ML18153B714

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/89-10 & 50-281/89-10 on 890327-0404. Violations Noted.Major Areas inspected:motor-operated Valve Deficiency Followup,Ie Bulletin Followup & Power Operated Valve Inservice Stroke Time Testing
ML18153B714
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/03/1989
From: Belisle G, Lenahan J, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153B712 List:
References
50-280-89-10, 50-281-89-10, IEB-85-003, IEB-85-3, NUDOCS 8905170075
Download: ML18153B714 (13)


See also: IR 05000280/1989010

Text

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION 11

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/89-10 and 50-281/89-10

Licensee:

Virginia Electric and Power Company

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.: DPR-32 and DPR-37

Inspection Conducted:

March fo7 - April 4, 1989

Inspectors:

If ;j{,_L

J. Lena ha Ir .

Date Signed

~ls/gc,

e'Signed

Accompanying Personnel:

E. Brown, Office of Nuclear Reactor Regulation

by:

c.P-~ ~__.I?/

G~ I

_ Approved

l'f:--J-f-"f

Date Signed

Scope:

Results:

Test Programs Section

Engineering Branch

Division of Reactor Safety

SUMMARY

This special, announced inspection was in the areas of motor operated

valve deficiency followup, IE Bulletin followup, and power operated

valve inservice stroke time testing.

Within the areas inspected, one violation was identified which

involved failure to take prompt corrective action in response to

motor operated valve deficiencies, paragraph 2.a.

Weaknesses were

identified in the licensee's motor operated valve recovery program,

paragraph 2.b, in the licensee's motor operated valve overhaul

procedures, paragraph 3, and in the licensee's corrective action for

excessive valve stroke times, paragraph 4.

The licensee committed to provide, in writing, to the NRC details of

the motor operated valve recovery program, and to review MOVATS test

reports issued prior to 1988, paragraph 2.b .

8905170075 890509

PDR

ADOCK 05000280

Q

PDC

-

...

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

L. Adkins, Mechanical Maintenance Foreman

R. Bilyeu, Licensing Engineer

  • R. Blount, Superintendent of Technical Services
  • D. Christian, Assistant Station Manager
  • P. Doody, Project Engineer, Motor Operated Value (MOV) Repair Project
  • E. Greckeck, Assistant Station Manager

S. Hanson, Electrical Maintenance Foreman

  • M. Kansler, Station Manager
  • H. Miller, Director, Operations and Maintenance Support

K. Moore, Vice-President, Engineering

R. Saunders, Manager of Licensing

Other licensee employees contacted during th is inspection included

engineers, mechanics, technicians, and administrative personnel.

Other Organizations

D. Eshleman, Site Supervisor, Atlantic Nuclear Services

R. Bowen, MOV Supervisor, Atlantic Nuclear Services

NRC Resident Inspectors

  • W. Holland, Senior Resident, Operations

J. York, Senior Resident, Construction

L. Nicholson, Resident Inspector

  • Participated in telephone conference call on April 4, 1987

2.

MOV Deficiency Followup (92701)

(Open) 280,281/88-45-01; MOV Deficiency Followup.

During the present

Uni ts 1 and 2 outages, the licensee filed approximately 450 station

deviations against MOVs.

Examples of MOV deficiencies encompassed by the

station

deviations

are

provided

in

NRC

Inspection

Report

Nos. 50-280,281/89-03.

During this inspection, the inspectors performed

an in depth review of the testing and maintenance associated with three

valves required to be operational in order to mitigate the consequences of

a loss-of-coolant accident (LOCA).

The inspectors also reviewed the

licensee's program to restore Units 1 and 2 safety-related MOVs.

a.

Review of MOVs 2-CH-MOV-2289A, 2-CH-MOV-2289B and 1-CH-MOV-1286B

Testing and/or Maintenance Histories.

.-.

( 1)

2

Reviewing valve 2-CH-MOV-2289A Motor Operated Valve Actuator

Test System (MOVATS) test reports from 1986 revealed that the

following deficiencies were identified but not subsequently

corrected:

MOVATS test report dated November 25, 1986, identified that

the valve was not shutting off flow as crisply as a similar

valve that had recently undergone disk and seat repair.

The test report recommended checking the valve's disk and

seating ~urfaces during the next outage.

MOVATS test report dated February 10, 1987, identified that

the valve

1 s stem to disk connection was damaged.

This was

detected by observing that the stem rotated approximately

45 degrees while the valve was seating.

The test report

concluding the following:

The stem to disk movement may be do to the over torquing

of the valve into the seat.

Comparing the valve thrust signatures with similar valve

thrust signatures that underwent disk and seating surfaces

repair indicated that valve seat damage was evident.

Due to the high thrust on this valve, and the fact that

the MOVATS test performed November 25, 1986, showed seat

damage, it can only be concluded that more damage has

been done including the stem to disk connection.

The inspectors review of the valve's work orders from 1986

revealed that the valve's disk,and seating surfaces had not been

inspected for damage, nor had the damaged stem to disk

connection been repaired. After the MOVATS testing performed on

February 10, 1987, the valve was again tested on May 25, 1988;

June 12, 1988; and November 4, 1988.

None of the 1988 MOVATS

test reports identified disk to stem movement or seating surface

damage.

On April 1, 1989, the valve was scheduled to be tested

following the actuator overhaul.

The inspectors requested the

licensee to observe if disk to stem movement occurred when

performing this test.

On April 3, 1989, the inspectors wer~

informed by the licensee that valve disk to stem movement was

observed when testing and that corrective action was being

initiated.

The inspectors were also informed that disk to stem

movement was difficult to detect, which may explain why the

movement was not detected during any of the three MOVATS tests

accomplished in 1988.

The 1986 and 1987 valve MOVA TS test reports identified that

valve degradation and actuator over thrusting were occurring,

and that actual stem to disk connection damage had occurred.

The inspectors considered that these deficiencies could result

(2)

3

in va 1 ve failure, but were not promptly corrected by the

licensee after being identified.

Review of the licensee's

program during the 1986/87/88 time period indicated that MOVATS

test reports were not a 1 ways adequately being reviewed by

1 icensee personnel.

MOVATS contractors performed the testing

and submitted test reports, but the deficiencies were not being

reviewed by licensee personnel to ensure that corrective action

was being initiated.

Review of valve 2-CH-MOV-22898 i nservice test stroke time

results, station deviations, and

MOVATS test results

accomplished in 1987 indicated that valve degradation was

occurring but was

not subsequently corrected.

Valve

2-CH-MOV-22898 is categorized as a cold shutdown valve;

consequently, it is only stroke time tested during shutdown

periods.

Sta ti on records indicated that on March 15, 1987,

December 19, 1987, and on December 21, 1987, the valve's stroke

times exceeded its maximum stroke time limit of ten seconds.

The* corrective action for the March 15, 1987, valve failure

involved stroking the valve two additional times.

Since the two

additional stroke time results did not exceed ten seconds, the

valve was considered operable.

During the December 19, 1987,

stroke time test, the valve again failed since the stroke time

was 10.85 seconds.

Based on this failure the valve was MOVATS

tested.

The MOVATS test report revealed that an actuator high

running load condition existed and that the valve stroke time

was 10.4 seconds.

The test report did not indicate that limit

switches were out of adjustment.

On December 21, 1987, the

valve was tested and the stroke time was 10.37 seconds.

On

December 21, 1987, the valve's open limit switch was adjusted in

accordance with Work Order 3800059847.

The work order stated

that the excessive stroke time was due to the open limit switch

being out of adjustment.

The work order did not specify how

much the limit switch was out of adjustment or what the final

open limit switch setting was left at.

Contrary to the

licensee's policy to MOVATS test this valve following limit

switch adjustment, the valve was not MOVATS tested following the

December 21, 1987, limit switch adjustment.

After the open

limit switch was adjusted, the valve was satisfactorily stroke

time tested at 9.71 seconds.

On December 23, 1987, Unit 2 was

started up.

As previously discussed, valve 2-CH-MOV-22898 failed to stroke

within the allowable ten second time period four times; three

failures occurred during stroke time testing, and the fourth

occurred during MOVATS testing when actuator high running load

was also identified.

Since MOVATS testing did not reveal limit

switches out of adjustment it can be assumed that the open limit

switch setting was adjusted to shorten the valve stroke

distance, resulting in a decreased stroke time. This is not

considered acceptable. corrective action.

The valve may have

...

b.

4

been able to accomplish its intended function with a shortened

stroking distance; however, the degraded condition causing the

(3)

In 1985 the licensee was aware that both lithium and calcium

based greases had been added to Surry MOV actuators, and that

Amolith Grease No. 2, which was utilized in some MOV actuators

at Surry, was an inadequate lubricant.

In a September 26, 1985,

letter from Limitorque Corporation to Virginia Power, Limitorque

actuator lubricants were discussed, and Limitorque Corporation

recommended that Amolith Grease No. 2 not be used in Limitorque

actuators. Additionally, the 1 etter stated that under no

circumstancess should lubricants of dissimilar bases be mixed.

In a Surry inter-office memorandum from W. E. Patterson to

H. L. Miller dated September 4, 1985, corrective action

involving initiation of an aggressive MOV actuator grease

replacement program was recommended.

During the present 1988/1989 Units 1 and 2 outages, numerous

station deviations were written that describe actuator grease

deficiencies.

Examples of such deficiencies included, bad

grease in actuator housings and wrong grease types in actuator

housings.

On July 7, 1988, Station Devi.ation Sl-88-1668 was.

written against valve 1-CH-MOV-1286B and identified that*

hardened grease was found in the actuator, that metal filings

were found in the grease, that the worm gear would not turn and

had. severa 1 broken teeth.

The inspectors reviewed the work

order history for this valve from 1985.

There was no record of

grease replacement occurring until July 1988.

Valves 2-CH-MOV-2289A, 2-CH-MOV-2289B and 1-CH-1286B, are.all

included in the

IE Bulletin 85-03, Motor Operated Valve Connnon

Mode Failure During Plant Transients Due to Improper Switch

Settings program.

Inclusion into the IE Bulletin 85-03 program

means that operation of these MOVs is essential in mitigating

the consequences of a loss of coolant accident by repositioning

as required to allow injection of high pressure water into the

reactor core.

Reviewing

work orders~ station deviations, and

MOVATS test reports associated with these valves revealed that,

in all cases, known deficiencies existed that were not promptly

corrected.

Failure to promptly correct MOV deficiencies is

identified as violation 280,281/89-10-01.

Review of the Licensee's Actions to Restore MOV's for Units 1 and 2

The responsi bi 1 ities for accomplishing actions required to restore

MOVs were divided between several organizational groups.

Surry

Maintenance Department personne 1 were performing MOV el ectri ca 1

activities and directing Atlantic Nuclear Services (ANS) contractors,

who were performing the MOV mechanical activities. Surry Maintenance

Department personnel were also directing the MOVATS contractors, who

...

5

were performing MOV diagnostic testing activities.

Corporate,

Operations and Maintenance Support Branch, personnel were developing

a comprehensive program to ensure that MOVs would be properly

maintained in the future. Surry Operations Department personnel were

involved in determining which safety related MOVS were required

to be operational in order to mitigate the consequences of an

accident and safey shutdown the plant to hot standby.

As a result of

the Operations Department review, some MOVs in safety-related systems

were not included in the licensee's effort to restore MOVs because

they were not required to be operated in order to mi ti gate the

consequences of an accident or safety shutdown Uni ts 1 and 2.

One hundred Unit 1 MOVs and 103 Unit 2 MOVs ,were being evaluated to

ensure operability.

An MOV Task Group composed of Surry, North

Anna, and Corporate personnel knowledgeable of MOVs was formed to

direct, coordinate~ and provide the required engineering support to

restore the 203 Units 1 and 2 MOVs.

The activities of the Task Group

involved the following:

Review MOVATS test reports dating back to 1988.

Evaluate defi ci enci es encountered during MOVATS testing and

actuator disassembly.

Review and revise as necessary MOV switch settings.

Review adequacy of IE Bulletin 85-03 response.

Review and revise as necessary engineer sketches that provide

MOV limit switch settings.

Establish what actions are required to restore MOVs and track

the required action status.

Perform MOV wa l kdowns to verify that MOV nameplate data

corresponds to data being used to determine MOV thrust values.

Ensure all Surry MOV commitments. are met.

Review MOV work orders dating back to 1988.

Review MOV station deviations dating back to 1986.

Assign root cause and corrective action to MOV station

deviations generated in 1988 and 1989.

Valve thrust requirement ca lcul ati ons, using the la test industry

standards were being requested from applicable valve vendors.

Until

these thrust values can be obtained, the MOV task group provided

thrust values using standard equations.

Two train limit switches are

being replaced with four train limit switchs which allows the torque

switch bypass ~ettings to be increased.

MOV task group reviews of

...


  • , .

6

engineering sketches that provided MOV 1 imit switch setpoints

revealed that because of the numerous revisions, it was difficult to

obtain the required information from the sketches.

Consequently, the

task group is being required to rewrite the sketches.

Another

finding of the task group was that MOVATS test reports have not been

adequately reviewed.

One of the first task group actions was to stop

MOVATS testing and prepare written guidelines to ensure that MOVATS

test reports would be adequately reviewed.

The MOV task group

identified that the Unit 1 and 2 power operated relief valves (PORVS)

were marginally sized.

The licensee is planning to replace the

actuators with larger actuators prior to the respective unit startup.

The MOV task group also identified five valves in Units 1 and 2 that

have undersized actuators.

The undersized actuators are l-CH-MOV-

I287A and B, 2-CH-MOV-2287A and B, and 2-SI-2869.

All five valves

and actuators were involved in plant modification packages previously

accomplished.

Valve 2-SI-2869 actuator will be replaced with a

larger actuator prior to startup and the charging valves' actuators

will be deenergized and locked in position until the actuators are

replaced with larger actuators.

During the MOV recovery program review, the inspector noted the

following MDV issues that have not yet been fully resolved:

As discussed in parigraphs 2.a(3) and 2.c, actuator grease was

identified as a problem.

The corrective action to resolve this

issue has not been determined.

All Surry safety-related MOVs contain either 460 volt or 440

volt alternating current motors.

The voltage specifications for

these motors is plus or minus 10 percent of the motor name plate

voltage.

Bus voltage to these motors is approximately 525 volts

AC which exceeds the manufacturer

I s recommended vo 1 tage.

The

440 volt motors are being replaced with 460 volt motors.

The

effect of high bus voltage on the 460 volt motors is being

evaluated.

The MOV recovery program review also indicated that the following

areas required clarification:

The inspector was informed that to verify operation, MOVs will

be differential pressure tested p~ior to startup.

What MOVs to

be tested, and at what pressure has not been determined.

Although there have been station deviations written against

actuators involving missing parts, modified parts, and incorrect

assembly-, the licensee does not intend to disassemble and

inspect a 11 actuators.

The criteria for determining when

disassembly would be performed was not clear .

...

7

Station deviations have been written for modified and homemade

tripper fingers, yet not all tripper fingers have been

inspected.

The criteria for not inspecting all tripper fingers

was not clear

One finding contributing to the cause of present MOV problems is

the 1 ack of a good MOV program.

As a result, Corporate is

developing a comprehensive program that was scheduled to be

issued prior to startup.

The program will involve training

qualification for station and contract personnel and a

department reorganization to ensure that all MOV related

maintenance and testing go through a central person.

Implementation of this program will take time and will likely

not be accomplished prior to startup.

In addition, after

determining root cause and corrective action in response to

station deviations, it is probable that procedural and personnel

training will be identified which may or may not be accomplished

prior to startup.

During the inspection it was not clear what

would be accomplished relative to procedural changes, training,

or other changes to the MOV program prior to startup.

The MOV recovery program indicated that the fo 11 owing action items

need to be accomplished, in addition to the action items presently

being ~ccomplished:

The MOV stroke time review indicated that some MOVs were not

stroking within specified times.

Examples of valve stroke times

exceeding allowed limits are 1-RC-MOV-1536, 2-CH~MOV-2289A, and

2-CH-MOV-22898.

In addition, the inspector reviewed a licensee

memorandum issued by J. Laflam to A. McNeill, dated February 26,

1988, that discussed MOV excessive stroke times.

As discussed

in paragraphs 2.a(2) and 4, the licensee's corrective action for

excessive stroke times did not always identify and correct the

root cause; therefore, MOV stroke times need to be reviewed and

valves with excessive stroke times need to be evaluated in order

to ensure that root cause and corrective action are performed.

As discussed in paragraph 2.a(l), MOVATS testing accomplished

in 1987 on valve 2-CH-MOV-22898 identified valve damages that

could have gone undetected during the present recovery program.

As a result, the inspectors consider it necessary for the

licensee to review all MOVATS test reports dating back to 1985.

Previous plans were to review MOVATS test reports dating back to

1988.

During the exit interview the licensee indicated that

MOVATS test reports issued prior to 1988 would also be reviewed.

In order to determine if MOV repeated problems are occurring the

licensee is reviewing work orders dating back to 1988 for

applicable MOVs.

The inspectors reviewed work orders for

various MOVs from 1985, and considered that in order to

8

determine if repeat problems were occurring, like frequent

replacement of motors for example, then the licensee needs to

review work orders as far back as practicable.

Valves 1-RH-MOV-100 and 2-RH~MOV-200 are pressure boundary, lock

closed, isolation valves backed by manual isolation valves.

In

the case of a control room fire which results in control room

. evacuation, the licensee emergency procedures require these

valves to be opened in order to provide a letdown path. Since

automatic actuation for* the valves is located in the control

room which had been evacuated, the valves would be required to

be opened manually.

The valves have been excluded from the MOVs

that are currently being evaluated.

Since there are station

deviations written for valves that do not manually cycle

properly, the inspectors consider it necessary to take the

appropria_te action to ensure that valves 1-RH-MOV-100 and

2-RH-MOV-200 are able to be manually cycled when required.

During the inspection, areas in the MOV recovery program were_

identified that needed clarification, were not fully resolved,

or in some cases not sufficient.

As a result, the inspectors

noted that personnel in different groups were diligently working

toward restoring MOVs; but how all this work would come together

to ensure that MOVS were operable prior to restart was not

clear. This was discussed during the exit interview where the

licensee committed to provide a letter to the NRC detailing how

the MOV recovery program would be accomplished.

c.

MOV Lubrication

On August 18, 1985, Station Deviation SI-85-430 was written to

document the failure of MOV-SW-104B to cycle on command from the main

control room.

Investigation of this problem by the licensee

disclosed that the cause of the MDV failure was presence of grease in

the electrical side of the housing which affected the contacts.

A

detailed investigation of this problem by the licensee's Human

Performance Evaluation System (NPES) staff disclosed weaknesses in

MDV maintenance procedures and training of maintenance personnel in

repairing MOVs.

One problem identified during the investigation

involved the type of_ grease used to lubricate the valves.

The MDV

manufacturer, L imitorque, stated that the only grease wh.ich they have

certified for their MOVS was Exxon Nebula EP-0 or EP-1, a calcium

soap based grease.

However, licensee maintenance personnel had used

Amoco Ryken No. IEP or Amolith Grease No. 2, which

are lithium

based, when lubricating the MOVs.

Maintenance personnel were not

aware of the differences in the greases, and did not properly

document which type of grease was used to lubricate various MOVs.

The maintenance procedure did not specify the type grease to be used.

As a result, the various types of greases, lithium based and calcium

based greases, were mixed.

The problems identified by the licensee

regarding MDV grease problems were documented in a Virginia Power

9

memorandum dated September 13, 1985, Subject:

Lubrication of

Limitorque Operators, Surry Power Station, NP 1175.

Investigations

performed by other licensees and the NRC have shown that the effects

of mixing lithium base and calcium base grease is that the grease

hardens resulting in unacceptable wear to MOV components, leading to

eventual failure of the MOV.

The mixing of small quantities of

lithium base grease, as little as three to five percent by weight,

with a calcium base grease, has been found to result in hardening of

the grease.

This data is documented in a Safety Evaluation Report,

dated April 28, 1988, prepared by the NRC Office of Nuclear Reactor

Regulation for the Braidwood Nuclear Plant (Docket Numbers 50-456 and

50-457, TAC Nos. 67627 and 67626).

As stated in paragraph 2.a(3),

the licensee failed to take adequate corrective action to resolve

problems noted from August - September 1985 regarding improper types

of grease used to 1 ubri cate MOVs, and the effect of mixing the

various types of greases in MOVs.

This resulted in numerous MOV

grease problems being identified during the current outage.

The inspectors questioned licensee Maintenance Supervisors regarding

planned corrective actions to address grease problems.

These

discussions disclosed that the licensee was evaluating a method which

cleans the MOV with a solvent (varsol) to remove. the old grease.

The

inspectors examined an MOV which was cleaned using this method and

noted that a 11 the grease .had been removed with the exception of some

o 1 d grease under and around the bearings. As a result of the

discussions with licensee personnel, the inspectors had the following

questions pertaining to identifying and removing grease from

safety-related MOVS.

Wbich valves have mixed grease or grease other than Exxon EP-0 or

EP-1?

How was the appropriate grease identified during valve inspection?

What limits are used to determine if grease is contaminated.? What

is maximum percentage of lithium based grease permitted to be present

in the qualified calcium based grease?

What method will be used to remove contaminated grease from MOVs?

How will valves be inspected to verify that all grease is removed.

d.

MOV Technician Qualifications

The inspectors reviewed the qualifications of the ANS mechanics,

titled MOV techs, who perform mechanical inspections and repairs to

MOVs.

The inspectors also observed two MOV techs disassemble, clean

and inspect MOV-SI-28628.

This work was performed in accordance with

procedure MMP-C-MOV-178.

The inspectors interviewed the MOV techs

and determined that they were knowledgeable and cognizant of MOV

. .

10

corrective maintenance requirements.

Based on, review of the MOV tech

qualifications and observations of work activities, the inspectors

concluded that the MOV techs were qualified and had proper training

and experience to perform MOV maintenance.

Within the areas inspected, one violation was identified.

3.

IE Bulletin 85-03 Follow-up (25573)

(Open) 50-280, *281/85-BU-03, T2515/73, Motor Operated Valve Corrmon Mode

Failure During Plant Transients Due to Improper Switch Settings.

The bulletin required licensees to develop and implement a program to

ensure that switch settings for High Pressure Coolant Injection and

Emergency* Feedwater System MOVs, subject to testing for opera ti ona 1

readiness in accordance with 10 CFR 50.55a(g), are properly set, selected,

and maintained.

The information in this Inspection Report supplements the IE Bulletin

85-03 follow-up contained in Inspection Report Nos. 50-280/89-03 and

50-281/89-03.

In order to evaluate the Surry IE Bulletin 85-03 program, the inspector

held discussions with the appropriate licensee personnel and reviewed the

following:

Procedure MMP-C-MOV-178.1, Removal and Overhaul of Limitorque Model

SMB-0 Through SMB-4 and SB-0 Through SB-4, dated March 23, 1989.

Procedure MMP-C-MOV-178, Removal and Overhaul of Limitorque Model

SMB-000 Through SMB-00 and SB-00, dated October 21, 1988.

Procedure EMP-C-MOV-18, Safety Related MOVs - Repair, Replacement,

Checkout and Adjustments, dated October 11, 1988.

Procedure EMP-L-MOV-11, Disconnect and Reconnect Safety Related MOVs,

dated October 10, 1988.

Procedure EMP-C-MOV-151, Testing MOVs Using MOVATS System; dated

March 10, 1989.

Procedure SUADM-M-08, Repair/Replacement Program, dated January 26,

1989.

Procedure EMP-L-MOV-198, Testing Butterfly MOVs using MOVAT BART

System, dated March 4, 1989.

The following comments are based on the inspector review of the licensee's

MOV procedures:

l

11

Procedure

MMP-C-MOV-178 contains actuator illustrations with

reassembly instructions. Several of the illustrations were not clear

and; therefore, would not aid the mechanics during actuator

reassembly.

Procedure MMP-C-MOV-178.1, provides instructions for removal and

overhaul of Limitorque SMB-0,1,2,3,4 and SB-0,1,2,3,4 rising stem and

butterfly actuators.

These various types and sizes of actuators

contain significant differences.* In lieu of providing detailed

illustrations, the procedure references the Limitorque

SMB

Instruction and Maintenance Manual.

For SB actuators; however, the

Limitorque maintenance manual is not referenced by the procedure.

Procedure SUADM-M-08 provides MOV retest requirements following IE

Bulletin 85-03 valve maintenance.

The retest requirements appear to

be adequate if adhered to.

Step 3.8.1.3c in this procedure allows

the Superintendent of Engineering, with the coordination with the

Superintendent of Operations or their designees, to modify these

retests requirements when plant conditions make retest performance

impractical.

As previously discussed in paragraph 2.a(2), MOVATS

testing of valve 2-CH-MOV-2289B was not performed following limit

switch adjustment which is contrary to Procedure SUADM-M-08

guidelines.

Within the areas inspected, violations or deviations were not identified.

4.

Power Operated Valves Inservice Stroke Time Testing (73756)

The criteria for stroke time testing power operated valves is contained in

Section XI of the American Society of Mechanical Engineer (ASME) code.

The licensee is committed to the 1980 edition of Section XI.

The stroke

times for the following MOVs from 1986 were reviewed by the inspectors:

2-CH-MOV-2289A

2-CH-MOV-22898

1-FW-MOV-160B

2-CH-MOV-2115B

1-RC-MOV-1535'

1-RC-MOV-1536

2-RC-MOV-2535

2-RC-MOV-2536

2-FW-MOV-251A

1-FW-MOV-1510

1-SW-MOV-105A

2-SW-MOV-204B

1-SI-MOV-1842

Review of these MOV stroke time results indicated that the stroke

frequency requirements required by Section XI of the ASME Code were met.

The only deficiencies noted were the licensee's corrective action involving

an MOV initially failing to stroke fully open or closed, initial stoke

time exceeded the maximum allowed, and adjusting the of limit switches to

shorten valve stroke to obtain the desired stroke time results.

When a

MOV fails to stroke initially fully open or closed or if the stroke time

is excessive, it had been previous licensee practice to stroke the valve

two more times.

If these two stroke times were acceptable, then the valve

was returned to service.

In early 1988 the resident inspector informed

12

the licensee that this practice was not in accordance with ASME Section XI

requirements.

As result, the 1 i censee now requires that a station

deviation be generated if a valve initially fails the first attempt, but

subsequently passes two additi ona 1 stroke time tests.

The station

deviation must be evaluated with 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of the initial failure. If the

reason for the first failed attempt cannot be corrected, then the valve

will be declared inoperable.

The valves that failed initial stroke

testing were 2-CH-MOV-2289A, 2-CH-MOV-22898, and 1-RC-MOV-1536.

These

valves were subsequently stroke time tested satisfactory on second and

third attempts and returned to service.

These initial stroke failures

occurred prior to licensee's corrective action in response to the resident

inspector's findings.

The inspectors also noted instances where

corrective action for excessive stroke times involved adjusting of valves

2-CH-MOV-2289A and B open and/or closed limit switches.

Station records

that accomplished limit switch adjustments for these valves did not

provide enough information to confirm that limit switches were actually

out of adjustment oi if limit switches were adjusted to shorten valve

stroke; however, the valves did have a history of exceeding stroke time

limits or just barely passing stroke time testing specifications.

In paragraph 2.a, a violation was issued when valves 2-CH-2289A and B were

identified as examples of valve deficiencies where sufficient corrective

action was not taken.

Within the areas inspected, no violations or deviations were identified.

5.

Exit Interview

The inspection scope and results were summarized during a telephone

conference call on April 4, 1989, with those persons indicated in

paragraph 1.

The inspectors described the areas inspected and discussed

in detail the inspection results listed below.

Proprietary information is

not contained in this report.

Dissenting cornnents were not received from

the licensee.

Violation 280,281/89-10-01, was identified for failure to take corrective

action in response to MOV deficiencies, paragraph 2.a.

The licensee committed fo the NRC to provide in writing details of the MOV

recovery program, and to review MOVATS test reports issued prior to 1988,

paragraph 2.b .