ML18152A921

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Insp Repts 50-280/88-13 & 50-281/88-13 on 880425-29.No Violations or Deviations Noted.Major Areas Inspected: Radiological Environ Monitoring,Liquid & Gaseous Effluent Processing,Liquid & Gaseous Effluent Monitoring
ML18152A921
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/26/1988
From: Bermudez H, Kahle J, Stoddart P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A920 List:
References
50-280-88-13, 50-281-88-13, NUDOCS 8806070242
Download: ML18152A921 (12)


See also: IR 05000280/1988013

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION 11

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/88-13 and 50-281/88-13

Licensee:

Virginia Electric and Power Company

Richmond, VA

23261

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

.. ermu ez

Approved by,(, ~i}_,/(c.J,L,

License Nos.: DPR-32 and DPR-37

J/a:e,ict ion Chief

,~7on of Radiation Safety and Safeguards

SUMMARY

Scope:

This routine, unannounced inspection was conducted in the areas of

radiological environmental monitoring, liquid and gaseous effluent processing,

liquid and gaseous effluent monitoring and confirmatory measurements.

Results:

No violations or deviations were identified .

8806070242 880526

PDR

ADOCK 05000~80

r

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • D. L. Benson, Station Manager
  • P. F. Blount, Assistant Health Physics Supervisor
  • B. A. Garber, Health Physics Supervisor
  • E. S. Grecheck, Plant Manager
  • G. D. Miller Licensing Coordinator
  • S. P. Sarver, Health Physics Superintendent

Other licensee employees contacted included engineers, technicians, and

office personnel.

NRC Resident Inspector

  • W. E. Ho 11 and
  • Attended exit interview

2.

Exit Interview

3.

The inspection scope and findings were summarized on April 29, 1988, with

those persons indicated in Paragraph 1 above.

The inspectors described the

areas inspected and discussed in detail the inspection findings.

No

dissenting comments were received from the licensee.

Semi-annual effluent reports for January-June and July-December 1987 were

reviewed and found to be adequate.

Tests of the HEPA and charcoal ESF

filter systems were reviewed and found to be adequate.

The radiological

environmental air sampling program was reviewed and found to be adequate.

Radioactive effluent monitoring, samp 1 i ng and analysis programs were

reviewed.

Containment particulate and iodine monitor channels were

out-of-service for Unit 2 to a result of mechanical problems with the

filter tape drive; resolution of the problem was being actively pursued by

station personnel.

A total of 14 outstanding items were closed.

The licensee did not identify as proprietary any of the materials provided

to or reviewed by the inspectors during this inspection.

Licensee Action on Previous Enforcement Matters

(Closed) 50-280,281/87-22-0l (SL-4) Inability to Perform Source Check On

1-RM-LA-108 Liquid Radwaste Monitor in Accordance with Table 4.1-l(A) of

the Technical Speci fi cat ion.

The inspectors observed a control room

operator perform a source check on 1-RM-LA-108 liquid radwaste monitor.

The meter needle was observed to move from a reading of approximately

2

500 cpm to a reading of approximately 3,000 cpm upon source actuation.

There were two major factors which made the source check successful.

The

first was the system decontamination effort noted in the closure of

IFI 50-280,281/87-02-02 (see Paragraph 11 of this inspection report).

The

second was installation of a 22 uCi Cs-137 source in place of the original

8 uCi Cs-137 source.

The combined effects of 1 ower background through

decontamination and higher count rate through provision of a larger source

produced a positive source check instead of the imperceptible movement of

the meter needle observed in earlier source checks.

This matter is

considered closed.

(Closed) 50-280,281/87-22-02 (URI):

Perform An Evaluation to Determine If

Slightly Contaminated Sludge Was Shipped to the Surry County Landfil 1.

The licensee performed the requested evaluation.

The licensee was unable

to identify any specific source for the low level sludge contamination

referenced in Inspection Report 50-280, 281/87-22.

In the evaluation the

licensee conceded that it was possible that shipments to the Surry county

1 andfi 11 of sanitary s 1 udge, at radioactivity 1 eve 1 s undetectab 1 e by

normal survey methods, but detectable by laboratory analysis, could have

been made on an approximately twice-annual basis in volumes of 10 to 20

cubic feet of material for each shipment and at radioactivity

concentrations of Cs-137 and Co-60 on the order of 2-3 pCi/gram.

At the

levels of activity seen in sludge samples to date, the licensee considered

that it was possible that previous shipments to the Surry County landfill

had contained radioactive materials at levels within an order of magnitude

higher or lower than the levels reported in Inspection Report

Nos. 50-280, 281/87-22.

It was a 1 so cone 1 uded that extern a 1 radiation

levels from packages of dried sludge, as shipped, were such as to be

undetectable with portable survey instrumentation, and it was therefore

highly unlikely that previous shipments could be located

11 in-situ

11 at the

Surry County 1 andfil 1.

The inspectors' review concluded that the

evaluation was adequate.

The licensee had adopted procedure revisions to

prevent future shipments of potentially radioactive materials to the Surry

County landfill.

The inspectors agreed with the licensee's position that

attempts to locate and retrieve past shipments of dried sanitary waste

treatment sludge would be unproductive.

This matter is considered closed.

(Closed) 50-280,281/87-22-03 (SL-4):

Failure to Conduct An Evaluation and

To Determine The Concentrations of Radioactive Materials Contained in the

Sanitary Sewage Sludge.

The licensee conducted an evaluation which

acknowledged the presence of radioactivity at low concentrations in dried

s 1 udge raked from the sand fi 1 ter drying bed.

Efforts to 1 ocate the

source of the contamination were not successful.

Licensee representatives

stated that the source was considered likely to have been concentration

within the sewage digester from low-level or undetectable levels of

contamination as no apparent radioactive inputs could be i dent ifi ed.

Procedure CAP-53.0 was issued March 11, 1988, and incorporated periodic

sampling of dried sludge, and sampling, analysis and sign-off by the

Supervisor of Health Physics Technical Services before future sludge

quantities can be disposed of.

The licensee's response to this matter was

considered adequate and this matter is considered closed.

3

4.

Semi-Annual Radioactive Effluent Release Reports (84723, 84724)

5.

The inspectors reviewed the the 1 icensee' s Semi-Annua 1 Radio 1 ogica 1

Effluent Release Reports for the first half of CY 1987 (January-June 1987)

and for the second half of CY 1987 (July-December 1987).

The reports

appeared to be complete and to contain the information specified in

Regulatory Guide 1.21.

A summary of the releases for the year (1987) is

shown below.

Gases

'FTssTon and Activation Products

Iodine - 131

Particulates (>8 day Half-Life)

Tritium

Liquids

Fission and Activation Products

Tritium

Dissolved Gases

Alpha Emitters

Volume of Liquid Released (liters)

Volume of Dilution Water (liters)

~uantitb (Curies)

.08 E+ 2

1. 81 E-02

2.84 E-03

3.04 E+Ol

5.17 E+OO

8.15 E+02

2.65 E+OO

3.91 E-05

2.96 E+08 liters

2.21 E+12 liters

Gaseous releasas of fission and activation products were lower than the

average annual releases of 22 operating PWRs in NRC RII (4,400 Ci/yr/unit

in CY 1986).

On the other hand, 1 i quid re 1 eases of fission and

activation products, per operating unit, were 225% of the average releases

of 22 operating*PWRs in RII for the CY 1986 (last year for which all data

was available at the time of inspection).

It should be noted, however,

that the licensee's CY 1987 releases were lower than in previous years.

Fission And Activation Products In Plant Effluents

(Surry, Units 1 and 2, Combined Releases)

Year

Liquids

Gases

1987

5.1 Ci

308 Ci

1986

8.77 Ci

1,990 Ci

1985

8.50 Ci

2,070 Ci

1984

9.73 Ci

6,960 Ci

1983

14.5 Ci

5,490 Ci

1982

6.7 Ci

21,100 Ci

1981

6.11 Ci

14,100 Ci

No violations or deviations were identified.

Radioactive Effluent Monitoring, Sampling and Analysis (84723, 84724)

The inspectors, accompanied by a licensee representative, inspected the

plant gaseous and liquid radioactive effluent monitors and samplers.

4

The liquid radwaste monitor, RM-108, appeared to be operating

satisfactorily.

The licensee had experienced a number of problems with

this monitor, principally the result of buildup of contamination over

extended periods of time, the resultant high background count rate, and a

check source which was too small to provide a measurable increase in

metered countrate when the check source was actuated.

Remedial actions

taken by the licensee to correct these conditions inc 1 uded the

modification of piping to incorporate spool piece connections instead of

an all-welded configuration to facilitate access to the monitor's internal

chamber, providing a new electro-polished samp 1 e chamber for ease of

decontamination, revision of procedures to provide for system flushing

with uncontaminated water to minimize contamination plateout on sample

chamber surfaces, and a 1 arger check source to provide an increased

countrate upon check source actuation.

The inspectors observed that the

system's normal background (at the time of this inspection) was about

500 cpm and that check source actuation resulted in a visible meter

deflection to about 3,000 cpm.

Containment particulate and iodine monitoring channels RM-159, -160, -259,

and -260 were inspected at the request of the senior resident inspector.

In discussion with licensee representatives, the inspectors were informed

that the two monitoring systems concerned (i.e., RM-159/160 and RM-259/260)

were Victoreen noble gas, particulate aerosol, and iodine aerosol monitors

of a new type installed April 1987.

These monitors incorporated a new type

of filter paper drive.

The vendor apparently encountered a number of

mechanical breakdowns of the tape drive mechanism in the production models

of the new monitors.

The breakdowns began on a generic basis shortly after

the licensee received and installed the units (about April 1987).

When the

licensee encountered failure of the tape drives and ordered spare parts for

repair purposes, the vendor notified the licensee that repair parts could

not be provided because of a "design change hold.

11

In early March 1988,

vendor factory representatives came to the licensee's facility and

installed new components in the licensee's monitors.

Both monitors worked

we 11 until the night of April 23, 1988, when the filter tape drive

mechanism on the Unit 2 monitor RM-259/260 jammed again and the iodine and

particulate channels were declared inoperable.

As of the end date of this

inspection, licensee electronics maintenance personnel had been unable to

resolve the jamming problem and the licensee was considering bringing in

vendor personne 1 to correct the prob 1 em.

With the Unit 2 monitor

RM-259/260 inoperable, the licensee met Technical Specification

requirements by sampling and analysis of the containment atmosphere.

This matter was further discussed with the Senior Resident Inspector.

The inspectors noted that the Unit 1 component cooling water system (CCWS)

monitors RM-105/106 were reading at levels of approximately 1 E+OS cpm at

both the local and control room panel readouts.

A licensee representative

stated that these levels were the result of system contamination which

occurred prior to 1983 .

5

The process monitor (RM-107) for the component cooling service water

system (CCSWS) was noted to have been out-of-service for over a year.

A

licensee representative stated that this monitor detector was located in a

well inside a pipe of the CCSWS and had been contaminated sometime prior

to 1983, under the same circumstances which contaminated the CCWS and

resulted in high readings on RM-105/106.

The high radiation background

resulting from the contamination made the monitor incapable of performing

its intended function of responding to small intersystem leaks from the

CCWS into the CCSWS.

For this reason, the monitor had been declared

out-of-service and the sampling and analysis program required by the

Technical Specifications had been implemented.

The licensee has discussed

proposing a Technical Specification change removing RM-107 from the

Technical Specification and adding sampling and analysis of water from the

CCWS to the routine sampling and analysis table of the Technical

Specification. In the cases of all three monitors (RM-105/106/107), the

detectors are located in wells which are not accessible for

decontamination.

In discussions between the inspectors and licensee personnel, it was noted

that the licensee did not do regular correlations between sample analyses

of * 1 i quids and gases from tanks to be discharged and corresponding

effluent monitor readings as the tank are discharged to the atmosphere.

The inspectors noted that many licensees follow the correlation practice

and consider it to be an important tool in verifying the validity of

discharge permits, calculations of total releases and effluent monitor

operability.

During the above discussion, it was also noted that the licensee did not

calculate a new effluent monitor alarm setpoint for each release of

liquids, preferring instead to base alarm levels on the offsite MPC for

iodine-131, assuming minimum dilution.

Such a value was lower than any

that would be calculated on the basis of sample analysis results.

Such

. alarm settings were conservative and placed more restrictive bounds on

licensee operation than using setpoints established separately for each

use and based on both 10 CFR Part 20, Appendix 8, and 10 CFR Part 50,

Appendix I, as implemented by the Offsite Dose Calculation Manual (ODCM).

No violations or deviations were identified.

6 .. Environmental Radiological Monitoring (8072)

The inspectors accompanied licensee representatives during regular

collection of week-long air samples from the eight environmental

monitoring air sampling stations established for the Surry site.

The

eight designated stations were:

Surry Station; Hog Island; Bacon

1s

Castle; Alliance; Colonial Parkway; Dow Chemical; Fort Eustis; and Newport

News.

The inspectors observed sample change methods and noted that good

sampling handling practice was used.

The licensee representatives knew

the sample route and locations and performed their tasks in a competent

and professional manner.

6

All sampling equipment was functioning properly and appeared to be

well-maintained.

Sample enclosures were clean and free of debris and

extraneous material. Collected samples were clearly labelled as to sample

location, sample on and off times, air flow rate, and sample volume.

Samples were to be shipped to the vendor laberatory for analysis.

No violations or deviations were identified.

7.

Radioactive Gaseous Effluent Treatment System (84724)

The inspectors reviewed the licensee's system maintenance, leak testing,

and charcoal iodine retention for the safety-related HEPA - charcoal

gaseous filtration and adsorption systems.

Technical Specification 4.12

requires, in part, that safety-related filtration and adsorption systems

undergo the following operational testing:

0

0

0

0

0

0

0

0

Each redundant train to be operated monthly for a period of at least

15 minutes if it has not already been in operation during the month.

Once per refueling cycle, the operability of the entire

safety-related portion of the auxiliary ventilation system is to be

demonstrated.

The fan fl ow rate is to be determined once per refueling eye le

(approximately 18 months) or after each partial or complete high

efficiency particulate air (HEPA) filter or charcoal adsorber change.

A visual inspection to be made prior to air flow distribution tests,

HEPA filter leak tests, or adsorber freon (halogenated hydrocarbon)

leak tests; in accordance with ANSI NSl0-1975.

Cold dioctylphthalate (DOP) leak test to be made initially, once per

refueling cycle (approximately 18 months), after partial or complete

high efficiency particulate air (HEPA) filter or charcoal adsorber

change.

A visual inspection is to be made prior to air flow distribution

tests, HEPA filter leak tests, or adsorber freon (halogenated

hydrocarbon) leak tests, in accordance with ANSI NSl0-1975.

Cold dioctylphthalate (DOP) leak test to be made initially, once per

refueling cycle (approximately 18 months), after partial or complete

replacement of HEPA filters or charcoal adsorbers, or after any

structural maintenance, per ANSI N510-1975.

Freon (halogenated hydrocarbon) leak test to be made initially, once

per refueling cycle, after partial or complete replacement of HEPA

filters or charcoal adsorbers, or after any structural maintenance,

per ANSE NSl0-1975.

0

7

Laboratory test for re tent ion efficiency of charcoa 1 for methyl

iodide, initially, once per refueling cycle, and after 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> of

operation, in accordance with ASTM 03803.

The inspectors toured the HEPA filter and charcoal adsorber installations

and reviewed licensee documentation on selected tests performed to meet

the TS requirements.

Items reviewed included .procedure PT-32.9, issued

June 17, 1985, for details on HEPA filter and charcoal adsorber testing.

Test records for 1987, and the first three months of 1988, were reviewed

for the following installations:

1-VS-FL-3A and 38

1/2-VS-FL-8

1/2-VS-FL-9

HEPA filter and charcoal adsorber testing was performed under contract by

qualified personnel of the Charcoal Service Corporation, Bath, North

Carolina, except that charcoal adsorber methyl iodide retention efficiency

1 aboratory tests were subcontracted to Nuclear Containment Systems,

Co 1 umbus, Ohio.

The most recent series of tests was conducted in late

March and early April 1988.

The contractor 1 s test data, test results,

test instrument calibration documentation and quality assurance program

appeared to be satisfactory; in one system tested, charcoal did not meet

the required TS criteria and the charcoa 1 was rep 1 aced with a new

pre-tested module, with required leak testing and fan testing being

repeated fo 11 owing adsorber module changeout, in accordance with TS

requirements.

Operational records of filter and adsorber system operation to meet the TS

requirement for at least 15 minute of operation monthly were reviewed for

the period of March 1, 1987 through March 31, 1988.

The required

operations appeared to have been done in conformance with the

specification.

No violations or deviations were identified.

8.

Audits (84723, 84724, 84725)

The inspectors reviewed licensee audit files for audits concerning matters

within the scope of this inspection and performed or issued since the

previous inspection (50-280,281/87-22, August 3-7, 1987).

Audit 587.17, dated July 29, 1987, but issued subsequent to the inspection

of August 3-7, 1987, was concerned with the Process Control Program (PCP)

and with the Offsite Dose Calculation Manual (ODCM).

The audit documented

two concerns of administrative nature:

(1) Two procedures OP.22.1,

11High

Level Waste Drain System," (January 1979) and OP.22.2,

11 Low Level Drain

System

11 (July 1982) were noted to be obsolete; and (2) Section 12.1 of the

ODCM referenced an incorrect section of the Technical Specification in

reference to the Semi-Annual Effluent Release Report.

The later concern

was a repeat finding, previously noted in a 1984 audit 584-32.

8

The licensee's responses to the audit concerns appeared to be timely and

were considered to be adequate to meet the specified concerns.

The audit

appeared to have been performed in satisfactory depth.

No violations or deviations were identified.

9.

Licensee Quality Assurance for Confirmatory Measurements (84725)

The inspectors requested and were supplied information concerning licensee

internal quality assurance activities, including analyses of cross-check

samples prepared by Virginia Power Company Corporate Health Physics for

analysis in the Surry Count Room.

ln a memorandum dated September 30,

1987, the corporate Health Physics group reported that Surry analyses of

three mixed gamma emitter liquid samples and one tritium liquid sample

were all in agreement.

All three liquid samples were analyzed on all

three Surry intrinsic germanium detectors; the one tritium sample was

analyzed on the one Surry Tritium analyzer.

In a memorandum dated June 15, 1987, from Corporate Health Physics to the

Surry Plant, documentating an earlier cross-check, the memo noted

disagreement on the Ce-144 result for detector No. 1 and agreement for

Cs-134, Cs-137, Mn-54 and Co-60 for detector No. 1.

For detectors No. 3

and No. 4, agreement was noted on all nuclides (Ce-144, Cs-134, Cs-137,

Mn-54, and Co-60).

In a Ce-144 re-check on detector No. 1, the re-check

was in agreement.

The inspectors reviewed Corporate HP procedure CHP-9,

11Confi rmatory

Measurements Using Spiked Samples.

11

The criteria for agreement or

disagreement appeared to be the same as that set forth in NRC Inspection

Module 84725.

The inspectors reviewed data provided by the licensee's contract laboratory

concerning the laboratory's participation in the EPA crosscheck program

for the period between January 1, 1987 and December 11, 1987.

The data

consisted of statements of agreement or disagreement of the contractor

laboratory analysis with EPA results on identical samples.

The contractor

laboratory's performance in analyses of some 35 separate samples appeared

to be adequate.

The licensee's quality assurance programs, including those of the

contractor laboratory appeared to be comprehensive and responsive to needs

and were considered to be adequate.

No violations or deviations were identified.

10.

Licensee Event Reports (92700)

(Closed) LER 50-280,281/87-040 (January 29, 1988)

On December 31, 1987, the licensee discovered that two week-1 ong

particulate filters from the effluent sampler servicing the containment

9

vacuum system gaseous discharge had been uni ntent iona lly discarded.

Technical Specification 4.9, table 4.9-2 required that all weekly

particulate samples taken during a calendar quarter be composited

quarterly for analysis of Sr-89 and Sr-90 at an LLD of IE-11 uCi/ml.

The

specification was implemented by Health Physics Procedure HP.3.2.1.

The

analysis of the missing filters for principal gamma emitters had been

accomplished prior to the discarding of the filters; results were typical

of previous analyses for principal gamma emitters.

The releases due to

discharges from the vacuum system for the October-December 1987 calendar

year quarter were estimated by Heal th Physics personnel from previous

data; based on these estimates, the licensee calculated that releases for

the quarter were within established limits for Sr-89 and Sr-90.

Health Physics supervision and management were notified of. the missed

analyses and reviewed the requirements of HP Procedure 3. 2.1 and the

Technical Specification with concerned HP personnel.

HP Procedure 3.2.1

was revised March 31, 1988 to provide better control over retention of

samples where required for compositing for weekly, monthly, and quarterly

periods. Counting room personnel were counseled on the importance of

maintaining strict control and accountability over samples to be analyzed

in accordance with Technical Specification requirements and received

training on the revision to HP Procedure 3.2.1.

Licensee initiatives in resolving the root cause of this event were

considered appropriate and adequate to prevent a recurrence.

This matter

is considered closed.

(Closed) LER 88-004, Issued March 4, 1988,

11 Iodine Spike Due to Defective

Fuel Element.

11

On February 16, 1988, at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br />, the Unit 1 reactor coolant spiked at

1.17 uCi/ml of dose equivalent iodine-131, which exceeded Technical

Specification (TS) 3.1.2.d (Limit 1.0 uCi/ml).

This followed a reactor

trip.

Corrective action was to implement actions of T.S. Table 4.1.2.8,

calling for four-hour interval sampling until dose equivalent

iodine-131 (DEI) level dropped below 1 uCi/ml.

The next sample, taken at

1725 hours0.02 days <br />0.479 hours <br />0.00285 weeks <br />6.563625e-4 months <br /> on February 16, 1988, was 0.75 uCi/ml DEI, which was below

1 uCi/ml.

The event duration was considered to be three hours, the

approximate time interval between the two samples.

At the ti me of this inspection, Unit 1 was shutdown for scheduled

refueling.

Prior to defueling, the licensee planned to conduct ultrasonic

testing of each fuel assembly in an effort to locate the defective fuel,

which was believed to be limited to one fuel pin.

If the assembly

containing the defective pin could be identified, it was to be removed

from the core.

If not, the scheduled refueling operation would proceed.

The licensee considered that it was probable that the fuel assembly with

the defective pin would be among those scheduled for removal and

replacement with new fuel during the outage.

10

The event was an iodine spike which exceeded the TS limit of 1 uCi/ml of

dose-equivalent I-131 by a small margin in the period immediately

following a reactor shutdown.

The followup sample, taken three hours

later, was analyzed at 0. 75 uCi/ml.

Such transient conditions are

characteristic of power changes in nuclear power plants and are known to

occur both on startup and shutdown, particularly in plants with known

defective fuel; however, such spikes do not always occur where defective

fuel is known to exist.

The NRC does not consider iodine spiking of the

order of magnitude seen in this event to be a significant safety problem.

The 1 i censee' s proposed actions to 1 ocate the defective fue 1 and the

actions taken upon detection of the iodine spike were considered adequate

and this matter is considered closed.

11.

Inspector Followup Items

(Closed) 50-280/84-02-06, (IFI):

Vendor Calibration of High Range Noble

Gas Monitor (TMI-0737, II.F.l, Attachment 1).

The inspector reviewed the

vendor's Report of Calibration, Model KMG-HRH, High Range Channel," which

described calibration of the high range detector channel at gamma energies

provided by Xe-133 gas and solutions of Ba-133, Cs-137, and Co-60.

Associated gamma energies were 81, 345, 662, and 1,250 KeV.

Reference

point sources of Cs-137, with NBS traceable calibration, were also used.

The principal NRC guidance in the calibration of the high range monitors

responsive to the criteria of NUREG-0737, Item II.F.1, appears in a

memorandum dated August 16, 1982, from D. G. Eisenhut, NRR, to Regional

Administrators, Subject:

"Proposed Guidance for Calibration and

Surveillance Requirements for Equipment Provided to Meet Item II. F.1,

Attachment 1, 2 and 3, NUREG-0737.'

The inspectors' review of the vendor

calibration report concluded that the data provided in the report appeared

to meet the guidance contained in the NRR memorandum of August 6, 1982,

for type calibration and, therefore, were considered adequate.

This

matter is considered closed.

(Closed) 50-280, 281/86-IN-76 (Information Notice):

Control Room

Emergency Ventilation Problems.

The inspectors and a licensee

representative discussed actions taken by the licensee with respect to the

concerns of Information Notice IN-86-76.

The licensee had received the IN

and had initiated several actions responsive to the IN.

At the time of

this inspection, two ventilation engineers were assigned full-time to work

on the plant control room envelope, with assistance also provided from the

Richmond, Virginia, corporate engineering staff.

The North Anna control

room habitability report was being used as a reference for possible

related problems.

This matter is considered closed.

(Closed) 50-280/86-06-XX (IFI):

Review Licensee Action On Submitting

Environmental Technical Specification Changes to Tables 4.9-5 and 4.9-4.

The licensee submitted a proposed Technical Specification revision to the

subject tables on May 14, 1987.

As of the date of this inspection, the

Office of Nuclear Reactor Regulation (NRR) had apparently not taken action

~~~~

-

- - - - - - -

11

on this matter.

For tracking purposes, the inspectors concluded that the

1 i censee had taken appropriate act ion and this matter is considered

closed.

(Closed) 50-280, 281/87-02-01 (IFI) Define Zero In Semi-Annual Effect

Release Reports and Provide LLDs.

The licensee's Semi-Annual Radiological

Effluent Release Report for the period July-December 1987 provided the

requested information.

In discuss ions with 1 i censee representatives, the

inspectors were assured that future reports would be issued in the correct

format.

This matter is considered closed.

(Closed) 50-280, 281/87-02-02 (IFI):

Improve Maintenance Program for

RM-108 Liquid Radwaste monitor background.

The licensee had modified

monitor RM-108 by providing an electropolished sample chamber with access

by removable spool pieces to facilitate decontamination.

Additionally,

operating procedures were revised to provide adequate flushing of lines

with uncontaminated water after each potentially radioactive discharge.

The inspectors observed that the instrument background 1 eve 1 was

approximately a factor of ten lower than had been observed in a previous

inspection. This matter is considered closed.

(Open) 50-280, 281/87-02-03 (IFI) Resolve the Inoperability Problem of

Component Coo 1 i ng Service Water Mani tor RM. SW-107.

The 1 i ne which

RM.SW-107 monitors was contaminated several years ago.

Residual

contamination was such as to produce high background count rates which

kept the monitor continually in alarm status, although a valid alarm

condition did not exist.

The licensee had been performing periodic

sampling and analysis as required by technical specifications. * At the

time of the inspection, the licensee was developing a Technical

Specification change request to delete the monitor from the Technical

Specifications in favor of periodic sampling and analysis.

Since the

licensee had not submitted the requested change, NRR had taken no action.

This item remained open pending licensee and NRR actions.