ML18152A295

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Insp Repts 50-280/89-03 & 50-281/89-03 on 890123-27 & 0201-02.No Violations or Deviations Noted.Major Areas Inspected:Followup on Recently Identified Operating Events Re motor-operated Valve Deficiencies
ML18152A295
Person / Time
Site: Surry  Dominion icon.png
Issue date: 03/14/1989
From: Conlon T, Merriweather N, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A296 List:
References
50-280-89-03, 50-280-89-3, 50-281-89-03, 50-281-89-3, NUDOCS 8904040005
Download: ML18152A295 (19)


See also: IR 05000280/1989003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/89-03 and 50-281/89-03

Licensee:

Virginia Electric and Power Company

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.: DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

S. Tingen

Other Contributors to this Report:

C. Paulk

Approved bc;/.~~,p;;y,/,,';,,,A~

T. E. Conlon, Chief

Plant Systems Section

Engineering Branch

Division of Reactor Safety

SUMMARY

1-2, 1989

3*- /fL-t'J

Date Signed

,:'?

'

9.-,

.,;, .. - It-*/ r.* /

Date Signed

37~ 11/-CZ-9'

Date Signed

Scope:

This special announced inspection was conducted to followup on

recently identified operating events involving motor operated valve

deficiencies and degraded Silicone Rubber power feeder cables

supplying power to the Inside Recirculation Pump Motors.

Subsequent

to the inspection, a special inspection was also conducted on

February 1-2, 1989, at the GE Safe Apparatus Center in Memphis,

Tennessee, to examine damage discovered on the Inside Recirculation

Pump Motor cable leads.

The results of this inspection are* also

summarized in this report.

Results:

No violations or deviations were identified; however, one Unresolved

Item (URI) 280, 281/89-03-01, paragraph 4.a., was opened to further

investigate the root cause for the degradation of Inside Recircula-

tion Pump Motor Power Cables.

The cables were previously qualified

to the requirements of IEB 79-018,

11Guidelines for Evaluating Environ-

mental Qualification of Class IE Electrical Equipment in Operating

Reactors

11 *

The licensee 1 s actions in regard to this concern appear

to be reasonable and sound.

Management appears to be supporting this

effort at all levels.

040005 890317

8904

05000280

PDR

ADOCK

PNV

G

2

In paragraph 3.b, a weakness was identified that involved the licensee

1 s

slow response in evaluating root cause and determination of corrective

action to prevent reoccurrences for Station Deviations written against

motor operated valves during the present Units 1 and 2 outages.

During

the exit interview the licensee verbally committed to perform root cause

analysis of Station Deviations written against motor operated valves and

establish measures to prevent reoccurrences prior to the respective Unit

restarc.

In paragraph 3.b, deficiencies in the licensee

1 sBulletin 85-03 program

were identified that involved testing motor operated valves without

appropriate different i a 1 pressure which is not in accordance with the

Bulletin requirements, and an excessive amount of station deviations

written against Bulletin valves after completion of the Bulletin

program .

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • D. A. Christian, Outage Coordinator
  • E. Grecheck, Assistant Station Manager
  • R. Green, Supervisor - System Engineering
  • G. D. Miller, Licensing Coordinator

W. Murray, Virginia Power Representative at GE Safe Apparatus Center

  • J. W. Ogren, Superintendent of Maintenance
  • T. B. Sower, Superintendent of Engineering

Other licensee employees contacted during this inspection included

craftsmen, engineers, technicians, and administrative personnel.

NRC Resident Inspectors

W. Holland, Senior Resident Inspector, Operations

  • L. Nicholson, Resident Inspector
  • J. York, Senior Resident Inspector, Construction
  • Attended exit interview

Acronyms and initalisms used throughout this report are listed in the

last paragraph.

2.

Action on Previous Inspection Findings (92701)

(Open)

Inspector Fol lowup Item 50-280, 281/88-45-01,

MOV Deficiency

Followup.

For discussion of findings, see paragraph 3.a below.

3.

Motor Operated Valve Deficiency Followup and IE Bulletin 85-03 Followup

(92701)

a.

(Open) 280, 281/88-45-01 MDV Deficiency Follow-up

During the. present Units 1 and 2 outages, the licensee has identified

numerous MOV deficiencies.

In order to become familiar with the MDV

defi ci enci es and the licensee responses to the defi ci enci es, the

inspector held discussions with licensee Technical Engineering and

Maintenance personnel and reviewed the following:

0

0

Approximately 200 Station Deviation. Reports written by

licensee personnel against Units 1 and 2 MDVs.

MDV

wa l kdown

data sheets for Unit 1 SMB-000 and 00

Limitorque actuators.

0

0

0

0

2

Engineering Work Request 89-061, dated January 22, 1989,

which documents the activities and decisions made for

inspection, repair, and replacement of Units 1 and 2 MOVs.

Surry Site Office Memorandum, dated November 10, 1988, to

R. H. Blount from

R. V. Green/J. LaFlam, Motor Operator

Evaluation, Surry Power Station Units 1 and 2, NP-1657/

PES NP-1718.

Section 5 of Surry Administrative Procedure SUADM-0-12,

Station Deviation Reports.

Licensee Event Report 50/280-43, dated December 9, 1988,

RSHX SW MOVs Discovered with Wrong Size Motors.

(1) Administrative Procedure SUADM-0-12 provides instructions for

reporting, processing, and disposition of Station Deviation

Reports.

Once a Station Deviation Report is initiated, it is

reviewed by station supervisory personnel to determine if

immediate action is required. Station Deviation Reports with a

fi na 1 response that include actions to prevent recurrence are

reviewed by the Station Safety and Operating Committee.

In

addition, Station Deviation Reports are trended in order to

identify problem areas.

Examples of Station Deviation Reports

written against Units 1 and 2 MOVs during the present Units 1

and 2 outages are as follows:

Valve

ID No.

2FW-251E

1CH-1275B

1SW-105A

1SW-104B/105C

2CS-202B

SW-1068

Deviation

Re12ort No.

S2-88-929

Sl-88-1667

Sl-89-53

Sl-88-1250

S2-88-779

Sl-88-1261

Deficiency

New motor installed without tee

drains

Homemade tripper fingers installed

Non-factory tripper fingers

installed

Wrong size motors installed.

Have

2 ft.-lb. motors where other SW-104

and 105 valves have 5 ft.-lb. motor

(also addressed in LER 50/280-43)

Wrong tripper finger bolt installed

Tripper spring incorrect, appears

to be cutdown larger spring

Valve

ID No.

2FW-254E

2FW-254B

2FW-254A .

1SW-102A

1SW-102A

1SI-1869A

2RH-2700

2CS-202B

2CW-200D

2CW-206D

1SW-106B

1RH-1720B

lSI-1842

1SW-103A

1SW-104A

2VS-202

2CH-2864B

Deviation

Report No.

S2-88-934

S2-88-935

S2-88-936

Sl-88-1246

Sl-88-1262

Sl-88-1463

Sl-88-995

S2-88-779

S2-88-779

S2-88-800

3

Sl-88-1278

Sl-88-634

Sl-88-600

S 1-88-611

Sl-88-593

S2-88-289

S2-88-904

Deficiency

Spring pack assembled incorrectly

Spring pack assembled incorrectly

Spring pack assembled incorrectly,

stem lock nut not tight or staked

Bevel gear on worm shaft backwards,

declutch spacer missing

Extra spacer in worm gear shaft,

pinion gear backwarps

Cracked limit switch block

Torque switch wired incorrectly

Drive sleeve staked incorrectly,

required drive sleeve replacement

Pinion gear installed correctly but

not complete contact with shaft*

Wiring in

MDV was found spliced

with unacceptable splice method

Incorrect

number

of

Belleville

washers installed and incorrectly

stacked

Va 1 ve would not open, draws high

current

Valve would not close with high

Differential Pressure

Would not operate during PT 25.2

Failed to open on Hi Hi containment

isolation signal per PT 8.5A

Valve

would

not

operate

electrically

Will not open electrically

Valve

ID No.

Deviation

Report No.

4

lVS-lOOC

Sl-88-417

2SI-28908

S2-88-496

SW-204A, C,D

S2-88-079

2SW-2058, D

S2-88-356

2SW-206A

S2-88-709

2SW-2068

S2-88-374

2SI-28648

S2-88-853

2CH-28698

S2-88-774

1SW-105A

Sl-88-117

2CH-22878,C

S2-89-026

1SW-102A

1SW-105D

1CH-1287A

2VS-201

lCH-12878

Sl-88-298

Sl-88-1252

Sl-88-524

S2-88-958

Sl-88-1672

Deficiency

Valve cannot ,be opened electrically

from main control room, it can be

closed electrically

Would not fully close electrically,

had leakage, had to manually close

Would not fully close

Would not fully open

Valve tagged shut but disc is one

inch from shut seat

Valve will not close electrically

Did not open when had Differential

Pressure across va 1 ve seat, va 1 ve

made clanking noise

With Differential Pressure valve

would

not

fully

close,

after

securing pump it closed

Valve goes past closed seat when

operated remotely

Motors 1 ocked up when attempt to

cycle from main control room

In

attempt to open

from

main

control room, valve would go to

intermediate position

and

motor

would keep running

Would

not

open

during

MOVATs

testing

Will

not close at Differential

Pressure

Did not indicate fully closed

Won't engage manually

Valve

ID No.

2SI-2867A

2CW-200D

SI-1885A

2SI-2850D

2SW-206A

2SW-206B

2SW-206B

2SI-2865B

1SW-103C

lCW-1068

1CH-1275B

2CW-206B

1S~!-105A

Deviation

Report No.

S2-88-899

S2-88-799

Sl-88-1514

S2-88-707

S2-88-736

S2-88-512

S2-88-807

S2-88-741

Sl-89-35

Sl-88-1564

Sl-88-1667

S2-88-985

Sl-89-53

lCH-12878

Sl-88-1072

1SI-1865C

Sl-88-1034

1SW-105A,B,C

Sl-88-647

1SW-104A,B,C

2RS-256A

S2-88-499

5

Deficiency

Motor grounded

Motor grounded

Motor leads have improperly sealed

Raychem channe 1 s *

Torque switch cracked due to

improper installation

Motor 1 eads terminated with wire

nuts, should be Raychem splices

Open/close indication incorrect,

problem was incorrectly wired limit

switch

Worm shaft "O" ring missing, no

grease in actuator, worm shaft

bearing cracked and badly degraded

Pinion gear installed in reverse

direction

Torque switch installed backwards

No lubricant in actuator housing

Bad grease

Unapproved

lubricant in motor

housing

Tripper

finger

damage,

metal

filings in grease

Bad grease

Wrong type grease

Missing manual engage levers, signs

of use of pipe wrench to manually

engage valve

Valve found torn apart with yellow

tag on handwheel

( '))

,'-

Valve

ID No.

lRC-1593

2SW-204A

2RC-2591

Deviation

Report No.

Sl-88-527

S2-88-837

S2-88-826

6

Deficiency

Working wrong valves, in process of

repack when run into water

Adapter between HBC actuator and

valve broken

Declutch handle broken and wired in

place, handwheel removed and laying

in pump room corner

On November 3, 1988, Limitorque Corporation issued a 10 CFR

Part 21 Notification identifying a defect in SMB-000 and 00

actuators supplied with Mel amine torque switches that have

failed and recommended replacement with Fiberite torque

switches.

In response to this notification, the licensee

conducted a walkdown of all Limitorque SMB-000 and 00 actuators

to identify Melamine torque switches.

While performing these

wa 1 kdowns,

actuator extern a 1 components and 1 i mit switch

compartment internal components were inspected and deficiencies

documented in

MOV

Walkdown Data Sheets.

Examples of

deficiencies noted duri~g the walkdowns are as follows:

Valve

ID No.

1CH-1287C

1CH-1287B

1CH-1115E

1PG-107A

Deficiency

Dirt and debris on valve stem and drive sleeve.

Severa 1 broken conductors at 1 ugs on fie 1 d and

jumper wires.

Several wires had tape at lug*to

wire junction.

Four 1 imit switch coverbolts

could not be torqued to 20 ft.-lb. because they

were stripped.

Stem not visable due to cover for contamination

and leak.

Upper bearing housing cover has slight

bow.

All power leads (field leads) have elec-

trical tape at lugs.

Dry Stem.

Wires have broken strands.

One upper

bearing housing bolt is stripped.

(

Dirty Stem.

Packing leak.

Fingerboard missing

from lower set of limits.

Limit switch contacts

corroded.

D~clutch shaft is bent .

Valve

ID No.

(con 1d)

1SW-104A

lCH-1370

lRC-1587

7

Deficiency

Deel utch 1 ever is very 1 oose due to worn key

slot.

Valve position indicator missing six of

Eight rivets.

Some separated grease at limit

switches.

Upper bearing and motor gaskets are

old and leaking.

SMB to HBC adapter has two

different size of bolts.

HBC mounting bolts do

not have full engagement (too short).

Dry dirty valve stem.

Wires exposed on lug,

broken connectors.

Operator * grease found

in

limit switch body.

Valve stem is dry and dirty with some oxidation.

Upper bearing housing gasket extremely worn.

No

stem

cover

on

operator.

Drive

sleeve

is

extremely dirty.

Both open torque switch wires

are broken completely at terminal lugs on limit

switch.

Limit switch cover missing 2 bolts.

During the walkdowns numerous deficiencies were identified that

involved disconnected torque and limit switch wiring and broken

wire strands.

Past Surry practice has been to in sta 11 wiring

that is environmentally* qualified with wiring identifcation

number markings visible.

This resulted in excessively long

wires being installed in a small area.

The licensee considers

the cause of the broken wire strands and wires to be rubbing of

the limit switch cover on the wires during removal of the cover.

Corrective action involves installation of shorter limit and

torque switch wires.

b.

IE Bulletin 85-03 Follow-up (25573)

(Open) 50-280, 281/85-BU-03, T2515/73, "Motor Operated Va 1 ve Common Mode

Failure During Plant Transients Due to Improper Switch Settings.

11

The purpose of this Bulletin is to require licensees to develop and

implement a program to ensure that switch settings for High Pressure

Coo 1 ant Injection and Emergency Feedwater System Motor Operated Va 1 ves

subject to

testing for operational

readiness

in

accordance with

10 CFR 50.55a(g) are properly set, selected and maintain-ed.

In order to evaluate the Surry Bulletin 85-03 program, the inspector held

discussions with the appropriate licensee personnel and reviewed the

fo 11 owing:

0

Approximately 30 Stati.on Deviation Reports filed against Bulletin

85-03 valves.

0

0

0

8

Virginia Electric and Power Company's letter dated May 13, 1986,

Serial No.86-276, Surry Power Station Unit Nos. 1 and 2, Response to

IE Bulletin 85-03.

Virginia Electric and Power Company's letter dated October 17, 1986,

Serial No. 86-276A, Supplemental Response to IE Bulletin 85-03.

Virginia Electric and Power Company's letter dated September 30,

1988, Serial No. 86-276B, Surry Power Station, Units 1 and 2,

Response to IE Bulletin 85-03.

Twenty-nine valves in each unit are in the Bulletin 85-03 program,

and per the licensee, all Bulletin action items were completed, with

the exception of submittal of the final response, during outages in

1987.

On September 30, 1988, Virginia Power issued their final

response to Bulletin 85-03 which implied that adequate measures had

been taken to ensure that valve operator switches are selected, set,

and maintained properly. During review of Station Deviation Reports

generated during the present Units 1 and 2 outages, the inspector

noted that there were deficiencies written on 17 of the 29 Unit 1

Bulletin valves and 8 of the 29 Unit 2 Bulletin valves.

Examples of

deficiencies written on Bulletin valves are as follows:

Valve

Deviation

ID No.

Report No.

1CH-1267B

Sl-89-067

2CH-2289A

Sl-88-0719

2CH-2289A

S2-88-0281

1CH-1289A

Sl-88-1450

2FW-251F

S2-88-0124

2CH-28670

S2-88-151

1FW-151F

Sl-88-577

1CH-1269A

Sl-88-1503

Deficiency

Non-factory

installed

tripper.

fingers

Roll pin installed in lieu of dowel

pin, no shims installed in lower

bearing cup which caused improper

alignment of gears and subsequent

damage.

Va 1 ve wi 11 not close under differ-

ential pressure

Motor grounded

Valve failed to open

Would not close on termination of

safety injection

Valve

not

completely

closing

against fl ow

Motor will not engage electrically

and valve will not cycle electri-

cally

Valve

ID No.

1CH-1286B

lFW-151,B,D,

E,F

lFW-151,B,D,

E,F

Deviation

Report No.

Sl-88-1668

Sl-88-107

Sl-88-167

9

Deficiency

Valve wil 1 not manually engage,

hardened grease, worm gear won

1t

turn, broken teeth on worm shaft.

Metal filings in grease.

Bad motor

bearing

Valve will not go into manual and

grease separated

Tripper fingers are same length

Status of Surry Units 1 and 2 Bulletin 85-03 action items a. through f.

(1)Bulletin 85-03, Action Item a. requires the design basis for the

operation of each bulletin valve be reviewed and documented.

This

item has been completed.

The licensee documentation of the design

review states that an 80% degraded voltage criteria was applied to

the design thrust value~ for the Bulletin valves .

(2)

Bulletin 85-03, Action Item b. requires correct switch settings be

established and methods for selecting switch settings be reviewed and

revised as necessary.

The licensee has completed this item.

(3)Bulletin 85-03, Action Item c. requires that switch settings be

changed as appropriate based on the design review performed, and each

valve be demonstrated operable by testing the valve at the maximum

differential pressure it will

see during the design accident

condition. If a valve is not differential pressure tested, justifi-

cation is then required, and at a minimum, the valve is required to

be stroke tested at static conditions to verify switch settings. All

Surry bull et in valves have been stroke tested with MOVATS test

equipment to verify proper switch settings.

Surry Bul 1 et in 85-03

program has identified 29 valves in each Unit. Differential pressure

testing has been performed on the following seven valves.

Valve No.

Manufacturer

Size

Valve Type

1CH-1289A

Anchor-Darling

311

Gate

1CH-1289B

Anchor-Darling

311

Gate

1SI-1867D

Anchor-Darling

3

Gate

2CH-2289B

Anchor-Darling

311

Gate

2FW-251F

Walworth

311

Globe

2FW-260B

Crane

611

Gate

2SI-2867D

Anchor-Darling

311

Gate

( 4)

10

Exmaples of* valves in Surry Bu 11 et in 85-03 program that were not

differential pressure tested.

Valve No.

Manufacturer

Size

Type

1CH-1115B

A 1 oyco

311

Gate

1CH-1115C

Aloyco

411

Gate

1CH-1267A

Aloyco

511

Gate

1CH-1275A

Velan

211

Gate

1CH-1286A

Velan

311

Gate

The purpose of Bull et in 85-03 differenti a 1 pressure testing is to

verify that the formula to determine required thrust to operate a

va 1 ve is correct.

The results of the Surry different i a 1 pressure

testing proves that the thrust formulas for 311 Anchor-Darling Gate

valves, 311 Walworth globe valves and 611 Crane valves are correct.

However, the thrust formulas for the Aloyco and Velan gate valves has

not been proven.

In addition, the Unit 2 FW-251 valves have been

replaced.

If the replacement valves are a different type than the

ori gi na 1 2FW-251 va 1 ve, then their thrust formulas must a 1 so be

vetified.

The inspector considers that the licensee Bulletin 85-03

program does not fully meet the differe~tial pressure test require-

ments in reference to the Aloyco and Velan valves in that these

valves were not differential pressure tested at maximum design

differential pressure, nor was acceptable justification provided for

not differential pressure testing.

Bulletin 85-03, Item d. requires procedures to be prepared or revised

to ensure that switch settings are maintained throughout plant life.

Applicable industry standards are considered in these procedures, and

procedures should include provisions to monitor valve performance.

The inspector did not review Surry MOV procedures or bulletin valve

post-maintenance test requirements during the inspection.

These

areas will be reviewed during a future inspection.

Per the licensee

bulletin valves are MOVATS tested during each refueling outage as one

of the means to verify valve performance through out plant *life.

During a future inspection the inspector will review the implementa-

tion of the diagnostic testing that is performed each refueling

outage and following post-maintenance testing.

(5)

Bulletin 85-03, Action Item e. is complete and documented in Inspec-

tion Report Nos. 50-280, 281/88-28.

(6)

Bulletin 85-03, Action Item f. requires that a written report be

issued to the NRC

on completion of the bulletin program.

The

licensee issued this report on September 30, 1988 .

11

The deviations for Bulletin valves questions the validity of the

licensee'sBulletin 85-03 program completed during previous outages.

All these valves were previously MOVATS tested as part of the

Bulletin 85-03 program.

The actuator grease was also replaced as

part of the Bulletin program.

The inspector considers that the Surry program does not fully meet

Bulletin 85-03 for differential pressure testing requirements.

Other

areas such as post-maintenance testing, monitoring of valve

performance and MOV procedures wi 11 be reviewed during a future

inspection.

The purpose of this inspection was to determine if licensee actions

in response to the MOV deficiencies identified during the present

Units 1 and 2 outages are adequate to restart Units 1 and 2.

Per

EWR-89-061, the licensee program to resolve MOV deficiencies

involves the following:

0

0

0

0

0

C

0

0

Resolve Environmental Concerns

Determine if valve operators with deficiencies were or were not

operable.

Trr date one Licensee Event Report, 50/280-88-43, has

been issued discussing the undersized motors inadvertently

installed on valves 1SW-104B and 1SW-105C.

Correct the deficiencies identified

MOVATS test all Bulletin 85-03 valves, valves that receive an

automatic signal, and valves that are operated per EOPs, and

correct deficiencies identified by MOVATS testing.

Remove motors and inspect mechanical parts (pinion gears for-

reversed installation, hardened grease, tripper fingers, etc.)

for safety-related valves.

If the grease in safety-related valves was not replaced during

the previous outage, replace it during present outage.

Actuators that have been identified to be undersized perform

differential pressure testing to verify operability.

Develop a long-term compre~ensive MOV program.

In addition to the actions specified in EWR 89-061, the licensee has

raised the awareness of MOV deficiencies with all station personnel

and has encouraged people to write station deviations when a

deficiency exists or if not sure if a condition is acceptable .

12

During outages, the licensee has extensively utilized contractors to

perform MOV corrective maintenance.

Prior to the start of the

current outages, the licensee requested resumes for contractor

personnel and reviewed the resumes to verify MOV experience.

Prior to restarting each unit, the inspector considers that the

licensee needs to complete the action specified in EWR 89-061 and in

addition perform root causes analysis of station deviations written

against MOVs and establish measures to prevent recurrence of the

i dent i fi ed MOV problems.

The licensee committed to perform these

additional actions during the exit meeting.

The licensee was

informed that prior to the restart, the inspector will return to

review root cause analysis, corrective measures, and

fo 11 ow-up on

Bulletin 85-03 valve deficiencies.

During the exit meeting it became

apparent that performing root cause analysis and determining

corrective actions would delay Unit 1 restart.

Surry Nuclear Site Memorandum from

R. V. Green/J. LaFlam to

R. H. Blount, dated November 10, 1988, indicates that the licensee

management was aware of MOV program problems.

This memorandum stated

that the problems were attributed to 1 ack of guidance either

procedurally or supervisory, lack of root cause evaluation program,

and lack of a comprehensive MOV program.

The inspector agrees with

the licensee's assessment of the MOV program contained in the

November 10, 1988, memorandum; however, with the exception of

increasing supervisor involvement, little or no action has been taken

in the areas of procedure improvement, root cause determination, and

program development since the memorandum was issued.

c.

Followup on Motor Operator Valve EQ Concerns

The 1 icensee identified on Station Deviation S2-88-0069 that

potentially non-EQ wire may have been installed in EQ L imitorque

valve operator 2-CH-MOV-2275B.

In a memorandum dated November 10,

1988, from R. V. Green to R. H. Blount, the licensee stated that all

EQ motor operators had been inspected or walked down in 1986 with

qualified EQ wire being installed.

Subsequent to this walkdown, EWR 88-224 was worked to add jumpers in some IEB 85-03 valves.

This EWR

required the use of qualified wire to be installed; however, it did

not specifically name what type of wire to use.

In working

EWR-86-224, the licensee indicated that the craft did not follow the

EQ program procedures by installing jumpers of appropriate length

with the vendor name and type of wire.

Thus, the jumpers discovered

were not identified by vendor and wire type.

The proposed corrective

action recommended in the subject memo was that the limit switch

compartment covers be removed on several EQ valves as identified in

13

the memo and inspected for uni dent ifi ed wiring.

The inspector

questioned the licensee regarding the qualifications for the

non-identifiable wire found in

EQ operators.

The licensee was

requested to provide the records of the cable reels, issue tickets

and any other supporting documentation that would demonstrate that

the wire was indeed EQ qualified and did not change the qualified

status of the EQ operator.

The licensee indicated in the exit that

this information had been reviewed by them and confirmed that the

wire was qualified.

However, it was not provided to the inspector.

The inspector informed the licensee that this would be examined

further as part of the follow-up to Inspector Follow-up Item 280,

281/88-45-01.

Other concerns identified during this outage regarding the EQ

qualified status of motor operated valves involves. separation of

grease or grease hardening and

non-EQ torque switches in

EQ

operators.

The inspector discussed these two concerns with licensee

representatives to understand what the licensee had concluded as far

as the root cause for these problems.

Based on these discussions,

the inspector determined that no previous qualification problem

existed regarding non-EQ torque switches in EQ operators.

The EQ

operators all contained torque switches with white colored melamine

torque switches that had been previously qualified by the vendor.

As

stated earlier, the vendor, Limitorque, recommended in a Part 21

report to NRC, dated November 3, 1988, that Melamine torque switches

in SMB-000 and 00 operators be replaced with qualified Fiberite

(brown) torque switches.

Thus, when the licensee began these

walkdowns in 1988, there was some confusion regarding the qualified

status of the Melamine torque switches and the craft annotated on

several station deviations that non-EQ torque switches were found in

EQ operators.

This was further compounded by the fact that the

licensee staff issued a memorandum to Electrical Maintenance, dated

April 22, 1988, which identified the qualified limit switches and

torque switches as (brown) Fiberite.

In addition, the licensee had

information discussing a generic concern regarding unqualified SMA

style torque switches which were supplied by the vendor in some EQ

motor operators.

The licensee indicated during this inspection that

the walkdowns did not identify any non-EQ torque switches in EQ valve

operators.

The torque switches were Melamine and were identified on

station deviations to be replaced as recommended by the vendor.

However, several non-EQ valve operators were observed with SMA style

torque switches installed.

The valves were safety-related both

bulletin 85-03 and non-bulletin valves.

The licensee has proposed to

replace these SMA torque switches when replacement parts become

available.

The last EQ issue concerning MOVs involves hardening of grease or

separation of grease in EQ operators.

Interviews with licensee

personnel revealed that all EQ operators were inspected and reworked

in 1986 by Station Maintenance Procedures.

The scope of the rework

included replacement of the gear case grease with Exxon EPO or EPl

14

which is the qualified lubricant for EQ valves.

The inspector

requested the documentation that changed out the lubricant in 1986.

The licensee was not able to provide this documentation for the

inspector prior to the conclusion of the inspection. Therefore, this

concern wil 1 a 1 so be examined during fo 11 ow-up of the i tern 280,

281/88-45-01.

4.

Inside Recirculation Pump Motor Feeder Cables

a.

Degradation of Inside Recirculation Pump Motor Cables

On January 20, 1989, the Unit 1

118

11 Inside Recirculation Spray Pump

(IRSP) motor feeder cable was found to have deteriorated insulation.

The braided outer jack.et of the power feeder cable was frayed in

several locations and the conductor insulation was cracked.

As a

result of this finding, the licensee began inspecting all power

  • feeder cables to the Inside Recirculation Spray Pump motors on both

Units.

The results of the visual

inspections revealed that

significant degradation had occurred on Unit 1 1 s

118

11

IRSP and

Unit 2

1 s

11A

11 and

118

11 IRSP motors.

The 1 i censee sent samples of the

Silicone Rubber cable, manufactured by Continental, to an independent

lab offsite for further testing and final determination of equipment

operability.* As part of this review, the licensee is conducting an

engineering evaluation to determine the root cause for the insulation

damage.

The

NRC

inspector accompanied

licensee personnel

in

inspecting Unit l's

11A

11 IRSP motor power cable and Unit 2 1 s

11A

11 and

118

11 IRSP motor power cables. * The damage appears to be consistent

with earlier reports provided by the licensee, fraying of the jack.et

and cracking of the insulation.

Additionally, when the licensee

determinated the feeder cable to pump motor 2-RS-P-lB, the crimped

termination lug came off of one of the motor pigtail leads.

The

licensee is also investigating the root cause for why this occurred.

The qualification documentation for the Continental Silicone Rubber

Cable is contained in Qualification Documentation Report QDR-S-6.4.

The report identifies the cables installed in Surry Units 1 and 2 as

Continental Silicone Rubber insulation with an overall glass braid.

The formulation for the cable is identified as CC2115 with a maximum

conductor temperature rating of 200°C.

The basis for qualification

is the DOR Guidelines.

The QDR states that the cable has a qualified

life of 40 years in an ambient environment of 125°F based on test and

analysis.

The cable is considered qualified for a TIO radiation

exposure of both beta and gamma of 1 x 10 8 rads (required 5.93 x 10 7

TIO using IEB 79-0lB).

A large part of the qualification for this

cable is based on the assumption that this cable is the same as the

cable formulation that was tested in Franklin Test Report F-C2935.

During the inspection, the licensee failed to provide installation

records to the inspector such that the as-built installation could be

15

traced back to the qualification records.

In the QDR the licensee

states that type NJA and NPA cable codes are installed on Units 1 and

2, respectively (page G.1-25).

However, the file only shows that

type NPA cable code was procured from Continental under Specification

NUS-326 and Purchase Order SN-330.

As part of the continuing

investigation into the degradation of this Silicone Rubber cable, the

inspector requested the licensee to provide additional information

regarding the traceability of these as-built cable installations.

This item is considered unresolved pending further review of the test

report and review of installation/qualification records on the

as-built cable installations.

This item will be tracked as URI

50-280, 281/89-03-01, Degraded IRSP Motor Power Cables.

Preliminary

results from a licensee representative *indicated that the cable

damage may be mechanical in nature caused by overstressing the cable

during installation.

Other failure modes such as. high ambient

temperatures, overcurrent due to bad cri~ps resulting in high contact

resistence on the motor leads does not appear to be the most likely

cause of the damage.

The licensee also believes the discoloration

identified was due to corrosion in the PVC jacketed flex conduit.

Other possible failure modes being investigated are radiation and

chemical interaction.

b.

Inspection of IRSP Motors at GE Safe Apparatus Center in Memphis,

Tennessee

The Unit 1 Inside Containment Recirculation Pump motors (1-RS-P-lA,

18) were sent to the GE Safe Apparatus Center in Memphis, Tennessee,

for evaluation and repair and arrived on February 1, 1989.

The

Unit 2 motors were scheduled to arrive on February 3, 1989.

The Unit 1 motors were heavily contaminated (up to 270,000 dpm) and

required respirators to be worn

during the disassembly.

The

disassembly and decontamination were lengthy but thorough.

Both

motors exhibited signs of over-lubrication of the bearings. Grease

had leaked out of the end cap and was blown around by the cooling

fan.

The GE representatives provided information to the 1 icensee

representatives as to what measures should be taken for the lubrica-

tion.

The licensee indicated that a formal transmittal shol]ld be

made by GE to VEPCO on the lubrication issue.

The motor leads were visually inspected.

The leads with the lugs

were about four inches long.

The cable had two Raychem shims from

the lug to the potting material that provided the seal to the.motor.

No evidence of overheating or damage was apparent.

The Raychem shims were then removed.

The licensee. provided verbal

instructions to the vendor technicians who had never removed Raychem

previously.

During the removal process, some damage may have been

done to the varnish coated glass tape.

The function of the varnish

was to hold the glass tape in place and prevent it from unraveling .

16

The glass tape was a mechanical protection for the Kapton Mica Mat

Silicon tape.

No damage was noted to the Kapton tape.

Electrical tests were performed on the motor and no indication of a

problem with the motor was found.

There was no discoloration on the

terminal lugs, no carbonization on the cable, nor any discoloration

or hardening of the cables.

There were no indications of degradation

as the result of heat or radiation.

The brittleness referred to in

the initial report is presumably the varnish coated tape.

This would

be as expected since the varnish would not be very thick.

It would

not be a concern since it. was for mechanical protection, not a

moisture seal.

The repair of the leads was under discussion between the licensee and

the vendor. " Both parties were ensuring that whatever the method

decided upon would result in the motor being in a qualified configu-

ration with the supporting documentation.

5.

Exit Interview

The inspection scope and results were summarized on January 27, 1989, with

those persons i ndi ca ted in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection results listed

below.

Although reviewed during this inspection, proprietary information

is not contained in this report.

Dissenting comments were not received

from the licensee.

In the exit, the licensee verbally committed to perform root cause

analysis of Station Deviations written against motor operated valves

during the present Unit Nos. 1 and 2 outages and establish corrective

measures to prevent recurrences prior to the respective Unit restart,

paragraph 3.b.(6).

Unresolved Item 50-280, 281/89-03-01, Degraded IRSP Motor Power Cables,

paragraph 4.a.

The status of a previous Inspection finding is discussed in paragrah 2 .

17

6.

Acronyms and Initial isms

CH

- Charging

CS

- Containment Spray

EQ

- Environmental Qualification

EWR

- Engineering Work Request

FW

- Feedwater

GE

- General Electric Company

IRSP

- Inside Recirculation Spray Pump

LER

- Licensee Event Report

MDV

- Motor~Operated Valve

RSHX

- Recirculation Spray Heat Exchanger

SI

- Safety Injection

SW

- Service Water

VEPCO - Virginia Electric and Power Company