ML18152A173

From kanterella
Jump to navigation Jump to search
Special Insp Repts 50-280/91-31 & 50-281/91-31 on 911104-06. Determined That Several Issues Require Addl Attention.Major Areas Inspected:Verification of Activities & Equipment Mods Taken Credit for to Reduce Vulnerability to Flooding
ML18152A173
Person / Time
Site: Surry  Dominion icon.png
Issue date: 12/18/1991
From: Fredrickson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A174 List:
References
50-280-91-31, 50-281-91-31, NUDOCS 9201140076
Download: ML18152A173 (20)


See also: IR 05000280/1991031

Text

UNITED STATES

NUCLEAfl REGULATORY COMMISSION

REGION II

Report Nos. :

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/91-31 and 50-281/91-31

Licensee: Virginia Electric and Power Company

5000 Dominion Boulevard

Glen_Allen, VA

i3060

Docket Nos.: 50-280 and 50-281

License Nos.:

DPR-32 and DPR~37

Facility Name:

Surry 1 and 2

Inspection Conducted:

November 4-6, 1991.

Inspection Members:

M. W. Branch

Team Leader:

Scope:

J. 0. Schiff gens

J. E. Tatum

J. F. Wechs~lb~rger

P. E. Fre

Division of

SUMMARY

.Date

This special inspection was conducted to verify specific activities and

equipment modifications taken credit for to reduce the vulnerability of the

plants to Turbine Building flooding, as discussed in an October 29, 1991

licensee letter.

This inspection also reviewed interim measures taken by the

licensee as discussed in an October 28, 1991 letter ..

Results:

T~e inspection det~rmined that, based on a combination of actions taken prior

to *the inspection and completion of commitments provided during the inspection,

the items stated in the two licensee letters have or will be satisfactorily

. implemented.

Subsequent NRC inspections wi 11 review implementation of the

licensee's commitments.

9201140076 911218

PDR

ADOCK 05000280

G

PDR

ENCLOSURE 1

TURBiNE BUILDI~G FLOOD COMMITMENTS

1.

Expansion Joints

a.

Currently, th~ Circulating Wa~er.system is o~erating with fciur main

condenser outlet expansi6n jc~nts per unit that h~ve an indeterminate

service li.fe.

The primary cc~cern is whether the* remaining service

life is sufficient for the u~its to operate until the 1992 Unit 1

outage.

The licensee has pre-posed three methods to determine the

actual rem'aining service life .

.First, there. is some re:ollection that the licensee replaced

these expansion joints d~ring the 1980 time frame.

The licensee

is ~eviewing maintenance and procurement documents in an attempt

to verify this assertion.

  • *

Second,. the licensee is contacting the vendor, Garlock, in* an

.attempt to determine the remaining useful service life.

Third, if one of the at:ive two methods is unsuccessful, the

licensee plans to inspe:t one of the main condenser outlet

expansion joint on .Unit 1 during .a water box cleaning. to

estimate rem~ining service life of the 8 affected expansion

joints.

'

.

The licensee committed to satisfactory verification of serviceability

by one of these t.hree methoc:s for the. four per unit not-replaced.

Circulatin£ Water expansion j-:,ints by November 29, 1991.

b.

In .additi.on, assuming the above evaluation supports current

serviceability, the licensee corrunitted to replace the four main

condenser outlet expansion j6ints during the Unit 1 refueling outage

'", scheduled for February 1992 and for Unit 2, no later than the outage

scheduled for February 1993.

For Unit 2, the licensee conmitted to

provide the basis for extending the replacements to the Unit 2

  • outage.

If a review reveals that these expansion joints were

.

replaced in the 1980 time fra..e, the licensee corruni.tted to provide an

evaluation, documenting their service life beyond the Unit. 1 and 2

outages.

c.

The flow ~hields.around the 36" Circulating Water ex~~ns~on joints

wer~ not in their as~deiigne~ condition, but would be effective in

fulfilling their design fun:tion for the postulated flooding

scenario.

The licensee committed to upgrade the material condition

of the flow shields by Decem::::er 31, 1991, to include replacement of

missing bolts.

Enclosure*l

2

  • d.

In addition the Service Water *system has 12 expansion joints that

were not.replaced in 196~w

These expansion joihts are not considered

as significant a contrfbutor to risk as a result of their physical

location in the piping s1stem; .that is they are connected to smaller

diameter pipes and have two isolation valves upstream of the

expansion joints.

The ~icensee colTITlitted to visually inspect these*

expansion joints by N*ovember 29, 1991. and provide a schedule for

replacement of any expa~~{on joints that warrant it.

2j

Turbine Building Sump Pumps

Based on the identified *need to further improve sump pump reliability in

order to maintain seven of nine pumps operable, the licensee committed to

develop a periodic test prosram for these pumps, to include the pumps,

level switches, check valves and power supplies.

This testing would

verify quantitative flow and operability of equipment. -The program will

be developed by December 31, 1991 with the first series of periodic tests

completed by January 31, 199Z

3.

Turbine Building Sump Backflcw Limiters

Based on inspection concerns that annual inspection without testing may

not be frequent enough to er.sure functionality of the Turbine Building

sump backflow limiters, *whi.:h are an important. part *of the flood

propagation mitigation scher..:,. the licens.ee co1T1T1.itted to develop and .

implement a testing and/or re~lacement program for these backflow limiters

by February 28, 1992.

.

.

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • W. Stewart, Senior Vice President, Nucle~r
  • E. Harrell, Vice President, Nuclear Operations
  • M. K~nsler, Station Manager

W. Benthall, Supervisor, Liceniing * .

  • D. Benson, Manager, Nuclear Engineering
  • R. Berryman, Manager Nuclear Analysis and Fuel

D. Buchett, Senior Staff Engineer, Nuclear Engineering

'*M. Bowling, Manager, Nuclear Licensing and Programs

  • D. Christian, Assistant Station Manager

J ,. Downs, Superintendent of Outage and Planning

J. Graf, Supervisor, Project Engineering, Nuclear

R. Green, Supervisor, System Engineering

R. Gwaltney, Superintendent of Maintenance

A. Hall, System Engineer

D. Hanson, Supervisor, Maintenance Support

  • L. *Hartz~ Mana~er, Nuclear Quality Assurante

D. Hart, Supervisor, Quality Assurance

J. McCarthy, Supertntendent of Operations

  • J. Price, Assist~nt Station Manager

R. Scanlon, Senior Staff Engineer, Licensing

T. Sowers, Superintendent of Engineering

J. 'Stauffer, MDV Program Coordinator

  • . R. Thomas, Nuclear Analyst

NRC Personnel

  • S. Ebneter, Regi~nal Administrator, Region II*
  • F. Congel, Director, Division of Radiation Protection and Emergency

Preparedness, Office of Nuclear Reactor Regulation (NRR)

  • W. Beckner, Risk Applications Branch Chief, NRR
  • H. Berkow, Project Director, NRR
  • M. Branch, Senior Resident Inspector, Region II
    • s. Buckley, Senior Project Manager, Region II
  • K. Clark, Public Affairs Officer, Region II
  • P. Fredrickson, Section Chief, Region II
  • J. Schiffgens, Risk Analyst, NRR
  • J. Tatum, Senior Reactor Engineer, NRR
  • J. ~echselberger, Senior Regional Coordinatdr, Office of the Executive

Director of Operations*

  • S. _Tingen, Re~ident Inspector, Region II
  • Attended exit interview.

2

Other licensee * technical staff rr:-embers we.re contacted during * the

inspection.

2.*

Background

On August 30, 19.91, Virginia Electric and Power Co. submitted an

Individual Plant Examination (IPE) on Surry, in response to Generic Letter 88-20, "Individual Plant Examination for Severe Accident Vulnerabilities".

This Generic Letter stated that 1icensees of existing plants should

perform a systematic examination,. IPE, to identify any plant-specific

vul nerabil i ti es to severe acci der.ts and report the results to the

Commission: * The internal events portion of the IPE, excluding internal

flooding, resulted in a point estimate core damage frequency (CDF) of.

, 7 .4E-05 per .reactor year.

CDFs of this magnitude are not unusual.

However, the internal .flooding portion of the li.censee's IPE analysis,

which yielded a point estimate CDF of l.lE-03 per reactor year, identified

internal flo.oding as a vulnerability.

The NRC staff ag_rees that a CDF of

this magnitude is unusual and indicative of a signjficant vulnerability.

The licensee's analysis showed that the most important flooding sequences

result from failures in the gravity fed, Circulating Water (CW) and*

connecting Ser~ice Water (SW) sys:ems in the Unit 1 or Unit 2 Turbine

. Buildings which cause flooding in :he Emergency Switchgear Room (ESGR) and

the subsequent loss of A~, and eventually DC, power.

The flow rate into

each of eight, 96 inch diameter C-" pipes at the intake is about 190,000

gpm during normal operation-. .

The identified sequences, similar: to

unrecovered station blackout sequences, are responsible for about 90

percent of the total internal flocding CDF.

The unique design feature of SurrJ* responsible for its vulnerability to

internal flooding is the location of the ESGR off the lowest level.of the

Turbine Building, 20 feet below the level of the intake canal.

  • Consequently, breaks in CW or S\\.i pipes or equipment which cannot be

isolated by closing a~propriate irtake or isolatibn valves, and leak more

water into the turbine Building than its sump pumps can remove, which is a

total of about 9,100 gpm, would, in the absence of mitigativ~ measures,

lead.to core damage.

The licensee, while acknowledging that this vulnerability is real, also

believes the CDF estimate is v.ery conservative.

In a letter dated October

28, 1991, the' licensee presented a schedule for planned, internal flo6ding

related modifications, proposed. 7'urther discussion. of its ongoing

reanalysis of internal floodihg, and stated the following:

11 In the interim, Virginia Ele::tric and Power Company will augment the

present shift coverage of pctential flood areas with a dedicated

flood watch for those areas.

The* dedicated flood watch would *

specifically be observing internal flood~importani valves, pip~s, and

. expansion joints on. a contir.uous basis for early indications of

1 eakage or other degraded ;:,erfonnance.

Furthennore, as an

enhancement to flood mitigation capabilities, administrative controls

wi 11 be added, on an i nterirr. basis, to reql!i re opera bi 1 ity of a 1l

3

nine sump pumps to further increase expected availability.

in the

event of a sump pump being jnoper.able, priority will be given to

prompt restri~ation of the pu~p to an operable condition.

Finally,

procedures for installation of stop logs at the high level intake

will be forma 1 i zed and the resources ( both material and personne 1)

reqtiired for installation will be identified and dedicated to ensure

the most timely action possible tri the* use of stop logs for flood

mitigation.

11

1~ a letter dated Octobe~ 29, 1991,.the licensee discussed its reanalysis

aimed at better understanding the internal flooding issuei and obtaining a

more realistic* CDF.

In this letter, the licensee stated that reanalysis

yielded.a CDF of l.7E-04 per reactor year, taking into account specific

equipment changes that had not been_ considered in the initial analysis and*

additional modifications resulting from the IPE identification of the

internal flooding vulnerability.

Accprding to the October 29 letter, the

following items have been factored into calculation of a reduced CDF for

inter~al flooding:

a)

~)

c)

"Expansion joints on the Circulating Water and Service Water

systems and associated MOVs, which are significant contributors

to any flood damage state frequency, have recently been

replaced.

11

_

"Inspections on MDV bolting have recently been completed.-

(MOV

bolt failure was considered a significant initiating event in

the original IPE analysis.)"

.

11A -minimum of seven of nine turbine building sump pumps are

being maintained operable."

The NRC believes that, if satisfactorily implemented, the above actions

and interim measures will reduce the risk to internal flooding.

This

inspection. was to verify statements a), b), and c) in the October 29, 1991

letter and to review the interim measures taken by the licensee discussed

in the October 28, 1991 letter.

3~

Systems Descriptions--Turbjne Building

a.

Circulating Water System

The CW System draws water from the James River to provide cooling water

for the main condensers and to provide water for the SW System.

The eight

CW* pumps discharge into* a common; one and one-half mile long,

concrete-lined intake canal that directs CW to the station area.

The High

Level Intake St~ucture on each unit di~ects the watet into four concrete

pipes.

For maintenance purposes, i.e. with th~ relevant portion of the CW

System in a maintenance configuration, isolation of flow at this point can

be made by the insertion of large plates (4 per pipe) called stop logs.

The concrete pipes connect to* four buried 96 inch diameter steel pipes

that. carry water from the concrete pipe to the individual condenser

half-shells in the Turbine Building.

Condenser inlet flow is secured by

fo~r butterflj motor operated valves (MOVs). In addition, each inlet line

contains Jn expansion joint do~nstream of the inlet MOY, which allows .for

settling of system* components after installation without putting*

unacceptable stresses on the piping. ** Each condenser half-shell has two

tube bundles.

Water leaving*each tube bundle flows through a 96 inch

outlet line, two expansion joints and another butterfly MOY isolation

valve.* Tbe four outlet lines tie* into a discharge tunnel which also

receives SW System flow~

The discharge tunnels from both units go to the

  • common discharge canal, which returns the water to the James River.

b *. Service Water System

Th.e SW piping taps off the CW intake piping in the Turbine Building

between the High Level Intake Structure and the condenser inlet MOVs.

Gravity provides the motive forc.e for the .flow of the SW to the various

loads an*d subsystems of the SW System.

The SW System supplies cooling

. water through th~ plant with several supply headers, which can be isolated

by hand operated valves or MOVs.

The Bearing Cooling Water. Sys tern and the

Ccimponent Cooling Water System are the main systems that use SW in the

Turbine Building (36" and* 42" lines, respectively).* Both contain SW water

butterfly isolation MOVs and expansion joints..

Return headers collect

'th~ SW from th~ cooled com~onents and. subsystems and return the water to

the James.River via the Discharge Tun~el and the Dischijrge Canal.

c.

Condenser Flood C~ntrol Subsystem

The purpo~e of the Condenser Flood Control Subsystem is to alert the

operator through alarms that flooding is taking place in the Turbine

Building that could impair safety-related equipment.

This subsystem

. allows the operator some period of time, depending on the severity of the

flood, to isolate the source of the flboding after receipt of the first

alarm before the condenser C~ inlet valves are automatically closed.

The

system consists of six level sensing *detector assemblies, three for alarm

and three for CW valve-closing.

The alarm*.assemblies are located in both

the condenser and amertap pits.

The isolatioh assemblies are mqunted 9"

off the Turbine Building floor.

This system also contains associated

. alarm circuitry, and a control system using a redundant matrix to initiate

automatic closing of the associated condenser CW inlet valves.

4.

Replacement of CW System and SW System MOVs

a.

Description

During the approximately one year period between May 1988 and July 1989,

the licensee replaced the following MOYs in the SW and CW Systems on both

Unit 1 (100 series) and Unit 2 (200 series):

100A,B,C,D/200A,B,C,D

Condenser Waterbox Outlet

Isolation Valve (96")

101A,B/201A,B

102A, B/202A, B

103A,B,C,D/203A,B,C,D

106A,B,C,D/206A,B,C,D

5

Bearing* Cooling Water Heat Exchanger fol et.

Isolation Valve {36")

Comp.:inent Coolin9 Heat Exchanger Inlet

Isolation Valve (42"/10") *

Recirculation Spray Heat Eichang~r Inlet

Isolation Valve {30")

Con~enser Waterbox Inlet Isolation Valve

(96")

Except for the condenser waterbox outlet isolation valves (100/200), these

are the first isolation valves in the CW and SW systems and there ar~ ~o

expansion joints upstream of these valves.

b.

Problem History

. The original recirculation spray heat exchanger inlet isolation. valves

(103/203) were aluminum bronze butterfly valves and they were replaced

with butterfly valves of the sarrie material that were designed to provide

better s~at tightness.

The origi~al valves were leaking sw* through th~ir

seats and allowing hydroid growtr. formation and fouling of the heat

exchangers. * The other va 1 ves ( lCJ/200, 101/201, 102/202, and 106/206)

were replaced in .response to NRC Information Notice 84-71, "Graphitic

Corrosion of Cast Iron in Salt wc.ter,

11 to eliminate graphitic corrosion

problems.

The original valves were cast iron butterfly valves and over

time graphitic corrosio11 would have reduced the strength of these valves,

. so they were replaced with ductile iron butterfly valves.

c.

Valve Replacement and Design Review

The inspectors* reviewed the foll O'fl'ing documents to verify the adequacy of

the valve replacement activities that were.previously completed:

NUS 2074

DC 86-10

DC 86-11

DC 85-17

_DC 85-18

Specification for Motor-Operated Butterfly Valves for

Service Water and Circulating Water Systems (Rev. 1)

Servite Water and Circulating Water Butterfly Valve

Replacement/Surry 1

Service Water and Circulating Water Butterfly Valve

Replacement/Surry 2

Service Water ~otor Operated Butterfly Valves Surry 1

Service Water Motor Operated Butterfly Va 1 ves Surry 2

These valves were designed to withstand at least 50 psi normal operating

pressure whereas the no~inal syste~ operating prissure was about 9 psig.

The.valves were also designed for a maximum differential *pressure of 20

6

psig; the worst-case pipe break would result in a maximum differential

pressure of about 10 psig.

d.

Current Practices

The licensee monitors valve performance by cycling the valves quarterly

per the ASME Code in accordance with the following procedures:

. 1-PT-25 .1

2-PT:.. 25.1

Quarterly Testing of Circulating Water and Service

. Water System Valves

Quarterly Testing of Circulating Water and Service

Water System Valves

Local and remote valve~ position is* verified per the ASME Code each

refueling outage by the following procedures:

1-PT-18. lOP

2-PT-18. lOP

Verification of Local and Remote Valve Position

. Indic~tions in.the T~rbine and Servite Buildings

Verification of Local and Remote Valve Position**

Indications in the Turbine and Service Buildings

Valve seat leakage is_ monitored each refueling outa.ge by the following

procedures:

. 1-0PT-CW-001

Lea~ Test of the Circulating Wate~ Inlet and Outlet

9611-Valves

2-0PT-CW-001

Leak Test of the Circulating Water Inlet and Outlet

96

11 Valves

l-OPT-SW-001

Leak Test of SW Valves 1-SW-MOV-lOlA and

1-SW-MOV-lOlB

2-0PT-SW-001. Leak Test 6f SW Valves 2-SW-MOV-lOlA and

2.-SW-MOV-lOlB

1-0PT-SW~002

2-0PT-SW-002

Leak Testing. of Component Cooling Water Heat Exchanger

Service Water .Valves

Leak Testing of Service Water Valves

2-SW-MOV-202A and 2-SW-MOV-2028

. e.

Conclusion and Recommendations

Based on a review of the information discussed above, the inspectors

concluded that the replacement of CW and SW System valves in conjunction

with the current* practices of. monitoring valve status and perfonnance

provide an increased level of assurance that: (1) the CW and SW isolation

valves will be maintained intact, and (2) the CW and SW isolation valves

will be capable of isolating a flooding event. The inspectors.did identify

7

that, although* these valves are in the MOV Program, the licensee should

con-sider including these MOVs as part of the station Reliability-Centered*

Maintenance Program

5.

Valve and Fastener Inspection

a.

-Description

In order to minimize the risk of flooding in the Turbine Building, the

licensee performed.a visual inspection of CW and SW System valves.which

serve to isolate the high level intake canal.

The accessible parts of the

valves and exposed adjacent piping were inspected for general pressure

boundary integrity including bolt engagement and condition, condition of

expansion joints, integrity of connecting bolts for the valve operators,

and overall general condition. The following valves (and adjacent piping)

from both Unit 1 and Unit 2 were included in the inspection:

100A,B,C,0/200A,B,C,O

101A,B/201A,B

102A,B/202A,B

103A,B,C,D/203A,B,C,D

106A,B,C,D/206A,B,C,D

Condenser Waterbox Outlet Isolation

Valve (96

11

)

Bearing Cooling Water Heat Exchanger Inlet

Isolation Valve (36

11

)

Component Cooling Heat Exchanger Inlet

Isolation Valve (42

11/10

11 )

Recirculation Spray Heat Exchanger Inlet

Isolation Valve (30

11

)

Condenser Wat~rbox Inlet Isolation

Valve (96

11

)

Several other SW valves were also included in the inspection.

b.

Inspection Basis

The licensee's inspection was not based on site-specific problems that had

been experienced previously at Surry, but rather the inspection was based

on industry experience in general.* Excessive corrosion and degradation of

fasteners, valve bodies, and piping; inadequate tensioning of fasteners,

and fatigue failure of fasteners used to secure valve operators in place

have resulted in piping system transients and failures.

c.

Inspection Results

The licensee documented the resu1 ts of the inspection in a memorandum

dated October 7, 1991.

The following discrepancies were identified:

a.

The amertap barrel upstream of 1-CW-MOV-1000 (4- bolt flange)

was missing one bolt.

b.

The amertap barrel upstream rif 2~CW-MOV-iOOA had one nut out of

a~proximately 80 cross-:~~eaded.-

c .. All of the flow shields around expansion Joints upstream of

1/2-CW-MOV-lOOA,B,C,0 ar.d -200A,B,C,D did not have the bottom 10

to 20 bolts installed ~~ich caused a gap to exist between the*

pipe and expansion join~ shield in excess of one irich.

-The inspecto~s reviewed the inspe:tion results and not~d that, although

th~*inspection appeared to be -adecuately implemented, the licensee did not

have a for_mal procedure for perfonning the in*spection.

The licensee is

currently developing a procedure for inspecting CW and SW bolted

connections.

Maintenance. requests were submitted on these deficiencies

and several were corrected prior tci the inspection team .arrival *. *

Inde~endent of the licensee's effort, the inspectqrs selectively inspected

some of the CW and SW fastners and valves and made the following

observa hons:

a.

The

expansion joints . downstream of 1-SW-MOV-103C

and

. 2~SW-MOV-203A had faste~ers *contacting the rubbei expansion joint.

b..

The expansion joints do'f'l*:--,stream of 1-SW-MOV-103C&D had been

nicked and gouged in places.

d.

Conclusion and Recommendations

The inspectors concluded that the licensee.

1s valve and fastener inspection

provided an increased level of assurance that the equipment that was

inspected would co_ntinue to provice the pres*sure boundary integrity it was

designed to provide.

However,

the inspectors did identify some

discrepancies, as dis.cussed above, that were not identified by the

licensee.

The licensee's inspect.ion procedure w_hich is cufrently being

developed

should include consiteration for such discrepancies.

Additionally, the licensee is expected to teview the specific observations

identified by the NRC and resolve them accoraingly.

a

6.

Expan~ion Joint Replacement

a.

Description

The expansion joints are used to a1low for the thermal expansion of the CW

and SW piping systems.

In addition to thennal expansion, the expansion

joints permit ease of maintainability of the butterfly valves in the CW

and SW systems.

The expansion joints va*ry in size from 96

11 diameter for

the CW system to 42

11

, 36

11

, 30

11 ar.d 10

11 diameters* for the SW system.* The

expansion joints are concentric s~ool type rubber joints with galvanized

retaining rings.

The compositior of the rubber joints, as specified* in

the original ~pecification (NUS-32, revised July 3, 1969), is essentially

synthetic rubber.

A more recent specification (NUS~2076, dated December

16, 1987), describes the materia~ as EPDM (ethylene propylene diamine .. *

rubber) and polyester.

The licer.see indicated that NUS-2076 was used to

9

procure the expansion joints for the MOV and expansion joint maintenance

conducted in 1988 (see paragraph 4).

The expansion joints function in

brackish, untreated~ river water and are considered nuclear safety related

com*ponents.

As a result of an earlier study on internal flooding, the _

licensee installed flow shields around the circumference of the 96" CW

  • system, expansion joints. The purpose of the shields is to limit the flow

from an expansion joint should it fail.

b. * History of Replacement

In reviewing the CW and SW expansion joints, the 1nspectors reviewed the ..

status of the ,2 expansion joints that the licensee determined can cause

Turbine Building flooding.

Thirty-two of these expansion joints had been

  • replaced in 1988.

The remaining. 20 expansion joints comprise 8 main

condenser outlet expansion joints in the CW system and 12 expansion joints

, in the SW supply to the bearing cooling water heat exchangers.* The

following list identifies these 52 joints:

  • Description

Number EJ Replaced

Total EJ's

REJ-2: 96

11 (CW).

8

.8

REJ-3 & 4: 96

11 (CW)

8*

16

REJ-7: 42"(SW to

2

2

c'omponent cool i_ng)

REJ-8: 36"(SW to

4

4

bearing cooling)

REJ-5: 30"(SW to

0

12

bearing tooling)

REJ-6: 30"(SW,to

8

8

component cooling)

REJ-16: lO"(SW pump)

2

2

Totals:

32 EJs replaced.

52 EJs

The inspectors questioned the apparent discrepancy between the October 29,

1991 letter, in which the licensee stated that expansion joints that are

"significant contributors" to flood damage had been replaced and the fact

that several important expansion joints had not been. replaced.

The

licensee stated that these not-replaced expansion joints were not

significant, but initially did not provide a documented technical basis

for this determination.

P.ending .receipt of this evaluation, the

inspectors decided to review the material condition of the not-replaced

expansion joints. Later in the inspection period the licensee provided an

evaluation memorandum dated November 6, 1991, stating that the *

'

!

10

not-replaced expansion .joints were not

11significant contributors" in that

they are located sighificantly downstream of the first CW or SW isolati_on

valve.*

Although these expansior. jofots .were not .considered as

"significant contributors

11

by the licensee, the *inspectors* and the

l ice.nsee determined that their importance was s i grli fi-cant enough to

warrant inspection and evaluation for serviceabil!ty.

c. Present Status

The service life of the not-replaced expansion joints has exceeded the

vendor's recommendations and an engineering evaluation for extending the

life of these expansion joints has n*ot been*conducted by the licensee.

NUS-38 specifica~ion indicated that the .servic.e life for the original type

of expansion joint was about 15 to 17 y~ars whil~ NUS-2076 iMdtcates for

that particular materfal specified, the expected service life would be

  • about 8 to 10 years.

The licensee ini.tiated discussions with the original

manufacturer who indicated that the useful service life may bt extended *

due to the mild service condition experienced for the specific CW system

installation at Surry.

T~e inspectors*also reviewed the installation of the flow shiel~s on the

C\\./ system.

The inspector's review as* well as two previous licensee

inspections found missing bolts and gaps between the shield and the

mounting flange.

On October 7,. 1991, the systems engineer and a VT-2

  • . Level II Inspector in$pected the CW and SW system va*lves and .adjacent

piping whi~h included the ~xpansion joints. Results of these inspeftions

are discussed further *in paragraph 5 of this report.

Between October 30

and November 2, 1991, Quality Assurance conducted an assessment of the.

flood protection p_rogram and compensatory actions.

The original analysis

assumed a uniform 1/2 inch gap around the flow shield, but in the actual

installation the gap ~aries. * In some locations the gap may be as large as

1 to 1.5 inches wide.

The inspectors questioned, assuming a uniform 1

inch gap, if this would significantly effect the flooding analysis.

Through discussions with the licensee and by reviewing the original

flooding analysis, .the inspectors determined that the flow shield*

restricted flow would increase from approximately 16,000 gpm to about

32,000 gpm.

The 1 icensee contends that this would not significantly

effect the overall CDF ..

The inspectors reviewed procurement documentation to determine if any

significant failures had occurred in the past. Maintenance histories were

not specifically kept in the past at th~s component level. Apparently an

expansibn joint (REJ-5) was replaced in the SW outlet line to a bearing

cooling water heat exchanger.

This occurred in July 1985.

A procurement

document indicated that a 96

11 condenser distharge expansion joint (REJ-4)

was also replaced in June of 1987.

T.he documentation did not clearly

indicate a specific failure mechanism.

No definitive conclusions on

expansion joint maintenance or failure could be drawn from these

replacements.

11

.The inspectors examined a Goodall 36

11 expansion joint in the warehouse an*d

verified that ex~ansion joints. were bejng properly stored in. a dark, dry

location. _ This particular expansion joint did not hav.e- a "filled arch

11

The

11filled arch

11

  • expansion joint is generally used in safety related

systems in horizontal applications.

In this appli~ation the

11filled arch

11

prevents debris buildup in the arch ~hich could restrict free movement of

the expansion joint.

The inspectors were concerned that this expansion

joint could be inadvertently installed in a safety related system.

The

licensee agreed to review this* and ens*ure that the expansion joint would

only be used in the intended application.

The inspectors questioned the licensee with regard to testing and

installation of the expa~sion joints.

Hydrostatic testing was conducted

  • for the expansion joints by the supplier of the .joints. The* inspectors

reviewed some hydrostatic test reports and NUS-2076 to verify that the

joints were tested at 1.5 timei the maximum design pressure and at the

specified v~cuum pressure.

NUS-38 specifies a maximum design pressure of

40 psig and NUS-2076 lists a maximum design pressure of 80 psig for*the

96

11

expansion. joints.

The operating pressure of the system is

approximately 9 psig with the d_esign maximum operating pressure of 20

psi g.

The inspectors* al so reviewed the o*es i gn Change Package ( DCP)

"."

86.;.11-2 to ensure proper installation methods were specified and* followed.

The licensee installation piocedures were faun~ .to be adequate, including

the requirement to tighten the bolts and nuts in a uniform star pattern,

achieving uniform gasket compression and developing the required bolt.

torque in a minimum of three steps.

Testing and installation practices

were adequate._

The licensee has not yet formerly developed a maintenance program for the

expansion joints.

The inspectors questioned the licensee with regard to

the basic maintenance program elements and time of implementation.

The

  • major effort of the program will involve a visual inspection of the

expansion joints.

The licensee indicated the visual inspection will

  • i nvo 1 ve examination to determine if any significant off set has occurred,

dry rot, cracks, abrasions, cuts, leaks or other signs of mechanical

damage.

It is anticipated that this inspection.of the expansion joints of

concern wi 11 be conducted on an annua 1 or every refueling outage basis.

Specifics of the program have not been filia 1 i zed, but the l i c*ensee did

indicate that a visual *inspection would be conducted during the next

outage. * Based on the* results of the periodic inspections* the licensee

will determine if any expansion joints should be replaced.

Irt addition

the licensee anticipates having the expansion joint manufacturer measure

the expansion joint configurations and fabricate expansion joints to the

precise measurements to account for any slight_ misalignments that may

exist.

These are some of the considerations for the ne~ program, but the

_ specifics have not been finalized by the licensee.

Recently, the licensee has begun injecting hypochlorite in the SW system

to achieve 10 ppm chlorine concentration.

The purpose is to reduce the

amount of fouling that occurs in the springtime_ in the SW system.

The

inspectors wanted to ensure the licensee had adequately evaluated any


12

  • effect the addition* of hypoch'i:rite might have on the expansion joints.

The l~censee had conducted an engineering evaluation of the effect on the

material.

This evaluation cetermined that non-metallic materials

_ indicated satisfactory perforr..ance after exposure to chlorine water

treatment.

The inspectors we'"e satisfied that this question had been

appropriately addressed.

d.

Commitments and Recommenda:ions

Currently, the CW system is c;erating with four main condenser outlet

-* expansion joints per unit tha: have an indeterminate. service life.

The

primary concern is whether the remaining service life is sufficient for

the units to operate until the 1992 Unit 1 outage.

The licensee has

proposed three methods .to dete_;.:iine the actual remaining service life.

First, there is some reccllection that the licensee replaced these

expansion joints during ~he 1980 time frame.

The licensee is

reviewing . maintenance anc procurement documents in an attempt to

verify this assertion.

Second, the licensee _is ccntacting the vendor, Garlock, in an attempt

to determine the remainin; useful service life.

Thi~d~ if one of the abo~e two methods is unsuccessful, the licensee

plans to inspect one of t~e main condensef outlet expansion joints on

Unit 1 during a wate~ b6x cleaning to _estimate remaining setvice life

of the 8 affected expansicn joints.

The licensee committed t_o satisfactory verification of serviceability by

one of these three methods for the four per unit not-replaced CW expansion

joints by November 29, 1991.

.In

addition,

assuming

the above

evaluation supports current*

serviceability~ the licensee ccrTTTli t ted to rep 1 ace the four main condenser

outlet expansion joints durin; the Unit 1 refueling outage scheduled for

February 1992 and for Unit 2, no later than the outage scheduled for

February 1993.

For Unit 2., tr:e licensee coiranitted to provide the basis

for extending the replacements to the Unit 2 outage. If a review reveals

that these .expansion joints were replaced in the 1980 time frame, the

licensee conunitted to provide an evaluation, documenting their service

life beyond the Unit 1 and 2 outages.

The flow shields around the 95" CW expansion joints were not in their

as-designed condition, but, as discussed above, would be effective in

fulfilling their design function for the postulated flooding scenario.

The licensee committed to upgrade the material condition of the flow

shields by December 31, 1991, to include replacement of missing bolts.

In addition the SW system has 12 *expansion joints that were not replaced

in 1988.

These expansion joints are not considered as significant a

contributor to risk as a* result of their physical location in the piping

! **

13

system; that is they are 1 connected to smaller diameter pipes and have two

isolation valves upstream of the expansion joints.

The licensee committed

. to visually- inipect these by November 29, 1991 and provide a schedule for*

replacement of any expansion joints that warrant it *.

The SW system has no flow shields installed. The licensee stated ;~_their

October 29, 1991 letter that the flow shields will be installed on 6 SW

expansion joints in the- SW supply 1 ines to bearing and component .cooling

by November 22, 1991. * The inspectors identified that the licensee needs

to ensure that these flow shields are properly installed;

e.

Conclusion

The inspectors concluded that. through the combination of *inspection,

remaining service life determinati.on and replacement when required, the

licensee has improved t.he reliability of the SW and CW expansion joints.

7.

Turbine Building Sump Pump (TBSB) Improvements

a.

Description

The Turbine Building Sump and Floor Drain Subsystem is composed of the

three sumps; with three sump pumps for each sump; and the associated

.

valves, instruments and piping.

The major components are the sumps .and

the sump pumps.

The Unit 1 sump is called floor drain sump number 1.

The

common sump between Unit 1 and Unit 2. is referred to as floor drain sump

number 2.

The Unit 2 sump is floor dr_ain SUlf!P number 3.

The sumps

receive floor and equipment drainage from components in the Turbine

  • Building and some areas of the Service Building.

The sumps are

approximately 12 fe~t wide, 12 feet long, and 8.5 feet deep.

Each sump

has metal plate covers for access, -as necessary.

The

three-per-sump. high volume

(1300

g~m)

sump pumps

operate

automatically, based upon signals from sump level switches.

The tombined

discharge of the three pumps for each sump is directed to the Yard Drain

System, which empties into the discharge canal.

The Turbine Building sump*

pumps discharge through individual check and isolation valves to prevent

reverse flow and to permit isolation of a pump, respectively._

b. Performance History

The TBSPs are not designed as-safety related components.

Therefore, there

are no safety related electrical power supplies, nor is there built-in

redundancy of equipment or control circuits.

Because of the system* s

initial design there are several ways that the system could become non-

functional.

For example the failure of the single sump level switch for*

the 36 inch pump shutoff could render a 11 three pumps for that sump

inoperable.

Additionally, the failure of a single pump discharge check

  • valve could result in bypass flow, back to the sump, of the other two

pumps for that sump.

'

\\

I*

14

The inspectors reviewed the following infonnation in order to assess the

.reliability of the TBSPs:*

Maintenance History

.* Reliability Information

Planned Changes to Improve Re 1 i ability

Spare Parts Management

Testing

Control Circuits and Power Supply Reliability

, Attendant Equipment

The inspectors reviewed a compu~er printout of the TBSP maintenance

history.

The printout covered the period from 1985- when the history

program was established to the present.

The TBSP history covered the

attendant equipffie~t such*as the level switches and the discharge check

valves since those items did not have unique identifiers assigned.

The

history indicated that all of the nine pumps and associated equipment have

experienced frequent fai.lures.

The inspectors discussed the TBSP pas_t

reliability with the mainten*ance PM coordinator and the system engineering

. supervisor.

c.

Present Status

When the inspectors arrived on site, the only inspection and testing of

the TBSPs was a review of switch and breaker ~osition per Operational

Checklist OC-47, dated October 29, 1991.

This procedure required the

.administrative maintenance of 9 out of 9 TBSPs operable, as initially

stated in the licensee's October 28, 1991 letter .. ' If the operators

determined that less than* 9 of 9 were operable, the procedure required*

immediate attention to initiate pump repair.

This reliability level was

changed to 7 of 9 by the licensee's October 29, 1991 letter.

Based on the

non-safety related status of these pumps and their relatively high failure

rate, the inspectors determined that this procedure was insufficient to

ensure that TBSP reliability could be maintained at either the 9 of 9 or 7.

of 9 level as stated in the licensee's October 28 and 29 letters.

The TBSPs, level switches,* and discharge check valves ar~ not currently in

the

PM program, nor are the TBSPs covered by the licensee's

Reliability-Centered Maintenance Program.

However, the motors have been

in the PM program since 1986.

Additionally, the level switches, check

valves, and the pumps are not periodically tested to verify performance.

A 11 nine pumps were tested during the period between October 3, and

November 4, 1991, and pa_ssed the* criteria established.

MDAP 0009

specifies frequency of predictive testing and provides program guidance.

The actual controlling instruction is provided by a computer based program

that specifies frequency of testing.

15

The check valves and level switch history is* not completely weil known

since there. is no unique identifier assigned to this equipment arid the

failu*re history of the breaker protective devices is .not known.

In

addition, the power supplies for the TBSP motors are located at an

elevation where flooding could result in a loss of power to the motors.

The warehouse supply of spare parts is limited and currently consist of

the following: 1) three impellers, 2) bearings and seals for approximately

three pumps, 3) two pump shafts, 4) no motors, 5) no pump casings, and 6)

no. level switches.

The licensee did however indicate that some spare

parts are on order and some are stored at North Anna.

, d;

Corrrnitments and Recommendations

Based on the inspectors' evaluation that the licensee's actions to improve

sump pump reliability were insufficient to maintain seven of nine ~umps

operable, the_ licensee committed to develop a periodic test program for

these pumps, to iric l ude the pu'mps, . level switches, check valves and. power

supplies.

This.testing would verify quantitative flow and operability of

equipment.

The progr_am will be developed by Deceml;>er 31, 1991 with the

first series of periodic tests completed by January 31; 1992

Th.e inspectors also identified that the licensee needs to consider

including the TBSPs and *related equipment in the Reliability-Centered

Maintenance Program.

In addition, the *inspectors determined that the

licensee should place more emphasis on improving parts staging for sump

pump repair.

e.

  • Conclusion

Based on the above, the ins~ectors verified that the licensee has placed

addition a 1 emphasis on improving the re 1 i ability of the TBSP.

However,

without a~ on-going PM and testing program, the inspectors did ~ot believe

that the degree of TBSP reliability stated in the October 29, 1991 letter

could be assured.

After complete implementation of *the licensee

corrnnitments in this area the licensee-stated TBSP reliability should be

realized.

a~

Turbine Building Sump Backflow Limiters

a.

Current Status

Although not specifically addressed in the October 28 or 29, .1991 letters,

an important issue involving Turbine Building sump backflow limiters was

identified during the inspection~

Through reviews of the drawings

associated with the Turbine Building sumps the inspectors determined that

Turbine Building sumps receive floor drains from several adjacent areas

that contain safety related. equipment.

The areas involved included the

Unit 1 and 2 ESGR as well as Mechanical Engineering Room (MER)-3, MER-4

and the Unit 1 and 2 cable vaults.

Thrbugh the floor drain system Turbine

Building flooding could communicate with the other areas and possibly

16 .

incapacitate safety related equipment.*

The licensee has installed

  • back-flow* limiters in the floor drains in the areas above.

The backflow

limiter resemble a rubber float that checks flow into the room.*. The*

inspedors performed a visual inspecti*on of the backflow limiters in MER-3

arid the ESGRs for Units 1 and 2. * The three backflow limit~rs in MER-3

appeared to be clogged with debris. and non-functional.

The backflow

limiter in both the Unit 1 and Unit 2 ESGR were cov~red with water .and.

there was also a_ large amount of debris in those sumps as well.

The

inspectors' review of the recent test of the backflow limiters revealed

se~eral problems.

First, .the backflow limiters in the ESGRs and the cable vaults for both

units had been tested per STP-70.4, Flood Protection Floor Drain Back**

Water Sewer Stop Valve Operability Test, dated February 20; 1990.

This

procedure is an annual test and base~ on review of past test results and

discussions with plant personnel, the inspectors* determined that the

back fl ow 1 imi ters do not meet test criteria every time the test i.s

conducted.

Second, the backflow limiters in MER.,.3 and MER-4 are not periodically

tested and* based on the condition observed by the inspectors are not

routinely maintained. * The licensee indicated that the backflow devices in

. th~ two MERs are not easily tested Since there is no adjacent standpipe to

allow back ftll of -the Arain system.

b.

Conclusion and Corrmitments *

The inspectors consider that annual inspection without testing may not be

frequent enough to ensure functionality of the backflow limiters which are

an important part of the flood propagation mitigation scheme .. Based on

the inspectors' concerns the licensee replaced the backflow limiters in

MER-3.

In addition the inspectors questioned the accepta~ility of current*

testing methods and frequency for the backflow limiters in the Unit 1 and

2 ESGRs and cable vaults.

Based on these concerns, the licensee committed

to develop and implement a* testing and/or replacement program for these

backflow limiters by February 28, 1992.

With this program, the inspectors

consider that the Turbine Building sump backflow limiters should be

maintained in an operable condition.

9.

Interim Miasures

In their October 28, 1991, letter, the licensee committed to several*

interim administrative.measures to reduce the risk .of.*plant damage due to

internal flooding~

An important note is that these measures are no1;

included in the actions necessary to reduce the CDF.

The inspectors

reviewed the implementation of two specific interim measures; dedicated

flood watch and proced~ral controls for stop log installation.

. . ~- ..

17

.

. .

a.

Dedicated Flood Watch

The flood watch patrol was initially implemented by utiliiing the existing

fire watch in thi area.

This resulted in a dil~tion of the individual's;

ability to perform either function *well. !he inspectors *discussed this

concern with station management and a dedicated flood watch was

established and procedures were developed.to implement*this interim

administrative control.

Procedure GMP~012, Roving Flood Watch

Responsibilities, dated*October 21, *1991, was issued.

This procedure

specifie*d the level of training required, the equipment* necessary, the

vulnerable equipment, and the route to foll ow.

The inspectors verified

adequate implementation of this interim action by interviewing several

flood watches, as well as witnessing several of them performing their

duties.

h.

Procedur~l Controls for Stop Log ~nstallation

The inspectors also verified that the commitment- to proceduraliie stop log*

. installation was also implemented. Procedure GMP-011, Installation and

Removal of Stop Logs, dated November 1, 1991, was reviewed.

This

procedure ensures that equipment is prestaged and that personnel are

._

trained to perform the task.

The procedure instructs the mechanics to

attempt to install the four logs* per intake bay and, if problems are

encountered, *they are to request assistance from the Station Emergency

Manager or the Technical Support Center, if manned:

.

.

It should be noted that under high flow condiiion~, talculations indicate

that the stop logs may not be able to be inserted.

Additionally, the

station did not test the ability to insert the stop logs under flow

conditions.

However, they did review previous stop log installations foi

maintenance purposes and factored that experience into the new stop log_

procedure.

10.

Exit Interview

Th~ inspection scope and results were summarized on Novemb~r 6, 1991, with

those individuals -identified by an asterisk in paragraph 1. Specifically,

the

recommendations and conclusions from paragraphs 4.e, 5.d, 6.d and e,

7.d and e, 8.b, and 9 were discussed with the licensee. The licensee

  • acknowledged the inspection conclusions with no dissenting comments and

provided the corranitments as discussed in the above paragraphs.

The

licensee did not identify as proprietary any of the materials provided to

or reviewed by the inspectors during this inspection.