ML18152A457

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Insp Repts 50-280/93-30 & 50-281/93-30 on 931205-940101. No Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint Insp,Balance of Plant Insp,Review of Plant Modifications,& Previous Insp Items
ML18152A457
Person / Time
Site: Surry  
Issue date: 01/26/1994
From: Branch M, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A458 List:
References
50-280-93-30, 50-281-93-30, NUDOCS 9402080023
Download: ML18152A457 (13)


See also: IR 05000280/1993030

Text

. .

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-280/93-30 and 50-281/93-30

Licensee: Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos .. : DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

December 5, 1993 through January 1, 1994

Inspectors:

. Approved by:

Scope:

M. W.an~ Resident

Inspec or

.

L

~*

/i,i--

J.~k, Resident Inspector

G. A~ seis,ection Chief

Division of Reactor Projects

SUMMARY

//}Gljf-

Date S1gned

I U-~ t_,r 't

Date. STgned

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, balance of

plant .inspections, revi~w of plant modifications, and action on previous

inspection items.

While performing this inspection, the resident* inspectors

conducted reviews of the licensee's backshifts, holiday or weekend operations

on December 10, 12, 19, 22, and 28, 1993 .

--,

9402080023 940127 *

PDR

ADOCK 05000280

G

. PDR

2

Results:

Operations functional area:

Adequate implementation of the freeze protection program was noted

(paragraph 3.b).

Maintenance functional area:

Repetitive process vent Kaman radiation monitor problems continued to occur

throughout 1993.

The licensee's trending programs have identified this as a

recurring problem.

Ccirrective actions have been implemented and plans to

implement additional corrective action were ongoing (paragraph 4.a).

  • Engineering functional area:

Station Nuclear Safety Operating Committee review of a safety evaluation

identified an area that -required additional engineering analysi~. This

analysis resulted in a procedural change for injecting temporary leak sealant

into the-packing of the Unit 2 loop fill control valve (paragraph 4.b).

An unresolved item was identified associat~d with the fire barrier adequacy

(i.e., MER-5 chiller cable protection), pending demonstration by the licensee

that the installation and design meets commitments to and regulatory

requirements of 10 CFR, Part 50, Appendix R (paragraph 6) .

REPORT DETAILS

1.

Persons Contacted

. Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer

H. Blake, Jr., Superintendent of Nuclear Site Services

  • R. Blount, Superintendent of Maintenance
  • D. Christian, Assistant Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

  • J. Downs, *superintendent of Outage and Planning

D. Erickson, Superintendent of Radiation Protection

A. Friedman, Superintendent of Nuclear Training

  • B. Hayes, Supervisor, Quality Assurance
  • M. Kansler, Station Manager

C. Luffman, Superintendent, Security

J~ McCarthy, Superintendent of Operations

    • A. Price, Assistant Station Manager

R. Saunders, Assistant Vice President, Nuclear Operations

E. Smith, Site Quality Assurance Manager

  • T. Sowers, Superintendent of Engineering

J. Swientoniewski, Supervisor, Station Nuclear Safety

  • G. Woodzell, Nuclear Training

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S.*Tingen, Resident Inspector
  • J. York, Resident Inspector
  • Attended Exit Interview *

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors *and other plant personnel.

  • Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 began the*reporting period at 80% power on day 31 of the power

coastdown for refueling.

On December 21, power was reduced from 72% to

approximately 62% in order to remove one tandem drive motor fr6m one of

the two main feedwater pumps for use ~n Unit 2.

The unit operated*at

62% power for the remaining period, limited by only ona MFWP.

The.

refueling outage is sti.11 scheduled to commence on January 21, 1994.

2

Unit 2 began the reporting period at 100% power.

On December 22, power

was reduced to appr9ximately 60% in order to replace a main feedwater

pump motor that was experiencing vibration problems. After the Unit 1

motor was installed in Unit 2, the unit was returned to 100% power* on

December 25.

3.

Operational Safety Verification (71707, 42700}

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability. Frequent plant

toufs were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and.

housekeeping.

Deviation reports we~e reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

Unit 2 Control Rod Drive System Urgent Failure Alarm and NOED

On December 15, at 8:37 a.m., a rod control sy~tem urgent fatlure

occurred on Unit 2 during scheduled control rod exercising~

The

urgent failure rendered group 1 rods powered from cabinet (2-RC-

CAB-lAC} immovable (TS i_noperabl e}.

The rods affected included

group 1 rods in SDB "A" as wel 1 as CB

11A

11 and "C".

In SDB

11A

11

,

the first bank tested, the four group 2 rods had inserted three

steps into the core while the four group 1 rods that were also

selected remained.fully withdrawn.

At 8:37 a.m., a LCO was

entered in accordance with TS 3.12.C.3.

TS 3.12.C.3 required that

inoperable control rod assemblies be restored to operable status

within two hours or that the plant be put into a hot shutdown

condition within the next six hours.

Initial troubleshooting began immediately and was witnessed by the

inspectors. This* troubleshooting involv~d looking for lit *

indicator lamps or blown fuses as well as taking electrical

reading at test points itiside the rod control cabinet. There were

no lit indicator lights or indication of blown fuses and the

electrical readings appeared normal.

The K-2 failure detector

card appeared loose (i.e., _about 1/8-inch from fully seated}.

This card was removed, reinstalled, and additional electrical

measurements made with no change in readings noted.

The K-2 card

was replaced and again there was no noted change in electrical

readings.

The old card was reinstalled. However, when the I-2

card, removed to ensure the gripper coils would stay de-energized

during troubleshooting, was reinserted, I&C personnel noted that*

lights on the J-1 failure detector card began flashing.

The J-1

card was replaced and the urgent failure reset. After re~ligning

the SDB "A" _rods to fully withdrawn per a temporary change to the

3

rod realignment procedure, the operators attempted to again

perform the rod exercise PT.

The rod urgent failure reoccurred.

After determining that further troubleshooting and repairs could

not be completed wtthin the action time_ of the TS, the licensee

requested enforcement discretion.

The NRC verbally granted enforcement discretion from TS 3.12.C.3

for Unit 2 only during a telephone conference on December 15,

1993.

Written enforcement discretion was issued the next day.

The discretion permitted continued operation of Untt 2 at power

for a period of 24_hours versus the two hours specified in TS 3.12;C.3.

The additional time was projected to allow

troubleshooting and repairs to the Control Rod Drive System .

. Although the control rod assemblies were immovable on demand from

the Control Rod Drive System, the ability of the control rod

assemblies to perform their intended safety function (trip into

the core) when a safety system setting was reached was not

affected.

Additional troubleshooting after the second urgent failure

revealed that the removed J-1 failure detection card had two loose

capacitors that were not correctly soldered. This defective J-1

card had masked the problem that caused the first urgent failure.

The second urgent failure resulted in the J-1 card indicating that

the failure occurred in the phase "C" stationary gripper

circuitry.

Both the phase control and firing cards for this

circuit were replaced and the control rods_~ere realigned and

satisfactorily tested in accordance with periodic test 2-PT-6,

Control Rbd Assembly Partial Movement.

The Control Rod Drive

System was returned to service and the LCO terminated at 3:06 p.m.

on the December 15.

This NOED is considered closed.

The inspectors noted that these rod equipment failures were-

further examples of continuing equipment malfunctions associated

with the Control Rod Drive System.

The inspectors discussed their

concerns with the Station Manager who indicated that a Station

Level I priority had been opened for engineering to review past

failures and make recommendations for improvements.

The

licensee's cufrent schedul~ for this project indicates that the

review should be completed in time to allow for the implementing

improvements during the upcoming (January 1994) Unit 1 RFO.

Unit

2 improvements should be factored into the next RFO, scheduled for

September 1994.

b.

_ Cold Weather Protection (71714)

During a plant tour on December l2, the inspectors noted that the

licensee was performing operations che~k list procedure no. OC-21,

Severe Weather OC, dated September 7, 1993. This procedure covers

the following forecast weather conditions: high winds and/or heavy

rains, extreme cold and/or heavy snow, and severe hot weather. -.

4

High winds and freezing weather had been forecast for this period

of time.

High winds and below freezing temperatures were expected

in the area and operations, maintenance, etc., used this procedure

to ensure that proper preparations have been made for the expected

inclement weather.

In addition, the inspectors discussed the normal freeze protection

program with the licensee. This program was implemented by

monthly performance (October through March) of STP-52, Cold

Weather Protection, dated April 3, 1992. This procedure contained

a detailed checklist of areas and components that need to be

routinely inspected to ensure that there was adequate protection

to prevent freezing. This procedure, STP-52, was performed by

both operation~ and maintenance personnel~

Deficiencies that were

noted while performing STP~s2 were documented and discrepancy

reports/work requests ~ere written to schedule corrective action.

On December 20, the inspectors reviewed the latest deficiency list

and noted that they were either complete, being worked, or

scheduled.

Walkdowns of exposed areas susceptible to freezing was

conducted by the inspectors.

No discrepancies were identified

that would indicate that the program.was not being adequately

imp 1 emented. *

Within the areas inspected, no violations were identified~

4.

Maintenance Inspections (62703, 42700)

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

a.

Proc~~s Vent Radiation Monitor

  • During this inspection period the inspectors reviewed the

reliability of the Kaman process vent high range effluent

monitors.* Previous !Rs have addressed recurring problems with the

Kaman radiation monitors.

Most recently, IR 93~23 addressed

spiking on the Kaman ventilation vent effluent monitor 1-VG-RI-l

(TS Table 3.7.6 Item 12).

TS Table 3.7.6, specified operability requirements for accident

monitoring instrumentation. Item 11 of this table specified

.

operability requirements for the process vent high range effluent

radiation monitors.

Kaman radiation monitors l-GW-RM-130-1/2

fulfill this requirement.

Whenever these radiation monitors are

declared. inoperable, an alternate method for monitoring the

process vent effluent was implemented in accordance with TSs .

The process vent Kaman radiation monitors have a history of

operational problems~

In 1991, approximately 11 DRs were written

due to operational problems. Ten DRs were written in 1992.

5

Twenty DRs were written in 1993. Recurring problems associated

with these radiation monitors involved defaulting setpoints, the

iodine/particulate sample becoming saturated with water, check

source failures, and miscellaneous other problems.* The licensee's

trending programs have identified this as a recurring problem.*

Corrective actions have been implemented and plans to implement

  • additional corrective action are ongoing.

The inspectors will

continue to monitor the performance of the process vent Kam.an

radiation monitors in order to evaluate the corrective action's

ef feet i veness.

.

b.

Valve Packing Repair with Temporary Leak Sealant

TS 4.11.A.4 and 3.3.A.12 specify that total system uncollected

leakage from SI system valves, flanges, and pumps located outside

of containment not exceed 3836 cc/hr. The SI system leakage is

monitored by performing periodic testing and wal kdowns.

Syste.m

leakage measurements are recorded and tracked in accordance with

procedure 2-NPT-ZZ-001, Quantifying of System External Leakage.

While performing a system leakage inspection on December 23,

operators identified a signiffcant leak rate coolant increase from

the packing of the Unit 2 loop fill control valve, 2-CH-FCV-2160.

The packing leak rate which was previously identified as 6 cc/hr

had increased to 1800 cc/hr.

On December 27, the coolant leak

rate from the packing increased t~ 3120 cc/hr.

Leakage from ihe

  • remaining components in the SI system was very low and therefore

the system's total leakage rate remained below the TS maximum

value of 3836 cc/hr.

On December 31, the loop fill control valve packing leak was

stopped by injecting a temporary leak sealant into the packing

area. This maintenance was accomplished by WO 260090-3 and

procedure O-MCM-1918-01, On Line Repairs.

The inspectors reviewed

the procedure and verified that there were provisions for limiting

the amount of leak sealant injected into the packing area and

restricting the leak sealant injection pressure.

The inspectors

also reviewed the work history dating back to 1991 for the Unit 2

loop fill control valve ~nd verified that the valve had not

previously been injected with a temporary leak sealant. The valve

was repacked during the previous Unit 2 1993 RFO.

The inspectors

also verified that there was a WR initiated to return the valve to

it's original condition.

The loop fill control valve is a containment isolation valve that

. is normally closed and not repositioned while the plant is

operating.

Injecting temporary leak sealant into the packing area

precluded further valve operation.

SE 93-246, dated December 30,

was prepared to evaluate operating the unit with the loop fill

control valve permanently shut.

The SE concluded that it was

acceptable to operate the unit in this condition until the next

6

RFO.

The inspectors reviewed SE 93-246 and attended the initial

SNSOC meetings that reviewed the SE.

The inspectors noted that

the SE was not initially approved by SNSOC.

SNSOC had questioned

if the design pressure rating of the packing leak off piping was

evaluated when determining the maximum temporary leak sealant

injection pressure. The packing leak off piping was the injection

point for the temporary leak sealant and the design pressure of

this piping was not -Originally evaluated~

As a result of SNSOC

questioning, the maximum temporary leak sealant injection pressure

was reevaluated and lowered.

The SE was subsequently approved by

SNSOC.

The inspectors concluded that the initial engineering

review for the temporary leak repair was incomplete.

However, the

SNSOC review and approval added value-to the leak repair process,

resulting in an acceptable temporary repair.

Within the areas inspected, no violations were identified.

5.

BOP Inspection (71500)

The inspectors conducted tours _of selected TB and other plant areas

susceptible to flooding.

During these tours, the inspectors verified

the availability of the non-safety related TB sump pumps which the

licensee relies upon to mitigat~ certain flooding scenarios.

Additionally, the inspectors we~e sensitive to ~ny work activities that

would increase the possibility of TB flooding such as openings in the

condenser waterboxes or piping systems.*

On December 29, the inspectors witnessed the licensee performing

maintenance associated with replacing TB sump pump l-PL-P-2F discharge

isolation valve l-PL-12. This maintenance was accomplished in

accordance with WO 279713-04.

In order to accomplish this maintenance,

the power supplies to three of the nine TB sump pumps were danger tagged

in the off position. The three TB sump pumps were inoperable for

approximately 2. 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> while the maintenance was performed.

Previous licensee commitments to the NRC stated that at least seven of

the nine TB sump pumps would be operable. The licensee reevaluated the

!PE calculations and c9ncluded that for short periods of time it was

acceptable to have at least six TB sump pumps operable.

Installing

improved SW expansion joint spray shields was one of the contributors in

reducing the critical flood flow rate which allowed operating with six

TB sump pumps.

The licensee was drafting a letter to the NRC revising

their commitment.

The insp~ctors concluded that l-PL-12 replacement was accomplished in

accordance with the licensee's procedures for minimizing the impact*of

flooding in the TB.

Within the areas inspected, no violations were identified.

7

6.

Review of Plant Modifications {37828)

The inspectors have been closely monitoring the plant modification to

improve the reliability of the control room and emergency switchgear

room chillers. This project is commonly referred to as the MER-5

modification.

The modification basically consisted of constructing a

seismic structure to contain two additional chiller units with their

support systems. Additionally, the modification added flexibility to

.

the power supplies for the two new and the three existing chiller units.

On December 28, the inspectors witnessed/reviewed two activities

associated with the MER-5 modification.

The first involved a freeze

seal to allow valve replacement and tying chill water to one of the

three existing chillers. The second involved installing 3-M fire wrap

over cables and conduit in order to establish fire separation between

the two electrical trains that power the chiller units.

The freeze seal was installed using WO 262059-08 and was controlled by

procedure O-MCM-1918-03 revision 0, Freeze Seal of Piping.

The

procedure required that a SE be performed and approved by SNSOC.

The

inspectors reviewed t~e SE {93-239A) and found it acceptable.

The

piping being frozen was 3-inch diameter carbon steel piping. The

inspectors noted that the piping surface in the freeze seal vicinity was

very rusty and would be difficult to perform the NDE required prior to

freeze seal installation. The Site Services personnel working the job

showed the inspectors IPR 93-431 that documented th~ surface condition

and provided the engineering disposition of the concern prior to the

freeze seal installation~ Specifically, surface grinding to smooth the

area being frozen was performed followed by a successful NDE of the

area.

The conduit fire wrap was being installed per DCP 90-07.

The fire

barrier being installed on the conduit that housed "H" bus power supply

cables was necessary since the "H" bus conduit was routed through the

11 J

11 bus switchgear room within approximately 1-2 feet of the switchgear.

IO CFR 50, Appendix R requires that train {bus) separation be

established by physical distance {20 feet), or by 3-or I-hour fire

barriers ~epending on the specific circumstances.

The stated purpose of

the modification was to provide a I-hour fire barrier between the two

electrical power trains.

The inspectors revi~wed the work package at the job site and noted that

the 3-M installation/qualification instructions discussed a

configuration that was different from that being installed. The 3-M

qualification for a I-hour fire rating described a three wrap system for

< 5 inch aluminum conduit, consisting of two wraps of E-53 and one wrap

of E-54.

The system being installed consisted of three wraps of E-54

which was described by the licensee and their* contractor as thicker

material than the E-53 wrap.

The inspectors requested verification that

the actual installation configuration of 3 wraps of 3-M E-54 was bounded.

by test reports from the vendor.

8

The inspectors were provided a copy of a memorandum from the corporate

fire protection engineer to Site Engineering. This memorandum contained

the engineering evaluation for qualifying three wraps of E-54 material.

  • The basis for the fire wrap qualification configuration being installed

was stated to be several 3-M test reports. However, fire test. report

no. 3MFT87-11, wh i.ch was described as the c 1 osest to the actua 1

installation, in a memorandum from PROMATEC, the licensee's contractor,

was not referenced.

The inspectors requested a copy of fire test report

no. 3MFT87-1I for review.

The above referenced memorandum also contained engineering evaluati~n

no. 25 titled, "Evaluation of ~ack of an Automatic Fire Suppression

System in Unit 2 Emergency Switchgear Room Surry Power Station". The

evaluation's purpose was to allow using I-hour fire barrier (i.e., 3

layer fire wrap on power supply cables for- the chiller units). The

original design had specified a 3-hour fire barrier (i.e., 5 wraps of

3-M material) for the cables in question but, because of space

considerations, only 3 wraps could be installed. The evaluation

referenced 10 CFR 50, Appendix R, section III.G.2.c requirement that

stated that two trains of safe shutdown cables could be separated by a

I-hour rated fire barrier, witn fire detection and an automatic fire

suppression system installed in the area.

The licensee's evaluation was

addressing the fact that the emergency switchgear room, where the cables

in question were located, was equipped with a manual not automatic fire

suppression Halon system.

10 CFR 50, Appendix R, section III.G.2.c

would require J 3-hour barrier for this area and an exemption would be

necessary.

During subsequent discussions, the licensee produced* a Surry Appendix R

Report that states that the emergency switchgear rooms for Units I and 2

(fire zones 3 and 4) only had to meet the requirements of 10 CFR 50,

Appendix R, section III.G.3 in lieu of III.G.2.c since remote shutdown

capability existed~

Section III.G.3 only required a fixed suppression

system and did not require it to be automatic. Additionally, train *

separation was not specified.

Based on the conflicting data, it was

unclear as to the fire protection and cable protection design

requirements for-this area.

The fire protection design engineer stated

that for new installations, 111.G.2.c requirements were desired. Since

the control room and emergency switchgear room chiller system were

common to both units, the inspectors questioned the licensee as to

whether the system would be needed to cool equipment that was relied

upon for remote/alternate shutdown. Thereby, it would be required to

meet the requirements of 111.G.2.c (i.e., protected by a 3-hour barrier

or I-hour barrier with automatic fire detection and suppression).

The inspectors requested additional information and historical

correspondence as to the design requirements for protecting the cable in

question. This item is identified as URI 50-280, 281/93-30-01, MER-5

Power Supply Cables Fire Barrier Adequacy, pending demonstration by the

licensee that the installation and design meets commitments to and

regulatory requirements of 10 CFR 50,

Appendix R.

Additionally, 3-M

'

.

9

fire test report 3MFT87-ll has not been provided-by the licensee or

reviewed by inspectors.

The licensee has elected to maintain a fire

watch in the area until thi~ issue is resolved.

_ Within the areas inspected, no violations were identified.

7.

Action on Previous Inspection Items (92701, 92702)

a. - Closed VIO 50-280, 281/92-07-03, Failure To Prevent Foreign

Material From Entering SW System.

When flow testing the Unit I

RSHXs during the 1992 Spring RFO, it was identified that the* flow

rate through RSHX 1-RS-E-IB was low.

Inspection of the heat

exchanger revealed that a rain jacket and rain pants were present

in the tubesheet area which restricted the flow of SW.

It was

concluded that the rain gear was inadvertently left in the system

during maintenance that was performed during the previous fall

1990 RFO.

In a letter dated May 29, 1992, the licensee responded

to this violation.

The cause of this event was attributed to

inadequate implementation of FME controls during the maintenance

performed on-the RSHX system during the 1990 RFO.

As corrective

_action VPAP-1302; Foreign Material Exclusion Program, was

implemented after the Fall, 1990, Unit 1 RFO to establish station

wide FME controls. - In addition, VPAP-1302 was revised -following

rain gear identificat_ion to further enhance the FME program by

requiring additional requirements for documenting clpseout

inspection results. - The inspectors reviewed VPAP-1302, revision -

3, and verified that the corrective actions-in response to

violation were implemented.

b.

Closed VIO 50-280, 281/92-13-01, Failure to Perform Safety

Evaluations for Procedures That Were Used to Operate Plant Systems

Differently Than Described in the UFSAR.

This issue involved

three examples in which the licensee operated plant systems in.a

different manner than described in the UFSAR but had not first

prepared written safety evaluations pursuant to IO CFR 50.59.

The

licensee responded to this violation in a letter dated July 31,

1992.* As corrective action, safety evaluations were prepared for

each of the examples identified. The inspectors reviewed SEs 92-

126, dated June 4, 1992,92-127,.dated June 4, 1992 and 92-171;

dated July 22, 1992.

SEs92-171 and 92-127 identified that

additional procedural controls were necessary.

The inspectors

reviewed procedures 2-0P-49.7, Filling and Draining RSHX Service

Water Supply Piping, revision 2 arid O-OPT-FP-005, Ftre Protection

Water Pumps, revision I and verified that the additional

procedural controls were properly incorporated._

Within the areas inspected, no violations were identified.

10

8.

Exit Interview

The inspection scope and. findings were summarized on January 4, 1994,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection results

listed in the front of the report and those listed below.

Description

Status

(Paragraph No.)

Item Number

URI 50-280, 281/93-30-01.

Open

MER-5 Power Supply Cable*Fire

Barrier Adequacy

  • {parag.raph 6}.

VIO 50-280, 281/92-07-03

Closed

Failure To Prevent Foreign

Material From Entering S_W

System {paragraph 7.a}.

VIO 50-280~ 281/92-13-01.

Closed_

    • Failure to Perform Safety

Evaluations for Procedures

That Were Used to Operate

Plant Systems Differently Than

Described in the UFSAR

{paragraph 7.b}.

Dissenting comments were not received from the licensee. Proprietary *

information is not contained in this report.

9.

Index of Acronyms and Initialisms

BOP

CB

CC/HR -

DCP

DR

ECCS -

FME

I&C

IPE

IPR

IR

LCO

MER

.MFWP

NOE

NOED

NRC

QC

PT

RFO

RS

BALANCE OF PLANT -

CONTROL BANK

CUBIC CENTIMETERS PER HOUR

DESIGN CHANGE PACKAGE

DEFICIENCY REPORT

EMERGENCY CORE COOLING SYSTEM

FOREIGN MATERIAL EXCLUSlON

INSTRUMENTATION AND CALIBRATION

INDIVIDUAL PLANT EXAMINATION

I_NSTALLATION PROBLEM REPORT

INSPECTION REPORT

LIMITING CONDITIONS OF OPERATION

MECHANiCAL EQUIPMENT ROOM

MAIN FEED WATER- PUMP

NONDESTRUCTIVE EXAMINATION

NOTICE OF ENFORCEMENT DISCRETION

NUCLEAR REGULATORY COMMISSION

OPERATIONS CHECKLIST

. PERIODIC TEST

REFUELING OUTAGE

RECIRCULATION SPRAY

RSHX -

SOB

SE

SI

SNSOC -

SW

TB

TS

UFSAR -

URI

VIO

WO

WR 11

RECIRCULATION SPRAY HEAT EXCHANGER

SHUT DOWN BANK

SAFETY EVALUATION

SAFETY INJECTION

,

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SERVICE WATER

TURBINE BUILDING

TECHNICAL SPECIFICATION

UPDATED FINAL SAFETY ANALYSIS REPORT

UNRESOLVED ITEM

VIOLATION

WORK ORDER

WORK REQUEST