ML18152A396

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Insp Repts 50-280/94-21 & 50-281/94-21 on 940703-0806.No Violations Noted.Major Areas Inspected:Plant Status,Ler Followup,Operational Safety Verification,Maint & Surveillance Insps & Safety Assessment
ML18152A396
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/26/1994
From: Belisle G, Branch M, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A397 List:
References
50-280-94-21, 50-281-94-21, NUDOCS 9409130067
Download: ML18152A396 (14)


See also: IR 05000280/1994021

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-280/94-21 and 50-281/94-21

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

July 3 through August 6, 1994

Inspectors:

W. Branch,

Inspector

M~-1tekspector

Accompanying Personnel: ~

W. Garner, Project Engineer

M. Tamai, Intern .

Approved by:

~~-~--~

Scope:

~G.

lisle, Chief

Rea to Projects Section 2A

Division of Reactor Projects

SUMMARY

~6~

Date S,ged

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance and surveillance

inspections, safety assessment and quality verification, Licensee Event Report

followup, and engineering technical specification review project.

Inspections

of backshift and weekend activities were conducted on July 13, 14, 15, and 28 .

9409130067 940826

PDR

ADOCK 05000280

G

PD8_

L

2

Results: *

Plant Operation fun~tional area

Housekeeping in the Unit 2 containment spray pump safeguards area was not up

to the normal station standards. Housekeeping and equipment condition was

good in the emergency service water pump house (paragraphs 3.1.1 and 3.1.2).

Maintenance functional area

The weekly service water flow method of determining component cooling heat

exchanger heat transfer capacity was conservative and provided useful

information to operations and system engineering as to when a component

cooling heat exchanger needed to be .cleaned.

In addition the heat transfer

capability was in excess of that required by Technical Specifications (TSs),

(paragraph 4.1).

The maintenance and surveillance associated with replacing the train A

charcoal filter media were satisfactorily accomplished.

However, an

unresolved item was identified in the area of required charcoal

testing/sampling following a chemical release in the Unit~ containment during

steam generator chemical cleaning activities (paragraph 4.2).

Engineering functional area

The licensee's review of the TS surveillance program was thorough.

The

identification and correction of deficiencies significantly improved the TS

surveillance program.

However, three concerns identified by engineering

involving monthly surveillance functional testing may not have been properly

evaluated.

Resolution of these three concerns was identified as an unresolved

item (paragraph 7) .

REPORT DETAILS

1.

Persons Contacted

2 .

I.I

Licensee Employees

  • B. Allen, Acting Superintendent Operations
  • W. Benthall, Supervisor, Licensing

H. Blake, Jr., Superintendent of Nuclear Site Services

  • R. Blount, Superintendent of Maintenance
  • D. Christian, Assistant Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

  • J. Downs, Superintendent of Outage and Planning
  • D. Erickson, Superintendent of Radiation Protection

A. Friedman, Superintendent of Nuclear Training

  • B. Garber, Licensing
  • L. Hartz, Manager, Nuclear Quality Assurance

B. Hayes, Supervisor, Quality Assurance

  • D. Hayes, Superintendent of Administrative Services
  • M. Kansler, Station Manager
  • C.;Luffman, Superintendent, Security

J. McCarthy, Superintendent of Operations

A. Price, Assistant Station Manager

  • R. Saunders, Vice President, Nuclear Operations
  • V. Shifflett, Licensing
  • E. Smith, Site Quality Assurance Manager
  • T. Sowers, Superintendent of Engineering
  • B. Stanley, Procedures
  • J. Swientoniewski, Supervisor, Station Nuclear Safety
  • G. Woodzell, Nuclear Training

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics,

security force members, and office personnel.

1.2

NRC Personnel

M. Branch, Senior Resident Inspector

  • S. Tingen, Resident Inspector
  • D. Tamai, Intern

L. Garner, Project Engineer

  • Attended Exit Interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

Plant Status

Units I and 2 operated at power for the entire inspection period.

2

3.

Operational Safety Verification (71707)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability. Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping. "Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

3.1

Biweekly ESF Inspections

3.1.1 Unit 2 CS System

The inspectors walked down the Unit 2 CS components located

in the safeguards building, the CS valves adjacent to the

~WST and chemical addition tank and control board

indications for CS pumps and valves.

The inspectors noted

that housekeeping in the safeguards area was not up to the

normal station standards. The area was in the process of

being painted. The area was not being painted on the day of

the walkdown.

There were rags, sand paper, and rubber

gloves on the floor and CS components.

The licensee was

informed and took corrective action by cleaning the area.

3.1.2 ESW System

The inspectors walked down the three diesel driven ESW pumps

located at the low level intake structure.

Items checked

were positions of diesel trip and fuel oil valves,

housekeeping and general condition of equipment.

Equipment

appeared to be in good overall condition and housekeeping

was acceptable. Trip and fuel-oil-valves were in the*

correct positions.

3.2

10 CFR 50.72 Report on Early Warning System Siren Failure

On July 26, the licensee made a non-emergency one-hour

10 CFR 50.72 report due to the Early Warning System being

inoperable.

While performing the Early Warning System polling

functional test, the Early Warning System sirens did not respond

to the polling signal. A failed transistor in the Early Warning

System power supply caused the system failure.

The power supply

was repaired and the system was returned to service at 2:51 p.m.

of the same day.

.*

3

3.3

Unit 2 SG Cleaning Activities

Unit 2 was shutdown between June 4 and 24, 1994, in order to clean

the secondary.sides of the SGs.

The final estimates, in pounds,

of materials removed during the SG cleaning process were:

SG A

SG B

SG C

Copper

350

470

500

2600

3050

3900

Sludge

1258

984

610

The inspectors discussed the sources of corrosion/erosion products

with the licensee and concluded that the most likely source of

copper was from the copper/nickel tubes in the main feedwater

heaters.

The SGs at Surry were replaced in the 1981 time frame.

At that time, the main feedwater heat exchangers had copper/nickel

tubes.

In the 1991 timeframe, all the feedwater heaters in Unit 1

were replaced with new feedwater heaters having titanium tubes.

In 1990 stages 6, 5, 4 and 3 of Unit's 2 feedwater heaters were

replaced with the new design.

The two remaining Unit 2

copper/nickel tube feedwater heaters are scheduled to be replaced

with titanium tube heaters during the 1995 refueling outage which

is currently scheduled to start in February 1995.

Flow assisted

corrosion/erosion of the main feedwater piping is the source of

the iron in the SGs.

The licensee's Flow Assisted Corrosion

Program has replaced iron piping with chrome molly piping in many

instances where wall thinning was identified.

Other than restricting power operations due to oscillating SG

level and causing the operators to be distracted, the SG tube

scaling did not appear to have an adverse effect on plant safety.

The inspectors based this conclusion on the following:

The number of tubes plugged in*the Surry SGs is very low.

Eddy current testing performed during refueling outages have

not identified significant SG tube problems such as denting

or degradation.

Regional inspectors routinely review eddy

current test results and have not identified any significant

problems during these reviews.

The shell sides of SGs are routinely inspected during

refueling outages and no significant problems have been

identified. The resident inspectors accompanied

Westinghouse personnel on one of these inspections and did

not identify any problems.

The licensee utilized cameras to inspect the support plate

regions of the SGs prior to, during and after cleaning.

The

4

results of these inspections were recorded.

With the

exception of plugged tube support quatrefoil assembly

openings identified before cleaning the SGs, no problems

were identified. These films were reviewed by the resident

inspectors and problems were not identified.

In the past the licensee has utilized ammonia and hydrazine for

feedwater pH control. Very recently secondary chemistry controls

was changed for Unit 2 and ETA is being injected into the

feedwater/condensate systems to enhance pH control.

Improved pH

control should reduce the corrosion rate of the feedwater piping.

If this is successful in Unit 2, the same method of feedwater pH

control will be implemented in Unit 1.

Within the areas inspected, no violations or deviations were identified.

4.

Maintenance And Surveillance Inspections (62703, 61726)

During the reporting period, the inspectors reviewed the following

maintenance/surveillance activities to assure compliance with the

appropriate procedures.

4.1

Measuring Macrofouling Blockage in the CCHX

On July 14, the inspectors reviewed completed procedure

l-OSP-SW-005, Measurement of Macrofouling Blockage of

CCHX 1-CC-E-lD, revision 4.

The procedure had just been completed

by the evening shift when the inspectors performed their review.

The procedure's purpose was to provide instructions to monitor

flow through the SW side of CCHX 1-CC-E-lD, and to use the flow

readings obtained to determine the CCHX operability with respect

to the amount of tubesheet macrofouling. All four of the CCHXs

were tested each week to ensure operability.

Procedure l-OSP-SW-005 contained instructions to measure and

record DP across the SW side of the CCHX, as read on the Barton

and Annubar gages .. The SW discharge valve*was throttled-and

several sets of DP measurements were recorded.

The highest set of

DP measurements recorded were plotted on one of six graphs in

attachment 2 of the procedure.

SW temperature was recorded in

attachment 1 and this SW temperature determined which graph to

use~

The six graphs were for different SW temperatures starting

at 70 degrees F and going up to 95 degrees Fin 5 degree

increments.

Each graph had three regions titled "Inoperable",

"Alert" and "Operable".

The results of the July 14 performance of procedure l-OSP-SW-005

were that CCHX 1-CC-E-lD was in the "Alert" region but still

operable.

The operator used the 85 degree F graph in the

procedure since the recorded SW temperature was 84.3 degrees F.

Step 6.2.17 of the procedure instructed using a graph

corresponding to a temperature equal to or higher than the actual

4.2

5

recorded temperature.

The inspectors were in the control room at

10:00 p.m., and noted the following temperatures based on

condenser water box inlet temperatures, which is what the operator

used to measure SW temperature.

The temperatures were taken from

the P-250 monitor and were all in degrees F.

The A CWB inlet

temperature was 85.9, B was 85.4, C was 89.6 and D was 86.1.

Based on the temperatures noted by the inspectors at 10:00 p.m.,

CCHX 1-CC-E-lD would have been inoperable based on the 90 degree F

graph.

The inspectors questioned both the STA and the unit SRO as

to the apparent data discrepancy.

The SRO indicated that CWB

inlet temperature changed with the time of day as well as the

tide. At the time of the test, the data that was recorded was

correct.

The SRO also indicated that the data would be verified.

It was not apparent from the procedure what, if any, margin was

included in the graphs.

As noted above, a CCHX could be operable

or in alert at the time of testing but would be inoperable with an

increase in SW temperature. After questioning by the inspectors

the licensee reperformed the test of 1-CC-E-lD with the elevated

temperature and declared the CCHX inoperable.

DR S-94-1471 was

written to document the unsatisfactory condition.

The inspectors discussed this issue with the system engineer.

Additional information as to the margin contained in the

acceptance criteria used in procedure l-OSP-SW-005 was provided.

Technical Reports ME-0047, revision 0, and ME-0076, revision 0,

CCHX Performance Testing, contained an accurate comparison of

between.the SW flow measurement heat transfer determination and

the CC heat transfer determination.

Periodically more accurate

test equipment including RTDs and ultrasonic flow meters were

temporarily connected to the CCHX's CC side and measurements were

taken.

This CC side heat transfer information was compared to

that obtained from the weekly SW Annubar flow instrument

measurement to determine margin in the weekly measurement.

The

comparative measurements indicated that the Annubar flow

determination was conservative by approximately 30%.

The actual

heat transfer would* be approximately 50 mi 11 ion* Btu/hr verses *

38.5 million Btu/hr.

The inspectors determined that the weekly SW flow method for

determining CCHX heat transfer capacity was conservative and

provided useful information to operations and system engineering

as to when a CCHX should be cleaned.

In addition, the heat

transfer capability was in excess of that required by TSs.

After

reviewing the additional information provided by the licensee the

inspectors had no concerns with the test observed on July 14.

Train A Charcoal Filter Replacement/Testing

On June 16, 1994, a hydrazine concentration of 6 ppm and an

ammonia concentration of 30 ppm were detected in the Unit 2

containment. These fumes were identified after the manways were

6

removed from SGs that had just completed chemical cleaning.

In

order to decrease the concentrations of hydrazine and ammonia *in

containment, ventilation flow rate was increased.

The train A and

train B" AVEF systems were operated to increase the containment

flow rate. The emergency ventilation system charcoal supplier was

contacted and informed the licensee that exposing charcoal to

these fumes was not detrimental to the charcoal.

On June 28, 1994, charcoal samples were obtained for the train A

AVER system and sent to a contractor for analysis. This sample

was obtained to meet the requirement of TS 4.12.A.8.d.

TS 4.12.A.8.d requires that laboratory analysis on charcoal samples

be performed following painting, fire, or chemical release in a

ventilation zone communicating with the system during system

operation.

On July 15 the licensee was notified that analysis

results for the methyl iodide removal rate was 93.43%.

The

minimum methyl iodine removal rate specified in TS 4.12.B.4 was

96%.

The AVEF system train A was declared inoperable.

On July 19 through 22, the inspectors witnessed the licensee

replacing and testing the AVEF system train A charcoal filter

media.

The maintenance was accomplished in accordance with WO 292920 01 and procedure O-MCM-0620-02, Ventilation System Pre-

Filter, HEPA and Carbon Cell Removal, Inspection and Installation,

revision 0.

The inspectors verified that station procedures were

adequate and were adhered to, supervision and maintenance

engineering support was sufficient and appropriate radiological

controls were implemented.

The inspectors concluded that this

maintenance was efficiently accomplished.

No significant problems

were identified and the job progressed smoothly.

After replacement, the train A filter media was tested in

accordance with O-MPT-0620-01, Auxiliary And Control Room

Ventilation System HEPA And Charcoal Filter Test Criteria

Documentation And Verification, revision I.

In order to

accomplish this testing a flow rate of approximately 35,000 CFM

was established and an in-place DOP test was performed.

Results

of the DOP test indicated that the HEPA filters were 99.99%

efficient which was acceptable. After completing the DOP test, a

halogenated hydrocarbon leakage test was performed.

The test

results indicated that the filter media tray seals were 100%

efficient. The DOP and halogenated hydrocarbon leakage testing

was accomplished by a contractor.

The inspectors concluded that

the new filter media was properly tested in accordance with TSs

and licensee oversight of the contractor performing the testing

was adequate.

On July 28 the AVEF train B charcoal filter media was sampled.

On

August 4, the licensee was notified that results of the analysis

was 90.7% methyl iodide removal rate which was below minimum TS

requirements.

The AVEF system train B was declared inoperable.

The charcoal was replaced and DOP and halogenated hydrocarbon

5.

7

leakage tests were performed prior to returning the system to

service.

On August 5 Train B was successfully returned to

service.

At the end of the inspection period, the inspectors were reviewing

the time constraints associated with TSs 4.12.A.6.c, 4.12.A.7.c

and 4.12.A.8.d for sampling/testing the emergency ventilation

filters following exposure to chemical fumes.

This issue was

identified as URI 50-280, 281/94-21-01, Time Constraints For

Sampling/Testing Emergency Ventilation Filters Following Exposure

To Chemicals, pending further review by the inspectors.

Within the areas inspected, one URI was identified.

Safety Assessment and Quality Verification (40500}

The inspectors met with management level personnel at the corporate

Innsbrook office to discuss recent self assessments and ongoing

projects. The Manager of QA described the results of recent self

assessments and provided insight as to focus changes planned by QA to

provide better support to the operating units.

The Vice President of

Engineering shared information and details for several projects his

organization was involved with, including DBD efforts and changes to the

design control process to better control calculation results and ensure

timely incorporation into station design. Additionally, timeliness of

processing internal PPRs was discussed.

The licensee indicated that

their program meets the intent of GL 91-18 as to evaluating

indeterminate or questionable design concerns.

The inspectors will

continue to evaluate design issue resolution as part of the licensee's

corrective action program review.

Within the areas inspected, no violations or deviations were identified.

6.

Licensee Event Report Followup (92700}

The inspectors reviewed the LERs listed below to evaluate adequacy of

the corrective action. The inspectors' review also included followup of.

the licensee's corrective action implementation.

6.1

(Closed} LER 50-280/92-003-01, Incomplete Engineered Safety

Features Testing Due to Procedure Deficiency. This issue involved

calibrating the Units 1 and 2 PRZR PORV channels.

The licensee

identified that the main control room alarm that occurs when a

PORV opens was not being tested during performance of the channel

function test as required by TS 4.1.8.1.b.

Once this condition

was identified the PORV alarm was satisfactorily tested for both

units.

The inspectors reviewed procedures l/2-0PT-ZZ-005,

Verification of Local and MCB Valve Position Indication for the

PRZR PORVs, revision 1, and verified that the upgraded procedures

contained instructions to routinely test the alarm. Also as

corrective action, the licensee performed a review of the TS

8

surveillance program.

Results of this review are discussed in

paragraph 7.

6.2

(Closed) LER 50-280, 281/92-003-02, Incomplete Engineered Safety

Features Testing Due to Procedure Deficiency. This issue involved

calibration of the Units 1 and 2 RMT channels.

The licensee

identified that portions of the RMT channels were not being tested

during the performance of the monthly channel functional test as

required by TS Table 4.1-1, Item 15, in that not all test switch

contacts and interconnecting wiring were being tested.

Once this

condition was identified the test switch contacts and wiring were

satisfactory tested. The inspectors reviewed procedures l/2-PT-

2.19, Refueling Water Storage Tank Level, revision 6, and verified

that the procedures contained instructions to test the switch

contacts and wiring that were previously not tested. Also as

corrective action, the licensee performed a review of the TS

surveillance program.

Results of this review are discussed in

paragraph 7.

6.3

(Closed) LER 50-281/92-002, Two Charging Pumps And One Charging

Pump Service Water Pump Removed From Service Simultaneously Due To

Personnel Error.

With one charging pump and one charging pump SW

pump removed from service for preventive maintenance, an SRO

authorized a surveillance test that rendered each of the remaining

charging pumps inoperable at different times.

With a 24-hour LCO

in effect for the charging pump service water pump being out of

service, a 24-hour LCO was entered each time the two charging

pumps were rendered -inoperable. However, the SRO failed to

recognize that these two simultaneous conditions were a condition

not allowed by TS 3.3 and thus should have required entry into a

six-hour LCO per TS 3.0.1.

In all cases, while not recognized,

the six-hour limitation was not exceeded.

The inspectors verified that the three actions listed in the LER

to prevent recurrence were completed as committed.

Two of the

three actions, the committed test procedure changes and the

station'directive-requiring-specific TS lCO references to be

incorporated into procedures, were no longer in effect. A

philosophy change in the procedure upgrade project resulted in a

different approach to addressing LCOs in procedures than that

reflected by the above two items.

References to specific TSs were

replaced by notifications that certain steps would involve the

potential for or actual entry into a TS LCO.

Identification of

the specific TS LCO to be entered was then based upon existing

plant conditions and the SRO's knowleqge of TS requirements.

The inspectors verified that the latest revisions to the six

upgraded procedures, 1(2)-0PT-CH-001(2 or 3), Charging Pump

Operability and Performance Test For 1(2)-CH-P-lA(B or C), that

replaced 1(2)-PT-18.7, Charging Pump Operability and Performance

Test, were written in accordance with the latest guidance.

The

inspectors also verified that training was conducted and was

9

planned for future training sessions to reinforce that

.

simultaneous TS 3.3 LCO conditions require entry into the TS 3.0.1

LCO.

Specifically, in 1992, classroom training was provided on

LER 50-281/92-002 per requalification lesson plan RQ-92.4-TS-7,

TS 3.3 Safety Injection System.

The simulator lesson plan

RQ-6.SE-l (Loss Of Operating CP, Inleakage To SI Accumulator, Loss

Of MFW, Failure Of Pressurizer Safety Valve) used this year and

next scheduled for 1996 had licensed operators demonstrate proper

entry into TS 3.0.1 LCO for simultaneous TS 3.3 equipment

failures.

In addition, the inspectors confirmed that the initial

licensed training program lesson plan ND 80.3 LP-10, Operation of

eves, provided training on the event discussed in LER 281/92-002.

The inspectors concluded that the upgraded procedures and the

training provided sufficiently complement one another to ensure a

reasonable level of confidence that a similar event will be

precluded.

6.4

(Closed) LER 50-281/92-007, Auxiliary Feedwater System

Recirculation Piping Missile Shielding Removed Due To Personnel

Error.

The licensee determined that failure to follow

administrative procedures resulted in not recognizing that removal

of soil above the full flow AFW recirculation line to the ECST

created the potential for a missile to damage the line and

partially drain the ECST.

The inspectors verified via

documentation reviews that the event was reviewed with the

involved individuals and organization as committed in the LER.

These actions were considered appropriate.

6.5

(Closed) LER 50-281/92-008, Reactor Coolant System Leak Rate

Greater Than 10 GPM Due To Failure Of A Swagelok Fitting On A Flow

Transmitter. The LER indicated that a RCE would identify actions

to prevent recurrence.

The inspectors reviewed RCE Report No.92-009.

The event was caused by a failure to correctly assemble

the flow transmitter Swagelok fitting and an improper method for

repairing leaks on Swagelok fittings.

The inspectors verified

that VPAP-2002, Work Requests And Work Order Tasks, revision 3,

was revised as recommended by the RCE to* delete*tightening

instrument tubing from Attachment 13 as an example of work that

can be performed as minor maintenance.

On February 11, 1994, the

licensee identified that the October 1993 edition of The Accident

Prevention Manual was not revised to include the warning not to

tighten pressurized fittings.

The RCE recommended warnings are

now planned to be incorporate in the manual's next revision.

In

addition, the licensee identified that Gyrolok and Swagelok

fittings are not interchangeable.

The licensee indicated that

Gyrolok fittings had been removed from the stock room.

The

inspectors reviewed documentation that 13 other similar fittings

were inspected and found to be properly assembled.

The actions

taken should be sufficient to preclude recurrence.

Within the areas inspected, no violations or deviations were identified .

10

7.

Engineering TS Review Project (37551)

All TS surveillance and implementing procedures were reviewed by the

licensee in order to verify that the required surveillances were being

properly performed.

The inspectors reviewed the results of the

licensee's TS review Project.

The following issues were identified as a

result of this review:

Three surveillances were identified as not being properly

performed and LERs were issued as a result.

It was identified that the charging pump low pressure auto start,.

accumulator discharge MOV auto open at 2000 psi RCS pressure, loop

stop valve interlock to reactor protection and RHR inlet MOV

interlock circuits were not being functionally tested.

The

licensee concluded that TSs did not require these circuits to be

tested.

The inspectors reviewed TSs and verified that these

circuits were not required to be tested.

    • --

Three surveillance procedures were identified as not providing

adequate instructions for entry into LCOs.

It was concluded that

LCO time constraints were not exceeded but procedures were changed

to;provide guidance for entry into the applicable LCO.

Three surveillances were identified where reactor protection/ESF

circuits were not being fully tested on a monthly basis with the

unit at power because testing required the use of jumpers or

disconnecting wires. These circuits were the auto start of TDAFWP

on lo-lo SG level and RCP UV and opening the reactor trip breakers

on low RCS flow.

The licensee concluded that the circuits were

not designed to test at power and therefore not required to be

tested monthly.

This issue is further discussed below.

The inspectors concluded that the licensee's review of TS surveillance

and implementing procedures was thorough and significantly improved the

quality of the TS surveillance program.

At the end of the inspection

period the inspectors were reviewing -the licensee's justification for*

not completing monthly TS tests on circuits where jumpers or

disconnected leads were required. This was identified as URI

50-280, 281/94-21~02, TS Monthly Testing That Requires Jumpers or Leads

Disconnected to Complete.

Within the areas inspected, one URI was identified .

11

8.

Exit Interview

The inspection scope and findings were summarized on August 10, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection results addressed

in the Summary section and those listed below.

Item Number

URI 50-280, 281/94-21-01

URI 50-280, 281/94-21-02

LER 50-280/92-003-0l

LER 50-280, 281/92-003-02

LER 50-281/92-002

LER 50-281/92-007

LER 50-281/92-008

Status

Open

Open

Closed

Closed

Closed

Closed*.

Closed

Description/(Paraqraph No.)

Time Constraints for Sampling/

Testing Emergency Ventilation

Filters Following Exposure to

Chemicals (Paragraph 4.2).

TS Monthly Testing That

Requires Jumpers or Leads

Disconnected to Complete

(Paragraph 7).

Incomplete Engineered Safety

Features Testing Due to

Procedure Deficiency

(Paragraph 6.1).

Incomplete Engineered Safety

Features Testing Due to

Procedure Deficiency

(Paragraph 6.2).

Two Charging Pumps and One

Charging Pump Service Water

Pump Removed from Service

Simultaneously Due to

Personnel Error (Paragraph

6.3).

Auxiliary FeedwaterSystem*

Recirculation Piping Missile

Shielding Removed Due to

Personnel Error (Paragraph

6.4).

Reactor Coolant System Leak

Rate Greater Than 10 GPM Due

to Failure of a Swagelok

Fitting On a Flow Transmitter

(Paragraph 6.5).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

..

9.

12

Index of Acronyms and Initialisms

AFW

AVEF

BTU/HR

cc

CCHX

CFM

CFR

CP

cs

eves

CWB

DBD

DOP

DP

DR

ECCS

ECST

ESF

ESW

ETA

F

GL

GPM

HEPA

LER

LCO

MOV

MFW

NRC

PORV

PPM

PPR

QA

RCE

RCP

RCS

RHR

RMT

RTD

RWST

SG

SI

SRO

STA

SW

TDAFWP

TS

URI

UV

WO

AUXILIARY FEEDWATER

AUXILIARY VENTILATION EXHAUST FILTER

BRITISH THERMAL UNITS/HOUR

COMPONENT COOLING

COMPONENT COOLING HEAT EXCHANGER

CUBIC FEET PER MINUTE

CODE OF FEDERAL REGULATIONS

CHARGING PUMP

CONTAINMENT SPRAY

CHEMICAL VOLUME CONTROL SYSTEM

CONDENSER WATER BOX

DESIGN BASIS DOCUMENT

PENETRATION OF DIOCTYL PHTHALATE

DIFFERENTIAL PRESSURE

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY CONDENSATE STORAGE TANK

ENGINEERED SAFETY FEATURE

EMERGENCY SERVICE WATER

ETHANOLAMINE

FAHRENHEIT

GENERIC LETTER

GALLONS PER MINUTE

HIGH EFFICIENCY PARTICULATE AIR

LICENSEE EVENT REPORT

LIMITING CONDITIONS OF OPERATION

MOTOR OPERATED VALVE

MAIN FEEDWATER

NUCLEAR REGULATORY COMMISSION

POWER OPERATED RELIEF VALVE

PARTS PER MILLION

POTENTIAL-PROBLEM REPORT

QUALITY ASSURANCE

ROOT CAUSE EVALUATION

REACTOR COOLANT PUMP

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

RECIRCULATION MODE TRANSFER

RESISTANCE TEMPERATURE DETECTOR

REFUELING WATER STORAGE TANK

STEAM GENERATOR

SAFETY INJECTION

SENIOR REACTOR OPERATOR

SHIFT TECHNICAL ADVISOR

SERVICE WATER

TURBINE DRIVEN AUXILIARY FEEDWATER PUMP

TECHNICAL SPECIFICATION

UNRESOLVED ITEM

UNDER VOLTAGE

WORK ORDER