ML18152A013

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Enforcement Conference Repts 50-280/86-12,50-281/86-12, 50-338/87-32,50-338/87-38,50-339/87-32 & 50-339/87-38 on 880121.Violation Noted:Failure to Place Inoperable Steam Flow Instruments in Trip in Required Time
ML18152A013
Person / Time
Site: Surry, North Anna, 05000000
Issue date: 02/05/1988
From: Cantrell F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A014 List:
References
50-280-86-12-EC, 50-281-86-12, 50-338-87-32, 50-338-87-38, 50-339-87-32, 50-339-87-38, NUDOCS 8802250416
Download: ML18152A013 (78)


See also: IR 05000280/1986012

Text

i

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ENCLOSURE 1

ENF.0.RC,EMENJ. CONEERENCE .S.UMMARY

  • Licensee:

Virginia Electric and Power Company

Docket Nos.:

50-280, 50-281, 50-338, and 50~339

License Nos.:

DPR-32, DPR-37, NPF-4, and NPF-7

Facility Name:

Approved By:

Surry and North Anna

~Chief

SUMMARY

"'/S~'i ~

Date 1gned

Scope:

An Enforcement Conference was held in Region II on January 21, 1988.

Mr. M. L. Ernst opened the meeting by expressing concern with a number of post

outage problems at North Anna as documented in several Inspection Reports in

.1987.

Virginia Electric and Power *Company (VEPCO) . then made a presentation

covering the failure to place the inoperable steam flow instruments in trip

within the required time and-recent problems at North. Anna. 'VEPCO then covered

the equipment qualification problems at Surry and North Anna.

Enclosure 3

contains information from the presentations.

  • Results:. The results of the NRC findings in. this area will be forwarded under

separate*cover *

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    • Enclosure 1

2

ENFORCEMENT CONFERENCE DETAILS

1.

Attendees - see Enclosure 2

2.

Enforcement Conference

Mr. M. L. Ernst opened the meeting by expressing concern with a number of

of post outage problems at North Anna as documented in several Inspection

Reports in 1987.

Mr. J. Wilson of Virginia Electric and Power Company

(VEPCO) ~ave a brief description of the VEPCO position including concern

with the lack of sensitivity by operations and management on making timely

decisions for non-conforming conditions. Mr. M. L. Bowling then presented

the background, root cause, description of events, safety considerations

and corrective actions associated with the North Anna Unit 2 inoperable

steam flow instrumentation.

Mr. Bowling then discussed the summary of

events, root causes, and management plan associated with the 1987

- -,;refue-li:ng ,:outage and-:startup problems at North-,Anna. *

Equipment Qualification (EQ) problems identified at Surry and documented

in Inspection Report

280/86-12 and 281/86-12 were then discussed by

Mr. E. S. Grecheck.

Mr. Bowling then discussed the EQ problems identified

at North Anna and documented in Inspection Report 338/87-32 and 339/87-32.

With regard to the failure to place the inoperable steam flow instruments

in trip with in the required time, the licensee stated.that management

tolerance of steam flow indication problems at low steam flows contributed

to the violation.

Technical Specifications (TS) require inoperable steam

flow channels be placed in trip within one hour.

However, at

approximately 1200 on November 4, 1987, two steam flow channels were found

to be inoperable and were not placed in trip. Plant shutdown was started

at 10:00 p.m., ten hours later.

The 1 icensee * stated that the safety

sig.nificance of this event was low since redundant channels and signals: *

. wete aVailabl'e.

Co_rrective actions include _specifying channel *check

"requ'irements and *maxiinum *-power levels for *ins:trument *res*ponse.

The

licensee also committed to revising Licensee Event Report CLER)87-015 on.

this event due to numerous deficiencies in the report.

The 1 icensee s~ated that the root causes for the problems encountered

during the 1987 outages* and startups were due in part to

management/supervisor failure to enforce standards, failure to follow

procedures, and inadequate procedures.

Corrective actions include

strengthening accountability, requiring safety committee review prior to

changing procedure initial conditions, and increasing management

involvement.

3.

Conclusions

"Jh~JfiH: .,~b~res __ :,V{PCO .conc.erns .. with respect to management :tolerance of

  • non-conforming conditions, failure to follow procedures, and inadequate

procedure.

Future inspections wi 11 be conducted to monitor performance

in these areas. * We are continuing our review of these issues and *our

conclusions will be forwarded under separate cover.

. * .. *~ :

ENCLOSURE 2

Enforcement Conference Attendees

Virginia Electric and Power Company

J. L. Wilson, Manager, Nuclear Operations Support

M. L. Bowling, Assistant Station Managert North Anna

E. S. Grecheck, Assistant Station Manager, Surry

N. E. Hardwick, Manager, Nuclear Power and Licensing, Corporate

G. l. Pannell, Director, SEC

R. W. Calder, Manager of Nuclear Engineering

R. Mo Kritch, Licensing Engineer

J. E. McDonald, Public Affairs Coordinator

E. T. Shaub, Licensing Engineer

P. T. Knutsen, Supervisor, Nuclear Engineering

Nucl~ar Regulatory Convnission

M. L. Ernst, Deputy Regional Administrator

C. W. Hehl, Deputy Division Director, Division of Reactor Projects (DRP)

G. R. Jenkins, Director, Enforcement and Investigations Coordination Staff

B. A. Wilson, Branch Chief, ORP

F. S. Cantrell,Section Chief, DRP

F. Jape, Section Chief, Test Programs, Division of Reactor Safety (DRS)

R. P. Croteau, Project Engineer, DRP

W. E. Holland, Senior Resident Inspector, Surry

J. L. Caldwell, Senior Resident Inspector, North Anna

L. B. Engle, Project Manager, Nuclear Reactor Regulation (NRR)

L. P. King, Resident Inspector, North Anna

B. Uryc, Enforcement Coordinator

M.A. Scott, Project Engineer, DRP

C. J. **Paulk, Reactor Inspector, ORS

C. F. Smith, Reactor Inspector, DRS

U. Potapovs, Section Chief, NRR

T. E. Conlon, Section Chief, DRS

E. W. Merschoff, Deputy Director, DRS

A. J. Szczepaniec, Reactor Inspector, DRS

W. Levis, Reactor Inspector, DRS

  • .:** .. ,: .* ,: ~ -~:

,.

ENCLOSURE 1

ENFORCEMENT CONFERENCE SUMMARY

Licensee:

Virginia Electric and Power Company

Docket Nos.:

50-280, 50-281, 50-338, and 50-339

License Nos.:

DPR-32, DPR-37, NPF-4, and NPF-7

Facility Name:

Approved By:

Surry and North Anna

~Chief

SUMMARY

~!sf,}/~

  • Date 1gned

Scope:

An Enforcement Conference was held in Region II on January 21, 1988.

Mr. M. L. Ernst opened ~he meeting by expressing concern with a number of post

outage problems at North Anna as documented in several Inspection Reports in

1987.

Virginia Electric and Power Company (VEPCO) then made a presentation

covering the failure to place the inoperable steam flow instruments in trip

within the required time and recent problems at North Anna.

VEPCO then covered

the equipment qualification problems at Surry and North Anna.

Enclosure 3

contains information from the presentations.

Results:

The results of the NRC findings in this area will be forwarded under

separate cover.

. >'..

  • -;*** . .,. .- '

~ .**

, Enclosure 1

2

ENFORCEMENT CONFERENCE DETAILS

1.

Attendees - see Enclosure 2

2.

Enforcement Conference

Mr. M. L. Ernst opened the meeting by expressing concern with a number of

of post outage problems at North Anna as documented in several Inspection

Reports in 1987.

Mr. J. Wi 1 son * of Vi rgi ni a Electric and Power Company

(VEPCO) gave a brief description of the VEPCO position including concern

with the lack of sensitivity by operations and management on making timely

decisions for non-confonning conditi.ons.

Mr. M. L. Bowling then presented

the background, rocit cause, description of events, safety considerations

and corrective actions associated with the North Anna Unit 2 inoperable

steam flow instrumentation.

Mr. Bowling then discussed the summary of

events, root causes, and management plan associated with the 1987

refueling outage and startup problems at North Anna.

Equipment Qualification (EQ) *problems *identified at Surry and documented

in Inspection Report

280/86-12 and 281/86-12 were then discussed by

Mr. E. S. Grecheck.

Mr. Bowling then discussed the EQ problems identified

at North Anna and documented in Inspection Report 338/87-32 and 339/87-32.

With regard to the failure to place the inoperable steam flow instruments

in trip with in the required time, the licensee stated that management

tolerance of steam flow indication problems at low steam flows contributed

to the violation.

Technical Specificati-ons (TS) require inoperable steam

flow channels be placed in trip within one hour..

However, at

approximately 1200 on November 4, 1987, two steam flow channels were found

to be inoperable and were not placed in trip. Plant shutdown was started

at 10: 00 p.m., ten hours later.

The 1 icensee * stated that the safety

significance of this event was low since redundant channels and signals*

  • were available.

Corrective actions include specifyin*g channel check

requirements and maximum power levels for instrument response.

The

licensee also committed to revising Licensee Event Report (LER)87-015 on

this event due to numerous deficiencies in the report.

The licensee stated that the root causes for the problems encountered

during the 1987 outages and startups were .due in part to

management/supervisor failure to enforce standards, failure to follow

procedures, and inadequate procedures.

Corrective actions include

strengthening accountability; requiring safety committee review prior to

changing procedure initial conditions, and increasing management

  • involvement.

3.

Conclusions

... * .. -**.

The NRC sha*res VEPCO :Concerns w'lth respect to management tolerance of

non-conforming conditions, failure to follow procedures, and inadequate

procedure.

Future inspections will be conducted to monitor performance

in these areas *. We are continuing our review of these issues and our

conclusions will,be forwarded under separate cover *

.

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ENCLOSURE 2

Enforcement Conference Attendees

Virginia Electric and Power Company

J .* L. Wi.lson, Manager, -Nuclear Operations Support

M. L. Bowling, Assistant Station Manager, North Anna

E. S. Grecheck, Assistant Station Manager, Surry

N. E. Hardwick, Manager, Nuclear Power.and Licensing, Corporate

G. L. Pannell, Director, SEC

R. W. Calder, Manager of Nuclear Engineering

R. M. Kritch, Licensing Engineer

J. E. McDonald, Public Affairs Coordinator

E.T. Shaub, Licensing Engineer

P. T. Knutsen, Supervisor, Nuclear Engineering

Nuclear Regulatory Commission

M. L. Ernst, Deputy Regional Administrator

C. W. Hehl, Deputy Div-ision Director, Division of Reactor Projects (DRP)

G. R. Jenkins, Director, Enforcement and Investigations Coordination Staff

B. A. Wilson, Branch Chief, DRP

F. S. Cantrell, Section Chief, DRP

F. Jape, Section Chief, Test Programs, Division of Reactor Safety (DRS)

R. P. Croteau, Project Engineer, DRP

W. E. Holland, Senior Resident Inspector, Surry

J. L. Caldwell, Senior Resident Inspector, North Anna

L. B *. Engle, Project Manager, Nuclear Reactor Regulation (NRR)

L. P. King, Resident Inspector, North Anna

B. Uryc, Enforcement Coordinator

M.A. Scott~ Project Engineer, DRP

C. J. Paulk, Reactor Inspector, DRS

C. F. Smith, Reactor Inspector, DRS

U. Potapovs, Section Chief, NRR

T. E. Conlon, Section Chief, DRS

E.W. Mer.schoff, Deputy Director, DRS

A. J. Szczepaniec, Reactor Inspector, DRS

W. Levis, Reactor Inspector, DRS

. )

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ENCLOSURE 3*

NRC Enforcement Conference

North Anna 2 Inoperable Steam

Flow Instrumentation

Agenda

  • I. Background

U. Root Cause

UL Description of Event

IV. Safety Considerations

V:' Corrective Actions

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Purposes of Steam Flow Instrumentation

-

Control Room Indication

-

Steam Generator Level Control System

-

Reactor Protection

-

Engineered Safety Features

i*'.

Technical Spec*ifications Requirements

Reactor Protection

-

Steam/FeedWater Flow" Mismatch Coincident with tow

Safety Injection and'."

Steam Generator Level ih Any One Loop

- * Two Channels per Steam Line, One Channel to Trip

-

Minimum Operable Channels -

One per Steam line

-

Action for Inoperable Channel -

Place in Trip within 1

Hour

-

Channel Check each 12 Hours, Channel Functional Test

Monthly, Channel Calibration each 18 Months

Steam Line isolation -

High Steam Flow in Two Steam Lines Coincident with

Either Low-Low* TAVG or Low Steam Line Pressure in

Any Two Loops

-

  • Two Channels per Steam Line, One Channel to Trip

-

Minimum Operable Channels -

One per Steam Line

-

Action for Inoperable Channel -

Place in Trip within 1

Hour

  • *

-

Channel Check each 12 Hours, Channel Functional Test

Monthly, Channel Calibration each 18 Months

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Technical Specifications Requirem:ents

Specification 3.0.3

-

When LCO is Not Met, Except as Provided in Action

  • Requirements, within One Hour Initiate Action to Place

Unit in Mode in Which Specification Does Not Apply

Channel Check

-

A Qualitative Assessment of Channel Behavior During

Operation by Observation

Shall Include, Where Possible, Comparisons with

Independent Channels Measuring Same Parameter

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Figure 21-l

HAIN STE.AH SYSTEH (SHEt:r l)

REV 01/ll/86

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VENTURI STEAM FLONC-*

INDICATION

STEAM FLOW VERSUS VENTURI DIFFERENTIAL PRESSURE

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STEAM FLOW INDICATION ERROR VERSUS REACTOR POWER.

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ERROR ~S CORRESPOND TO

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15

20

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30

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REACTOR POWER, O/o

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Root Cause

Personnel Error

-

Inadequate Post-Maintenance Testing

-

Untimely Operator Action

-

Inadequate Use of Alternate Indications

-

Management Tolerance * of Steam Flow Indication

Problems at Low Steam Flows

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Reasons for Untimely Operator Action

-

Attention Directed at Delta T/TAVG Instrument Failure

-

Influenced by Past Experience with Steam Flow Indication at Low Steam Flows

-

Time Required to Make Containment Entry

-

Concern Over Prevention of an Unnecessary Safety Injection When Placing Failed

Channels in Trip

-

Steam Flow Indication from ERF Computer

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,. Sequence of Events

8/29/87

9/11/87

9/14/87

9/17/87

9/19/87

9/21/87

Steam Generator A Steam Flow Channel Ill (FT-2474) was

Calibrated within Specified Accuracies *

-Steam Gen*erator "A" Steam Flow Channel Ill (fl-2474) was

Removed from Service for Raychem Repair

Raychem Repair Completed for FT-2474

Tagging Record was Written for Approximately 40 Instruments

The Circuits were Tagged and Deenergized at the Loop Power

Supply Cards

The Tagging Record Indicates That Card at Location C1-221 was

Tagged for FT-2474

This is Actually the Card for LT-2474

The Reverse Error Occurred for LT-2474

Card C3-425 was Tagged for LT-2474, but is Actually the Card for

FT-2474

Raychem Repair Completed for LT-2474

C1-221 Tag: Removed and Card Inserted to Energize FT-2474

LT-2474 w~s Energized Instead*

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Sequence of Events

9/24/87*

9/29/87

9/29/87*

10/08/87

10/25/87

Post-Maintenance Test of FT-2474 Performed by Reading Voltage

Output at Card location C1-221

Test was Satisfactory Because LT-2474 was Actually Tested

C3-425 Tag Removed and Card Inserted to Energize LT-2474

FT-2474 was Energized Instead

Post-Maintenance Test of LT-2474 Believed to have Been Performed

by Verifying Level in Control Room and Found Satisfactory

EWR 87-206 Documentation for FT-2474 Resigned and Redated to

Meet Documentation Requirements

Maintenance Procedure for Verifying RPS Transmitter Operability

Prior tb Startup was Performed with the Unit in Mode 5

Channel 'Check Could Not be Performed Because Steam How was

Zero

Therefore, in Accordance with Procedure, the Valve Lineup was

Verified to be Correct to Establish Operability for the Mode

Change

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Sequence of Events

. 11/04/87:

1200*

Steam Generator A Steam Flow Channel m and Steam

Generator "B" Steam Flow Channel IV were Reading Outside of

the Acc'eptance Criteria

CRO Log flagged Problem with Steam Generator Steam Flow

Channels as Being Due to Steam Flow Conditions at Less Than

5010 Power

1719

Entered Mode 1

1754

1816

1838

1845*

  • App_roximate

Unit at 24°/o Power

Steam Generator A Steam Flow Channel ill and Steam Generator

B Steam Flow Channel IV Observed Reading Zero flow

B Loop Delta T/TAVG Channel II Observed Reading 10010 Low and

Declared Inoperable

Entered AP-3

. SRO-on-call Departed Plant After Briefing by Shift Supervisor on

Instrumentation Problems Believing that Steam Flow Channels

Would Indicate with Higher Steam Flow

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POWER ANO STEAM FLOWS FROM STRIP CHARTS

POWER

40%

0

SIG C

STEAM FLOW

20%

0

SIG B

STEAM FLOW

20%

0

SIG A

STEAM FLOW

    • 20%

0

2

3

4

5

a

7

8

TIME AFTER ENTERING MOOE 1, HOURS

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J2 "A" S/G

oou_, __ ,...~

0000

224'3*"

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Level

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Sequence of Events

11/04/87:

1900

Power Stabilized at 26-27DAJ

1904

Instrument Techs_ Started Calibration of B: Loop Delta T/TAVG

Channel I

1915

B Loop Delta T/TAVG Channel II Placed in Trip

2000*

CRO Log Readings for Steam Generator Steam Flows Indicated that

2009-

both Steam Generator A Steam Flow Channel Ill and Steam

Generator "B" Channel IV were Indicating Zero and Not

within the Channel Check Acceptance Criteria

CRO Log Flagged Problems as Being Under Investigation

2041

SRO On-call had Several Discussions on Plant Status with Shift

Supervisor

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. Sequence of Events

11/04/87:

2048

Assistant Station Manager {O&M), Who was the Acting Station

Manager, Notified of Instrument Failures by SRO On-call

2054

SRO On-call Advised Shift Supervisor of the Need to Declare Steam

Flow Channels Inoperable, to Enter T/S 3.0.3 and the EPIPs, and

to Enter Containment to Check the Transmitters

2120

SRO dn.-call Confirmed with Shift Supervisor the Need to Enter IS.

3.0.3

2122

Acting Station Manager Notified Corportation Management of Plant

Status

2130*

Assistant Station Manager {NS&L) Notified by STA that Two Steam

  • Approximate

Flow Channels were Not Indicating but Could Not be Placed in

Trip per _the AP

AP Required Entry into T.S. 3.0.3

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Sequence of Events

11/04/87:

2139

SRO On-call Notified Acting Station Manager that Steam Flow

Channels will be Declared Inoperable and Unit will be Declared

Inoperable and Unit will be Ramped Off Line IAW T.S. 3.0.3

2150*

Assistant Station Manager (NS&L) Notified by STA that T.S. 3.0.3

was to be Entered

2150

Acting Station Manager Notified Corporate Management of Planned

Shutdown and Entering EPIP

2153

Steam Flow Channels Declared Inoperable

Although Te.ch. Specs. Permit STARTUP and POWER

OPERATION to continue Provided the Inoperable Channel are

Placed in : Trip, AP-3. 7 Requires Action within 1 Hour to Place the

Unit in HOT STANDBY within the Next 6 Hours

2155

Acting Station Manager Discussed Instrument Problems with

Superintendent of Tech. Services

  • Approximate

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Sequence of Events

11/04/87:

2200

2200

Commenced Unit Shutdown

Instrument Department Began Analyzing Reactor Protection and

ESF Logic to Determine if "A" or "B" Steam Flow Channels

Could be Placed in Trip with B Loop Delta T/TAVG Channel II

Already in Trip

2201

Operations Entered Containment to Attempt to Check Steam Flow

Transmitters and Valve Lineups

2205*

Assistant Station Manager (NS&L) Verified with Unit 2 SRO that

Requirements of T.S. 3.0.3 are Being Met and the Emergency

Plan has Been Entered

2207*

Assistant Station Manager (NS&L) Advised NRC Resident Inspector,

Who was in Control Room, of Planned Action

2210*

Assistant Station Manager (NS&l) Notified NRC Senior Resident

2215

2216

2240

2345*

  • Approximate

Inspector of Plant Status

Steam Generator B Steam Flow Channel IV Returned to Service

State and Local Governments Notified of Unusual Event

NRC Notified of Unusual Event

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Station Nuclear Safety and. Operating Committee Initiated Telephone

Conference to Review Deviation to AP 3.7 : . i

Safety Commitee Included Acting Station Manager

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Sequence of Events

11/05/87:

0012

0015*

0030*.

0220

0539

0800

12/04/87

12/10/87*

12/17/87

12/18/87

  • Approximate

Steam Generator A Steam Flow Channel Ill Placed in Trip

A Temporary Change was Made to AP-3. 7 Allowing this Channel to

be in Trip at the Same Time as "B" Loop Delta T/TAVG Channel

II Shutdown Terminated

Assistant Station Manager (NS&L) Briefed NRC Senior Resident

Inspector on Plant Status

Assistant Station Manager (NS&L) Reviewed T.S. Requirements with

Shift Supervisor to Ensure that Technica*1 Specifications were

Being Complied with

Steam Generator A Steam Flow Channel Ill Returned to Service

"B" Loop .Delta T/TAVG Channel II Returned to Service

Assistant Station Manager (NS&L) Met with NRC Senior Resident

Inspector to Review T.S. and AP-3

LER Submitted

Data from Most Recent Startup was Obtained and an Assessment

. of Steam flow Inaccuracies. at Low Power was Initiated .

NRC Resident Inspectors Met with Supervisor, NSE and then *.

Station Manager on the Steam Flow Issue *

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NRC Resident Inspector Exit Meeting and Notification by NRC of

Potential Violation and Enforcement

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Safety Considerations

Reactor Protection and ESF Logics

.

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Reactor Protection

-

1 of 2 Steam/Feedwater Flow Mismatch (40°/o of Full

Safety Injection .

Steam Flow) Coincident with 1 of 2 Steam Generator

Low Level (250/o Narrow Range Span)

-

No Credit Taken for this Trip in USFAR

-

1 of 2 High Steam Flow in 2 of 3 Steam Lines

Coincident with Either Low-Low TAVG (543°F) in Any

Two Loops or Low Steam Pressure (600 PSIG) in Any

Two Loops

-

2 of 3 High Differential Pressure (100 PSI) Between One

Steam Line and Each of the Other Two Lines

-

2 of 3 High Containment Pressure (17 PSIA)

-

2 of 3 Low-Low Pressurizer Pressure (1765 PSIG)

-

Manual Initiation

Steam Line Isolation -

1 of 2 High Steam Flow in 2 of 3 Steam Lines

Coincident with Ei.ther Low-Low TAVG (543°F) in Any

Two ~oops or. Low Steam Pressure (600 PSIG) in Any

Two Loops

-

2. of, ~ lntermeqiqte High-High Containment Pressure

(17.8 PSIA)

'

. '. .'

..

~

0 ,-

0

., .

)>

0

I\\)

0

% OF FULL STEAM{Flow

O>

0

0)

0

....

....

0

....

0

0

o-.----------l'-------+------~~-------------1-__.

I\\)

0

~

0

m

0

0)

0

...

0

0

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I

en

-i

m

)>

s:: ,,

r 0

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en

m

-i

-u

0 z

-i

Reactor Protection

No Credit Taken in Safety Analysis for Reactor Trip on Lo Steam Generator Level in

Coincidence with Steam Flow Greater than Feedflow

Loss of Heat Sink Protection Provided by Steam Generator Lo Lo Level Trip

  • ,

Safety Analysis

Scope and

Assumptions

-

Assumed an Inoperable Steam Flow Indicator on Steam

Generators A and B

-

Con*sidered Complete Spectrum of Steam Une Breaks

Inside and Outside Containment

-

Evaluated Impact On:

Steam Line Isolation and Safety Injection

Redundancy

Emergency Operating Procedures

Appendix R Safe Shutdown Procedures

Post Accident Monitoring Instrumentation

(Reg Guide 1.97)

Core Shutdown Margin

SCENARIO NO.

TABLE 1

STEAM LINE ISLOLATION AND SAFETY INJECTION

REDUNDANCY EVALUATION - HIGH STEAM FLOW CHANNELS

The Fo 11 owing, '.Stearn flow

Channels

Inoper~ble: Loop A/Channel 3 (LAC3)

Loop B/Channel 4 (LBC4)

BREAK .LOCATION

SOURCE OF PROTECTION

ADDITIONAL

FAILURES

TO LOSE

PROTECTION


~------

1.

Loop A, Upstream of

Loop A Nonreturn

Failure of

Flow Transmitter (FT) . Valve (NRV)* OR

NRV ANO

(4.6 Sq. Ft. Max)

LBC3/LCC3 OR LBC3/LCC4

LBCJ AND

OR Hi-2 Containment

Hi-2 CP

    • Pressure {Some delay)

2.

Loop A,*Between FT

Loop A NRV

Failure of

and NRV (1.4 Sq. Ft.)

OR LAC4/LBC3

NRV

OR LAC4/LCC3

ANO LAC4

OR LAC4/LCC4

AND LBC3

OR LBC3/LCC3

AND Hi-2CP

OR LBC3/LCC4

OR Hi-2CP (Some

delay)

3.

Loop B, Upstream of

Loop B Nonreturn

Failure of

Flow Transmitter (FT)

Valve (NRV) OR

NRV AND

(4.6 Sq. Ft. Max)

LAC4/LCC3 OR LAC4/LCC4

LAC4 AND

OR Hi-2 Containment

Hi-2 CP

Pressure.(S~me delay)

4.

Loop B, Between FT

Loop B NRV

Failure of

and NRV (1.4 Sq. Ft.)

OR LAC4/LBC3 *

NRV

OR LAC4/LCC3 *

AND LAC4

OR LAC4/LCC4

AND _LBC3,

OR LBC3/LCC3

ANO Hi-2CP

OR LBC3/LCC4

OR Hi-2CP (Some

delay)

  • If NRV functions as designed, then a Safety Injection Signal is

Generated on High Steam Line Delta-P .

. .. ;:;,

.

. *~ .... ' ..

SCENARIO NO.

TABLE 1 (CONT.)

STEAM LINE ISLOLATION ANO SAFETY INJECTION

REDUNDANCY .. EVALUATION 7" HIGH STEAM. FLOW CHANNELS

BREAK LOCATION

SOURCE OF PROTECTION

ADDITIONAL

FAILURES

TO LOSE

PROTECTION


*--~--------------------~-----------~---~---------

5.

Loop C, Upstream of

Loop C Nonreturn

Failure of

Flow Transmitter (FT)

Valve (NRV) OR

NRV ANO

(4.6 Sq. Ft. Max)

LAC4/LBC3

LAC4 ANO

OR Hi-2 Containment

Hi-2 CP

Pressure (Some delay)

6.

Loop C ,. Between FT

Loop C NRV

Failure of

. and NRV (1.4 Sq. Ft.)

OR LAC4/LBC3

NRV

OR LAC4/LCC3

ANO LAC4

OR LAC4/LCC4

ANO LBC3

OR LBC3/LCC3

AND Hi-2CP

OR LBC3/LCC4

OR Hi-2CP (Some

delay)

7.

Inside Containment,

LAC4/LBC3

Failure of *.

Outside NRV's

OR LAC4/LCC3

LAC4

(1.4 Sq. *Ft./Loop)

OR L.AC4/LCC4

ANO LBC3

OR LBC3/LCC3

AND Hi-2 CP

OR LBC3/LCC4

OR Hi-2 Cont. Press.

8.

Outside Containment

LAC4/LBC3

Failure of

Outside NRV's

OR*LAC4/LCC3

LAC4

(1.4 Sq. Ft./loo~~

OR .LAC4/LCC4

ANO LBC3

OR LBC3/LCC3

OR LBC3/LCC4

  • - ...

-

.:*,

"i': .

. ,

To Safety Valves.Atmospheric Steam Dumps,

and Decay Heat Release Valve

MSIV

--EH

Flow Restrictor

Steam Generator

MSIV

From S/G B

MSIV

From S/G C

NRV

NRV

NRV

To Auxiliary Steam System

J

To HP Turbine Throttle Valves

To Steam Dumps, Moisture Separator Reheaters,

and Gland Steam Regulator (Sheet 2)

Safety Analysis .

Conclusions

-

No Loss of Safety Function, Even Assuming an

Additional Single Failure

-

Diverse Means (Other than Steam Flow) of Initiating

Safety Injection and Steam line Isolation were Available

-

No Post.:rrip Return to Power Would Have Occurred for

Core Conditions, at Time of Event

-

Adequate Information was Available to the Operator for

Post-Accident Monitoring, Assessment and Management

as Defined in EOPs

-

Event Bounded by UFSAR Safety Analysis

Safety Committee Reviewed Safety Analysis

and Approved Conclusions

. '\\

' t

,, '.

. '

cc

i: -
E

ID

...J

co

0 ,-

X

3: g

u.

C w 5

C z -

ERROR PROPAGATION IN ACTUAL VERSUS INDICATED STEAM FLOW

2

.5

0

.25

.5

8

MAXIMUM INDICATION ERROR 29 INCHES

  • VENTURI ERROR 8 INCHES

.75

18

1

30

ACTUAL FLOW X 106 LBM/HR

2

.. *~*-*. -

_ . .,..,., ___ ._,.,

I

I

.

Corrective Actions

Issue Operations

Directive

-

Maximum Power Level for Instrument Response

Enhance Training

Identified *

-

Use of Alternate Indication Emphasized

. -

Channel Check Requirements Specified

-

Review in LORP

-

Incorporate Instrument Failure/Indication Problems to

Simulator Startup Scenarios

-

Emphasize Use of Alternative Indications in Simulator

Scenarios

I .

,

':

I

I

':

'

I *

'

  • "

'

,

    • ..

,

.c*

I :

--1

"

__ ..

  • 1

Corrective Actions

Review and Upgrade Post Maintenance Test Procedure Development

and Documentation Criteria

Inspect Transmitter Wiring at Next Available Outage

Prepare Revised LEA

Evaluate and Upgrade Instrument Calibration Procedures as Required

to Better Insure Transmitter Operability Prior to Entering Mode 3

Present and Disclass Event with Station Supervisors, and Address

Management Concern with Tolerance of Non-Conforming Conditions

Conclusions

Operations Directive Will Provide Assurance That Steam Flow

Instruments are Capable of Performing Their Intended Safety

Functions

  • -

Based on 10 CFR 50.59 Evaluation Reactor Protection and Engineered

Safety Feature Actuations Would Have Occurred as Required Even

Considering an Additional Single Active Failure of a Steam Flow

Instrument

Corrective Actions will be Adequate to Prevent Recurrence

\\ .. :, ... , ..

I*.'

I.

..

I;

I

  • ,.

NRC Questions

1. Why were the steam flow channels not declared inoperable when they failed the

Tech. Spec. channel 'Check?

2. Why did operation continue at about 21010 power for approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

with both steam flow channels indicating zero before declaring the channels

inoperable?

3. Why were the post-maintenance test data sheets not properly signed off?

4. What actions are beihg taken to obtain more reliable steam *flow indication at low

powers?

5. Are the steam flow channels capable of performing their intended safety function in

Modes 1, 2 and 3?

6. What corrective action was taken with regards to flow indicator 2485 being

inoperable but not placed in trip?

7. Was management * aV'!'are of the fact that the steam flow channels were not

indicating properly ahd not placed in trip vriolation of Tech. Specs.?

i'~

i

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..

I.

1

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I .

1 *.

.*

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1* .*.*

i

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ENCLOSURE 3 .

1987 Refueling Outage and Startup Events

  • Agenda

I. Summary of Events

11. Root Causes

111. Management Plan

-

-_. :*-* __ *

I

-1

    • (_.'

1987 Refueling Outage and Startup Events

6/21/87

Loss of RCS Inventory (Unit 1)

6/29/87

Trip on High Level in #5 Feedwater Heater (Unit 1)

7/11/87

Shutdown Due to Inoperable MSR Stop Valve (Unit 1)

10/22/87

Accumulator Injection into RCS (Unit 2)

10/26/87

Inadvertently Aligned Charging Pump to RCS Causing PORV Lift

(Unit 2)

10/30/87

Inadvertent Cooldown to Below TIS Limit (Unit 2)

i I,

..

..

Root Causes

Personnel

Procedure

-

Failure to Use Multiple or Alternate Indications

Failure to Follow Procedure

Failure to Meet or Maintain Initial Conditions

Failure to Adhere to RWPs

Failure to Use Appropriate Procedure

Personnel Error

-

Management/Supervisor Failure to Enforce Standards

-

Lack of Procedure

-

Inadequate Procedure

'

,.

'*

.

I

..

. ,

Management Plan

-

Procedures

-

Personnel Performance

-* Management Involvement

  • ,

'

,.;

Procedures

Require Safety Cd,mmittee Review and Approval Prior to Use for Any

Deviation to a Prcicedure Initial Condition

Continue Assignnient of Licensed RO from Operations Procedure

Group to PT and ISi Groups for Surveillance Testing Development and

Procedure Revisioh:

Review Current Sqrveillance Procedure Development

Enhance Review Process for Determining Applicability of PTs for Use *

in Post-Maintenance and Post-Modification Testing

Oevel'.op and lmpl.ment Mode Change Reactor Operator Checklists to

Verify Required T.S. Equipment Status Prior to Each Mode Change

f ,t;'

. , .

. ,,

Personnel Performance*

Continue HPES Program

Implement "Coaching" Concept

Strengthening Supervisor and Employee Accountability

Ensure Employees U.nderstand Significance of Events and are Briefed

on Root Causes and; Corrective Actions

-,.,,

Management Involvement

Improve Scheduling ofi' Operability Testing Prior to Startup After Major

Outage

  • strengthen Management Involvement in Operability Testing Prior to
  • startup After a Major Outage by Assignment of Dedicated Operations

Co9rdinator(s)

Continue Managem*ent Walkdowns and Safety Committee Review of

Deficiencies Prior to Startup After a Major Outage. Extend Walkdown

Concept to Maintenance Personnel

Continue Station and Corporate Management Review of Significant

Events with Vice President -

Nuclear Operations

Revise Station Deviation Report Program to Augment Root Cause

Determination

.. r-*lll.

_j

ENCLOSURE 3

Agenda

EQ Enforcement Conference

January 21, 1988

Introduction

EQ Program

Enforcement Items

-

Surry

-

North Anna

EQ Enforcement Summary

.,

f

..

. ' "

Virginia Power

Equipment Qualification Program

, r *

.. '

. '

.**

Virginia Power -

Equipment Qualification Program

Virginia Power's EQ

Program Covers the

Principle Areas of

-

Policy, Standards and Procedures

-

Assignment of Responsibilities

-

Development and Maintenance of Equipment List

(EQ Master List -

EQML) and Qualification files

(Qualification Documentation Reviews -

QDRs)

-

Procurement Process

-

Modifications Affecting/Involving EQ

-

EQ Training

-

Involvement of QA/QC

-

Maintenance of Equipment on EQML

-

Review and Incorporation of Regulatory and Industry EQ

Information

"*

f

-

J:

_ Virginia Power :-- Equipment Qua~ification Program

Virginia Power's EQ,i

Program Objective Is

to Ensure that

.;._ Equipment Required fiy 10CFR50.49 to be Qualified is

'I

Identified on the EQML

-

Qualification Files (QDRs) Contain the Necessary

Information to Clearly Demonstrate Qualification in

Accordance with 10CFH50.49

-

Equipment is* Procured and Maintained in Accordance

with Procedures which Incorporate EQ Requirements as

Appropriate

-

Modifications and Engineering are Controlled Such that

Equipment Qualification is Properly Maintained

-

Relevant Information Provided by the NRC and Industry

is Evalu~ted and Incorporated, as Appropriate, in a

Timely* Manner

.1* ,{

  • ,

.. '

.*.

! .,

, .;

Surry and North Anna

Enforcement Items

.. '1

  • ,
  • t*

Surry EQ Inspection Results

June 16-20, 1986

-

Concluded that Program has been Implemented

which Meets Requirements of 10CFR50.49

-

No Deficiencies Identified in Implementation of

SER/TER Corrective Action Commitments

-

Six Potential Enforcement/Unresolved Items

' .

Potential Enforcement Items

I

. '

Unqualified Internal

Limitorque Wiring *

-

Corrective Prior to Startup (June 1986)

-

Generic Industry Issue

High Head SI Pump

Motor Lube Oil

-

Change to QDR Not Reflected in Procedure

-

Maintenance Procedure Changed

-

Revision Process Enhanced

LHSI Motor Rewind

-

Misleading Documentation in File

Raychem Splices

Unqualified :.

-

Documentation Strengthened; Fully Qualifiable at Tim*e

of Inspection

-

Bend Radius Inconsistency with Raychem Installation

SPEC

  • ~ Completed Inspections and Repairs

Rockbestos Cable

-

Inadequate Documentation in File ,

-

Documentation Revised; ODA Updated

. ' '

'!

':

'

Potential Enforcement Items

Potentially Unqualified Equipment in MSVH (IEIN 84-90)

Background

-

June 1984 -

Initial Notification from Vendor

-

July 1984 -

Original Evaluation Concluded Ea

Equipment in MSVH Not Affected

-

December 1984 -

Issuance of IEIN 84-90 on Superheat

with MSLB

-

March 1985 -

Engineering Tech. Report Issued Did Not

Adeq*uately Address Ea Concerns

..:... June 1986 -

Revised Tech. Report Issued -

Determined Capability Existed to Detect, Isolate and

Recover From MSLB

Recommended Action:

  • Move Steam Pressure Transmitters
  • Isolate Openings in MSH
  • Reevaluate New Accident Assumptions

-

April 1987 -

Final Engineering Tech. Report Issued -

Evaluated Operability of Equipment on EQML Including *

RG 1.97 Indication . :

.*,-*:

Potential Enforcement Items

Potentially Unqualified Equipment In MSVH (IEIN 84-90)

Root Cause

. -

Inadequate Review of Industry EQ Information

Immediate Corrective

Actions

-

Moved Steam Generator Pressure Transmitters

\\'

'

-

Modification Performed in Unit 1 MSVH to Isolate

Elevations

-

In Accordance with GL 85-15/86-15, Virginia Power

Reevaluated Effects of Superheat on Equipment .

Qualifications in MSVH:

  • Equipment Located in MSVH Would Have

Performed Safety Function Prior to Experiencing

Harsh Environment

  • Functions of *Equipment Not Capable of Qualification

or Relocation are Provided by Alternate Equipment

  • Results of Equipment Failure Due to MSLB

(Elevated Temp), was Analyzed and Found to

Remain Bounded by the Safety Analysis

. ' .

. ;:

-;, ..

Potential Enforcement Items

Potentially Unqualified Equipment in MSVH (IEIN 84-90) ....

Current Qualification

I

.

Status

-

Main Steam Pressure transmitters were Moved to

Long Term Corrective

Provide Qµalificaton

-

RG 1.97 Indication (Valve Position) is Being Provided by

Alternate Instrumentation

-

Therefore Equipment on EOML in MSH is Qualified* in

Accordance with 10CFR50.49

Action

-

Enhanced Review/Evaluation Process for EQ

lndustry/NRC Information

-

Strengthened Potential Problem Review Process

-

Lowered Threshold for Initiating Station Deviations

. '

., '

North Anna EQ Inspection Results

October 5-9, 1987

_

_

Concluded that Program has Been Implemented Which

Meets Requirements of 10CFR50.49

No Defeciencles Identified In Implementation of

SER/TER Corrective Action Commitments

Four Violations/

One Unresolved Item -

Unqualified Raychem Splices

-

Unqualified Limitorque Valve Actuators

-

Ea Maintenance Requirements in ODA Not Adequately

Adequately Addressed in Maintenance Procedures

-

Performance Characteristics

-

Victoreen Qualification Test Anomalies Not Adequately

Addressed in QDR

. : .

Unqualified Raychem Splices

(Heat Shrinkable Tubing)

Background

-

Deviant Raychem Splice Categories:

Installation

Acceptance Criteria

Evolution

Undersize Wire

Oversize Bolt

Splice Seal

Overlap

General Workmanship

Criterion

Overlap

Undersize Wire

. Holdout

Raychem Guide

2"

VP Repair

3.A" to 1/2"

0°/o

. Minimum Bend

Radius

QO/o

2 .0 x Use Range

5 x Outer

Resolved Dia.

2.4 to 2.6-. *

to 2.7 x Use

. _. 1 Range

\\'

VP Operability

1/a"

31°/o

  • 3. 7 x Use Range

Unqualified Raychem Splices

Sequence of Events

Fall 1985

Identified Problems with Installation of Raychem Splices Being

Worked During Outage; Repairs Made During Outage

12/13/85

A Particular Configuration Problem Identified on 8 Devices Inside

Containment -

Station Deviation Report Initiated

12/17/85

Deficiency Evaluated and Judged Not to 1*mpact Equipment

Qualification nor Indicate a Generic Problem *

04/07/86

Contract Issued to Test Different Configurations of Raychem Splices

. 06/26/86

NRC IN 86-53 Issued

08/11/86

Raychem ;Issues letter to Customers to Aid in Response to IN 86-53

10/27/86*

Decision Made to Delay Inspections Until Testing was Complete

!

... * . . ;

.;.*:

  • ~-*

,,*,,

...

Unqualified Raychem Splices

Sequence of Events

11/9/86

Comprehensive Splice Inspection Effort Conducted During Surry

Refueling Outages

11/26/86

Surry Inspection Identified Additional Splice Configuration

Deficiencies; However Only a Small Number Did Not Meet Virginia

Power Qualification Operability Criteria

Results from Testing Contract Received and Raychem Splices

Determined to be Qualified

12/19/86

JCO Provided for Raychem Splices Installed on Narrow-range RTD

Based on Results of Surry Inspections and Belief that North Anna

had Same Problem

12/29/86

New Qualification Acceptance Criteria for Installed Configurations

Developed,, Based on Applicable Industry Testing Results; New

Criteria Showed that Vendor Installation Requirements were Highly

Conservative

01/15/87

EWA Issued to Inspect and Repair Accessible Splices Outside

Containment

02/02/87

Ouside Containment Inspections* Initiated

- ,* .

,. ,**

  • .

1.'.,

..

.. i

Unqualified Raychem Splices

Sequence of Events*

02/1.8/87

Conference Calls with NRC on Status of Inspection and Plans for

and

Additional Inspection

02/20/87

. 02/23/87

Detailed Management Plan for Inspections Developed by

Engineering and Provided to Station

02/87 -

Conducted Remaining Inspections and Repairs for Both Units

'10/87

.

I

'

I,'

..

Unqualified Raychem Splices

Management Plan for

Raychem Inspections

-

Reviewed by NRC (Region and Resident

Inspector)

-

Initial Inspections Outside Containment; Planned

to Inspect Inside Containment During Refueling

Unless* Inspection Results Required Otherwise

-

Inspection Priotity Established; (1) IS.

Equipment, (2) Equipment in LOCA/HELB Area

-

Station Management Updates; Control Points

Established to Trigger Suppl*emental Review/Action

(Greater than 50/0 FaUures)

-

Deviation Reports Initiated for Failures; NRC

Guidance in Gls 85-15/86-15 Followed; Repairs

Completed Immediately Following Inspection

I i'

I

!

!,

'

.

I')*

i : *:*,: .

. ' -

.,

i

,:,:

Unqualified Raychem Splices

Application of Installation Acceptance Criteria

Use of Virginia Power

_Developed Criteria

-

Splices Meeting Repair/Replacement Criteria

Acceptable for Life of Plant

-

Splices Failing Repair/Replace111ent Criteria

Acceptable Until Next Outage

-

Splices Failing Operability Criteria, Gls

85-15/86-15 Actions Followed; Repairs Completed

Immediately following Inspection

,*

I

., ,.

Unqualified Raychem Splices

Inspection Results

(Total Units 1 & 2)

Inside

  • Containment .

No. of Devices Inspected

376

No. of Devices Repaired

319

No. of Splices Inspected

2068

No. of Splices Repaired

1301

No. of Devices with

Splices Outside

Operability Criteria

9

No. of Splices Outside

  • Operabiltiy Criteria

9

Outside

Containment

Total

382

758

185

504

1475

3543

578

1879

11

20

33

42

  • ,*.

Unqualified Raychem Splices

Root Cause

Corrective Action

-

Inadequate Installation Procedures and Training

-

Followed Guidance in NRG Gls 85-15/86-15; Investigated

T.S. Operability Requirements, Evaluated Safety Significance,

Developed Justifications for Continued Operation, and

Scheduled Repairs

-

Determined that Deficient Splices Did Not Cause

Significant Safety Concerns

-

Repaired Deficient Splices* in Accordance with More

Conservative Vendor Guidance

-

Updated Qualification * Documentation for Raychem

Splices to Incorporate Applicable Test Results

. *

'\\

  • '
    • ..:

1:

1*.

, ..

Unqualified Raychem Splices

Current Qualiflcatlon

Status

-

Raychem Splices Associated with Equipment on EQML

Corrective Action to

are Now Qualified in Accordance with Updated QDR

Industry Test Results Demonstrated that Majority of

NAPS and SPS Splices Installed in Configurations

Outside Vendor Requirements were aualifiable

Prevent Recurrence -

Detailed .Splice Installation Procedures have been Issued

-

Rigorous Splice Installation Training Conducted tor

Appropriate Personnel

-

Plant Modification Documentation Packages Include

Detailed References to Splice Installation Procedures

Where Appropriate

Unqualified Limitorque Valve Actuators

Background

Root Cause

-

Actuators Procured with Qualification Certification

Covering Complete Assembly; Motors Not Specifically

Identified

-

Uri.usual Actuator Motor IDs Identified on Actuators

During QDR Update Effort in February 1987

-

Vendors Unable to Certify that Existing Qualification *

Documentation Applied to Suspect Motors

-

Improper Documentation Provided by Particular Vendor

,.

.

.} .

'

1* :*

I

Unqualified Limitorque Valve Actuators

Sequence of Events

Fall 1986

Engineering Review of Limitorque QDRs

10/21/86

02/87 *

Limitorque Correspondence Indicating Potential Qualification

Problem with One Non IS. MOV

Discover. Serial Number Discrepancy on Several Actuator Motors

During Engineering Review of Walkdown* Data

02/24/87

Engineering Contacts limitorque on Incomplete Qualification

Documentation Provided to A-E in 1980 -

Motors lacked

Qualification Documentation

02/25/87

Limitorque* Responds that Stock Motors _are Qualified and North

Anna Special Motors Should be Qualified but Were Not Specifically

Tested with the Actuators

02/27/87

Engineering Notified Station of Potential Qualification Problems with

9 Actuator 'Motors; JCO also Provided

Q3/02/87

Station Deviation Report Submitted

i, .

~------~-

  • ,-:*

,*.

  • '

IJnqualif ied Limito-,que Valve Actuators

Sequence of Events

03/03/87

Station Safety Committee Reviews the Qualification Issue

03/04/87

First Motor Replacement Initiated (MOV-SW-1038)

03/05/87

One Service Water Actuator Motor Pulled and Destructively

Examined

03/05/87 *

Station Safety Committee Reviewed Results of Inspection and

Approved the JCO Developed on 2/27/87 for the T.S. Actuators

03/07/87

Initiated and Completed Six Motor Replacements

to

03/25/87 *

03/26/87 ._ *

Completed Replacement of 7 of 8 IS. Actuator Motors

10/06/87

The Remaining One IS. and One Non IS. Actuator Motors were

Replaced 'During the 1987 Refueling Outage as a Result of

Replacement Qualified Motor Procurement Lead Time

Last Two Motors Replaced

I

I!

*;

.

. .

Unqualified Limitorque *. Valve Actuators

Current Qualifcation

Status

-

Valve Actuators Now Fully Qualified *

Corrective Action to

Prevent Recurrence ** * -

Procedures Strengthened to Require that Procurement

of any Limitorque Part, Assembly, or Module that is Not

Explicitly Qualified to Test Reports Previously Reviewed

and Approved by VP (as Specified in the Procurement

Document), Must be Identified and Accepted by VP Prior

to Shipment

Conclusions

-

Followed Guidance in NRC Gls 85-15/86-15; Investigated

T.S. Operability Requirements, Evaluated Safety Significance,

Developed Justifications for Continued Operation, and

Scheduled Repairs'

-

Determined that Unqualified Valve Actuators Did Not

Cause Significant Safety Concern

-

Motors with Proper Qualification Certification Installed in

Timely Manner

.

- . Inspections of Questionable Motors and Subsequent

Vendor Information Indicate that Motors are Qualifiable for

  • the Envi~onmental * Zones in Which They. are * Located

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1

EQ Maintenance** Requirements in QDR Not

Adequately Addressed in Maintenance Procedures

Replacement of LHSI Pump Bearings

Safegu*rcl Bldg Fan Grease Changeout/Sampling

Re-Torque Specifications for Conax Connections in SOY Maintenance

Procedures

Overall Root Cause

-

Inadequate Reviews of New/Revised QDRs by the

Affected Station Departments to Ensure Requirements are

Incorporated into Station' Procedures

Corrective Actions

-

Evaluated Continued Applicability of QDR Requirements

-

Change Requests Issued to Delete LHSI Pump Bearing

Replacements and Safeguard Bldg Fan Grease

Changeout/Sampling Requirements from Applicable ODRs

-

Revised SOV Maintenance Procedure to Specify Conax

. Connector Re.:rorqueing Requirements

Current Qualification

.

Status

-

LHSI Pump Motor Bearings were~ and Remain, Qualified

-

Safequards Bldg Fans were, and Remain, Qualified

-

Conax Connectors to SOVs were, and Remain, Qualified

_ ~inc_e Conax Procedure Which Includes Torque Valves was

Used for Sov Repair

Corrective Action to

.

Prevent Recurre.nce -- * A Cross Reference Index Between QDR Requirements

and Implementing* Maintenance Procedures will be

Developed

'

<

..

  • ,,

.

.

Performance Characteristics Not Adequately

Addressed in QDRs

Root Cause

Corrective Action

Current Qualification

-

Deficient ODR Preparation, Note that Performance .

Characteristics were Considered in ODR Development,

but were Not Clearly Delineated in a Unique Section of

  • the Appropriate QDRs

-

Developed a Bounding Analysis for a Worst Case

Instrument loop

Re_sults Show that Total Installed System Accuracies are

within Design Allowable Levels

Status

-

Equipment on EQML is Fully Qualified, Including

Individual and Installed Accuracy Effects, for its Application

Corrective Action to

Prevent Recurrence

-

The Appropriate ODRs will be Enhanced to Clearly

Delineate Equipment Performance Requirements and

Characteristics

-

.

Victoreen Qualification Test Not Ar)equately

Resolved in QDRs

Root Cause

Corrective Action

Current Qualification

-

Inadequate QDR Preparation

-

Evaluated Test Anomalies, Including Accuracy Data

Concluded that Test Anomalies Did Not Impact Monitor

Qualification

Issued a Change Request to all QDR Holders on 11-5-87

Status

-

Victoreen Radiation Monitors Are Qualified for Their

Intended Purpose

This Deviation is Considered to be an Isolated Occurrence

Corrective Action to

Prevent Recurrence -

A Revision to the Victoreen Radiation Monitor QDR,

Addressing Each Anomaly (Including Accuracy Data), has

been Prepared and is being Processed

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  • . .:"

,.

.

1**.:

Equipment Not on EQML Specified in EOPs

NRC IR Documents Commitment

to Review* EOPs and Delete

References to Unqualified Equipment

After Further Evaluation,

Corrective Action Modified

as Follows:

-

EOPs to be Reviewed and Where Qualified and

Corrective Action

Status

Unqualified Equipment are Specified, the Unqualified

Equipment will be Identified

-

Affected EOPs Revised

Operators Trained

  • Guidance for Annual EOP Review has been Amended to

New Convention

r'*:

,.

.

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. .

EQ Enforcement Summary

    • .:

'.*

,*

EQ Enforcement Summary

Surry

North Anna

-

Identification of a Plant-Specific Problem and Initiation

of Corrective Action for Equipment in the MSVH was

Delayed Due to Inadequacies in the Evaluation of the

Effect of Superheated Steam on Environmental

Temperatures

-

Initial Problems Identified with Raychem Installation

were Evaluated to be Due to the Level of Craft

Workmanship

Once Subsequent Problems were Recognized. Inspection

Evaluation, and Repair Proceeded Based on the

Knowledge that '(1) the Raychem Installation Guide was

Highly Conservative, and that (2) Industry Test Results

were Showing that a Much Wider Range of Installation

Configurations were Oualifiable

C

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  • ,
  • '

EQ Enforcement Summary

North Anna

Conclusions

-

Qualification Documentation Obtained. When the Nine

Valve Actuators were Procured Satisfactorily Addressed

the Qualification of the Entire Assembly

Once the Vendors were Questioned Upon Discovery of

Unique Motor IDs, Appropriate Actions were Taken in

Accordance with NRC Guidance

-

Evaluation of Problems Resulted in the Conclusion that

There were Not Programmatic Breakdowns in the Virginia

Power Ea Program

-

The Identified EQ Problems Did Not Result in any Safety

Concerns

'