05000366/LER-1979-116-03, /03L-0:on 791025,HPCI Steam Line Inboard Valve Failed to Isolate During Calibr & Testing.Caused by Conservative Setting of Torque Switch.Engineering Package Review Revealed That Higher Setting Should Be Used

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/03L-0:on 791025,HPCI Steam Line Inboard Valve Failed to Isolate During Calibr & Testing.Caused by Conservative Setting of Torque Switch.Engineering Package Review Revealed That Higher Setting Should Be Used
ML19210D118
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 11/14/1979
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210D113 List:
References
LER-79-116-03L, LER-79-116-3L, NUDOCS 7911200551
Download: ML19210D118 (2)


LER-1979-116, /03L-0:on 791025,HPCI Steam Line Inboard Valve Failed to Isolate During Calibr & Testing.Caused by Conservative Setting of Torque Switch.Engineering Package Review Revealed That Higher Setting Should Be Used
Event date:
Report date:
3661979116R03 - NRC Website

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"EPOA 3o,gCE LO 61 OOCKETe.LY3EH 66 63 EVENT DATE 74 75 RtPORT D ATE 6J EVEN% DESCRIPTION AND PROBACLE CONSEQUENCES h l With ti,e reactor ~in the run mode, while performing procedure IINP-2-3307,, (!!PCI Steam l

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.. v O 3 l Line Differential Pressure Instrument Functional Test and Calibration), the llPCI Steam l 34 l Line Inboard Valve failed to isolate.' The HPCI Steam'Line Outboard IsolatiCn Valve l

was closed and secured and the HPCI system was declared inoperabic per Technical l

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[ Specification 3.5.1.

Public health and safety were not affected by this incident.

l This is a repetitive occurrence and was reported on LER 79-114.

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1

O l The failure of the HPCI Steam Line Inboard Valve to isolate was due to the torque l

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The valve was then cycled and found to be operating (Copt) l valve placed back in service.

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NAME OF PREPARER

Plant E. I, flatch Georgia Power Company Baxicy, Georgia 31513 Reportabic Occurrence Report No. 50-366/1979-116 Cause Description and Corrective Actions (cont) satisfactorily.

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