ML19209A121
| ML19209A121 | |
| Person / Time | |
|---|---|
| Site: | Catawba, Perkins, Cherokee |
| Issue date: | 09/13/1979 |
| From: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | Dail L DUKE POWER CO. |
| References | |
| NUDOCS 7910020577 | |
| Download: ML19209A121 (1) | |
Text
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UNITED STATES NUCLEAR REGULATORY COMMISSION
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REGION 11
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I i 101 MARIETTA ST., N.W., SulTE 3100 Yg
'o ATLANTA, G EoRGIA 30303 In Reply Refer To:
SEP 131979 y,_
RII:JPO 50-413, 50-414 50 491, 50-492 50-493, @ s C2fQ-489, 50-490 '
Duke Power Company Attn:
L. C. Dail, Vice President Decign Engineering P. O. Box 33189 Charlotte, North Carolina 28242 Gentlemen:
The enclosed IE Circular No. 79-19, is forwarded to you for information.
No written response is required.
Should you have any questions related to your understanding of this matter, please contact this office.
Sincerely, e.,,
Ja5es. O'Reill Director
Enclosures:
1.
IE Circular No. 79-19 2.
List of IE Circulars Issued in the Last Six Months 6
-1136 037~
7910020 6 774
SEP 131979 Duke Power Company.
cc w/ enc 1:
D. G. Beam, Project Manager Post Office Box 223 Clover, South Carolina 29710 J. T. Moore, Project Manager Post Office Box 422 Gaffney, South Carolina 29340 1136 088
SSINS:
6830 Accession No: 7908220111 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D. C.
20555 September 13, 1979 IE Circular No. 79-19 LOOSE LOCKING DEVICES ON INGERSOLL-RAND PUMP IMPELLERS Description of Circumstances:
Three reports have been submitted to the NRC regarding the loosening of locking devices on the impellers of pumps manufactured by the Ingersoll-Rand Company.
The first report was submitted as a significant deficiency (10 CFR 50.55[e])
by Arkansas Power and Light Company in letters of March 17, 1978 and May 9, 1978. The licensee reported excessive noise and vibrations in both Low Pressure Safety Injection (LPSI) pumps during the preoperational test program on Unit 2 of Arkansas Nuclear One (AN0).
It was discovered that the washers, jam nut and cap nut used to retain the impellers were missing on both pumps (Ingersoll-Rand Type 8X20WD). The licensee's corrective action involved the installation of a tab washer. This corrective action was, also, taken on the containment spray pumps (Ingersoll-Rand Type 6X23WD) because of similarity of design.
The second report was submitted by Duke Power Company in a licensee event report (LER 50-287/78-23) dated January 24, 1979.
The symptoms were similar to those observed at ANO Unit 2 in that high vibration was detected in a reactor building spray pump (Ingersoll-Rand Type 4X11A) for Oconee Unit No. 3.
The licensee found that the impeller had worked loose.
The corrective action included a revision to the m;intenance procedure to specify torque requir nts.
The third report was 10 CFR 21 Report No. 79-01 submitted by Portland General Electric Co. on April 16, 1979. This report identified a deficiency that may exist in the Trojan Nuclear Plant containment spray pumps (Ingersoll-Rand Type 6X23WD) in that there is a potential for the impeller lock nut to loosen.
The potential deficiency was identified because of the similarity of the containment spray pumps design to the residual heat removal (RHR) pumps (Ingersoll-Rand Type 8X20WD) and the discovery of a loose lock nut on an RHR pump during pump maintenance. The corrective action was to provide a positive mechanical lock on the impeller nut.
Westinghouse Nuclear Service Division has issued a Technic Bull H house plant owners on loose lock nuts pumps. Excerpts from that Technical Bi Engineering, Inc. has, also, informed ti DUPLICATE DOCUMENT 4
d same problem in a letter dated March Id ntire document Previously entered Enclosure No. 2.
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ANO No. of Pages:
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