Discharge Valves & Bypass Valves Were Found Routed in non-safeguard Cable Trays.Caused by Improperly Designated Cables During Design Phase | | | 05000277/LER-1979-010, Forwards LER 79-010/01T-0 | Forwards LER 79-010/01T-0 | | | 05000278/LER-1979-011-01, /01T-0 on 790323:during Routine Insp of Drywell & Torus Ventilation Valves,Inflatable Disc Seals Were Found Depressurized.Caused by Procedural Deficiency Following Mod to Drywell & Torus Vent Valves.Procedures Revised | /01T-0 on 790323:during Routine Insp of Drywell & Torus Ventilation Valves,Inflatable Disc Seals Were Found Depressurized.Caused by Procedural Deficiency Following Mod to Drywell & Torus Vent Valves.Procedures Revised | | | 05000278/LER-1979-011, Forwards LER 79-011/01T-0 | Forwards LER 79-011/01T-0 | | | 05000277/LER-1979-011-01, /01T-0 on 790302:engineering Review Determined Certain Containment Isolation Valves Incapable of Closing Against LOCA Pressure.Caused by Design Oversight.Future Mod to Expand Valve Open Alarm to Include Seal Low Pressure | /01T-0 on 790302:engineering Review Determined Certain Containment Isolation Valves Incapable of Closing Against LOCA Pressure.Caused by Design Oversight.Future Mod to Expand Valve Open Alarm to Include Seal Low Pressure | | | 05000277/LER-1979-011, Forwards LER 79-011/01T-0 | Forwards LER 79-011/01T-0 | | | 05000278/LER-1979-013-01, /01T-0 on 790613:main Steam Relief Valve RV3-2-71L Lifted,Causing Torus Water Vol to Exceed Tech Spec Limit by 2.6%.Reactor Manually Scrammed.Valve Replaced & Sent to Wiley Lab to Determine Cause for Failure | /01T-0 on 790613:main Steam Relief Valve RV3-2-71L Lifted,Causing Torus Water Vol to Exceed Tech Spec Limit by 2.6%.Reactor Manually Scrammed.Valve Replaced & Sent to Wiley Lab to Determine Cause for Failure | | | 05000278/LER-1979-013, Forwards LER 79-013/01T-0 | Forwards LER 79-013/01T-0 | | | 05000278/LER-1979-014, /O3L-0 on 790522:offsite Source Breaker SU25 Tripped on Low Air Pressure.Caused by Short Circuit in Light Socket & Dirty Contacts on Voltage Relay.Relay Contacts Cleaned & Socket Removed Pending Replacement | /O3L-0 on 790522:offsite Source Breaker SU25 Tripped on Low Air Pressure.Caused by Short Circuit in Light Socket & Dirty Contacts on Voltage Relay.Relay Contacts Cleaned & Socket Removed Pending Replacement | | | 05000277/LER-1979-014-03, /03L-0 on 790327:trip Setpoint Drift of Drywell High Pressure Switch Was Beyond Tech Spec Limit.Caused by Static-O-Ring Model 12N-AA4 Being Out of Calibr Due to Setpoint Drift.It Was Recalibrated & Returned to Svc | /03L-0 on 790327:trip Setpoint Drift of Drywell High Pressure Switch Was Beyond Tech Spec Limit.Caused by Static-O-Ring Model 12N-AA4 Being Out of Calibr Due to Setpoint Drift.It Was Recalibrated & Returned to Svc | | | 05000278/LER-1979-015, /O3L-0 on 790523:automatic Depressurization Sys a Auto Blowdown Timer Trip Setting Found 13-s Less than Tech Spec Min.Caused by Setpoint Drift of Time Delay Relay.Relay Readjusted,Tested & Returned to Svc | /O3L-0 on 790523:automatic Depressurization Sys a Auto Blowdown Timer Trip Setting Found 13-s Less than Tech Spec Min.Caused by Setpoint Drift of Time Delay Relay.Relay Readjusted,Tested & Returned to Svc | | | 05000278/LER-1979-016-03, /03L-0 on 790628:while at Power,Routine Surveillance Test Revealed Setpoint of Switch 2 Was Below Tech Spec Min.Caused by Barton Model 288 Instrument Out of Calibr from Drift.Instrument Recalibr | /03L-0 on 790628:while at Power,Routine Surveillance Test Revealed Setpoint of Switch 2 Was Below Tech Spec Min.Caused by Barton Model 288 Instrument Out of Calibr from Drift.Instrument Recalibr | | | 05000278/LER-1979-017-31, /03L-0 on 790615:while Reactor Subcritical,D Main Steam Line Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts. Condition Corrected by Repeated Testing | /03L-0 on 790615:while Reactor Subcritical,D Main Steam Line Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts. Condition Corrected by Repeated Testing | | | 05000278/LER-1979-017, Discusses LER 79-017/03L-0.While Reactor Subcritical & Less than 212 F,Main Steam Line D Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts.Repeated Testing Corrected Condition | Discusses LER 79-017/03L-0.While Reactor Subcritical & Less than 212 F,Main Steam Line D Radiation Monitor Hi-Hi Trip Failed.Caused by Dirty Trip Relay or Dirty Test Switch Contacts.Repeated Testing Corrected Condition | | | 05000278/LER-1979-018-03, /03L-0 on 790630:during Surveillance Testing, Reactor Water Sample Line Isolation Valve Failed to Close. Caused by Lack of Valve Operator Spring Tension.Valve Operator Spring Tension Was Increased | /03L-0 on 790630:during Surveillance Testing, Reactor Water Sample Line Isolation Valve Failed to Close. Caused by Lack of Valve Operator Spring Tension.Valve Operator Spring Tension Was Increased | | | 05000277/LER-1979-019-03, /03L-0 on 790501:during Surveillance Testing of Normally Open Primary Containment Isolation Valves,Four Oxygen Analyzer Sys Isolation Valves Failed to Close.Caused by Binding of Pistons in Valve Bodies.Valve Parts Rebuilt | /03L-0 on 790501:during Surveillance Testing of Normally Open Primary Containment Isolation Valves,Four Oxygen Analyzer Sys Isolation Valves Failed to Close.Caused by Binding of Pistons in Valve Bodies.Valve Parts Rebuilt | | | 05000278/LER-1979-019-01, /01T-0 on 790621:during Seismic Support Insp Program, Reactor Core Isolation Cooling Piping Anchor Discovered to Have Two Bolts That Could Not Be Torqued. Caused by Improper Installation of Bolt Shells | /01T-0 on 790621:during Seismic Support Insp Program, Reactor Core Isolation Cooling Piping Anchor Discovered to Have Two Bolts That Could Not Be Torqued. Caused by Improper Installation of Bolt Shells | | | 05000278/LER-1979-019, Forwards LER 79-019/01T-0 | Forwards LER 79-019/01T-0 | | | 05000277/LER-1979-020-03, /03L-0 on 790503:solution Temp in Standby Liquid Control Sys Found to Be 2 F Less than Tech Spec Requirement for Existing Boron Concentration.Caused by Incorrect Acceptable Temp Controller Setpoint Range | /03L-0 on 790503:solution Temp in Standby Liquid Control Sys Found to Be 2 F Less than Tech Spec Requirement for Existing Boron Concentration.Caused by Incorrect Acceptable Temp Controller Setpoint Range | | | 05000278/LER-1979-020-01, /01T-0 on 790621:radioactive Release Rate at Main Stack During Plant Startup Exceeded Tech Specs.Caused by Deficiency in Procedure for Depressurization Following Shutdown.Investigation Underway to Improve Procedure | /01T-0 on 790621:radioactive Release Rate at Main Stack During Plant Startup Exceeded Tech Specs.Caused by Deficiency in Procedure for Depressurization Following Shutdown.Investigation Underway to Improve Procedure | | | 05000278/LER-1979-020, Forwards LER 79-020/01T-0 | Forwards LER 79-020/01T-0 | | | 05000278/LER-1979-021-03, /03X-1:on 790630,during Surveillance Testing,Main Steam Sample Line Inboard Isolation Valve Failed to Close. Probably Caused by Valve Packing Binding or Solenoid Valve Sticking While Valve Was at High Temp | /03X-1:on 790630,during Surveillance Testing,Main Steam Sample Line Inboard Isolation Valve Failed to Close. Probably Caused by Valve Packing Binding or Solenoid Valve Sticking While Valve Was at High Temp | | | 05000277/LER-1979-022-03, /03L-0 on 790513:fire Hose Nozzles Were Missing from Two Hose Stations in Turbine Bldg.Cause Not Noted. Nozzles Replaced & Wrench Tightened to Inhibit Removal | /03L-0 on 790513:fire Hose Nozzles Were Missing from Two Hose Stations in Turbine Bldg.Cause Not Noted. Nozzles Replaced & Wrench Tightened to Inhibit Removal | | | 05000278/LER-1979-022-03, /03L-0 on 790719:annunciator Sys II Drywell Pressure Permits Containment Spray Alarmed During Routine Startup.Caused by Failure of Diaphragm on PS-3-10-119D. Switch Repaired,Tested & Returned to Svc within Five Days | /03L-0 on 790719:annunciator Sys II Drywell Pressure Permits Containment Spray Alarmed During Routine Startup.Caused by Failure of Diaphragm on PS-3-10-119D. Switch Repaired,Tested & Returned to Svc within Five Days | | | 05000277/LER-1979-023-01, /01T-0 on 790724:insp Program Performed in Response to IE Bulletin 79-02 Identified Two Anchors in One Support Which Failed to Torque Test Properly.Caused by Improper Installation.Anchors Replaced | /01T-0 on 790724:insp Program Performed in Response to IE Bulletin 79-02 Identified Two Anchors in One Support Which Failed to Torque Test Properly.Caused by Improper Installation.Anchors Replaced | | | 05000277/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000277/LER-1979-023-04, /04T-0 on 790515:routine Ph Analysis of Sewage Plant Effluent Identified Ph of 5.8 Which Exceeded Tech Specs.Caused by Air Blower Failure Which Allowed Dissolved Oxygen to Drop to 0 & Aeration Tank to Become Anaerobic | /04T-0 on 790515:routine Ph Analysis of Sewage Plant Effluent Identified Ph of 5.8 Which Exceeded Tech Specs.Caused by Air Blower Failure Which Allowed Dissolved Oxygen to Drop to 0 & Aeration Tank to Become Anaerobic | | | 05000277/LER-1979-024, Forwards LER 79-024/01T-0 | Forwards LER 79-024/01T-0 | |
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