ML18153A798

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Insp Repts 50-280/95-06 & 50-281/95-06 on 950305-0401. Violations Noted.Major Areas Inspected:Plant Status,Maint & Surveillance Insps,Operational Safety Verification,Plant Support & Action on Previous Insp Items
ML18153A798
Person / Time
Site: Surry  Dominion icon.png
Issue date: 04/13/1995
From: Belisle G, Branch M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153A796 List:
References
50-280-95-06, 50-280-95-6, 50-281-95-06, 50-281-95-6, NUDOCS 9504240045
Download: ML18153A798 (18)


See also: IR 05000280/1995006

Text

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/95-06 and 50-281/95-06

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

March 5 through April 1, 1995

Lead Inspector: £_ ltJJc~ ~

M: W. Branch, Senior Resident Inspector

'f-1J-pS-

Date Signed

Inspectors:

D. M. Kern, Resident Inspector

S. G. Tingen, Resident Inspector

Approved by:

G."~~Chief

Reactor Projects Section 2A

Division of Reactor Projects

SUMMARY

Scope:

r /;;;, ~--

~

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, surveillance

inspections, plant support, action on previous inspection items, and on-site

engineering.

Inspections of backshift and weekend activities were conducted

on March 10, 19, 20, 21, 28 and 30, 1995.

Results:

Operations

A violation was identified for exceeding the 100 degrees F per hour technical

specification pressurizer heatup rate on February 4, 1995, during a Unit 2

shutdown evolution (paragraph 7.2).

9504240045 950414

PDR

ADOCK 05000280

G

PDR

2

Maintenance

Work plan development on the Unit 2 main generator Voltage Regulator {VR)

repair, and return of the VR to automatic control were performed in a

professional manner {paragraph 4.1).

During Unit 2 Motor Operated Valve (MOV) testing, operators followed

procedures, craft were knowledgeable of the MOV diagnostic test equipment, and

the system engineer efficiently coordinated the efforts of operations and

craft personnel while performing the test (paragraph 5.1).

An apparent violation, pertaining to Unit 2 power operation from June 24, 1994

to February 3, 1995, with three channels of low pressurizer pressure reactor

trip protection and three channels of low-low pressurizer pressure Engineered

Safeguards Action instruments inoperable was identified (paragraph 5.2).

Engineering

Nuclear engineers and operations personnel communicated effectively to

maintain plant parameters within prescribed conditions for physics testing

(paragraph 3.2).

Plant Support

During the Unit 2 refueling outage, station personnel provided appropriate

focus to minimize personnel exposure and solid waste generation

(paragraph 6) .

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Benthall, Supervisor, Licensing
  • H. Blake, Jr., Superintendent of Nuclear Site Services
  • R. Blount, Superintendent of Maintenance
  • M. Bowling, Manager Nuclear Licensing

D. Christian, Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

D. Erickson, Superintendent of Radiation Protection

  • R. Garner, Outage & Planning

B. Hayes, Supervisor, Quality Assurance

D. Hayes, Supervisor of Administrative Services

  • D. Llewelyn, Superintendent, Nuclear Training

C. Luffman, Superintendent, Security

  • J. McCarthy, Assistant Station Manager
  • A. Price, Assistant Station Manager
  • S. Sarver, Superintendent of Operations

K. Sloane, Superintendent of Outage and Planning

  • E. Smith, Site Quality Assurance Manager
  • D. Sommers, Supervisor, Corporate Licensing

T. Sowers, Superintendent of Engineering

  • S. Stanley, Supervisor, Station Procedures
  • J. Swientoniewski, Supervisor, Station Nuclear Safety
  • T. Williams, Manager QA

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

NRC Personnel

  • M. Branch, Senior Resident Inspector

D. Kern, Resident Inspector

S. Tingen, Resident Inspector

  • A. Belisle, Section Chief
  • Attended Exit Interview

Acronyms used throughout this report are listed in the last paragraph.

2.

Plant Status

Unit 1 operated at full power for the entire inspection period .

Unit 2 started the inspection period with the reactor in cold shutdown.

A RFO was in progress. Reactor startup began on March 19 and the

2

turbine was ~laced on-line on March 21.

The Unit 2 RFO was completed in

47 days.

The unit was operating at full power at the close of the

inspection period.

3.

Operational Safety Verification (71707, 61710)

The inspectors conducted frequent tours of the control room to verify *

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability. Frequent plant*

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

3.1

Unit 2 Containment Walkdown

On March 14, the inspectors walked down the Unit 2 containment.

All RFO maintenance was complete and the inspectors verified that

containment was in a condition to support unit operation.

The

inspectors verified that the containment sump was clean and that

the remaining containment areas were reasonably free of debris.

The inspectors concluded that the overall condition of the

containment was adequate.

During previous inspections the inspectors have questioned the

acceptability of plant operation with the refueling transfer canal

drain valves closed (see NRG IR 50-280, 281/94-31).

The

inspectors verified, prior to the Unit 2 startup, that refueling

transfer canal drain valves (RL-11 and 12} were open based on a

valve lineup dated March 10, 1995.

3.2

Unit 2 Startup from Refueling Outage

The inspectors observed Unit 2 startup and low power physics

testing activities on March 19-21.

Communications and control of

activities within the control room were good.

This was the first

reactor startup following core reload. Operators were briefed to

anticipate criticality at any point during the startup and to

closely monitor the performance of a new IRNI detector which had

been replaced during the outage. Criticality was achieved very

close to the estimated critical position. Reactor power was

stabilized at approximately 1% power for physics testing.

Nuclear engineers conducted a detailed pre-evolution brief for low

power testing. Operators' questions regarding allowed plant

conditions were clearly answered. Several IRPis did not track

3

properly with control bank movement during physics testing.

Operators appropriately halted testing and had the IRPis adjusted

to match control rod bank demand position. Engineers verified

that the effected control rods were correctly positioned and were

not misaligned as the IRPis had indicated. The inspectors

observed that nuclear engineers and operations personnel

communicated effectively to maintain plant parameters within

prescribed conditions for physics testing.

The inspectors observed turbine startup and vibration monitoring.

Control room operators communicated closely with vendor personnel

during turbine roll-up to verify acceptable turbine vibration.

Operators exercised due caution when performing front panel trip

checks.

The turbine was placed on-line at 5:28 a.m., on March 21.

Operators manually maintained steam generator levels as the

turbine was loaded.

Within the areas inspected, no violations or deviations were identified.

4..

Maintenance Inspections {62703}

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

4.1

Unit 2 Main Generator VR Repair

The main generator exhibited voltage instability following unit

startup. Engineers and vendor personnel formed a VR task team to

identify the cause and recommend action to correct the voltage

instability. The team determined that vendor personnel had not

properly connected generator field forcing overexcitation

protection circuitry during outage maintenance activities. The

inspectors monitored resulting corrective maintenance activities

to verify appropriate measures were established to preclude

tripping the unit.

On March 29, the VR task team presented their findings and a

corrective maintenance work plan to SNSOC for approval.

SNSOC

closely reviewed the team findings and thoroughly questioned each

aspect of the on-line repair plan. Discussions included VR

cabinet vibration, positive identification of relays and contacts,

ICCE process controls, lessons learned from previous Unit 1 VR

work, worker communications, and interfaces between the station

and the off-site grid load dispatcher.

The inspectors observed

that SNSOC carefully evaluated whether the repair should be done

on-line or with the unit off-line. The decision to perform the VR

repair on-line and the detail of the work plan were sound.

The inspectors observed the repair prebrief and the corrective

maintenance to the VR circuits. An additional reactor operator

was assigned to operate and monitor the main turbine generator

4

controls in the control room.

Communications were established

between this reactor operator and the repair crew in the turbin~

building. Operations personnel coordinated closely with the load

dispatcher when shifting the VR from automatic control to base

load control to support the repair. The system engineer led the

repair effort and closely directed maintenance personnel through

all portions of the repair plan.

The inspectors particularly

noted excellent step by step communications between the system

engineer and the electricians in the high noise work environment

at the VR control cabinet.

The inspectors concluded that work

plan development, VR repair, and return of the VR to automatic

control were performed in a professional manner.

4.2

Review of Work Controls and Streamlining Efforts

In order to expedite work processes, several new initiatives were

implemented during the Unit 2 RFO in the area of MOV testing and

breaker maintenance.

MDAP-0002, Conduct of Maintenance, revision

2 was changed to allow the craft to review and sign MOV diagnostic

partial clearance forms, remove/install danger tags, and operate

the required breaker to energize MOVs in order to perform

diagnostic testing. Partial clearances were previously performed

by operations personnel.

MDAP-0002 was also revised to allow the

craft to relocate danger tags when removing and installing a

breaker in order to perform maintenance.

The inspectors verified

that craft personnel were trained on these new work process

methods.

The inspectors also reviewed deviation reports initiated

during the RFO due to tagging discrepancies and verified that

these new initiatives in danger tagging did not result in any DRs.

4.3

Modification to Waterproof MOV Operators

On March 5 through 9, the inspectors monitored portions of

DCP 93-17-03, Modify CW Limitorque Motor Operators to be *

Submersible, Surry/Units 1 and 2, field change 8. This design

change modified the eight condenser CW inlet MOV actuators to make

them watertight. Watertight actuators would enhance MOV operation

if these actuators were to become submersed in water during a

turbine building flood.

The inspectors witnessed the

modifications implemented by the design change and testing

associated with 2-CW.-MOV-206D.

The design change was accomplished

by WO 284426-01 and O-ECM-1504-01, Limitorque SMB Type MOV

Operator Maintenance, revision 1.

After the actuator was modified, an air drop test was performed.

The actuator was pressurized to 4.5 psig and the acceptance

criteria was that pressure could drop no more than .5 psig within

one hour.

The actuator failed the air drop test and a new motor

was installed. The air drop test was then satisfactorily

performed. The inspectors walked down the other CW inlet MOV

actuators and verified that they had been modified to be

watertight.

No deficiencies were noted.

5

4.4

Review of Unit 2 WO Backlog

Prior to the Unit 2 RFO on February 3, 1995, the inspectors

reviewed the licensee's WO backlog status. Prior to the outage,

Unit 2 had 3277 open WOs of which 2360 WOs were classified as

outage related and 824 WOs were classified as non-outage related.

After the outage completion, there were 1189 open WOs of which 401

WOs were classified as outage related and 788 WOs were classified

as non-outage related. The inspectors concluded that the licensee

was effectively tracking their WO backlog.

WOs were not

reclassified to reduce outage work scope.

4.5

Review of Selected RFO Maintenance and Testing Activities

During previous Unit 2 power operations, equipment degradation and

failures resulted in either plant transients or off-normal plant

operations. During this RFO, the inspectors monitored selected

maintenance and testing activities associated with correcting

these equipment problems.

Previously jumpered cell 52 and 17 other cells were replaced in

Station Battery 2A.

Work was performed per WO 303202-01 which

invoked procedure O-ECB-D102-0l, Large Exide Stationary Battery

Cell Replacement, revision 1.

IRPI coils for rods L-11 and M-10 were replaced per WO 301913-01

and 303204-01, respectively, using procedure O-ECM-1902-06, CRDM

and RPI System Maintenance, revision O.

During the disconnection

of the CRDM and IRPI cables to support refueling, the electricians

noted that several cables had heat damage.

The damaged cables

were sleeved with RayChem Kits which repaired the insulation

damage.

During the RFO, CRDR enhancements associated with main control

board single filament indicator bulb testing and replacement were

implemented.

New bulbs were tested (WO 313440-01} prior to

replacement.

The old bulbs were also tested as part of the

process and no failures were identified. There were 11 bulbs

involved in this maintenance activity.

The inspectors verified that Operations personnel were monitoring

the component cooling system radiation monitor when the Unit 2

excess letdown heat exchanger was pressurized during the ISI

hydrostatic test. Based on a review of station records, no alarms

were received when the heat exchanger was pressurized which

indicated tube integrity in the heat exchanger.

Within the areas inspected, no violations or deviations were identified.

6

5.

Surveillance Inspections (61726)

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedural and TS

requirements.

5.1

MOV DP Testing

On March 13, the inspectors witnessed the performance of

2-PT-25.1, Quarterly Testing of CW and SW System Valves,

revision 3. This test verified that valves 2-SW-MOV-202A and B

would shut at maximum DP.

The test was being accomplished to meet

the requirements of GL 89-10, Safety-Related Motor-Operated Valve

Testing and Surveillance, dated June 28, 1989.

In order to obtain

maximum DP across the valves, intake canal level was raised to a

level of 30 feet and the piping downstream of the valves was

depressurized. The valves were instrumented with diagnostic test

equipment and satisfactorily opened during the test. Operators

followed the procedure, the craft was knowledgeable of the MOV

diagnostic test equipment and the system engineer efficiently

coordinated the efforts of .operations and craft personnel while

performing the test. The inspectors were informed by the system

engineer that thirteen valves were successfully DP tested during

the Unit 2 RFO.

5.2

Calibration Problems Associated With Unit 2 Pressurizer Pressure

Transmitters

5.2.1 Licensee's Identification and Evaluation of Problem

On February 10, 1995, during refueling calibrations, all

three Unit 2 Pressurizer Protection pressure transmitters

were found out of calibration. The Unit had been on line

continuously since June 25, 1994.

The as-found conditions

for the transmitters were:

2-RC-PT-2455 was high by 121 mv;

2-RC-PT-2456 was high 143 mv; and 2-RC-PT-2457 was high 152

mv.

These voltages correspond to 24 psig, 28.5 psig, and 30

psig above the allowable setpoint value. A root cause team

was formed to evaluate the event and determine the cause of

the unusually high indications. The following is a sequence

of events and a summary of that root cause evaluation:

Sequence of Events

May 12, 1994 - Bench calibration performed on all

three new Rosemount 1154 transmitters designated as

2-RC-PT-2455, 2456, 2457.

June 18, 1994 - After installion of the new

transmitters, I&C technicians performed a field

calibration. All three transmitters were found out of

calibration high and required adjustment.

Heise gage

M&TE #SQC-437 was used to perform the calibration.

7

June 21, 1994 - Heise gage SQC-437 was checked into

the Metrology Laboratory for its normal quarterly

calibration check.

No problems were found.

June 24, 1994 - Operations noted that all three

protection channels were indicating lower than control

channels and DR S-94-1352 was written.

Test gage

SQC-437 was used to perform calibration check on all

three Pressurizer Pressure Protection transmitters.

All three transmitters were found out of calibration

low and required adjustments.

June 24, 1994 - Unit 2 Critical

June 25, 1994 - Operations received pressurizer

pressure alarms and noted that protection channels

were reading approximately 15 - 20 psig higher than

the control channels.

June 28, 1994 - Heise gage SQC-437 was returned to the

Metrology Laboratory for calibration check.

The gage

was found to be nonrepeatable and low at the high end.

February 10, 1995 - During refueling calibrations, all

three Pressurizer Pressure Protection transmitters

were found out of calibration high and required

adjustment.

Licensee's RCE

The licensee's RCE determined that the most probable

cause of the calibration error was the use of a non-

temperature compensated test.gage. Test gage

calibrations were affected by 3 psig/5 degrees F

change from 73 degrees F.

This resulted in an

estimated 24 psig error. Additionally, the gage was

identified as binding due to inadequate torque during

the manufacturing process.

The licensee also

determined that a contributing cause was inadequate

training in using compensated/noncompensated gages.

5.2.2 Inspectors' Review and Assessment of Causes

The inspectors reviewed the licensee's RCE and supporting

information.

Based on vendor information from the test gage

supplier, a non-temperature compensated gage could

contribute to a calibration error as much as 3 psig/5

degrees F change from the reference calibrated temperature

of 73 degrees F.

The inspectors reviewed operator's logs

for temperature in containment.

The logs reviewed did not

provide an ambient temperature during shutdown.

However,

other data indicated that ambient conditions were at the

8

reference temperature.

Containment temperature during hot

shutdown and power operations is normally between 100 - 115

degrees F and therefore the licensee's assumptions of error

associated with use of a non-temperature compensated gage

was reasonable.

The licensee used the same non-temperature compensated test

gage to calibrate all three pressurizer pressure channels

and along with minor binding of the bourdon tube resulted in

the (worst case of the three) pressure transmitters reading

approximately 30 psig greater than actual pressure.

After determining that non-temperature compensated test

gages were in the M&TE system, the licensee confiscated all

these type gages and locked them up.

The RCE also.

determined that the licensee had to flush all gages that had

been used in contaminated systems prior to release to the

non-contaminated calibration facility for calibrations.

The inspectors reviewed the two DRs issued by operations

when the instrument error was initially identified in June

1994.

The first DR (S-94-1352) was dispositioned by

maintenance as a personnel error associated with

difficulties in reading the test gage during calibration

while in a respirator. The second DR (S~94-1353), issued

after alarms were received during unit startup, was closed

out due to the corrective actions of DR S-94-1352.

These

two DRs provided early opportunities for recognition and

correction which could have prevented unit operation with

degraded pressurizer pressure channels.

Another opportunity to identify and correct the above

condition occurred when M&TE test gage SQC-437 was found out

of calibration on June 28, 1994.

Had the intent of

VPAP-1201, Control of M&TE, revision 2, been followed, a re-

calibration of the three pressurizer pressure transmitters

would have occurred with a different test gage.

Specifically, the following requirements of VPAP 1201 were

not followed:

1) Section 6.3.2.b states, "The reliability and

accuracy of M&TE may be affected based on

environmental conditions (e.g., temperature extremes,

high humidity, etc.) The use of M&TE in such

environmental conditions shall be in accordance with

manufacturer's equipment specifications". This was

not done.

2) Section 6.6 requires an evaluation be performed

whenever M&TE is found out of calibration. The stated

purpose of the evaluation was to review the impact of

the out-of-spec readings on plant equipment that may

9

have been calibrated with questionable M&TE.

The as-

found error of the M&TE is required to be compared

against the tolerance of the plant equipment

calibration procedure.

If the M&TE error exceeds the

allowable tolerance of the acceptance criteria for the

plant equipment, then the calibration is invalid and

must be repeated if justification to do otherwise

cannot be found and documented.

The evaluation

performed when M&TE test gage SQC-437 was found out of

calibration on June 28, 1994, did not require a re-

calibration of affected plant equipment and attributed

the problem to disassembly of the test gage for

decontamination which is prohibited by Section

6.4.4.e.2 of VPAP 1201.

5.2.3 Review of Safety Significance

The February 10, 1995, as-found calibration error associated

with each of the three pressurizer pressure transmitter£ was

evaluated by electrical engineering.

The inspectors

reviewed this evaluation dated February 20, 1995.

The

evaluation compared the actual calibration error found for

each transmitter with the error assumed in the instrument

set-point calculation.

The transmitter error was tabulated

along with other instrument loop errors to determine the

overall error associated with the reactor trip and ESA

channels.

The impact of the instrument loop error on low

pressurizer pressure reactor trip and low-low pressurizer

pressure ESA events was calculated. The margin between the

value used in the SA and the actual pressure where the

channel would actuate the safety function was determined ..

In all cases, the TS allowable values and SA values were

exceeded and, therefore, the pressure channels were

inoperable. The worst case low pressurizer pressure reactor

trip point was 21.38 psig below the 1850.3 psig used in the

SA and the worst case low-low pressurizer pressure ESA was

31.38 psig below the SA value of 1700.3 psig.

The worst

case values were rounded to 22 psig and 32 psig and this

information was provided to the licensee's NAF group for

review.*

The NAF review was documented in ET no. NAF-95031,

Evaluation of Impact on Safety Analyses Pressurizer Pressure

Transmitters for RPS Input, Surry Power Station, Unit 2,

revision 0. This evaluation analyzed the impact of the

worst case setpoint errors on the SA for DNB plant

transients, steam line break, and large and small break

LOCAs.

The evaluation determined that the worst case error

would result in a slight reduction of SA margin but was

still bounded by the SA for the cycle 12 operation (the

period of time that the instruments were

10

inoperable). The NRC questioned why ET NAF-95031, revision

0, did not review the error's impact on a SG tube rupture

event. This was discussed with the licensee and NAF-95031

was revised to include this information without changing the

results of the review.

The inspectors, along with other NRC

staff, found the licensee's safety impact review .acceptable.

5.2.4 Regulatory Issues

Technical Specifications 3.7.8 which references TS Table

3.7-1, and TS 3.7.C which references TS Table 3.7-2,

requires that Reactor Protection and Engineered Safeguards

Action channels and interlocks be operable as specified in

their respective tables.

TS Table 3.7-1, item 7, including

Operator Action 7 requires a minimum of 2 out of 3 Low

Pressurizer Pressure Reactor Trip channels be operable for

power operation.- TS Table 3.7.2, item l.d, including

Operator Action 20 requires a minimum of 2 out of 3

Pressurizer low-low pressure channels be operable for power

operations.

In summary, because of instrument calibration errors, Unit 2

operated at power from 9:25 pm on June 24, 1994, to 3:08 am

on February 3, 1995, with all three pressurizer low pressure

reactor trip and pressurizer pressure low-low ESA channels

inoperable. This item is identified as Apparent Violation

EEI 50-281/95-06-0l, Operation With All Three Channels of

Pressurizer Pressure Low Reactor Trip and Pressurizer

Pressure Low-Low ESA Inoperable.

Within the areas inspected, one apparent violation was identified.

-6,

Plant Support (71750)

The station established radiological performance goals for volume of

sold waste generated and cumulative personnel radiation exposure.

Station management remained actively involved in tracking performance

indicators to assess RP performance throughout the outage.

The

inspectors attended daily work status briefings and frequently toured

Unit 2 radiological work areas to observe RP practices.

RP technicians

provided comprehensive job coverage throughout the outage.

Both the

personnel exposure and solid waste generation goals were achieved.

The

total personnel exposure for the RFO was 157.7 Rem whfch is the lowest

RFO exposure achieved to date.

The inspectors concluded that station

personnel provided appropriate focus to minimize personnel exposure and

solid waste generation.

Within the areas inspected, no violations or deviations were identified.

.*

11

7.

Action on Previous Inspection Items (92901, 92902}

7.1

(Closed} VIO 50-280/93-23-01, Fuse Removal Not Accomplished in

Accordance with Tagging Record and OPAP-0010.

This issue involved electricians removing and danger tagging the

wrong fuses when establishing isolation for a maintenance

evolution.

In a letter dated November 19, 1993, the licensee

stated that electricians were not adequately trained or properly

qualified to install and verify electrical danger tags and that

the station tagging policy was revised to only allow Operations

personnel to install/remove electrical or mechanical danger tags.

The inspectors reviewed the station tagging policy contained in

VPAP-1402, Control of Equipment, Tag-Outs and Tags, revision 2,

OPAP-0010, Tag-Outs, revision 4, and MDAP-0002 and concluded that

the station policy to allow Operations personnel to install/remove

electrical or mechanical danger tags had been revised to allow

electricians to install/remove electrical danger tags in certain

instances.

VPAP-1402, Paragraph 4.2, discussed when electricians

are allowed to remove/install danger tags. The inspectors also

verified that electricians were trained. The inspectors concluded

that the revised policy was acceptable in that electricians were

thoroughly trained.

7.2

(Closed} URI 50-281/95-03-01, Unit 2 Pressurizer Excessive Heatup

Rate

On February 4, 1995, pressurizer heatup rate exceeded the 100

degrees F per hour TS limit during an RCS degas evolution. The

licensee identified that a 146 degrees F pressurizer heatup

occurred in one hour as operators adjusted charging flow to

maintain pressurizer level. Appropriate immediate actions were

taken to stop the pressurizer heatup and procedure revisions were

initiated to more clearly alert operators to the potential for

excessive heatup/cooldown during degas operations. This issue

remained unresolved pending inspector's review of the pressurizer

fatigue analysis.

IR 50-280, 281/95-03 discussed in detail the conditions that

caused the pressurizer heatup event.

Based on recent industry

events the licensee had modified their procedure to increase

operator sensitivity to pressurizer thermal transients. During

this event, operators had successfully terminated an unexpected

pressurizer cooldown because of their increased sensitivity to

thermal transients. However, plant conditions established for RFO

electrical surveillance testing hampered the operator's ability to

effectively control this event to prevent exceeding TS limits.

The licensee recently indicated that an industry group is

currently reviewing known startup and shutdown plant evolutions to

determine if better controls can be established to prevent future

events of this nature.

12

The vendor performed a pressurizer fatigue analysis to assess the

effects of the excessive heatup on pressurizer integrity. Station

records did not document pressurizer temperatures on an hourly

basis. Therefore, the licensee established 40 similar heatup

transients as a bounding case to account for potential excess

heatups during the current 40 year license. The inspectors

determined that this assumption was valid. The fatigue analysis

determined that the pressurizer inner wall was the limiting

component and concluded that cumulative fatigue was within

pressurizer design.

The resident inspectors discussed the fatigue

analysis with licensee personnel. It was determined that the

analysis was technically sound and that the fatigue associated

with this event was within pressurizer design.

TS 3.1.B.3 requires that pressurizer heatup rate not exceed 100

degrees F per hour.

On February 4, 1995, from 10:30 a.m. to 11:30

a.m., the Unit 2 pressurizer temperature increased 146 degrees F

(from 254 to 400 degrees) in one hour.

This excessive heatup is

identified as VIO 50-281/95-06-02, Pressurizer Excessive Heatup

Rate.

Within the areas inspected, one violation was identified.

8.

On-Site Engineering (37551)

8.1

Unit 2 HHSI Pump Motor Evaluation

NRC IR 50-280, 281/95-03 discussed a design issue associated with

the power requirements for the Unit 2 C HHSI pump motor. Testing

identified that the maximum motor power requirement was 711 HP

which exceeded the design value of 690 HP.

The motor

manufacturer, Westinghouse, was, contacted and evaluated motor

operation at 711 HP.

The inspectors reviewed Engineering Report CEE 95-23, HHSI Pump

Motor Overduty, dated March 10, 1995.

The report concluded that

the motor was operable and that EDG loading would not exceed the

2000-hour rating. The inspectors reviewed the Unit 2 HHSI pump

head curve and noted that the flow rates obtained during the

latest and previous flow rate tests were within twenty GPM of the

curve.

The inspectors concluded that small flow deviations from

the pump head curve resulted in large changes in motor power

requirements.

The inspectors also concluded that the licensee

satisfactorily resolved this issue prior to Unit 2 restart.

8.2

Pressure Locking of PWR Containment Sump Recirculation Gate Valves

(NRC TI 2515/129)

The inspectors reviewed the licensee's activities to evaluate

susceptibility of the CSRSVs (1-SI-1860A/B and 2-SI-1860A/B) to

the pressure locking phenomenon. These valves are designed to

13

open and provide a flow path from the containment sump to the LHSI

pumps for long term decay heat removal following a design basis

LOCA.

Initial assessment by the licensee indicated that the likelihood

of pressure locking would be greatly reduced or eliminated by

maintaining the containment sump suction piping full of water.

The containment sump suction piping and CSRSVs are located at a

lower elevation than the containment sump.

Operations personnel

visually verified the presence of water in the Unit 2 containment

sump and associated piping prior to restart. Engineers observed

water in the Unit 1 containment sump during the December 1994

outage. Operations and engineering personnel are developing a

plan to verify water in the containment sump during periodic

containment entries while at power and prior to each unit startup.

Engineering initiated a UFSAR change to document this design basis

configuration change.

The inspectors determined that these

actions were appropriate pending completion of a formal

engineering evaluation regarding susceptibility to CSRSV pressure

locking.

The licensee performed engineering evaluation ET CME 95-0018,

Engineering Review of OE 7107, revision 0, to evaluate

applicability of CSRSV pressure locking at Surry Station. The

evaluation concluded that l-SI-1860A/B and 2-SI-1860A/B were not

susceptible to pressure locking provided that the piping between

the containment recirculation sump and these valves was maintained

full of water.

The inspectors independently reviewed ET CME 95-

0018, the UFSAR, interviewed personnel, and visually inspected

associated valves and piping to evaluate the licensee's

conclusions.

The inspectors determined that assumptions used in evaluating ET

CME 95-0018 were generally conservative.

Assumed initial and post

DBA LOCA containment sump temperatures were more severe than

specified in the UFSAR.

The inspectors reviewed station drawings

and *visually inspected suction piping in the valve pits. The

actual piping length from the containment sump to the suction

valves was greater than assumed in the evaluation. Additionally,

credit was not taken for heat dissipation from the suction piping

to the surrounding concrete embedment.

Worst case assumptions

were also factored for valve seat leakage, packing leakage, and

presence of water inside the valve bonnet.

The resulting

calculated heatup rate inside the valve bonnet was 0.2 degrees F

per hour.

Engineering determined that the DBA LOCA leakrate would

necessitate shifting from LPCI to LPCI recirculation mode within 1

hour of the accident start. This resulted in a 0.2 degrees F

heatup of the water inside the valve bonnet and a maximum bonnet

pressure of 52 psig when the valve would be required to open.

The

evaluation concluded that valve operator design was sufficient to

overcome this amount of pressure within the bonnet.

14

The inspectors observed that the heat transfer calculations within

ET CME 95-0018 were technically sound.

However, the evaluation

did not address heat transfer to and from the atmosphere

surrounding the valve or heat transfer from the sump to the valve

via the piping metal.

Engineering informed the inspectors that ET

CME 95-0018 would be revised to address this concern.

Subsequent

to the inspection period, ET CME 95-0018 was revised and reviewed

by the inspectors. The inspectors concluded that the licensee's

actions to evaluate and address CSRSV pressure locking were

appropriate.

8.3

Shutdown Risk Assessment

SNS engineers performed an independent safety assessment of the

outage activity schedule in accordance with VPAP-2805, Shutdown

Risk Program, revision 1, to support safe integration of Unit 2

RFO maintenance activities. The Unit 2 Refueling Outage

Assessment Report was completed and distributed prior to the start

of the RFO.

The inspectors reviewed VPAP-2805, the Outage

Assessment Report, the outage work schedule, and daily

reassessments of safety critical parameters during the outage to

determine whether shutdown risk was properly managed.

VPAP-2805 provided detailed guidance regarding shutdown safety

system availability criteria. Several system requirements, in

addition to TS requirements, were specified to implement a defense

in depth philosophy.

The supplemental safety system requirements

encompassed decay heat removal, RCS inventory addition, reactivity

control, electrical power sources, and SFP operations.

The inspectors reviewed the Outage Assessment Report and observed

that scheduled activities which had the potential to degrade

critical shutdown safety attributes below established acceptance

criteria were clearly identified and evaluated.

Where

appropriate, the outage activities were rescheduled to maintain

acceptable availability of critical safety equipment.

One example

was a conflict between the monthly #3 EOG operability surveillance

test and maintenance on the B RSST.

Maintenance on the B RSST

required both Unit 2 4160 volt emergency buses to be supplied from

the C RSST.

The #3 EOG was the only available emergency power

supply to these buses in the event the C RSST. failed.

Unavailability of a backup power supply to the Unit 2 emergency

buses was identified as an unacceptable condition.

The #3 EOG

surveillance was rescheduled to eliminate this conflict. The

inspectors determined that the outage schedule had been thoroughly

evaluated and revised where appropriate to provide acceptable

defense in depth.

The outage schedule was frequently revised to accommodate

resource, work scope, and activity duration changes.

The licensee

used a computer application to assist in developing the Outage

Assessment Report.

The computer model tracked the impact of

.------:-...,....,,....----------------------------------------


al .~

, ***

15

outage activities on critical safety parameters including

reactivity, core cooling, electrical power availability,

containment, and RCS integrity.

SNS engineers effectively used*

this model to reassess the schedule on a daily basis during the

outage.

The inspectors reviewed selected daily shutdown safety

assessments and the resulting addendum to the Outage Assessment

Report.

Schedule revisions were evaluated in a timely manner and

addendum to the Outage Assessment Report were issued before the

schedule changes became effective. The inspectors concluded that

SNS review of outage activities was comprehensive and the licensee

had properly managed shutdown risk.

Within the areas inspected, no violations or deviations were identified.

9.*

Exit Interview

10.

The inspection scope and findings were summarized on April 5, 1995,

with those persons indicated in paragraph 1.

The inspectors described

the areas inspected and discussed in detail the inspection results

addressed in the Summary section and those listed below.

Item Number

Status

Description/(Paraqraph No.)

EEi 50-281/95-06-01

Open

Operation With All Three

Channels of Pressurizer

Pressure Low Reactor Trip and

Pressurizer Pressure Low-Low

ESA Inoperable

(paragraph 5.2).

VIO 50-281/95-06-02

Open

Pressurizer Excessive Heatup

Rate (paragraph 7.2).

VIO 50-280/93-23-01

Closed

Fuse Removal Not Accomplished

in Accordance with Tagging

Record and OPAP-0010

(paragraph 7.1).

URI 50-281/95-03-01

Closed

Unit 2 Pressurizer Excessive

Heatup (paragraph 7.2).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

Index of Acronyms

CFR

CROM

CRDR

CSRSV

cw

DBA

CODE OF FEDERAL REGULATIONS

CONTROL ROD DRIVE MECHANISM

CONTROL ROOM DESIGN REVIEW

CONTAINMENT SUMP RECIRCULATION SAFETY VALVE

CIRCULATING WATER

DESIGN BASIS ACCIDENT

~-

,**: .t '

,.

16

DCP

DESIGN CHANGE PACKAGE

DNB

DEPARTURE FROM NUCLEATE BOILING

DP

DIFFERENTIAL PRESSURE

DR

DEVIATION REPORT

ECCS

EMERGENCY CORE COOLING SYSTEM

EDG

EMERGENCY DIESEL GENERATOR

EEI

ESCALATED ENFORCEMENT ITEM

ESA

ENGINEERED SAFEGUARDS ACTION

F

FAHRENHEIT

GL

GENERIC LETTER

GPM

GALLONS PER MINUTE

HHSI

HIGH HEAD SAFETY INJECTION

HP

HORSEPOWER

ICCE

INFREQUENTLY CONDUCTED OR COMPLEX EVOLUTION

I&C

INSTRUMENTATION AND CONTROL

IR

INSPECTION REPORT NOS.

IRPI

INDIVIDUAL ROD POSITION INDICATION

IRNI

INTERMEDIATE RANGE NUCLEAR INSTRUMENT

ISI

INSERVICE INSPECTION

LHSI

LOW HEAD SAFETY INJECTION

LOCA

LOSS OF COOLANT ACCIDENT

LPCI

LOW PRESSURE COOLANT INJECTION

M&TE

MEASURING AND TEST EQUIPMENT

MOV

MOTOR OPERATED VALVE

MV

MILLIVOLT

NAF

NUCLEAR ANALYSIS AND FUEL

NRC

NUCLEAR REGULATORY COMMISSION

NRR

OFFICE OF NUCLEAR REACTOR REGULATION

PSIG

POUNDS PER SQUARE INCH GAGE

PWR

PRESSURIZED WATER REACTOR

QA

QUALITY ASSURANCE

RCE

ROOT CAUSE EVALUATION

RCS

REACTOR COOLANT SYSTEM

RFO

REFUELING OUTAGE

RP

RADIATION PROTECTION

RPI

ROD POSITION INDICATION

RPS

REACTOR PROTECTION SYSTEM

RSST

RESERVE STATION SERVICE TRANSFORMER

SA

SAFETY ANALYSIS

SFP

SPENT.FUEL POOL

SG

STEAM GENERATOR

SNS

STATION NUCLEAR SAFETY

SNSOC

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SW

SERVICE WATER

TI

TEMPORARY INSTRUCTION

TS

TECHNICAL SPECIFICATION

UFSAR

UPDATED FINAL SAFETY ANALYSIS REPORT

URI

UNRESOLVED ITEM

VR

VOLTAGE REGULATOR

VIO

VIOLATION

WO

WORK ORDER