ML18152A354

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Insp Repts 50-280/95-05 & 50-281/95-05 on 950212-0304. Noncited Violations Identified.Major Areas Inspected:Plant Status,Operational Safety/Refueling Activities Verification, & Maint & Surveillance Insps
ML18152A354
Person / Time
Site: Surry  Dominion icon.png
Issue date: 03/27/1995
From: Belisle G, Branch M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A355 List:
References
50-280-95-05, 50-280-95-5, 50-281-95-05, 50-281-95-5, NUDOCS 9504110094
Download: ML18152A354 (17)


See also: IR 05000212/2003004

Text

Report Nos. :

JNITED STATES

>JUCLEAR REGULATORY COMMISSiON

r1EGION II

101 MARIETTA STREET. N.W., SUITE 2900

ATLANTA. GEORGIA 30323-0199

50-280/95-05 and 50-281/95-05

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

February 12 through March 4, 1995

Lead Inspector:

i.':~r~~r k~dent Inspect

Inspectors:

L. W. Garner, Project Engineer

Approved by:

D. M. Kern, Resident Inspector

S. G. Tingen, Resident Inspector

£~ /

/1

'

'

.

  • E7 llK

G. if2 Bel i s1aition Chief

Reactor Projects Section 2A

Division of Reactor Projects

SUMMARY

Scope:

3- )_f -yJ-:-

Date Signed

This routine resident inspection was conducted on site in the areas of plant

status, operational safety/refueling activities verification, maintenance

inspections, surveillance inspections, on-site engineering, plant support,

Licensee Event Report followup, and action on previous inspection items.

Inspections of backshift and weekend activities were conducted on

February 15, 28 and March 1, 1995 *

950411()094 950328

DR

ADOCK 05000280

PDR

2

Results:

Operations:

The reactor vessel head lift was conducted in an efficient and professional

manner (paragraph 3.1.1).

Weaknesses were noted in the procedure used to establish refueling containment

integrity for fuel off-load.

The procedure specified an incorrect method for

establishing refueling containment integrity for some penetrations

(paragraph 3.1.2).

A non-cited violation was identified for failure to monitor the lo~d cell as

required by procedures when fuel was lowered into the spent fuel pool storage

location (paragraph 3.1.3).

Spent fuel pool parameters were properly monitored and maintained while the

of f-1 oaded Un it 2 fue 1 was stored in the spent fue 1 poo 1. ( paragraph 3 .1. 4).

Maintenance:

The scaffolding erected and equipment staged prior to the refueling outage did

not impact operation of Unit 2 (paragraph 4.1) .

Although damaged plastit chain barriers were observed, the oversight and

controls of switchyard activities were appropriate (paragraph 4.2).

Refueling calibration surveillances were performed within the required

interval (paragraph 5).

Plant Support:

During tours of the Unit 2 containment, good ALARA planning and training were

evident (paragraph 7.2).

r

I l

l

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Benthall, Supervisor, Licensing

H. Blake, Jr., Superintendent of Nuclear Site Services

  • R. Blount, Superintendent of Maintenance
  • D. Christian, Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

D. Erickson, Superintendent of Radiation Protection

B. Hayes, Supervisor, Quality Assurance

  • D. Hayes, Supervisor of Administrative Services

C. Luffman, Superintendent, Security

  • J. McCarthy, Assistant Station Manager
  • A. Price, Assistant Station Manager
  • S. Sarver, Superintendent of Operations

+R. Saunders, Vice President, Nuclear Operations

  • K. Sloane, Superintendent of Outage and Planning

E. Smith, Site Quality Assurance Manager

  • T. Sowers, Superintendent of Engineering
  • J. Swientoniewski, Supervisor, Station Nuclear Safety

G. Woodzell, Nuclear Training

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

NRC Personnel

  • M. Branch, Senior Resident Inspector*

D. Kern, Resident Inspector

  • S. Tingen, Resident Inspector
  • Attended Exit Interview

+Participated in Exit Interview By Telephone

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 operated at power during the entire inspection period.

Unit 2 remained shutdown for a planned RFO during the entire inspection

period .

L

3.

2

Operational Safety/Refueling Activities Verification (71707, 60710)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

aware~ess.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability.

Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

3.1

Unit 2 Refueling Activities

The licensee conducted refueling activities from February 12 to

March 4.

Refueling evolutions were performed by contractors under

the direct supervision of licensed personnel.

The inspectors

verified initial plant conditions, attended the pre-evolution

briefs, and observed refueling activities to determine whether

license conditions were*appropriately addressed .

3.1.1 Reactor Vessel Head Lift

On February 12, the reactor vessel head was removed and the

refueling cavity was filled with water in preparation for

fuel off-load. The inspectors observed that the pre-

evolution brief was detailed with communications, personnel

safety, and RP concerns being clearly emphasized.

A

licensed SRO was assigned to coordinate the head lift

evolution.

The inspectors toured the control room and

containment prior to the start of the head lift. Required

plant conditions (i.e., nuclear instrumentation, containment

integrity, RCS boron concentration, shutdown margin, etc.)

were properly established and maintained as required by

procedure 2-0P-FH-001, Refueling Operations, revision 2.

The inspectors inspected the refueling cavity area prior to

th~ head lift to determine whether VPAP-1302, Foreign

Material Exclusion Program, revision 6, was properly

implemented. A barrier was established around the refueling

area. All personnel and material which*entered the

refueling area were tracked using the refueling area

accountability log. Access to the area was kept to a

minimum.

The type and number of items brought into the

refueling area were properly packaged and handled.

The

inspectors considered that the FME controls were good .

Activitie.s inside containment were effectively coordinated

by the SRO in charge. Clear communications were established

I

3

between the main control room, the crane operator, and the

refueling floor.

The containment coordinator and RP

personnel directed all personnel not involved with the RV

head lift to leave containment.

RP technicians performed

continuous area dose rate surveys during the RV head lift

and effectively controlled access to minimize personnel

radiation exposure.

RP support inside containment was

comprehensive.

The RV head movement to the storage stand in

the containment basement level was effectively executed.

The inspector concluded that the RV head lift was conducted

in an efficient, professional manner.

3.1.2 Refueling Containment Integrity

The inspectors reviewed control room indications for the

containment isolation valves used to establish refueling

containment integrity required by TS 3.10.A.l.

Proce~ure

2-0PT-CT-210, Refueling Containment Integrity, revision 5,

was the controlling procedure.

The procedure contained

sheets which depicted the different penetrations and

provided instructions to ensure that the barriers were

acceptable.

The procedure provided for many contingencies

that might be encountered by the operators in establishing

integrity when other activities were in progress.

For the most part, refueling containment integrity was

established by tagging valves in the required position for

the entire period that integrity would be required.

However, there were some valves that were open during the

fuel movement evolution. The inspectors noted that

containment sump isolation valves 2-DA-TV-203A/B were open.

These two valves are designed to automatically close upon

receipt of a containment isolation signal, but the logic for

automatic closure of these valves was deenergized.

TS 2.10.A.l sta.tes in part, "For those penetrations which

provide a direct path from containment atmosphere to the

outside atmosphere, the automatic containment valves shall

be operable or the penetration shall be closed by a valve,

blind flange, or equivalent".

The inspectors questioned whether containment integrity was

properly established for refueling since the automatic

closure of the open isolation valves was not operable. The

SRO indicated that the valves remained operable since they

could be remotely shut from the control room.

The operators

also informed the inspectors that procedure 2-0PT-CT-210

allowed this specific configuration and that they had always

considered that integrity was acceptable with these

isolation valves open during refueling *

The inspectors did not agree with the licensee's

interpretation that valves capable of being remotely closed

,

4

constituted acceptable refueling containment integrity.: The

licensee's position was discussed with cognizant NRC staff

who indicated that remote manual closure capability did not

meet TS 2.10.A.1 for the small number of containment

penetrations that provide a direct path from the containment

atmosphere to the environment.

The licensee was informed

that their position was not acceptable.

2-0PT-CT-210 was

reviewed by the licensee and revised.

The procedure

revision included a list of penetrations where the TS would

apply and an acceptable isolation method for establishing

refueling containment integrity. These penetrations would

either be closed, water sealed, pressurized, or isolable by

an automatic valve actuated by a high radiation signal. The

inspectors noted that the containment sump penetration

valves that were open during the core off-load were

considered to be water sealed and therefore refueling

containment integrity had been established.

The previous 2-0PT-CT-210 instructions that implemented the

licensee's posftion that automatic containment valves

remained operable if they could be remotely shut from the

control room was identified as a weakness.

The inspectors

reviewed 2-0PT-CT-210, revision 6, prior to core on-load and

did not identify additional problems .

3.1.3 Fuel Off-Load

On February 13-15, the core was completely off-loaded using

controlling procedure 2-0P-FH-001.

The inspectors observed

off-load activities from the control room, the refueling

floor in containment, and the fuel building.

The inspectors

independently confirmed that TS requirements to begin fuel

movement were satisfied. Operators established the required

refueling cavity level band and monitored level using a cold

calibrated pressurizer level instrument.

This instrument

had been recalibrated to provide a control room alarm in the

event of decreasing refueling cavity level.

The main

control room was placed on emergency ventilation and direct

communications were established between the control room,

the refueling manipulator crane, and the fuel building.

The order of fuel movement was directed by the refueling

coordinator who tracked core status from the control room.

Fuel movements were specified in the order listed in the

refuel report. Communications were clear and fuel element

transfer times were consistent. The inspectors discussed

the refuel report with the refuel coordinator and determined

that fuel movements were being properly directed and

tracked *

A licensed SRO supervised fuel movements in the containment.

The inspectors discussed individual duties with contract

L

5

personnel operating the fuel manipulator crane and the fuel

transfer system.

Contractor personnel performed the fuel

movement in accordance with approved station procedures and

were knowledgeable of their responsibilities. The crane

operator closely monitored load cell tension when

raising/lowering the fuel gripper tool and when moving fuel

assemblies.

The refueling SRO and contractor personnel

independently verified core locations and positive latching

of fuel assemblies.

The FME area coordinator performed

frequent inspections of the refueling cavity area to confirm

that the area remained clear of foreign material. The

inspectors checked a sample of the items located inside the

FME boundary, and confirmed that each was properly tracked

in the refueling area accountability log.

The inspectors

concluded that the fuel movement within containment was

performed safely under close SRO supervision.

When monitoring the refueling activities in the fuel

building, the inspectors noted that only one person was on

the crane's bridge.

The person operating the bridge crane

was guiding the fuel element into the storage location with

one hand while he operated the electric hoist with the other

hand.

He was watching the fuel element the entire time from

when it entered the storage location to when it appeared to

be on the bottom.

The inspectors noted that refueling

personnel were not monitoring the weight load cell that was

attached to the rigging between the hoist hook and the

refueling tool.

The inspectors questioned the corporate NFA

person who was present in the fuel building as to the

acceptability of the practice of not monitoring the load

cell and the number of required individuals needed to

perform the evolution.

The NFA person indicated that he was

not sure of the Surry requirements but that at North Anna,

because of equipment design, two people were required and

they were also required to monitor the load cell. The

inspectors immediately notified operations management as to

the conditions observed. Activities were stopped and an

additional person was assigned to monitor the load cell.

Deviation Report S-95-0372 was written and later that

evening refueling activities were halted again for the

installation of a larger load cell that could be easily

monitored.

The inspectors reviewed refueling procedure O-OP-4.8, Spent

Fuel Assembly Handling Tool, revision 6.

Precaution 4.7 and

Step 5.3.2 required that the load cell be continuously

monitored while the fuel element was being lowered into the

storage location to detect any binding.

TS 6.4.0 requires

that refueling procedures be followed.

The failure to

monitor the load cell in accordance with O-OP-4.8 was

identified as NCV 50-281/95-05-01, Failure to Monitor load

Cell. This NRC identified violation is not being cited

6

because criteria specified in Section VII.B of the NRC

Enforcement Policy were satisfied.

3.1.4 Spent Fuel Pool Parameters

The inspectors monitored fuel pool parameters while the

Unit 2 fuel was temporarily stored in the spent fuel pool.

The inspectors verified the following:

Spent fuel pool water temperature, level, and boron

concentration were being properly maintained.

At least one spent fuel pool cooling pump and heat

exchanger were operating and the other spent fuel pool

cooling pump and heat exchanger were operable.

Spent fuel pool temperature and level instrumentation

and accompanying control room alarms were calibrated.

The spent fuel pool makeup rate was approximately 500

gallons per day.

The inspectors concluded that the spent

fuel pool parameters were properly maintained.

3.1.5 Fuel On-load

3.2

On February 28 and March 1, the inspectors monitored fuel

movement from the spent fuel pool to the Unit 2 reactor

vessel.

The inspectors verified that procedures for fuel

movement were followed, containment integrity was

established, ventilation was in the refueling alignment, FME

in the fuel building and containment refueling areas was

properly maintained and an SRO was stationed in containment

during fuel movement.

The inspectors concluded that

refueling operations were conducted in accordance with TS

requirements and that command and control were good.*

Unit 2 CV Integrity Inspection

With the assistance of the cognizant system engineer, the

inspectors examined accessible portions of the Unit 2 CV

liner for degradation. Special attention was place on

observing the areas where the CV liner and floor meet for

signs of pitting, general corrosion or wastage of CV liner

material due to abrasion.

No areas warranting repair were

found.

The inspectors noted that the caulking material and

paint at the floor's surface to CV liner interface had

separated from the CV liner at some locations to form

crevices.

In places the crevices allowed the steel CV liner

to be exposed and were sites where potential corrosive

materials might accumulate.

The inspectors noted that the

CV liner behind the containment sump was generally not

assessable for inspection since normally installed trash

,

7

racks and screens preclude access.

The system engineer

indicated, that to his knowledge, inspections performed per

l/2-NPT-CT-101, Reactor Containment Building Integrated Leak

Rate Test (Type A Containment Testing}, had n~ver included

the area were the CV sump is located.

The inspectors noted

that on occasions these racks and screens are removed for

various activities, and thus, this area becomes accessible

for short periods of time in which inspections could be

performed.

These observations were discussed with plant

management.

Within the areas inspected, one NCV was identified.

4.

Maintenance Inspections (62703}

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with appropriate procedures.

4.1

4.2

Unit 2 Pre-outage Sc~ffolding and Equipment Staging

The inspectors walked down areas of Unit 2 prior to the shutdown

for the RFO in order to evaluate the impact of early scaffolding

and equipment staging.

The Unit 2 turbine building had a

significant amount of scaffolding installed in order to support

replacing the MFW heaters and main turbine maintenance.

Scaffolding and equipment staged in the remaining areas of Unit 2

were minimal.

The inspectors noted that barriers were installed

to protect sensitive equipment in the areas where scaffolding was

installed. The inspectors concluded that early scaffolding and

equipment staging did not impact safe operation of Unit 2."

Review of Switchyard Work

The inspectors toured the Surry switchyard during periods of

extensive switchyard work.

The inspectors noted that switchyard

management personnel were present and were sensitive to the

consequences of their actions. The inspectors noted that the

entrance gate was locked and appropriate signs were attached to

inform personnel of risks.

The work in progress was the

installation of a third SOOkv ring bus to complement existing

SOOkv buses 1 and 2.

The inspectors noted vehicles moving within

the yard and observed that personnel were self-monitoring their

activities. The inspectors did note, however, that many small

yellow plastic chains used as vehicle barriers were damaged and

were no longer effective. The Assistant Stafion Manager, who

accompanied the inspectors, also noted the condition of the chains

and informed the switchyard management of the problem.

The

inspectors considered that the plastic chains provided only a

visible and not a physical barrier to vehicle movement.

The

licensee was reevaluating the barriers and considering a change in

8

material type.

The inspectors considered that the oversight and

controls of switchyard activities were appropriate.

Within the areas inspected, no violations or deviations were identified.

5.

Surveillance Inspections (61726}

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure and TS

requirements.

The inspectors reviewed the following TS refueling calibration

surveillances in order to verify that they were completed within the

required TS surveillance interval:

2-IPT-CC-CS-L-200B, RWST Level Loop L-200B Channel Calibration,

revision 1

2-IPT-SI-L-922, SI Accumulator Tank 2-SI-TK-lA Level Loop L-2-922

Channel Calibration, revision O

2-PT-26, RCS Pressure (P-2-403}, revision 4

2-PT-2.5, SG Level (L-2-474}, revision 2

TS 4.1 requires that these surveillances be performed on a refueling

cycle interval. The inspectors reviewed the performance copies of these

surveillances performed during the Unit 2 1993 RFO and verified that

they were completed.

The inspectors also verified that these

surveillances were being performed during the present RFO.

The

inspectors concluded that these surveillances were being performed in

accordance with the required TS surveillance interval.

Within the areas inspected, no violations or deviations were identified.

6.

On-Site Engineering (37551}

On February 23 and 24, the A and B RSSTs were deenergized to support

the switchyard bus 5 outage. This maintenance required that the

Unit 1 J* emergency bus be powered from the Unit 2 500Kv bus via the

station service transformers. During the time that this backfeed lineup

was in effect, voltage on the Unit 1 J emergency bus was higher than

normal.

The inspectors reviewed TS 3.16.B.4 which allows a unit to be

operated for up to seven days when a primary off-site power source is -

not available.

When a primary off-site power source is not available, a

dependable alternate source must be operable. While Unit 1 was in a

backfeed alignment, the action statement for TS 3.16.B.4 was entered.

The inspectors questioned if equipment operation had been evaluated with

the higher than normal voltages on the emergency bus.

The inspectors

reviewed Engineering Report NP-1912, Evaluate Station Voltage, dated

January 30, 1991.

The report stated that during normal electrical

9

lineups maximum emergency bus voltages are 509V and 4305V on the 480V

and 4Kv buses respectively. During the backfeed lineup, emergency bus

voltages could be as high as 554V and 4683Kv on the 480V and 4Kv buses,

respectively. This report concluded that cable and switchgear ratings

were typically 600V for 480V equipment and 5Kv for 4160V equipment and

that overvoltages conditions were therefore not a concern.

The report

also stated that higher than normal operating temperatures could occur

in motors when operated at increased voltages and the time on backfeed

should be minimized.

The inspectors concluded that operation of the

unit in a backfeed alignment was allowed by TSs and that the licensee

had adequately evaluated the equipment operation at higher than normal

voltages.

Within the areas inspected, no violations or deviations were identified.

7.

Plant Support (71750)

7.1

7.2

Injured Worker in Containment

On February 15, a rachet wrench fell approximately thirty.feet and

injured a worker in the C RCS loop room.

The worker received a

small cut to the head.

Another worker in containment promptly

reported the injury to the control room.

The Unit 2 SRO

immediately dispatched the First Aid response team.

EMTs provided

initial assessment of the individual's injury and evacuated the

worker from containment.

RP technicians verified the worker was

not contaminated. After exiting containment, the worker

complained of a sore neck.

EMTs reevaluated the individual's

condition and recommended transport via ambulance to a local

hospital for observation.

The worker was promptly evacuated,

treated at the hospital, and returned to work the next day.

The

inspectors observed licensee response to this event and discussed

followup actions with licensee management.

The inspectors

concluded that on-site medical response to the event was 9009 and

that follow-up actions were appropriate.

Containment ALARA

During tours of the Unit 2 containment the inspectors noted that

good planning and training were evident.

RP staff were

consistently challenging workers as to the purpose of their entry,

as well as, providing guidance and instructions to reduce

exposure.

Water shield tanks were observed surrounding the stored

reactor head and lead shielding was used extensively throughout

containment.

Within the areas inspected, no violations or deviations were identified *

  • 8.

10

Licensee Event Report Followup (92700}

The inspectors reviewed the LERs listed below and evaluated the adequacy

of the corrective action.

The inspectors' review also included followup

of the licensee's corrective action implementation.

8.1

8.2

(Closed) LER 50-280/93-001, Reactor Trip And Safety Injection Due

To Spurious High Consequence Limiting Safeguards Signal. The LER

reported a reactor trip and safety injection due to a single relay

failure in the safeguard circuitry. The response to the reactor

trip and inunediate corrective actions were discussed in NRC

Inspection Report Nos. 50-280/93-03 and 50-281/93-03.

The inspectors verified,that licensee's commitments contained in

the LER's Actions To Prevent Recurrence section were properly

implemented.

Specifically, the inspectors verified that the NSSS

vendor drawing 113E243 sheet 6, revision 12, included test switch

TS-CLS-lA and 18 contacts 2.

In addition, the inspectors verified

that the event was included in lesson resources that are used in

introductory and requalification training sessions for safety

evaluation preparers and reviewers.

The study to identify single

relays that can fail and cause a reactor trip and the preventive

maintenance practices to be implemented for these relays was

inspected as part of the closeout for LER 50-280/93-002 and is

documented in NRC Inspection Report Nos. 50-280/94-08 and

50-281/94-08.

(Closed) LER 50-281/93-002, Unit 2 Automatic Reactor Trip Due To

Low Steam Generator Water Level Coincident With Steam/Feedwater

Flow Mismatch Resulting From Main Feedwater Pump Trip.

The LER

discussed a reactor trip that resulted from a loss of feedwater

due to an electrical ground in the A MFP inboard motor.

The

reactor trip and inunediate corrective actions were addressed in

NRC Inspection Report Nos. 50-280/93-15 and 50-281/93-15.

In the

LER, the licensee committed to perform a RCE to determine why the

motor failed.

The inspectors reviewed RCE 93-11 that concluded

the failure was most likely due to foreign material that either

was left in the motor when it was rebuilt or fell into the motor

after it was re-installed. The inspectors verified that

O-ECM-1406-01, Main Feedwater Pump Motor Maintenance, revision 3,

step 6.3.1 required FME controls to be initiated. Proper FME

implementation should preclude similar motor failures.

8.3

{Closed) LER 50-281/93-004, Unit 2 Turbine-generator Trip Via

The Loss Of Field Relay.

The turbine-generator/reactor trip

reported in this LER was discussed in NRC Inspection Report Nos.

50-280/93-22 and 50-281/93-22.

In the LER the licensee conmitted

to review voltage regulator performance.

The licensee detennined

that the failure was not similar to previous voltage regulator

failures experienced at the station. However, in meetings with

Westinghouse and the voltage regulator vendor, several items were

identified which could improve the voltage regulators'

11

reliability. The inspectors verified that these items were being

implemented.

The LER also reported a spurious closure of Fire Door 18 and

discussed position indication problems with control rod M-10.

An

engineering review failed to identify the cause of the spurious

fire door closure.

No additional spurious actuations have

occurred. During the present refueling outage, repairs were made

to M-10 position indicating components.

However, success of these

efforts cannot be determined until the position indicator's

performance is observed during a reactor shutdown.

This later

item continues to be tracked by the licensee. Based upon the

completed commitments and the planned actions associated with

M-10, this LER is considered closed.

8.4

(Closed) LER 50-280, 281/93-009, Mechanical Equipment Room #4 Fire

Door Left Blocked Open Due To Personnel Error.

The LER involved a

failure to maintain a fire watch on an open fire door.

The LER

indicated that this event and fire watch responsibilities were

discussed with fire watch qualified personnel and .their

supervision.

The inspectors verified that training on this LER

had been included in fire watch lesson resource NET-9-LP-l, Fire

Watch Training, and in fire watch reverification lesson resource

NECT-9-LP-l, Fire Watch Reverification .

8.5

(Closed) LER 50-280/93-014, Delta Flux Not Logged While Alarm Was

Inoperable Due To Procedural Deficiency.

The LER described a

condition in which a partial failure in the Prodac-250 computer

resulted in the axial flux difference not being logged and

assessed as required by TS.

The need to perform the TS action was

not identified after a computer problem light was received because

the displayed values appeared reasonable.

However, a malfunction

in the computer's integration an4 averaging functions resulted in

the displayed values not being updated and thus invalid.

In the

LER's Action To Prevent Recurrence section, the licensee co11111itted

to revise O-AP-20.02, Loss of the Prodac-250 Computer, to address

partial and complete computer failures.

The inspectors reviewed

O-AP-20.02, revision 2, and confirmed that instructions, as well

  • as, entry conditions for partial loss of the Prodac computer were

incorporated into the procedure.

Proper implementation of this

procedure should help preclude similar events from occurring.

In

addition, the inspectors verified that the O-AP-20.02 revision

and this event were incorporated into LORP Training Synopsis

RQ-94-4TS-10 *

. 8.6

(Closed) LER 50-280/93-015, More Than One Individual Rod Position

Indication Channel Per Group Inoperable. The LER reported a loss

of all control and shutdown rod IRPis due to a momentary ground

created when a signal conditioning module with an extension board

was inserted into the instrument racks during calibration. The

LER attributed the fault to the insertion of the extension card

into the modular plug. Subsequent to the LER submittal, the

'

L

L

12

ground was attributed to a broken wire on the extension card.

The

card was repaired and no further corrective actions were taken.

The. inspectors concluded that the licensee's response to this

event was appropriate.

Within the areas inspected, no violations or deviations were identified.

9.

Action on Previous Inspection Items (92901, 92903)

9.1

(Closed) URI 50-280, 281/93-15-01, Use Of PRA For Unreviewed

Safety Question Determination.

SEs93-142 and 93-155 were

prepared to justify placing a MFRV on its jack. Both SEs were

based upon engineering judgement that was bolstered by PRA

considerations.

SE 93-155 superseded SE 93-142.

The inspectors

determined that the engineering judgements without the PRA

arguments were sufficient justification to support the

acceptability of SE 93-155.

The URI was opened to explore whether

PRA considerations, as provided in NSAC-125, Guidelines For 10 CFR

50.59 Safety Evaluations, could be used in performing 10 CFR 50.59

reviews. According to cognizant NRR personnel, the staff has not

approved a simple reference to NSAC-125 as an acceptable method of

evaluation against the criteria specified in 10 CFR 50.59.

Acceptable use of PRA and IPEs are currently being examined by the

staff. Since the subject is germane to the industry and not just

this licensee, this item is considered closed.

9.2

(Closed) URI 50-280, 281/93-26-01, EOP Adequacy.

The URI

concerned an interpretation of a WOG standard procedure relating

to when AFW flow could be throttled to limit RCS cooldown after a

reactor trip. After review, the licensee determined that AFW flow

should be throttled so that the RCS temperature would be

maintained at or trending toward 547 degrees F.

AFW flow would

not be throttled below the minimum value specified for

establishing an adequate heat sink.

The inspectors verified that

l-ES-0, Reactor Trip or Safety Injection, revision 15, step 20 and

l-ES-0.1, Reactor Trip Response, revision 12, step 1 contained the

appropriate instructions to limit cooldown by throttling AFW flow.

LORP lesson plan RQ-94-2-LP-DRR, Emergency Operating Procedure

Revisions, was utilized to inform operating personnel of this

change.

9.3

(Closed) IFI 50-280, 281/94-31-02, SRF Overpressurization NOUE -

Control of Work Activities. This item involved control of

licensee work activities which led to a chemical waste treatment

tank rapid overpressurization on November 25, 1994.

The

overpressurization injured one person and resulted in a NOUE.

Radiological contamination was not involved. The licensee

initiated RCE 94-24 and an independent incident review by a

contractor. The RCE detennined that existing procedures for

operating the SRF wet oxidation system did not address the

chemical addition method used on November 25.

In addition,

ineffective management oversight was identified as a contributing

13

cause.

These findings were consistent with those of the

independent contractor incident review. During followup~ the

inspectors experienced difficulty obtaining complete information

through personnel interviews. This difficulty did not alter the

inspectors' course of action or final conclusions. Licensee

management subsequently took action to assure complete and

accurate information was provided.

The licensee initiated several

immediate and long term corrective actions to address the event.

Actions included developing procedures to cover a wider variety of

system operations, safety evaluation of system operation, and

personnel actions. The inspectors concluded that these actions

were .appropriate to preclude recurrence.

Within the areas inspected, no violations or deviations were identified.

10.

Exit Interview

The inspection scope and findings were summarized on March 7, 1995, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection results addressed

in the Summary section and those listed below.

Item Number

Status

DescrigtionL(Paragragh No.}

NCV 50-281/95-05-01

Closed

Failure to Monitor Load Cell

(paragraph 3.1.3).

LER 50-280/93-001

Closed

Reactor Trip And Safety

Injection Due To Spurious High

Consequence Limiting

Safeguards Signal

(paragraph 8.1).

LER 50-281/93-002

Closed

Unit 2 Automatic Reactor Trip

Due To Low Steam Generator

Water Level Coincident With

Steam/Feedwater Flow Mismatch

Resulting From Main Feedwater

Pump Trip (paragraph 8.2).

LER 50-281/93-004

Closed

Unit 2 Turbine-generator Trip

Via The Loss Of Field Relay

(paragraph 8.3).

LER 50-280, 281/93-009

Closed

Mechanical Equipment Room #4

Fire Door Left Blocked Open

Due To Personnel Error

(paragraph 8.4).

' L

~ *

14

Item Number

Status

Description/(Paragraph No.)

LER 50-280/93-014

Closed

Delta Flux Not Logged While

Alarm Was Inoperable Due To

Procedural Deficiency

(paragraph 8.5).

LER 50-280/93-015

Closed

More Than One Individual Rod

Position Indication Channel

Per Group Inoperable

(paragraph 8.6).

URI 50-280, 281/93-15-01

Closed

Use Of PRA For Unreviewed

Safety Question Determination

(paragraph 9.1).

URI 50-280, 281/93-26-01

Closed

EOP Adeq~acy (paragraph 9.2).

IFI 50-280, 281/94-31-02

Closed

SRF Overpressurization NOUE -

Control of Work Activities

(paragraph 9.3).

Proprietary information is not contained in this report . Dissenting

comments were not *received from the licensee.

11.

Index of Acronyms and Initialisms

AFW

ALARA

CFR

CV

ECCS

EMT

EOP

FME

IFI

IPE

!RPI

Kv

LER

LORP

MFP

HFRV

MFW

NCV

NFA

NOUE

NRC

NRR

NSAC

NSSS

AUXILIARY FEEDWATER

AS LOW AS REASONABLY ACHIEVABLE

CODE OF FEDERAL REGULATIONS

CONTAINMENT VESSEL

EMERGENCY CORE COOLING SYSTEM

EMERGENCY MEDICAL TECHNICIANS

EMERGENCY OPERATING PROCEDURE

FOREIGN MATERIAL EXCLUSION

INSPECTION FOLLOWUP ITEM

INDIVIDUAL PLANT EXAMINATIONS

INDIVIDUAL ROD POSITION INDICATION

KILOVOLTS

LICENSEE EVENT REPORT

LICENSED OPERATOR REQUALIFICATION PROGRAM

MAIN FEEDWATER PUMP

MAIN FEEDWATER REGULATING VALVE

MAIN FEEDWATER

NON-CITED VIOLATION

NUCLEAR FUEL ANALYSIS

NOTICE OF UNUSUAL EVENT

NUCLEAR REGULATORY COMMISSION

NUCLEAR REACTOR REGULATION

NUCLEAR SAFETY ANALYSIS CENTER

NUCLEAR STEAM SUPPLY SUPPLIER

" *

PRA

RCE

RCS

RFO

RP

RSST

RV

RWST

SE

SG

SI

SRF

SRO

TS

URI

V

WOG

15

PROBABILISTIC RISK ASSESSMENT

ROOT CAUSE EVALUATION

REACTOR COOLANT SYSTEM

REFUELING OUTAGE

RADIATION PROTECTION

RESERVE STATION SERVICE TRANSFORMER

REACTOR VESSEL

REFUELING WATER STORAGE TANK

SAFETY EVALUATION

STEAM GENERATOR

SAFETY INJECTION

SURRY RADWASTE FACILITY

SENIOR REACTOR OPERATOR

TECHNICAL SPECIFICATION

UNRESOLVED ITEM

VOLTS

WESTINGHOUSE OWNERS GROUP