ML18347A797

From kanterella
Jump to navigation Jump to search
Monthly Operating Data & Summary of Operating Experience for March 1978
ML18347A797
Person / Time
Site: Palisades Entergy icon.png
Issue date: 04/07/1978
From: Adams W
Consumers Power Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML18347A797 (5)


Text

consumers Power company Palisades Nuclear Plant: Route 2, Box 154, Covert, Michigan 49043 April 7, 1978 USNuclear Regulatory Connnission \:o t:i Mail and Records Section (/) 03 Washington, D.C., 20555  :~l .(ll>

'*-  :.-0

~:.".'.:  ::0 Re: LICENSE REPORT OF MONTHLY OPERATING DATA DPR-20, DOCKET NO. 50-255 Gentlemen:

Enclosed is a copy of the Monthly Operating Data, of Operating Experience for the Palisades Nuclear month of March 1978.

{Jt~L William E. Adams, General Engineer cc: JGKepp~er, USNRC RBDeWitt DAB ix el GHPetitjean CVWaits DEVan Farowe, Div. of Radiological Health Lansing, Mich.

AKozlowski, Mich. Dept. of Labor RCallen, Mich. Public Service Comm., Lansing, Mich.

Document Control - (2) 950-22.35.10

CONSUMERS POWER CO.

PALISADES NUCLEAR PLANT DOCKET 50-255

SUMMARY

OF OPERATING EXPERIENCE FOR PERIOD MARCH 1 THROUGH MARCH 31, 1978 3-::-1-78 The Plant was in a refueling shutdown condition.

3-6-78 Completed plugging of tubes in both Steam Generators.

Completed refurbishment of Control Rod Drive packages.

3-13-78 Completed modifications to the 345KV line.

3-15-78 Completed ISI piping inspections.

3-16-78 Completed repairs to the Main Steam Isolation Valves.

3-20-78 Completed repairs to the Containment Air Coolers.

Completed main generator inspection and repairs.

3-22-78 Completed refurbishment of Primary Coolant Pump P-55B oil lift system.

3-23-78 Completed repairs to Containment purge supply and exhaust valves (CV-1805, 1806, 1807, and 1808).

3-24-78 Commenced the Integrated Leak Rate Test (ILRT).

3-28-78 Completed the ILRT.

3-30-78 Completed modifications to the Reactor vessel head cooling system.

OPERATING DAT A REPORT DOCKET NO. 50-255 DATE 4-4-78 COMPLETED BY DTBoJ inoK TELEPHONE 616-764-913 OPERATING STATUS I. Unit Name: Palisades Plant Notes

2. Reporting Period: 3~1-78 to 3-31-78
3. Licensed Thermal Power (MWt): 2530
4. Nameplate Rating (Gross MWe): 811.7
5. Design Electrical Rating (Net MWe): 805
6. Maximum Dependable Capacity (Gross MWe):
  • 675
7. Maximum Dependable Capacity (Net !\!We):
  • 635
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
9. Power Level To Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:

,(°'

This Month Yr.-to-Date Cumul:.itive

11. Hours Jn Reporting Period o* 2160 *55,071
12. Number Of Homs.Reactor Was Critical* 0 124.9 29.,524.3
13. Reactor Reserve Shurdown Hours 0
14. Hours Generator On-Line 0 124.8 27,957.0
15. Unit Reserve Shutdown Hours
16. Gross Thermal Energy GeP..erated (MWH) 0 270,336 50,292,000
17. Gross Electrical Energy Generated (~!WH) ----- 0 81,640 15,668,250
18. Net Electrical Energy Generated (M\VH) 0 76,464 14,689,831
19. Unit Service FactorI 0 5.8 50~8
20. Unit Availability F.actor 0 5.8 50.8
21. Unit C::ipacity f3ctor (Using MDC Net) 0 5.6 42.0 Unit Capacity Fa'cror (Using DER Net) 0 ~.4 33.1
23. Unit Forced Outage Rate 0 0 40.4
24. Shutdov,;ns Scheduled Over Next 6 Months (Type. D::ite. and Dur:Hion c>f Each):
25. If Shut Down At End Of Report Period. Estim::ited Date of St:::rtup:
26. Units In Test Status (Prior to Commercial Operation): forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY C0:\-1:\lERCf..\L OPERATION
  • Based on Condenser Backpressure Limitations

. (t) /77)

eVERAGE DAILY UNIT POWER LEVEL. e DOCKET NO.

50-255 UNIT Palisades DATE 3-04-78 COMPLETED BY DIBollnow TELEPHONE 616-764-8913 MONTH -March 1978 DAY A VER AGE DAILY POWER LEVEL DAY A VER..\GE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 0 17 0 2 0 0 18 o* 0 3 19 0 0 4 20 5 0 21 0 6 0 0 22

{ 0 7 -,~

0 0 0 8 24 9 0 0 25 0 0 10 26 11 0 27 0 12 0 0 28 0 0 13 29 0 0 14 30 15 0 0 31 16 0 INSlRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting Inlll1th. Compute to the nearest whole megawatt.

(9/77)

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. ___;5:....:0:......--=2-=5-=5--,-_- '~ -

UNIT NAME Palisades*

DATE 4-4-78 COMPLETED BY DIBollnow REPORT MONTH_ March 1978 616-764-8913 TELEPHONE

,.-L_

r-1 3  ::JJ ......

c

~V'I

~

-0 .:::

v Licensee E..q-

<l.l <l.l -*

0

<l.l

-0 Cause & Corrective No. Date n.

l

~

V>

'"' ..c ::;

~

O'.'. Event -V> "O

~

  • ~ 0 i;:::r;_;

Action to r-  ::j~

o::::. ~ ~ ..r: Report tt VJ u 0 Prevent Recurrence

E VJ ~ u 8

1 780106 s 2,035.2 c 1 None - - N/A 3 4 F: Forced Reason: Method: Exhibit G - Inst ructions S: Sche<l ulcd A-Equipment Failure (Explain)  ! -Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram. Entry Sheets for Licensee C-Rcfucling 3-Automatic Scram. Event Report (LER) File (NUREG-D-Reguiatory Restriction 4-0t her (Exp la in) 0161)

E-Opcrator Training & License Examination F-A<lministrative 5 G-Opcrational Error (Explain) Exhibit I - Same Sm1rrc

(\J /77) !I-Other (Explai11)