ML18152B118

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Insp Repts 50-280/88-29 & 50-281/88-29 on 880718-22. Violations Noted.Major Areas inspected:post-refueling Startup Tests,Thermal Power monitoring,post-trip Reviews & Surveillance of RCS Leakage
ML18152B118
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/24/1988
From: Burnett P, Jape F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152B116 List:
References
50-280-88-29, 50-281-88-29, NUDOCS 8809070170
Download: ML18152B118 (6)


See also: IR 05000280/1988029

Text

.. ,

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/88-29 and 50-281/88-29

Licensee:

Virginia Electric and Power Company

Richmond, VA

23261

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.: DPR-32 and DPR-37

Inspection Conducted:

July 18 - 22, 1988

Inspector: ~

P.

. Burne

Approved bcd.£k~~

Jtt/ F. Jape, Section Chief

t

Engineering Branch

Division of Reactor Safety

SUMMARY

y-11-f<?"

Date Signed

Scope:

This routine, unannounced inspection addressed the areas of

post-refueling startup tests (Unit 1), thennal power monitoring, post-trip

reviews, and surveillance of RCS leakage.

Results:

One violation was identified, incorrect constants were used in the

surveillance procedure (1/2-PT-10) for RCS leakage measurement - paragraph 5.

Post-inspection, in-office review of the approved topical report on rod swap

methodology revealed differences in the post-refueling startup test program as

defined in that report and as actually performed.

The issue will be tracked as

an inspector followup item for further inspection - paragraph 2.

The licensee has installed new transient recorders (GETARs). The GETARs monitor

a total of 450 points on the two units. Since the installation, the post-trip

reviews have become more quantitative and more detailed, reflecting the

improved quality of transient data.

8809070170 80~8~~80

PDR

ADOC~

PNU

G.

I.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • D. L. Benson, Station Manager
  • R. H. Blount, II, Superintendent of Technical Services

T. R. Brookmire, Nuclear Engineer, Nuclear Fuel Operations

  • R. W. Cross, Nuclear Specialist

C. A. Ford, Nuclear Engineer, Nuclear Fuel Operations

  • G.D. Miller, Licensing Coordinator, Surry
  • H. L. Miller, Assistant Station Manager
  • J. A. Price, Manager, Quality Assurance

Other licensee employees contacted included engineers, operators, and

office personnel.

NRC Resident Inspector

  • W. E. Holland, Senior Resident Inspector
  • Attended exit interview

Acronyms and initialisms used throughout this report are defined in the

final paragraph.

2.

Post-Refueling Startup Tests - Unit I (72700, 61708, 61710)

Unit I was made critical for Cycle IO on July 14, 1988, using procedure

I-OP-IC.

.

Startup testing was performed under the guidance and control of 1-PT-28.11

(Issue of July 4, 1988 ), Startup Physics Testing and the approved Surry

1, Cycle 10, Refueling Physics Test Schedule.

The ARO C was 1567 ppmB,

which was less than the predicted 1610 pp~B, but within ~he performance

criterion of+/- 50 ppmB.

At ARO, both the ITC and MTC were negative, -3.2

pcm/°F and -1.52 pcm/°F, respectively.

Prior to rod worth measurements

by rod swap, control bank B was designated the reference bank and its

worth measured against boron dilution. The measured worth of control bank

B was 1134 pcm, which was within acceptable agreement with the predicted

worth of 1242 pcm.

All of the remaining control rod banks were within

acceptable agreement with prediction when measured by rod swap methods.

The sum of the measured worths and the predicted sum agreed within the

performance criterion.

2

PT-28.11 controls only the collection of data for the measurements.

The

analysis of test data is performed off site by the Nuclear Fuels Operation

Subsection.

That work is not controlled by procedures approved by the

SNSOC, but by task instructions approved by departmental management.

The

following task instructions pertinent to startup testing were reviewed:

1.1

Preparation for Physics Test (Revision 4, 10/7/87)

1.10

Readiness Checklist for Startup Physics Testing (Revision 3,

6/12/85)

2.1

Analysis of Hot Zero Power Rod Worth Data (Revision 5, 12/18/85)

2.2A

Rod Swap Design Data Generation (Revision 4, 12/18/85)

2.2B

Analysis of Hot Zero Power Rod Worth Data (Rod Swap) (Revision 4,

12/18/85)

2.3

Analysis of Boron Endpoint Data (Revision 6, 12/18/85)

2.4

Analysis of Boron Worth Coefficient Data (Revision 3, 12/18/85)

2.5

Analysis of Hot Zero Power Isothermal/Moderator Temperature

Coefficient Data (Revision 2, 12/12/84)

These instructions appeared to provide the level of detail and guidance

necessary for an appropriately trained ~uclear engineer to perform the

subject activities.

The instructions require peer review of data

production or analysis activities.

Subsequent to the on-site portion of the inspection, the licensee provided

a copy of their NRR-approved topical report on Control Rod Reactivity

Worth Determination by the Rod Swap Technique,

VEP-FRD-36 A,

December

1980.

During the in-office review of that report, it was noted that the

test program conducted for Surry 1, Cycle 10 did not contain all* of the

elements described in the report. Specifically, there was no measurement

of ITC with the reference bank inserted as called for in Section 2.2 item

3) and in Table A.2.

Equation 1 on page 7 is used to correct observed

data for differences from a reference calculation plant conditions.

The

adjustment for temperature changes utilizes the measured ITC obtained with

the reference bank inserted.

Table A.2 also calls for flux distribution

map to be made at zero power under rodded conditions.

No zero power flux

map was made under any conditions.

Neither of these deviations from the test program described in the topical

report have a significant effect on the measurement of rod worth.

There

would be a small error in rod worth if the RCS average temperature did

vary a few degrees F during the rod swap measurements and went

u.ncorrected*.

In practice, procedure 2.2B uses the predicted ITC.

The

zero power flux map has no bearing on rod worth results.

In fact few

licensees perform zero power flux maps after refueling, because, in

general, they have proved to be uninformative.

Nevertheless, the licensee

should have formally evaluated and possibly reported their decision to

deviate from the commitments in the approved topical report.

Actual

licensee action will be addressed in a future inspection (Inspector

Followup Item 280, 281/88-29-01).

Otherwise, comparison of NFOS ~rocedures 2.2A and 2.2B with the topical

report showed the approved methodology was being implemented.

3

3.

Core Thermal Power Evaluation (61706)

(Closed)Inspector followup item 280,281/86-40-02:

Review steam and

feedwater flow venturi calibration and reliability. This item stems from

the observation that steam flow was used as the basis for thermal power

measurement rather th1-2,t the more commonly used feedwater fl ow.

The

licensee

1s evaluation of the relative merits and reliability of the two

measurements is presented in their internal report, Surry Power Station

Secondary Plant Performance Evaluation, Phase 2,. issued in August 1984.

Review of that report indicates the selection of steam flow for power

measurement appears to be well founded.

This item is closed.

The report makes numerous recommendations for improvements in pl ant

performance, and two of them are specific to the use of steam flow mea-

surement.

The first was to write a new computer program for steam flow

that wou 1 d determine the average of the square roots of the fl ow dPs

rather than taking th'e square root of the average dP and would solve for

the thermodynamic state of the steam at the steam generator outlet. The

second was to install steam pressure taps 10 to 20 feet upstream of the

flow venturis in place of those 60 feet down stream. This was to enhance

the measurement of the thermodynamic state of the steam.

Discussion with

plant personnel revealed that the computer program had been written and

installed* as discussed above and that in addition it contained a correc-

tion for the steam pressure drop between the point of measurement and the

steam generator outlet.

The latter correction is in lieu of installing

new pressure taps.

The relative precision of the calibrations of the steam and feedwater flow

venturis was not addressed in this inspection.

No violations or deviations were identified.

4.

Review of Reactor Trips (6i707)

Three recent reactor trip reports were reviewed: Unit 1 on May 16, 1987

and February 16, 1988 and Unit 2 on May 16, 1988.

In all cases, the

average RCS temperature cooled significantly below the no-load setpoint of

547°F, the expected post-trip temperature.

The actual minimum

temperatures were 533, 539, and 525°F, respectively.

Administrative

procedure SUADM-0-02 ( Issued 11/5/87), Post Trip Review, requires in

section X.b(l) that RCS temperature, be analyzed and evaluated by compari-

son with expected values.

The reviews clearly identified the excessive

cool downs to be at variance with expected performance and some evalua-

tions of actions or modifications to limit cool down to 547°F were initi-

ated.

The reviews also referenced an October 25, 1985 study of Unit 1

trips on August 8, and September 9, 1985.

In that review, the first trip,

with steam dumps available, had excessive cool down, but the second

without steam dumps

did not cool below 540°F.

However, none of the

reviews specifically correlated the reduced temperatures with reductions

in shutdown margin or addressed shutdown margin in any way.

A member of

the plant staff did state that cool dpwn effects on shutdown margin had

4

been considered, but had not been significant enough to include in the

trip reports.

He also stated that, in the cycle design process, shutdown

margin was evaluated at 522°F, the minimum temperature for criticality

specified in TS 3.1.E.4.

Typical Surry cores have EOL shutdown margins of 3200 pcm. The TS required

shutdown margin is 1770 pcm.

Typical MTCs at EOL are about -35 pcm/°F.

Using these nominal values, the excess shutdown margin would be expended

by a post-trip cool down to 481°F, which is well below the experience to

date.

Currently the plant staff expect to receive an engineering evaluation of

means to limit cool down in time to implement corrective action during the

forthcoming Unit 2 refueling outage.

In December 1986, the licensee installed new transient recorders (GETARs)

on a trial basis and installed them permanently in May 1987.

The GETARs

monitor a total of 450 points on the two units.

Since the installation,

the post-trip review have become more quantitative and more detailed,

reflecting the improved quality of transient data.

No violations or deviations were identified.

5.

Reactor Coolant System Leakage Measurement (61728)

(Closed) Inspector Foll owup Item 280, 281/86-40-01: Revise procedures

1/2-PT-10 to incorporate all of the parameters required for surveillance.

The procedures were re-issued in October 1987, and now contain all of the

required parameters. This item is closed.

However, review of the genera ti on of some of the required parameters

revealed significant errors.

a.

The constant used for making a correction for a change in average RCS

temperature from the beginning to end of the RCS leakage measurement

is not based upon the change in the mass inventory in the solid RCS

volume.

In fact, no basis could be determined for the calculations

on the engineering work sheet used in generating the constant.

b.

The constant for equating changes in pressurizer level with changes

in RCS inventory was calculated on an engineering work sheet which

indicates the wrong distance between pressurizer level taps was used

in the calculation of monitored pressurizer volume.

There is no

correction in the calculation for the density difference in the

pressurizer and VCT fluids.

The two errors are not fully

compensating.

These errors have been identified as violation 280, 281/88-29-02: The

procedures for RCS leakage calculations contained errors in constants that

could lead to under estimating the leakage.

It was also noted that the

5

procedure does not require summing all sources of identified leakage for

comparison with the 10 gpm limit.

The inspector reviewed 19 examples of 1-PT-10 performed in January 1988,

and 5 of them had changes in either pressurizer level or temperature or

both, which required use of the constants discussed above.

Completed

copies of 2-PT-10 completed in May and June 1988 included four cases in

which one or both of the constants were used.

In none of the cases reviewed, would use of the correct constants have led

to a calculation of unidentifed leakage in excess of one gallon per

minute.

7.

Exit Interview

The inspection scope and findings were summarized on July 22, 1988, with

those persons indicated in paragraph 1 above.

The inspector described the

areas inspected and discussed in detail the inspection findings.

No

dissenting comments were received from the licensee. Proprietary materi-

als were provided to and reviewed by the inspector during this inspection,

but are not included in this report.

The licensee.was informed by tele-

phone on August 12, 1988 of the inspector followup item discussed in

paragraph 2.

8.

Acronyms and Initialisms Used in This Report

ARO

-

~~

EOL

-

GETAR-

ITC

-

MTC

-

NFOS -

NRR

-

OP

pcm -

ppmB -

PT

RCS

-

SNSOC-

TS

VCT

-

a 11 rods out

boron concentration

differential pressure

end of life

General Electric transient recorder

isothermal temperature coefficient

moderator temperature coefficient

Nuclear Fuel Operations Subsection

Office of Nuclear Reactor Regulation

operating procedure

percent millirho (unit of reactivity)

parts per million boron

periodic test

reactor coolant system

Station Nuclear Safety and Operating Committee

Technical Specification

volume control tank