ML18152A540

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Insp Repts 50-280/94-11 & 50-281/94-11 on 940403-0507. Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint & Surveillance Insps & Onsite Engineering Review
ML18152A540
Person / Time
Site: Surry  
Issue date: 05/26/1994
From: Belisle G, Branch M, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A541 List:
References
50-280-94-11, 50-281-94-11, NUDOCS 9406060225
Download: ML18152A540 (12)


See also: IR 05000280/1994011

Text

Report Nos.:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/94-11 and 50-281/94-11

Licensee:

Virginia Electric and Po~er Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted: April 3 through May 7, 1994

Inspectors:

M. W. Branch, Senior

Inspector

Resident

S. G. Tingen, Resident Inspector

Accompanying Personnel: D. M. Tamai

L. W. Garner

Approved by:

G. A. VBe l isle, Sec'ffinCief

Division of Reactor Projects

SUMMARY

Scope:

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Date Signed

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Date Signed

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Date Signed

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance and surveillance

inspections, and on-site engineering review.

Results:

Operations functional area

The continued use of the not applicable prov1s1ons in procedure STP-33.6,

Instrument Air Slowdown, revision 2, resulted in not correcting deficiencies

in the procedure (paragraph 3.b).

P9DR406060225 940526

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2

Maintenance functional area

The post maintenance tests performed after replacing several Unit 1

consequence limiting safeguards relays did not fully verify, by testing, that

proper circuit continuity existed .. Relay bench testing and second party

verification of field wiring terminations provided an adequate confidence

level that the relays were properly installed (paragraph 4.b).

Engineering functional area

The failure to revise the Unit 1 steam flow calorimetric computer program to

incorporate changes implemented by Engineering Calculation EE-0418 prior to

unit restart following the refueling outage was identified as Violation

50-280/94-11-01 (paragraph 3.a).

A weakness in the operational readiness review process was identified. A non-

safety related procedure was not recognized as needing revision after the

hardware was changed/removed by plant modifications. Additionally, a system

engineering review of completed surveillance test procedures did not identify

the need to change the procedure (paragraph 3.b).

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer

H. Blake, Jr., Superintendent of Nuclear Site Services

  • R. Blount, Superintendent of Maintenance
  • D. Christian, Assistant Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

J. Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Radiation Protection

A. Friedman, Superintendent of Nuclear Training

  • B. Hayes, Supervisor, Quality Assurance
  • D. Hayes, Supervisor of Administrative Services
  • M. Kansler, Station Manager

C. Luffman, Superintendent, Security

  • J. McCarthy, Superintendent of Operations
  • A. Price, Assistant Station Manager

R. Saunders, Assistant Vice President, Nuclear Operations

E. Smith, Site Quality Assurance Manager

  • T. Sowers, Superintendent of Engineering

J. Swientoniewski, Supervisor, Station Nuclear Safety

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

NRC Personnel

  • A. Belisle, Section Chief
  • M. Branch, Senior Resident Inspector
  • D. Tamai, NRC Intern
  • S. Tingen, Resident Inspector
  • Attended Exit Interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Units I and 2 operated at power for the entire inspection period.

Unit 2 operated at reduced power due to steam generator level

oscillations.

2

3.

Operational Safety Verification (71707)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability.* Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

Operation of Unit 1 Above Licensed Maximum Power

On March 31, DR S-94-0804 was written to document a condition

where Unit 1 operated for a period of 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> and 12 minutes above

the licensed maximum power level of 2441 MWT.

Specifically, at

2:18 p.m. on March 30, reactor power based on the power range Nis

and the CALCALC computer program, was increased from 98% to 100%.

The unit had just completed a RFO and this was the first time the

unit had operated at full power following the RFO.

At 100%

reactor power, operators noted that the turbine generator

electrical output of 830 to 835 MWE was higher than normal and

also exceeded the design value of 828 MWE.

The unit operated at

this power level until 8:54 p.m., of the same day, when management

ordered power to be reduced in order to investigate the

discrepancies between indicated NI reactor power and turbine

output. At 9:30 p.m. on March 30, reactor power was stabilized at

98.3%.

The licensee later confirmed that Unit 1 had operated for

one shift at an average power level of 2453 MWT which exceeded the

maximum licensed power level of 2441 MWT.

On March 31 a reactor

power calorimetric was performed utilizing feed flow.

The power

range Nls were adjusted based on the results of this calorimetric

and the unit was then returned to full power operation.

On that

same day the steam flow calorimetric computer program was revised .

. Through subsequent reviews, the licensee concluded that the power

range Nls were not indicating the correct power level at full

power.

The Nls were indicating approximately 1% lower than the

actual power level. During the 1994 Unit 1 RFO, the main steam

flow transmitters were respanned and the main steam flow

instruments were rescaled. The steam flow calorimetric computer

program was not revised to incorporate these new parameters.

As a

result the power range Nls did not indicate the correct power

level because at approximately 85% reactor power they were

adjusted to match reactor power that was calculated based on the

inaccurate steam flow calorimetric computer program.

TS Table

4.1-1 requires NI power be verified daily against a heat balance

standard (calorimetric calibration). The licensee's method for

3

performing the TS required heat balance surveillance used the

CALCALC computer program and was contained in procedure

1-0PT-RX-001, Reactor Power Calorimetric Using CALCALC Computer

Program, revision 1.

The licensee performed RCE 94-11, Surry Unit 1 Operation Above

100% Power, in order to investigate this event.

The inspectors

also reviewed the circumstances surrounding this event.

RCE 94-11

concluded that root cause of this event was that the process for

implementing changes to instrumentation based on revised

Engineering Calculation EE-0418, Determination of Feedwater Flow

and Steam Flow Transmitter's Calibration Spans from CHEMTRAC and

Flowcalc Data Resulting from Special Test 1-ST-300, revision 1,

was not adequately coordinated.

In this case the process did not

ensure that the steam flow calorimetric computer program was

revised prior to unit restart following the RFO.

The inspectors

reviewed RCE 94-11 and considered it to be comprehensive and

thorough.

The RCE also identified other examples where the lack

of a formal process for controlling and implementing calculation

changes resulted in problems at Surry and North Anna power

stations. The RCE and corrective actions to formalize the process

were approved by SNSOC on April 28.

During this event the power range NI high flux, Overpower Delta T,

and Overtemperature Delta T protective settings were in error by

approximately 1% in the nonconservative direction. The inspectors

reviewed the licensee's policy for reactor trip protective

settings which required that 2% margins be established between

actual settings and TS limiting settings. The inspectors

concluded that the TS limiting settings were not exceeded during

this event.

During the 1992 Unit 1 RFO, feedwater flow measurements were

obtained by using a chemical trace via procedure CHEMTRAC,

revision 1.

These precision feedwater flow measurements were

analyzed by electrical engineering via Engineering Calculation

EE-0418 and were used to revise steam and feedwater flow

instrument scaling values during that outage.

During the recent

1994 Unit 1 RFO, main steam flow scaling values were further

refined in accordance with revision 1 to EE-0418.

The refined

main steam flow scaling values were implemented but the steam flow

calorimetric computer program was not revised.

UFSAR Chapter 14, Safety Analysis, describes the initial condition

at the onset of the accidents and transients analyzed.

Many

accident analyses assume a steady state power level of 102% since

that is the claimed accuracy of the calorimetric. The

calorimetric is the standard used to calibrate NI instruments and

thereby establish the setpoints of the safety actions that are

initiated from these instruments.

Some accident analysis state

that a power level of 102% of 2441 MWT (current license limit) was

assumed while others assumed 102% of 2546 MWT (engineering safety

b.

4

feature rating). The licensee indicated that all accident

analyses had been re-performed using the 2546 MWT rating although

this rating was not recognized in the current UFSAR revision.

The steam flow values used in the Unit 2 calorimetric were

reviewed and the inspectors verified that a similar condition did

not exist. Specifically, during the Unit 2 1991 RFO, the

feedwater flow venturis were replaced and a special test was

performed to verify calibration curves for the new venturis.

Main

steam flow scaling deficiencies were identified and corrected as a

result of this modification and this issue was discussed in NRC

Inspection Report Nos. 50-280, 281/91-21.

The Unit 2 steam and

feed flow calorimetric computer programs were properly revised.

10 CFR 50, Appendix B Criterion III, Design Control, as

implemented by section 17.2.3 of the Operational QA Program

Topical Report, VEP-1-5A (Updated), requires that measures be

established to assure that design requirements be correctly

translated into specifications, drawings, procedures, and

instructions. Electrical Engineering Implementing Procedure

EE-029, Calculation Controlling Procedure, revision 2, stated

scope (2.2) requires that calculation results be effectively

communicated to the applicable power station.

The failure to

revise the Unit 1 steam flow calorimetric computer program to

incorporate the changes implemented by Engineering Calculation

EE-0418, revision 1, prior to restarting the unit following the

RFO was identified as Violation 50-280/94-11-01, Failure To Revise

The Steam Flow Calorimetric Computer Program.

ESF Walkdown

The inspectors walked down portions of the Unit 1 and Unit 2

compressed air system.

The primary purpose of the system is to

provide pressurized air to pneumatically operated valves.

The

walkdown included the service, instrument, and containment air

compressors, instrument and service air receivers, and instrument

air dryers and filters. Major system valves were verified to be

positioned in accordance with procedure OP-46.lA, Instrument and

Service Air Compressors No.2 Turbine Building/Outside Valves

Alignment, revision 8, and system drawings.

During the walkdown,

the inspectors verified that valves were properly aligned and

locked as required, air lines were adequately supported, no

deficient physical conditions were present, housekeeping was

acceptable, and breaker positions were proper on equipment not in

operation.

Ten incidents of incorrect or missing tags were

identified by the inspectors and provided to the licensee for

correction.

The system engineer was interviewed on system operability, recent

modifications and outstanding maintenance items.

The inspectors

also walked down part of the system with the system engineer.

The

service air compressor control cabinets were opened and inspected

5

for adequate housekeeping and equipment material condition.

The

inspectors concluded that the system was being adequately

maintained.

Monthly surveillance procedure STP-33.6, Instrument Air Slowdown,

revision 2, test results from 12/93 to 4/94 were reviewed.

Two

examples were identified where the STP was not updated after

modifications to the plant were implemented.

The first example

was DCP-93-040, BS Groundwater Intrusion and Control, revision 6,

which removed valve 1-IA-735.

The Design Change Process, as

outlined in VPAP-0301, revision 3, is intended to identify

affected drawings and procedures.

Per the design change process

an ORR initiates the update of affected priority documents.

The

ORR for DCP-93-040 did not identify procedure STP-33.6 as an

affected procedure.

The second example involved DCP-90-08, MER-5

Chiller Installation - CR HVAC Upgrade, revision 38, which changed

valve 2-IA-211 from a test connection to a non-testable IA supply

valve to MER #5.

STP-33.6 was annotated for three consecutive months with N/A

instead of correcting the procedure, and in some cases alternate

test valves were utilized. The procedure allowed omission of any

valves at the discretion of the shift supervisor provided that an

explanation was given. A liberal use of these instructions

allowed Operations personnel to N/A valves that were not testable

and continue the surveillance without a procedure change.

Furthermore, the system engineer reviewed each completed procedure

through a post-surveillance critique and did not initiate a

procedure change.

The inspectors identified a weakness in the ORR process, in that,

non-safety related procedure STP-33.6 was not recognized as

needing revision after the hardware was changed/removed by plant

modifications. Additionally, Operations personnel's continued use

of ~he STP-33.6 N/A provision resulted in not correcting

procedural deficiencies and a system engineering review likewise

failed to identify the need to change the procedure.

Within the areas inspected, one violation was identified.

4.

Maintenance And Surveillance Inspections (62703, 61726} .

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

a.

Unit 1 A Reactor Trip Breaker

On April 12, while performing monthly l-PT-8.1, Reactor Protection

System Logic (for normal operation}, revision 6, the Unit 1 A RTB

failed to remain closed. The breaker had successfully closed

twice earlier in the procedure.

The A RTB was removed for repair

J

6

and replaced with the B RTBB.

Both the licensee and the vendor,

Westinghouse, determined that the C phase of the control relay

contact had insufficient contact tension. Additionally, the

vendor recommended that breaker closure timing be changed to

deenergize the closing.coil slightly after the breaker

mechanically latches. The inspectors observed the reinstallation

of the A RTB.

The B RTBB was removed from the A RTB position and

returned to its original position and the A RTB was reinstalled.

The work was done in accordance with procedures and adequate

coordination with the control room was noted.

The breaker was

successfully tested in accordance with l-PT-8.1.

The failure of the A RTB to remain closed also occurred on

March 24, 1994, during the monthly test, l-PT-8.2, Reactor

Protection System Logic {for shutdown), revision 4.

The cause was

diagnosed as a faulted latch pawl spring. After replacing the

spring, the breaker was tested satisfactorily and returned to

service.

b.

Unit 1 CLS Relay Replacement

In 1993, the licensee performed a Level 1 engineering study that

identified six Hi CLS relays in each unit that would result in a

reactor trip if a single relay failure occurred.

Prior to

performing this Level 1, several reactor trips occurred due to

single relay failures. During the Unit 1 spring 1994 RFO, these

six CLS relays were replaced.

In addition several other Hi CLS

relays and Hi-Hi CLS relays were replaced because the relays were

either chattering or had a crack in the coil case.

The inspectors

reviewed the maintenance, PMTs, and surveillances associated with

replacing relays 3/4-CLS-lA {WO 269580 01), 3/4-CLS-lB

{WO 269582 01), 3-CLS-lAM {WO 269581 01), 3-CLS-lBM

{WO 269583 01), CR-CLS-lAl {WO 269380 01), CR-CLS-1Bl

{WO 269589 01), CR-CLS-1B13 {WO 283983 01), CR-CLS-284

{WO 281784 01), and CR-CLS-2BM-X {WO 267272 01).

The relays were replaced in accordance with procedure

O-ECM-1801-01, Westinghouse Type BFD Relay Replacement,

revision 5, and in most cases old style BFD relays were replaced

with later model NBFD65NR relays. Prior to installation, each

relay was bench tested which included coil testing and

verification that the contacts opened and closed as required.

Since the new relays had a different contact configuration, the

system engineer specified the wiring configuration for each relay

O-ECM-1801-01 attachment 2.

The electricians who installed and

rewired the relays independently verified that the leads were

installed to the relay terminals as specified.

The PMT sheets for replacing Hi-Hi CLS relays CR-CLS-2B4 and

CR-CLS-2BM-X required that the relays be tested in accordance with

l-PT-8.5, Consequence Limiting Safeguards Logic {HI-HI Train),

revision 2.

The inspectors reviewed 1-PT-8.5 performed on

7

March 21, 1994, and concluded that the relays had been properly

tested.

The PMT sheets for replacing Hi CLS relays 3/4-CLS-lA, 3/4-CLS-lB,

3-CLS-lAM, 3-CLS-lBM, CR-CLS-lAl, CR-CLS-1Bl and CR-CLS-1Bl3

required that the relays be tested in accordance with l-PT-8.4,

Consequence Limiting Safeguards (Hi-Train), revision 2.

The

inspectors reviewed l-PT-8.4 performed on March 20 and 21, 1994,

and identified the following examples where operation of specific

relay contacts were not verified while performing this test:

RELAY

TRAIN

CONTACTS

FUNCTION

3-CLS-lAM

A

18,22

Actuate Hi CLS

19,23

3-CLS-IBM

B

18,22

Actuate Hi CLS

19,23

CR-CLS-lAl

A

1, 5

Actuate SI-CLS

CR-CLS-1Bl

B

1,5

Actuate SI-CLS

On May 11 the licensee discussed with the NRC the installation and

testing performed on the above relays. After consultation with

Region II management and cognizant NRR personnel, the inspectors

concluded that the bench testing performed on these relays prior

to installation combined with the testing performed after

installation provided an adequate level of confidence that these

relays were properly installed. The inspectors also concluded

that the CLS relays were installed and tested in accordance with

the licensee's PMT program.

No discrepancies were identified.*

Within the areas inspected, no violations or deviations were identified.

5.

On-Site Engineering Review (37551)

Seismic Qualification of the Turbine Building

During an UFSAR review, the inspectors observed in Table 15.2-1 a note

concerning the turbine building that stated, "By design, building

collapse will not damage any Class I structures and components during

earthquake, or tornado-resistant structures and components during

tornado." The inspectors inquired if this statement meant that the

turbine building was seismically designed.

Per UFSAR section 9.10.4.18,

safety related equipment located within the turbine building includes

control room and switchgear area emergency ventilating units, component

cooling water heat exchangers, instrument air compressors, service water

valves, and charging pump cooling water and service water system valves

along with related cables/cable trays.

No areas of the UFSAR reviewed

by the inspectors referenced the turbine building as being seismically

qualified.

..

8

On March 31, 1994, the inspectors met with the licensee's Supervisor of

Station Civil Engineering, Supervisor of Corporate Civil Engineering,

and the Supervisor of Corporate Engineering Mechanics to discuss this

apparent conflict in the design basis. During this discussion, the

following information documented in Calculation 11448 was presented:

The turbine building was designed for normal wind loading

(150 mph) considering full sail area of the siding.

The major

turbine building structural elements were designed for tornado

wind loading. The controlling turbine building loading was found

to be the tornado wind pressure applied to the major structural

elements.

A comparison of loads generated by tornado wind pressure and

seismic motion revealed that the tornado loads would be several

orders of magnitude higher.

The licensee concluded from this

calculation that no specific analysis to seismically qualify the

turbine building was necessary.

Discussion of the calculation

revealed that while the turbine building side panels may be blown

away during a tornado the building structural steel should remain

intact.

The inspectors reviewed pages 105-110 of Calculation 11448 which was

performed by Stone & Webster in July 1967.

This calculation concluded

that the turbine building structural loads associated with an earthquake

were less than the loads associated with a tornado (the limiting design

for the turbine building).

The inspectors further discussed the seismic adequacy of the safety

related equipment and the raceway systems inside the turbine building.

The following information and conclusions were discussed:

The licensee used EPRI report NP-7150-D, The Performance of

Raceway Systems in Strong-Motion Earthquakes, as a reference when

evaluating the seismic adequacy of the raceway system within the

turbine building. The measurement of the peak ground

accelerations in the seismic events discussed in this report

varied from 0.12g to 0.85g.

Seismic damage was limited to only a few items except for sites in

excess of 0.55 peak ground acceleration. Surry's peak ground

acceleration is 0.15 and therefore not likely to suffer notable

damage from a seismic event.

The inspectors reviewed EPRI Report NP-7150-D which demonstrated the

types of damage to electrical raceways and electrical conduit that could

be expected during specific seismic events. The licensee plans to use

this information in further reviewing the adequacy of raceways.

In December 1980, the NRC initiated USI 46, Seismic Qualification of

Equipment in Operating Plants, to address seismic adequacy of mechanical

and electrical equipment in older nuclear plants such as Surry.

The

9

inspectors discussed the walkdowns that are presently in progress (to be

completed by the end of 1995) for the electrical and mechanical

equipment that are required for the safe shutdown of the plant. These

walkdowns should verify the seismic adequacy of this equipment and

raceways.

Another objective.of this program is to verify the

interaction of non-safety related (and non-seismic) equipment and safety

related equipment.

The industry's efforts (SQUG) are for resolving USI

A-46 and IPEEE (seismic) issues.

Qualification of Personnel

The inspectors reviewed the qualifications of the three individuals

described above who were involved in resolving the seismic issues at

Surry. All of the individuals met the supervisory qualifications

required by ANS 3.1 and SQUG for seismic capability engineer.

The

requirements are as follows:

ANS 3.1, Standard for Qualification and Training of Personnel for

Nuclear Power Plants, stated that supervisory personnel should

have a BS in Engineering and should have six years of professional

level managerial experience in the power field.

In addition,

several of the individuals possessed PE licenses.

SQUG procedure, Generic Implementation Procedure For Seismic

Verification of Nuclear Plant Equipment, had requirements for a

seismic capability engineer (Sec. 2.1.2). These requirements were

an engineering degree, or equivalent, completion of a SQUG

developed training course on seismic adequacy verification of

nuclear power plant equipment, and at least five years experience

in earthquake engineering applicable to nuclear power plants.

The inspectors had no further concerns in this area.

Within the areas inspected, no violations or deviations were identified.

6.

Exit Interview

The inspection scope and findings were summarized on May 10, 1994, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection results addressed

in the Summary section and those listed below.

Item Tvpe/Number

Status

VIO 50-280/94-11-01

Open

Description/(Paragraph No.)

Failure To The Revise Steam

Flow Calorimetric Computer

Program (paragraph 3.a)

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

\\. "

10

7.

Index of Acronyms and Initialisms

ANS

AMERICAN NUCLEAR SOCIETY

BS

BACHELOR OF SCIENCE

CFR

CODE OF FEDERAL REGULATIONS

CLS

CONSEQUENCE LIMITING SAFEGUARDS

CR

CONTROL ROOM

DCP

DESIGN CHANGE PACKAGE

DR

DEVIATION REPORT

ECCS

EMERGENCY CORE COOLING SYSTEM

EE

ENGINEERING EVALUATION

EPRI

ELECTRICAL POWER RESEARCH INSTITUTE

ESF

ENGINEERED SAFETY FEATURE

g

GRAVITY

HVAC

HEATING VENTILATION AND AIR CONDITIONING

IPEEE

INDIVIDUAL PLANT EXTERNAL EVENT EXAMINATION

MER

MECHANICAL EQUIPMENT ROOM

MWE

MEGAWATT ELECTRIC

MWT

MEGAWATT THERMAL

N/A

NOT APPLICABLE

NI

NUCLEAR INSTRUMENTATION

NRC

NUCLEAR REGULATORY COMMISSION

ORR

OPERATIONAL READINESS REVIEW

PE

PROFESSIONAL ENGINEER

PMT

PREVENTATIVE MAINTENANCE TEST

PT

PERIODIC TEST

QA

QUALITY ASSURANCE

RCE

ROOT CAUSE EVALUATION

RFO

REFUELING OUTAGE

RTB

REACTOR TRIP BREAKER

RTBB

REACTOR TRIP BYPASS BREAKER

SI

SAFETY INJECTION

SNSOC

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SQUG

SEISMIC QUALIFICATION UTILITY GROUP

STP

SURVEILLANCE TEST PROCEDURE

T

TEMPERATURE

TB

TURBINE BUILDING

TS

TECHNICAL SPECIFICATION

UFSAR

UPDATED FINAL SAFETY ANALYSIS REPORT

USI

UNRESOLVED SAFETY ISSUE

VIO

VIOLATION

WO

WORK ORDER