ML18151A061

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Insp Repts 50-280/87-21 & 50-281/87-21 on 870705-0829.No Violations Noted.Major Areas Inspected:Licensee Action on Previous Enforcement Matters,Plant Operations,Maint & Surveillance & Followup on Inspector Identified Items
ML18151A061
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/15/1987
From: Cantrell F, Holland W, Larry Nicholson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18151A059 List:
References
50-280-87-21, 50-281-87-21, GL-83-28, IEB-84-02, IEB-84-2, NUDOCS 8709240552
Download: ML18151A061 (19)


See also: IR 05000280/1987021

Text

Report Nos.:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/87-21 and 50-281/87-21

Licensee:

Virginia Electric and Power Company

Richmond, VA

23261

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.: DPR-32 and DPR-37

Inspection Conducted:

Approved

SUMMARY

Date 'Signed

°//11~s/f 7

Date Signed

S7/; .5/~" 7

Date Signed

Scope:

This routine inspection was conducted in the areas of-licensee action

on previous enforcement matters, plant operations, plant maintenance, plant

surveillance, followup on inspector identified items, licensee event report

review, 10 CFR Part 21 review, and closeout of temporary instruction T2500/19.

Results: Two violations were identified in this inspection report which are

being considered for escalated enforcement action and will be forwarded under

separate cover.

In addition one violation is listed in this report from

findings identified in inspection report 280; 281/87-11 .

Or.::5r-, 970916

870924

~ ~ 05000280

PDR

ADOCK

'

PDR

Gl

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

2.

  • 0. L. Benson, Station Manager

H. L. Miller, Assistant Station Manager

  • E. S. Grecheck, Assistant Station Manager

J. A. Bailey, Superintendent of Operations

D. J. Burke, Superintendent-of Maintenance

S. P. Sarver, Superintendent of Health Physics

  • R. H. Blount, Superintendent of Technical Services

R. L. Johnson, Operations Supervisor

J. A. Price, Site Quality Assurance Manager

J. B. Logan, Supervisor, Safety and Licensing

G. 0. Miller, Licensing Coordinator

  • F. P. Mone, Supervisor, Quality Assurance
  • M. A. Griffin, Administrative Assistant
  • Attended exit meeting.

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

Exit Interview

The inspection scope and findings were summarized on August 31, 1987, with

those individuals identified by an asterisk in paragraph 1.

The following

new items were identified by the inspectors during this exit.

One

Violation (paragraph 4) was identified for failure to conduct

evaluations for unreviewed safety question determination as required by

technical specifications and 10 CFR 50.59. This item is being considered

for escalated enforcement.

One Violation (paragraph 4) was identified for inadequate procedures,

failure to follow procedures in testing the safety injection system, and

failure to perform a technical specification-required portion of the

diesel generator surviellance.

This item is being considered for

escalated enforcement.

One Unresolved Item (paragraph 9) was identified for review of the

licensee's revised response to IE Bulletin No. 84-02.

In addition, one violation (paragraph 13) was identified from findings of

an NRC headquarters vendor inspection as documented in inspection report

280; 281/87-11.

2

The licensee acknowledged the inspection findings with no desenting

comments in the findings relating to this report.

However, the licensee

did take exception to the findings identified in this report relating to

inspection report 280; 281/87-11.

The licensee did not identify as

proprietary any of the materials provided to or reviewed by the inspectors

during this inspection.

3.

Plant Status

Unit 1

4.

Unit 1 began the reporting period at power.

The unit operated at power

until August 7 when at 1:20 p.m. the unit was manually tripped from 100

percent power due to failure _of the cooling capability of the lB main

transformer.

Repairs were made to the transformer and the unit returned

to power operation the morning of August 8, 1987.

The unit operated at

power for the remainder of the inspection period.

Unit 2

Unit 2 began the reporting period at power.

The unit operated at power

for the duration of the inspection period .

Licensee Action on Previous Enforcement Matters

(92702)

(Closed) Unresolved Item (URI) 280; 281/87-17-01, Review of 10 CFR 50.59

safety

evaluation

for

emergency

busses

cross-connect

breaker

configuration.

The subject issue was discussed in inspection report 280; 281/87-17.

In

that* report, the inspector determined that the

emergency

busses

cross-connect breakers (5Hl) for both units were racked out; however, the

breakers remained in the cubicles. This condition was in conflict with

the condition described in the FSAR, paragraph 8.4.1.

The inspector

requested that the licensee provide the safety evaluation which was

required by 10 CFR 50.59 when the decision was made to leave the subject

breakers in their cubicles.

This request was being evaluated when the

last inspection period ended.

During this inspection period, several additional items relating to the

above concern have come to the attention of the inspectors.

One item

involved the licensee's decision to furmanite a leaking valve (2-WT-177)

which was a manual isolation valve for the chemical addition system to the

B steam generator main feed line in containment.

This repair, on July 4,

1987, resulted in the valve being left in the open position and

inoperable.

The

inspector requested that the licensee provide the

10 CFR 50.59 safety evaluation for this change in system configuration

and, at the time of the request, the evaluation had not been accomplished.

The inspector then reviewed the temporary modification (TM)

log and

determined that this condition had been. logged the evening of July 4,

1987.

However, additional review of the log entry determined that no

3

technical/safety .evaluation review was conducted for the modification.

Also, the inspectors were reviewing station deviation reports and noted

that report number Sl-87-512 dated June 19, 1987, identified a condition

which indicated that testing of the turbine inlet valves as identified in

the FSAR, Section 14.2.13 was not being accomplished.

The inspector also

requested the safety evaluation for this condition and was informed that

the deviation report was still under review.

These concerns were brought to the attention of station management on

July 8 and again on July 10, 1987.

The inspectors stressed that the main

issue was ev2.luation of plant configuration changes to assure that an

unreviewed safety question had not resulted when changes were made.

It

appears that deleting the turbine inlet valve test does involve an

unreviewed safety question and prior Commission approval should have been

sought prior to deleting the test.

After these meetings, another concern was i dent i fi ed to the 1 i cen see

regarding the use of the station fire protection system for purposes not

recognized in the FSAR.

A ring header is periodically installed on the

top of both containments during the hot summer months and fire water

pumped through the header and allowed to run down the outside to assist in

containment cooling. The inspectors questioned if an evaluation had been

performed to determine the impact this usage would have on the capability

to respond to a fire, as well as the consequence of the water running into

the p 1 ant.

A tour of the p 1 ant rev ea 1 ed water in safety-re 1 ated pump

rooms as well as water running down the wall beside the electrical

penetrations in the cable vault.

The inspector a 1 so conducted *a review of the admi n i strati ve procedure

which provides for requirements to conduct evaluations for unreviewed

safety questions.

Those procedures were:

SUADM-ENG-01

SUADM-ENG-03

SUADM-0-11

Engineering Work Request

Design Changes

Functional Bypass and Temporary Modification Control

The inspector concluded from the review that procedures do require

evaluation for unreviewed safety questions;

however,

the procedure

guidance did not always clarify those areas which could require reviews as

required by 10 CFR 50.59 or Technical Specifications.

Additional discussions with station management were held on August 21,

1987,

on

these issues.

Discussion of the issue involving station

deviation report Sl-87-512 resulted in the conclusion that an unreviewed

safety question determination was not conducted when the decision was made

4

to delete testing of the turbine inlet valves.

The licensee provided a

copy of a new station deviation to the inspector on Auqust 21, 1987, which

indicated that an adequate safety evaluation per 10 CFR 50.59 was not

performed when the periodic test for testing of the turbine inlet valves

was discontinued.

Based on the previous findings, the inspector determined that safety

committee (SNSOC) evaluations for unreviewed safety questions had not been

performed and documented in the above cases as required by Technical

Specification 6.1.7.f and g; nor .had the licensee followed the correct

process for conducting a safety evaluation in the above cases as required

by 10 CFR 50.59.

Deleting the turbine inlet valve test appears to involve

an unreviewed safety question.

This item is identified as a violation

(280; 281/87-21-0J) for both units.

(Closed) Unresolved Item 280; 281/87-17-02, Inadequate evaluation of

deficiencies noted during.surveillance testing.

Inspection report 280; 281/87-17 identified numerous concerns regarding

the documentation, evaluation, and corrective actions as a result of the

safety injection train undervoltage functional tests performed during the

1986 refueling outages for both units.

The specific test procedures

reviewed qy the inspector were PT-18.2 A & B for both units. Discussions

with the licensee following their search for additional documentation

revealed the following:

a.

Technical Specification 4.6.A.l.b requires testing demonstrate that

the loss of voltage and degraded voltage protection is defeated

whenever the emergency diesel is the sole source of power to an

emergency bus and that this protection is automatically reinstated

when the diesel output breaker is opened.

This requirement is not

included in the above procedures and consequently has not been

performed.

This is in violation of the Technical Specifications and

the licensee stated the test would be performed during the next

outages.

b.

1-PT-18.2A, "Safety Injection Train A - H Bus Undervoltage Functional

Test,

11 completed 7-7-86.

The completed test results were not reviewed by the surveillance

and test engineering group as required by paragraph 5 .1. 5 of

station administrative procedure SUADM-0-23.

Acceptance criteria was deleted with no reason for deviation

stated as required by paragraph 5.4.3 of station administrative

procedure SUADM-0-21 .

Verification that the emergency diesel generator was secured and

restored was not performed as required by step 5.24.4 of the

above test procedure.

5

The use of a special test to satisfy surveillance testing is

inadequate in that this procedure does not receive the review

and approval required by a normal periodic test.

Also, the

special test system is inadequate in that the performance of

these tests have routinely not been reported to the NRC in the

Monthly Operating Report as required by 10 CFR 50.59 and local

administrative procedure SUADM-0-18.

This is another example of

the violation of 10 CFR 50.59 cited above in this p-aragraph

(280; 281/87-21-01).

c.

1-PT-18 . .?B,

11Safety Injection Train B -

J Bus

Undervoltage

Functional Test," completed 7-6-86.

Test results were

11 unsati sfactory

11 and no corrective action was

performed; however, the unsatisfactory results were determined

to be from a procedure problem.

The licensee could not locate

any procedure change request forms which are required by

admi ni str.at i ve procedure SUADM-0-21

and

speculated that a

procedure change was at one* time initiated and subsequently

lost.

The required post-test position of high-head safety injection

pump 1-CH-P-lA was changed in Attachment I of the above test

procedure without a

procedure deviation

as

required by

administrative procedure SUADM-0-21.

d.

2-PT-18.2A,

11Safety Injection Train A

-

H Bus

Undervoltage

Functional Test

11 , completed 11-23-86.

Problems identified on the test critique sheet and changed on a

procedure deviation were evaluated as

11 procedure problems.

11

No

procedure change request form was initiated nor were the

problems corrected in the next revision as required by

administrative procedure SUADM-ADM-21.

The licensee stated that

the changes were submitted, but lost.

e.

2-PT-18.2B,

11Safety Injection Train B - J Bus Undervoltage Functional

Test,

11 completed 11-21-86.

The test critique sheet states that high-head safety injection

pump 2-CH-P-lA requires retesting.

No documentation can be

found that either retests this pump or evaluates the deficiency.

Technical Specification 6.4 requires that detailed written procedures with

appropriate check-off lists and instructions shall be provided and shall

be followed for the testing of components and systems involving nuclear

safety of the station.

The above findings represent both an inadequate

procedure and failure to follow procedures with regard to testing,

6

documenting,

and

evaluating

results

of

safety

injection

system

surveillance tests.

In add.ition, a portion of the emergency diesel

generator survei 11 ance test apparently has never been performed.

This

item is identified as a violation of Technical Specifications

(280; 281/87-21-02) for both units.

Within the areas inspected, two violations were identified.

5.

Unresolved Items

Wnresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or

deviations.

One new unresolved item is identified in paragraph 9.

6.

Plant Operations

Operational Safety Verification (71707)

The inspector conducted daily inspections in the following areas:

Control

room staffing, access, and operator behavior; operator adherence to

approved procedures, Technical Specifications, and limiting conditions for

operations; examination of panels containing instrumentation and other

reactor protection system elements to determine that required channels are

operable; review of control room operator logs, operating orders, plant

deviation reports, tag out 1 ogs, jumi:ier 1 ogs, and tags on components to

verify compliance with approved procedures.

The inspector conducted weekly inspections in the following areas:

Verification of operability of selected ESF systems by valve alignment,

breaker positions, condition of equipment or component(s), and operability

of instrumentation and support items essential to system actuation or

performance.

Plant tours which included observation of general

plant/equipment

conditions,

fire protection and preventative measures,

control

of

activities in progress, radiation protection controls, physical security

controls, plant housekeeping conditions/cleanliness, and missile hazards.

The inspector conducted biweekly inspections in the following areas:

Verification review and walkdown of safety-related tagout(s) in effect;

review of sampling program (e.g., primary and secondary coolant samples,

boric acid tank samples, plant liquid and gaseous samples); observation of

control room shift turnover; review of implementation of the plant problem

identification system; verification of selected portions of containment

isolation lineup(s); and verification that notices to workers are posted

as required by 10 CFR 19.

7

Certain tours were conducted on backshifts or weekends.

Backshift or

weekend tours were conducted on July 9, 11, 29, August 5, 7, 8, and 25.

Inspections included areas in the Unit 1 and 2 cable vaults, vital battery

rooms,

steam safeguards areas, emergency switchgear rooms,

diesel

generator rooms, control room, auxiliary building, cable penetration

areas,

independent spent fuel

storage facility,

low level

intake

structure, and safeguards valve pit and pump pit areas. Reactor coolant

system 1 eak rates were reviewed to ensure that detected or suspected

leakage from the system was recorded, investigated, and evaluated and that

appropriate actions were taken, if required.

The inspectors routinely

independently. calculated RCS

leak rates using the NRC

Independent

Measurements Leak Rate Program (RCSLK9).

On a regular basis, radiation

work permits (RWPs) were reviewed and specific work activities were

monitored to assure they were being conducted per the RWPs.

Se 1 ected

radiation protection instruments were periodically checked, and equipment

operability and calibration frequency were verified.

The Plant Risk Status Information Management System (PRISIM) was installed

in the resident inspectors' office during this inspection period.

This

personal computer program provides PRA results and other risk-related

information to the inspector for use on deciding inspection priorities.

This version of PRISIM is based on the PRA of Surry 1 performed by EI

International as part of the Accident Sequence Evaluation Program.

Idaho

National Engineering Laboratory modified the PRA in response to comments

made by the Virginia Electric and Power Company.

The PRA results obtained

from PRIS IM are based on core damage frequency.

PRIS IM does not

incorporate the results of assessments of plant damage, containment

responses, or public health consequences.

A meeting was. held on July 14,

1987, at Region II to introduce the Surry 1 PRISIM and to discuss the plan

for testing and evaluating the program.

On July 20, 1987, the inspector witnessed the 1 oadi ng of four spent fue 1

assemblies into a dry cask for storage at the Independent Spent Fuel

Storage Installation (ISFSI) located onsite at Surry. This fuel movement

from the spent fuel pool was being performed by licensed reactor operators

using a written procedure.

This was the fourth Castor V/21 Cask to be

loaded with twenty-one (21) spent fuel assemblies.

The three previously

loaded casks are presently in storage at the ISFSI storage pad.

On July 27, a malfunction of the Kaman radiation monitor RM-GW-103-1

caused the automatic isolation of the containment vacuum system to

atmosphere.

The subject monitor surveys the gaseous effluent release path

of the process vent stack in conjunction with the Victoreen monitors. A

radiation level above setpoint causes the containment vacuum

pump

discharge valves FCV-GW-160 & 260 to shut. The licensee notified the NRC

pursuant to 10 CFR 72 of an engineered safety system actuation, then

subsequently determined that this was not an ESF actuation since the

subject valves are not required for containment isolation.

The shutting

of these valves did, however, remove the one containment vacuum flow path

required by Technical Specification 3.15.8, and required the licensee to

reestablish a flow path or be in hot shutdown in at least six hours.

The

8

inspector expressed concern that during the troubleshooting of this

radiation monitor, a jumper was installed essentially around the monitor

to permit the reestablishment of the containment vaccum flow path.

This

jumper was not controlled by an entry to the station jumper log or

specified in an applicable approved procedure, as required by administra-

tive procedure SUADM-0-11.

The omission of the required administrative

controls prevented this temporary plant modification- from being properly

evaluated as required by 10 CFR 50.59.

This is another example of

violation (280, 281 87-27-01) identified in paragraph 4.

On several occasions during this inspection period, a high chlorine alarm

was received in the main control room from the

11A

11 train chlorine monitor.

This monitor is one of two installed in the main control room to sense

chlorine that could leak from the storage tanks at the site sewage

treatment plant.

Investigation revealed the alarm to be caused by an

erroneous spike on that detector.

This alarm did, however, actuate a

train to isolate the control room ventilation as required.

The licensee

notified the NRC of these ESF actuations as required by 10 CFR 50.72.

In the course of monthly activities, the inspectors included a review of

the licensee's physical security program.

The performance of various

shifts of the security force was observed in the conduct of daily

activities to include: protected and vital areas access controls;

searching of personnel, packages and vehicles; badge issuance and

retrieval; escorting of visitors; and patrols and compensatory posts.

Engineered Safety Feature System Walkdown

(71710)

The inspector performed a walkdown of the accessible areas of the safety-

related portions of the Emergency Diesel Generator system and the

Auxiliary Feedwater System for both units to verify their operability.

This verification

included the

following:

confirmation that the

licensee's system lineup procedure matches plant drawings and actual plant

configuration;

hangers

and

supports are operable;

housekeeping is

adequate; valves and/or breakers in the system are installed correctly and

appear to be operable; fire protection/prevention is adequate; major

system components are properly labeled and appear to be operable;

instrumentation is properly installed, calibrated and functioning; and

valves and/or breakers are in correct position as required by plant

procedure and unit status.

Within the areas inspected, one additional example of a violation cited in

paragraph 4 was identified.

7.

Maintenance Inspections (62703)

During

the

reporting period,

the inspectors reviewed

activities to

assure compliance with

the appropriate

Inspection areas included the following:

maintenance

procedures.

9

The inspectors followed the repair of a defective weld in the Unit 2

letdown line inside containment.

On July 22, the unidentified leakage

from the reactor coolant system increased from approximately 0.2 gpm to

0.6 gpm.

The operators also noted a slight increase in containment

activity. Containment entries were m~de and the leakage was determined to

be primarily from a defective socket weld on a two-inch pipe tee just

downstream of the letdown isolation valve HCV-2200C.

This condition was

documented on station deviation report S2-87-342. * On July 28, the

licensee had determined that a permanent repair as required by the ASME

Code Section XI was not possible due to the inability to successfully

isolate the leak; therefore, an Engineering Work Request (EWR 87-288) was

issued approving a temporary repair until the 1988 refueling outage. This

temporary repair consisted of encasing the defective weld in a can and

injecting a Furmanite sealant. The EWR considered this a temporary repair

as a gasket joint seal and included a safety analysis.

The inspector

reviewed all the documentation for this effort and expressed the following

concerns:

a.

An attempt to permanently repair the defective weld should be made no

later than the upcoming 10 day snubber outage scheduled for late this

year in lieu of the 1988 refueling outage.

The licensee agreed and

committed to a repair no later than the snubber outage; and

b.

A formal evaluation control with regard to containment integrity was

not performed for the time between the discovery of the defect and

the accomplishment of the temporary corrective action.

The subject

defect is located inside the containment between the inside

containment isolation valves and the letdown line containment

penetration. This results in the outside containment isolation valve

being the only barrier for this penetration.

These concerns and the resulting enforcement action are addressed in a

special inspection report (280;* 281/87-26).

8.

Surveillance Inspections

(61726, 61700)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

fo 11 ows:

Test prerequisites were met.

Tests were performed in accordance with approved procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test .

Test data was properly collected and recorded.

10

Inspection areas included the following:

On July 29, the inspector witnessed portions of periodic test 2-PT-18.7,

11 Charging Pump Operability and Performance Test.

11

This test was performed

following the replacement of oil on charging pump 2-CH-P-lC.

The licensee

noticed foaming of the oil in this pump and suspected it to be

contaminated with water.

Analysis of the oil removed, however, did not

indicate a presence of water.

The samples have been sent to an

independant lab for further evaluation.

No discrepancies were noted.

On August 7, 1987, the inspector witnessed portions of periodic test

1-PT-14.2,

11Main Steam Trip Valves and Main Steam.Non-Return Valves.

11

No

discrepancies were noted; however, the results observed did not meet the

requirements of the acceptance criteria. The test requires that the MSTVs

close from actuation of the switch to indication of closure in 5 seconds

or less.

Results being obtained were in the 6 to 7 second range.

The

inspector noted that this test is not a realistic test of closure time of

the valves in an accident.situation and also was informed that a Technical

Specification change had been submitted to resolve this condition.

A

deviated PT-14.2 was performed satisfactorily later that evening.

On August 18, 1987, the inspector witnessed portions of the periodic test

1-PT-15.lC,

11Steam Generator Auxiliary Feedwater Pumps.

11

This test

performed the monthly surveillance on the turbine driven auxiliary

feedwater pump l-FW-P-2.

The pump was started using the

11A

11 train steam

admission valve and appeared to start and perform within the acceptance

criteria specified for alert in the above procedure.

The recorded

vibration for the turbine to pump bearing was measured to be 0.19 in/sec,

thus placing the pump in the alert range. A vibration measurement greater

than 0.2 in/sec would constitute an inoperable pump.

The licensee is

continuing to evaluate this condition.

No discrepancies were noted.

Within the areas inspected, no violations or deviations were identified.

9.

Followup on Inspector Identified Items and IE Bulletins

(92701)

(Closed) Inspector Followup Item (IFI) 280, 281/84-31-01:

Implementation

of Licensed Operator Requalification Program (LORP) and its submittal to

the NRC.

The LORP required that persons failing to score satisfactorily

on requalification examinations be removed from shift duty, participate in

an

accelerated requalification program,

and pass a requalification

examination.

The accelerated training program required nothing other than

self-study.

The. inspector followup item involved upgrading accelerated

requalification to include more than self-study, and the submittal of a

revised requalification program for

NRC

review and approval.

The

inspectors

reviewed

the

present

status

of

1 i censed

operator

requalification and determined that in 1985 the licensee implemented

accelerated requalification training with individualized requirements

beyond self-study. The licensee stited that the LORP is being updated to

incorporate revised 10 CFR 55 requirements, and should be submitted to the

NRC within two months.

This revised LORP contains expanded requirements

11

for accelerated requalification.

Based on this information, the item is

closed.

(Closed) I FI 280, 281/85-31-01:

Admi n i strati ve Contro 1 s for Changes

Affecting the Work Planning and Tracking System (WPTS).

A previous NRC

inspection identified that the licensee was using a computerized Work

Planning

and

Tracking

System without a formal

method to ensure

incorporation of changes to applicable plant procedures, policies or

hardware.

To ensure work orders adhere to current requirements, the

1 i cen see returned to verifying information entered on the work orders

against the Technical* Specifications and hard copies of the procedures

addressing Environmental Qualification, Safety Related Equipment (Q-List),

and Inservice Inspection Requir~ments.

B~cause these inputs should have

adequate administrative controls, this item is closed.

The licensee is in

the process of updating the computerized WPTS to assure accuracy, improve

software contro 1 s, and enhance the tracking of work orders.

Ful 1

implementation of the computerized WPTS is expected to be completed within

two months.

(Closed) I FI 280, 281/85-31-04:

Preventive Maintenance Overdue Criterion

and Management Review of Overdue Items.

Licensee procedures had not

defined an overdue criterion for preventive maintenance or re qui red

management review of delinquent items.

The inspector verified that

Procedure SUADM-M-30,

Planned Maintenance System Manual,

which was

approved August 18, 1987, contains overdue criteria and management review

requirements. The item is closed.

(Closed) IFI 280, 281/85-31-05:

Review of Preventive Maintenance Program

for Adequate Procedures as Recommended by Vendor Manuals. The inspector

followup item involved assuring that preventive maintenance is required at

-the frequencies recommended by the vendors, and that the program provides

verification of the design basis dewpoint of the containment instrument

air system.

The licensee stated that all safety-related preventive

maintenance procedures will be updated and approved by September 1987 in

accordance with their commitment of October 1985 in response to Generic

Letter 83-28.

The inspectors reviewed a draft revision of procedure

IA-C-M/M entitled Nash Model 8045 Containment Instrument Air Compressor

Preventive Maintenance (Non-Safety Related).

The draft revision included

a post maintenance check that the air dryer is operating properly, and was

scheduled for final review on August 21, 1987.

Based on this information,

the item is closed.

(Open) IE Bulletin No. 84-02, Failure of General Electric Type HFA Relays

Used in Class IE Safety Systems.

During a review of the subject bulletin

for closeout, the inspector questioned the 1 icensee regarding current

status.

A review of the status was conducted by the licensee and they

determined that the original response to this bulletin, dated July 31,

1984, was incorrect in that eight relays per unit were not identified as

12

candidates for replacement.

This omission prevented these relays from

being inspected and subsequently replaced as required by the bulletin.

The licensee is in the process of preparing a revised response to the

bulletin.

This issue is identified as an

unresolved item (280;

281/87-21-03) pending review of the licensee's revised response.

Within the areas inspected, no violations or deviations were identified.

10.

Licensee Event Report (LER) Review

(92700)

The inspector reviewed the LERs listed below to ascertain whether NRC

reporting requirements were being met and to determine appropriateness of

the corrective action(s).

The review also included a followup on

implementation of corrective actions anp review of licensee documentation

that all required corrective action(s) were complete.

LERs that identify violation(s) of regulation(s) and that meet the

criteria of 10 CFR, Part 2, Appendix C,Section V are identified as

Licensee Identified Violations (LIV) in the following closeout paragraphs.

LIVs are considered first-time occurrence violations which meet the NRC

Enforcement Policy criteria for exemption from issuance of a Notice of

Violation. These items are identified to allow for proper evaluation of

corrective actions in the event that similar events occur in the future.

(Closed)

LER 280/84-10, Appendix R Review.

The

issue involved a

reanalysis of the station's compliance with 10 CFR 50, Appendix R design

requirements.

The reanalysis identified five areas which did not meet

Appendix R requirements.

The 1 i censee corrected the discrepancies.

Region II conducted an inspection in May 1987 of the Surry Power Station

which evaluated the licensee's actions regarding the implementation of the

requirement~ of Appendix R.

Based on that inspection, this LER is closed.

(Closed)

LER 280/87-01, Pressurizer PORVs Declared Inoperable Due to

Excessive Stroke Time.

The issue involved failure of the subject valves

to open within the required time frame when the emergency backup air

supply was used as the only pressure source.

The test deficiency was

identified by the licensee during review of IEN 86-50.

The licensee

determined that the air supply lines from the emergency air supplies were

undersized.

Corrective action included redesign and installation of

properly sized air lines and related components.

The corrective action

and retest was verified as complete by the inspector.

This item is

identified as LIV 280/87-21-04 for failure to provide adequate design and

testing of a safety-related system.

This LER is closed.

(Closed)

LER 280/87-03, Control/Relay Room Chiller Inoperable Due to

Inadequate Service Water Flow.

The issue involved loss of operation of

the subject chiller on three different occasions contrary to Technical

Specification 3.14.B.

The licensee has identified the root cause to be

inadequate flow of service water.

The inadequate* flow was due to pump

13

suction

strainer clogging,

service water

pump

failure,

excessive

throttling of service water, respectively, for the occasions.

Licensee

corrective action is to replace the three control room chillers with new

units.

In addition, an engineering evaluation has been conducted of the

control/relay room ventilation system,

including the service water

subsystem.

The

inspector reviewed the engineering conclusions and

considers that the licensee is taking appropriate long-term actions

(service water system upgrade) to eliminate this condition. This item is

closed.

(Closed) LER 280/87-04, Potential for Bypass of Safety-Related Filters Due

to Inadequate

Fan

Shaft Seal.

The

issue involved the licensee 1 s

determination that the control room ventilation fans have the potential to

admit more than the Technical Specification allowed limit ~f unfiltered

air into the control room due to inadequate fan shaft seals.

Corrective

action included installation of temporary shaft seals until permanent

bellows seals were procurred.

The inspector verified installation of the

new seals~

This item is closed.

(Closed) LER 280/87-05, Control Room Chillers Tripped Due to Clogging of

the Service Water Y-Type Strainers.

The issue involved clogging of the

Y-type strainers for the Band C chillers when the rotating strainer

upstream of the Y strainers was returned to service following maintenance.

Marine growth inside the rotating strainer became dislodged when the

strainer was

returned to service clogging

the Y-type

strainers.

Corrective action included cleaning of the Y-type strainers and returning

the chillers to service. Also, the Y-type strainers are now cleaned on a

bi-weekly basis and the maintenance procedure for the rotating strainer

was changed to require cleaning of the Y-type strainers prior to returning

the rotating strainer baci to service.

This item is closed.

(Closed)

LER 280/87-06, Control/Relay Room Chiller Inoperable Due to

Chiller Service Water Pump Trip.

The issue involved operator observation

that the service water pump for B, the control/relay room chiller, had

tripped rendering the chiller inoperable. Corrective action included the

operator reseting the thermal overload on the pump motor and restarting

the pump.

The exact cause of the pump trip could not be determined;

however, it was suspected that the thermal overload device at the motor

control center activated, tripping the pump.

The licensee considers that

this event was a random event due to no abnormal condition being

discovered during checkout of the motor control center.

This item is

closed.

(Closed)

LER 280/87-07, Control/Relay Room Chiller Inoperable Due to

Insufficient Service Water Flow.

The issue involved a trip of two of the

control room chillers.

The trips were due to insufficient service water

flow.

Corrective action included manual adjustment of the service water

discharge flow in addition to repairing a seal leak on one of the service

water

pumps.

An

engineering

evaluation

of

the

service

water

14

system has been conducted.

The inspector reviewed the engineering

conclusions and considers that the licensee is taking appropriate

long-term actions (servic.e water system upgrade) to eliminate this

condition.

This item is closed.

(Closed) LER 280/87-08, Control/Relay Room Chiller Tripped Due to Valve

Positioning Error.

The issue involved improper operation (repositioning)

of the condenser service water discharge valve causing the chiller to trip

on high condenser discharge pressure. The cause of the valve positioning

error was using the same operator (valve handle) to position several

valves.

Corrective action included installing of permanent valve handles

to each valve requiring operation. The inspector verified that corrective

action was accomplished. This item is identified as LIV 280/87-21-05 for

failure to provide adequate control of a safety-related system.

This LER

is closed.

11.

10 CFR Part 21 Inspections (36100)

(Closed) 280/P2186-0l, Power Supply Failures of GE SLV Relays. The issue

involved failure of the subject power supply due to potential material

problem of the core in the power supply transformer.

Corrective action

taken by the licensee included replacement of the subject relays with

newly designed versions of the relay.

The new relays were installed by

design change packages 86-01 and 86-02.

This action was completed in

1986.

This .item is closed.

(Closed) 280/P2186-04, Contromatics Actuators on Dampers Furnished by

Pacific Air Products (PAPCO) may have Jackscrew/Handwheel Installations

which are Improperly used for Routine Cycling.

The issue involved regular

cycling of the dampers by some plants using the jackscrew/handwheel which

was designed only for emergency manual operation of the component.

The

issue was identified to various utilities by the vendor along with a

listing of replacement parts available to allow for continued manual

cycling of the dampers.

The licensee reviewed this condition and

determined that dampers purchased from PAPCO that are air operated do not

have handwheels for manual operation. The licensee is also in the process

of determining whether any .PAPCO air-operated dampers

have

been

subsequently modified to include handwheels, and if so., whether proper

components were used.

Based on the licensee's action in this area, the

inspector considers that this item is being properly resolved. This item

is closed.

12.

Followup on Temporary Instruction 2500/19 (25019)

(Closed) Temporary Instruction 280; 281/T2500/19, Inspection of Licensee's

Actions Taken to Implement Unresolved Issue A-26: Reactor Vessel Pressure

Transient Protection for Pressurized Water Reactors .

During this inspection period, the inspector reviewed the licensee's

installed systems

and

program

for mitigation

of

low-temperature

overpressure transients in accordance with commitments.

This review

15

included verification of the design,

administrative controls and

procedures, training, equipment modification, and surveillance programs

implemented due to the subject concern.

The licensee completed all

r~quired commitments in 1985 and considers that the isiue is closed.

The

inspector reviewed each area as described below and concurs with the

licensee's assessment.

Design

The

inspector

reviewed

documentation

including

the

Technical

Specifications which requires that the overpressure protection system be

operable and in operation prior to the reactor coolant system temperature

decreasing below 351 degrees F if a bubble does not exist in the

pressurizer or if the RCS is not vented through an open power operated

relief valve.

Also, all but one charging pump must be demonstrated

inoperable every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

A review was also conducted of applicable

design drawings to verify that the two trains of overpressure protection

are independent and a single failure in one train does not disable the

other train.

Finally, documentation was reviewed to verify that the

pressure chosen for systems actuation was conservative to ensure that

10 CFR 50, Appendix G limits were not exceeded. No discrepancies were

identified.

Administrative Controls and Procedures

The inspector reviewed. administrative and operational procedures and

verified that:*

Controls are in place to minimize time in a water solid condition.

Controls are in place to minimize temperature differentials between

the steam generators and reactor vessel while solid and prior to

unisolating a reactor coolant loop or starting of a reactor coolant

pump.

Controls are in place to limit the number of operable charging pumps

during the time that the reactor coolant system is less than 351

degrees F.

Also, the inspector verified that the installed system is in accordance

with license requirements and that procedures for manual alignment of the

system when required, and removal of the system when not required, are in

place and being used during each startup and shutdown.

No descrepancies

were identified.

Training and Equipment Modifications

The inspector held discussions with the operations superintendent and

verified that all operators have received training in RCS low-temperature

overpressure events and that procedures require proper alignment of the

16

mitigation system and removal from service of unneeded pressure sources.

Also, modifications that are made to the overpressure mitigation systems

receive proper design reviews and are tested after installation to ensure

operability in accordance with requirements.

The inspector also verified

that alarms are installed in the control room to warn the operators of

pressure transients which could challenge the overpressure mitigation

systems.

Also, backup air bottle supplies are required to be pressurized

to 1000 psig prior to the system being declared operable.

No

discrepancies were identified.

Surveillance

The inspector reviewed the appropriate surveillance instructions and

determined that system operability is verified prior to entering a

condition requiring the systems. After performing corrective maintenance

on the system, and stroke times on the PORVs are verified using the backup

air bottle supplies.

No discrepancies were identified.

Based on the preceding review, the inspector considers that all action

necessary to clos~ this item has been accomplished.

13.

Inspection Report 280; 281/87-11 Findings

Inspection Report 280; 281/87-11 documented three potential enforcement

findings.

These findings were discuised during the inspection and in a

conference call between Region II, Vendor Inspection Branch, NRR, and the

licensee on August 31, 1987.

The findings are discussed in detail in

IR 280; 281/87-11 and constitute a violation (280; 281/87-21-06) of NRC

requirements.

ENCLOSURE 3

PROPOSED MEETING AGENDA

Virginia Electric and Power Co~pany Meeting with NRC

September 24, 1987

I. Opening Remarks

II. Issues of Concern

A.

Failure to perform a 10 CFR 50.59 safety evaluation

prior to deleting the turbine valve freedom test

described in the Final Safety Analysis Report.

1.

Discuss the VEPCO review process prior to

deviating from commitments described in the

FSAR.

Discuss the review process for deleting the

turbine valve freedom test and reason for

deleting the test.

3.

Does VEPCO believe that deleting this test

increases the probability of occurrence of

a turbine missile.

4.

Was obtaining prior Commission approval for

deleting this test considered?

5.

What actions will be taken by VEPCO concerning

performance of this test and performing

10 CFR 50.59 evaluations in general?

B.

Failure to perform a surveillance test required by

Technical Specifications 4.6.A.l.b and continued

operation without performing the test.

1.

Discuss the circumstances resulting in the

failure to perform the surveillance procedures.

2.

Discuss actions taken once the NRC pointed

out, on June 29, 1987, that the surveillance

had not been performed including actions taken

to ensure proper diesel generator operation .

NRC

VEPCO

Enclosure 3

3.

4.

5.

6.

2

Discuss operability as defined in the Technical

Specifications and how it relates to operability

of the diesels considering this surveillance

had not been done.

Why were the diesels not declared

inoperable?

Does VEPCO consider Surry Power Station to be in

violation of the Technical Specifications with

regard to this missed surveillance.

Discuss VEPCOs justification for continuing to

operate with a Technical Specification required

surveillance not performed and without seeking

any temporary waiver of the requirement.

Discuss the effect of a failure of the components

required to be tested by this surveillance.

III. Closing Remarks

.

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I

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NRC