05000366/LER-1979-096-03, /03L-0:on 790912,HPCI Flow Control Loop Inoperative.Caused by Bad Ramp Generator in Turbine Control Loop.Generator Replaced & Loop Functionally Tested to Ensure Operability

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/03L-0:on 790912,HPCI Flow Control Loop Inoperative.Caused by Bad Ramp Generator in Turbine Control Loop.Generator Replaced & Loop Functionally Tested to Ensure Operability
ML19208D431
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 09/19/1979
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19208D430 List:
References
LER-79-096-03L, LER-79-96-3L, NUDOCS 7909280416
Download: ML19208D431 (1)


LER-1979-096, /03L-0:on 790912,HPCI Flow Control Loop Inoperative.Caused by Bad Ramp Generator in Turbine Control Loop.Generator Replaced & Loop Functionally Tested to Ensure Operability
Event date:
Report date:
3661979096R03 - NRC Website

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