ML18153C042
| ML18153C042 | |
| Person / Time | |
|---|---|
| Site: | Surry |
| Issue date: | 12/22/1989 |
| From: | Reyes L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18153C041 | List: |
| References | |
| 50-280-89-34, 50-281-89-34, NUDOCS 9001090170 | |
| Download: ML18153C042 (3) | |
Text
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NOTICE OF VIOLATION Virginia Electric and Power Company Surry Units 1 and 2 Docket Nos. 50-280 and 50-281 License Nos. DPR-32 and DPR-37 During the Nuclear Regulatory Commission (NRC) inspection conducted between the period of October 29 through November 25, 1989, violations of NRC requirements were i dent ifi ed.
In accordance with the 11Genera l Statement of Policy and Procedure for NRC Enforcement Actions 11
, 10 CFR Part 2, Appendix C (1988), the violations are listed below:
A.
10 CFR 50, Appendix B, Criterion V, requires that activities affecting quality sha 11 be prescribed by documented instructions or procedures appropriate to the circumstances.
Contrary to the above, activities affecting quality were not prescribed by adequate instructions and/or procedures, in that:
- 1.
Operating Procedure, 2-0P-1. 3, Unit Startup Operation (350/450 to HSD),
Revision dated June 14, 1989, did not adequately caution the operators to maintain specific pressure control prior to testing reactor coolant system accumulator discharge valves. On November 21, 1989, during Unit 2 startup, operators a 11 owed the reactor coolant system pressure to exceed 1000 psig, prior to opening and de-energizing the accumulator discharge isolation valve motor operators, a violation of Technical Specification 3.3.A.10.
- 2.
On November 13, 1989, a resin waste transfer evolution was conducted without adequate procedure control resulting in three licensee employees being contaminated when a pipe cap was removed from a pressurized system.
- 3.
On approximately October 25, 1989, the Unit 2 flood control dikes, which protect against flooding of the service water supply motor control valves to the recirculation spray heat exchangers, were removed with inadequate modification and operation procedure control resulting in heatup of the unit above 350°F, on November 6 and 20, 1989, with inoperable recirculation spray systems, a violation of Technical Specification 3.4.
This violation has been categorized as a Severity Level IV violation (Supplement I) for Unit 2.
B.
10 CFR 50, Appendix B, Criterion VIII, requires that measures and controls shall be established to prevent the use of incorrect or defective material, parts, and components.
9001090170 891222 PDR. A:OOCK. 05(H)02BO Q
Virginia Electric and Power Company Surry Units 1 and 2 Docket Nos. 50-280 and 50-281 License Nos. DPR-32 and DPR-37 Contrary to the above, adequate measures were not established to prevent i nco_rrect gaskets from being i nsta 11 ed in components in that:
- 1.
Work Order 87218, dated October 28, 1989, identified that an incorrect gasket had been installed in safety injection check valve 2-SI-79 during the previous outage.
This condition had contributed to a failure of the valve to properly seat during subsequent unit operation.
- 2.
Inspection of safety injection check valve 2-SI-91 in accordance with Engineering Work Request 89-684B, dated November 3, 1989, indicated that an incorrect gasket had been installed during the previous outage.
- 3.
After interim corrective action was conducted for examples 1 and 2 above on November 1, 1989, incorrect gaskets were i nsta 11 ed in a Unit 2 pressurizer safety valve on November 14, 1989, and subsequent review revealed potential incorrect gaskets in the Unit 1 pressurizer safety valves.
This violation has been categorized as a Severity Level IV violation (Supplement I) for Units 1 and 2.
C.
Technical Specification 3.7, Table 3.7.5(a) requires that grab samples be collected and analyzed at least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> whenever radioactive liquid effluent monitoring instrumentatJon is out of service.
Contrary to the above, grab samples were not collected and analyzed at 1 east once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> in that, on August 2, 1989, samp 1 es for the component cooling service water effluent line were collected and analyzed 30 minutes outside the required 12-hour timeframe.
This violation has been categorized as a Severity Level IV violation (Supplement I) for Units 1 and 2.
Pursuant to the provisions of 10 CFR 2.201, Virginia Electric and Power Company is hereby required to submit a written statement or explanation to the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, within 30 days of the date of this Notice.
This reply should be clearly marked as a "Reply to a Notice of Violation 11 and should include (for each violation):
(1) admission or denial of the violation, (2) the reason for the violation if admitted, (3) the corrective steps which have been taken and the results achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved.
Where good cause is shown, consideration will be given to extending the response time.
If an adequate reply is not received within the time specified in this Notice, an
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Virginia Electric and Power Company Surry Units 1 and 2 3 -
Docket Nos. 50-280 and 50-281 License Nos. DPR-32 and DPR-37 order may be issued to show cause why the license should not be modified, suspended, or revoked; or why such other action as may be proper should not be taken.
Under the authority of Section 182 of the Act, 42 U.S.C. 2232, this response shall be submitted under oath or affirmation.
Dated at Atlanta, Georgia this 22nd day of December 1989 Luis A. Reyes, r, ctor Division of ac or Projects
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