ML18150A198

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Insp Repts 50-280/87-06 & 50-281/87-06 on 870323-27 & 0406- 10.Violations Noted:Maint Personnel Failed to Follow Procedures
ML18150A198
Person / Time
Site: Surry  
Issue date: 06/12/1987
From: Belisle G, Russell Gibbs, Moore L, Runyan M, Wright R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18150A195 List:
References
50-280-87-06, 50-280-87-6, 50-281-87-06, 50-281-87-6, NUDOCS 8706300886
Download: ML18150A198 (30)


See also: IR 05000280/1987006

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/87-06 and 50-281/87-06

Licensee:

Virginia Electric and Power Company

Richmond, VA

23261

Docket Nos.:

50-280 and 50-281

Liceri~; Nos.: DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

March 23-27 and April 6-10, 1987

Inspectors:

.~v~At:\\.-:-

M. * F. Runyan

{u14 .~,ft

R.

'. G"bbs

rd. t2 Wc?/'1f._

. Moore

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Assurance Department.

It is the total sum of all efforts to achieve

quality results.

This was a performance-based rather than compliance-based inspection.

Instead of verifying compliance to programmatic requirements, the prin-

cipal effort was to determine whether the results that the Quality

Assurance program were designed to accomplish were actually achieved.

The inspector reviewed trending indicators tracked by various groups and

any other information deemed pertinent to the overall evaluation of

quality performance.

In addition, a detailed review of ~ocumentation and

observation of activities in progress was conducted where applicable.

The inspection effort was divided into the following areas:

Operations and Surveillance

Design Control

Maintenance and Procurement

Quality Assurance Department

Each area is addressed separately in this report.

Included in this

assessment is an evaluation of licensee actions to correct situations

where performance has not met stated goa 1 s or where trends have been

adverse.

a.

Opera ti ans and Survei 11 ance

Quality assurance assessment of the operations functional area was

based on plant performance as reflected by management trending

indicators, improvement in previous SALP ratings, and effectiveness

of plant problem identification and correction processes.

The

following operations related management indicators were reviewed:

Forced outage rate

Reactor trips

Safety system actuation

Emergency generators (starts, failures to start)

Indicator trends were identified based on 1986 li~ensee performance

relative to previous performance in 1985.

Forced outage rate

reflects the inability of a unit to-operate when required for service

due to forced outages, thereby indicating the effectiveness of the

licensee to identify and correct problems at a; stage before major

corrective actions are mandated.

The industry average for 1986 was

projected to be 17.4 percent.

Surry Unit 1 was at less than 5

percent forced outage and Unit 2 at less than 15 percent.

A major

factor contributing to Unit 2 outage was the feed system piping

rupture which occurred late in* 1986.

With the exception of the

Unit 2 pipe rupture outage, the 1985 and 1986 forced outages for

Surry were approximately constant, although the industry average

increased by 5.5 percent.

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The unplanned reactor trips (while critical) indicator provides a

measure of the effectiveness of licensee training programs,* opera-

ti on s and maintenance procedures, and corrective action programs.

The annual goal established by the licensee for 1986 was 2 trips per

unit and the industry average was 4.3 trips per unit.

Unit 1 and

Unit 2 experienced two and three trips respectively in 1986, as

compared to seven and one trips for 1985. It was noted that the goal

for 1985 was three trips per unit which reflected the licensee's

effort to improve operations by attempting to achieve increasingly

ambitious goals.

Unplanned safety system actuations is also a broad scope indicator of

plant performance.

This indicator identifies unplanned actuation of

High Head Safety Injection, Low Head Safety Injection, and Cold Leg

Accumulator discharge which occurs when an actuation setpoi nt is

reached or a spurious or inadvertent actuation signal is generated.

This indicator also includes the start and load of an emergency

diesel due to an actual degraded bus voltage.

The licensee goal was

zero actuations per unit and the industry 1986 average was 1.3

actuations per unit. The licensee did not meet the established goals

in this area, nor the industry* average.

Unit 1 received three

actuations and Unit 2 received one actuation.

The actuations of

Unit 1 were caused by inadequate design change procedures (LERs 86-

014 and 86-018) and by maintenance personnel error (LER 86-017). The

Unit 2 actuation was caused by equipment failure due to improper

installation of a component (LER 87-001).

Safety system actuations*

were not trended by licensee management in 1985.

Emergency generator reliability for 1986 was trended by management.

Only one start-failure occurred of approximately 78 start-demands

made on the diesels. This indicator includes start-only demands and

start-and-load demands whether by automatic or manual initiation.

With the exception of safety-system actuations which were not fully

attributable to the operations functional area, the management

trending parameters indicate good performance by the licensee.

Operations performance trends can also be identified in the licensee

Quality Assurance Executive Summary and the previous SALP ratings.

In 1986, the licensee QA findings in operations-related areas such

as; procedures not followed, inadequate procedures, and personnel

errors, have shown a decrease from the first to fourth quarters. The

executive summary additionally identified the major area for con-

tinued management attention as inadequate procedures.

The SALP

rating in this area improved from category 2 to category 1 indicating

that management attention and involvement was aggressive and oriented

toward nuclear safety .

Discussions with operations management and review of activities in

this area demonstrated various factors and programs contributing to

improved

operations performance.

The basic factors for this

improvement were procedure upgrades, training, and

management

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attention in the plant.

Procedure rev1s1ons were performed by

personne 1 who utilize the procegur,es and are familiar with the

evolution and associated systemi.

A full time position was

established to perform the procedure review function.

The

QA

Executive

Summary

for

1986

reported that

adverse

findings

identified by the licensee's QA Department which related to

inadequate procedures, decreased from 20 in 1985 to 13 in 1986. The

executive summary highlights this area for .continued elevated

management

attention

in

1987.

Training,

both licensed and

non-licensed, appeared to be a contributing factor to effective

operations

performance.

The

training program

received

INPO

accreditation in November 1985. Maintenance personnel received basic

systems training which provided some awareness of plant operating

conditions and some degree of knowledge as to the impact of mainte-

nance activities on plant operations. Operations events occurring as

a result of operations and maintenance personnel errors have

decreased from 1985 to 1986.

For example, the number of licensee QA

findings attributable to personnel error has decreased from six to

two for these years, respectively.

Management attention in the plant appeared to be a positive contri-

butor to plant performance. Management focused attention directly by

management plant tours or indirectly through a QA inspector-at-large.

The NRC inspector reviewed the QA IOD program and accompanied the

licensee inspector on a plant tour.

The IOD surveillance consisted

of direct observation of activities, discussions with plant

personne 1, review of facility records to obtain information con-

cerning plant status, and general overview of ongoing activities in

the plant.

A checklist was utilized and a trending system had been

developed to identify recurring problems.

This program provided a

useful tool in identifying potential problems in the plant and

reinforced personne 1 adherence to admi ni strati ve contro 1 s during

plant activities. Additional contributors to operational performance

was effective root cause analysis within the post trip review process

and HPES actions such as clear labeling of equipment and systems with

respect to train and unit identification.

Several factors have

contributed

to

the

improvement

and

quality

of

operational

performance, the broad scope of which was to establish a heightened

awareness and sensitivity of all plant personnel on the impact of

their individual activities on plant performance.

Administrative controls and performance of TS surveillance activities

provide verification of the reliability of safety-related systems

and components.

Based on reviews of periodic test procedures,

documentation of previous tests, and observation of test perfor-

mances, the licensee surveillance program appeared adequate in

providing this verification.

The inspector reviewed the following

periodic test procedures to determine if procedures met the intent of

the associated TS requirements, were current, and had received the

required periodic review:

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2-PT-2.8

2-PT-18. 7

2-PT-2.5

2...;PT-17.2

2-PT-15.18

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Turbine First Stage Pressure, November 4, 1986

Charging Pump Operability and Performance Test,

February 11, 1986

Steam Generator Level, August 21, 1986

Containment Spray Inside Recirculation Pumps,

January 23, 1986

Motor Ori ven Auxiliary Feed Pump February 18,

1987

These procedures appeared to contain adequate detail and acceptance

criteria to meet the requirements of the associated TS.

No

deficiencies were identified. Test documentation for the previous 13

months was reviewed for completeness, timeliness, deviations, review

cycle, and retrievability.

The following periodic tests were

reviewed:

2-PT-2.5

2-PT-17.2

1-PT-17.1

1-PT-17.3

Steam Generator Level

Containment Inside Recirculation Spray Pumps

Containment Spray System

Containment Outside Recirculation Spray Pumps

All tests were adequately documented and performed in accordance with

specified periods of the surveillance test schedule.

Deviations

associated with specific periodic test performances appeared to be

adequately assessed, reviewed, and documented.

The inspector observed performance of a Steam Generator Level .

Periodic Test, 2-PT-2.5, and a Charging

Pump Operability and

Performance Test, 2-PT-18.7.

The- Shift Supervisor was notified prior

to initiation of test activity and communication was maintained with

the control room throughout the test. The tests were performed in a

professional manner and the procedural

sequence was* followed.

Personnel were knowledgeable of *the procedure and systems/equipment

associated with the test. At the point of a procedural deviation,

the test was stopped and a deviation request was processed as

required by the periodic test administrative procedure. The test was

then completed with the deviation documented and attached to the data

package.

The inspector's review of surveillances encompassed

procedure review, scheduling, and performance.

No adverse find1ngs

were identified, which indicates that management attention in this

area has been effective.

The inspector noted the management initiative to verify a safety-

related system's functional operability.

The licensee performed a

multi~disciplined review/inspection of the Auxiliary Feedwater

System. This SSFI was based on a similar NRC inspection performed at

the Turkey Point Nuclear Station. The inspection was completed late

in 1986 and the findings were entered into the commitment tracking

system.

Corrective action responses from responsible departments

were incomplete at the time of this QA assessment inspection.

The

licensee SSFI findings were generally significant, identifying weak

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areas with respect to design, maintenance, and operation of the

Auxiliary Feedwater System although the system was determined capable

of fulfilling its design function.

Providing the identified findings

are conscientiously- tracked and resolved, the licensee SSFI repre-

sents a* significant contribution from management -attention and

resources towards safety-related system operational confidence.

Based on these reviews, performance in the operations and surveil-

lance areas was assessed as above average.

b.

Design Control and Engineering

The licensee 1 s quality assurance effectiveness in the area of design

control and engineering was assessed through an overview and analysis

of information reflecting recent performance in this area, and an

in-depth review of one recent design change. Other sampling reviews*

were conducted to supplement this inspection effort.

E&C is designated the design authority for the licensee.

E&C is a

corporate department with a percentage of personnel located on site~

led by the Site Engineering Officer. A small portion of engineering

is performed on site; _a greater percentage is accomplished at the

corporate offices.

The licensee also frequently employs architect/

engineers and consul tan ts that are contracted on an ongoing or

j~b-specific basis.

The hired design organizations are responsible

for implementing the design control program as delineated in the

licensee 1s procedures.

The NOD has overall responsibility for the operational and safety ,

elem~nts of the design control program through review of design

outputs to ensure that plant safety and operability are not adversely

affected.

NOD 1 s site-based Design Control Engineer coordinates this

effort.

The. ultimate indicator of the performance achieved by a design

control organization is the frequency and severity of adverse plant

events which are caused by design errors. The inspector reviewed all

plant DRs and LERs since January 1, 1986,. for which the licensee 1 s

analysis concluded that design problems were the root cause:

The

following LERs fell into this classification:

1-86-07; the failure of bolting material in valve flanges was

caused by stress corrosion cracking.

The -bolting material was

installed as part of a valve bolting material design change

issued in 1979.

1-86-11; involving inoperable high-range radiation monitors .

1-86-32; a loss of service water was caused by lost pump suction

due to air in the system. The newly-installed alternate supply

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p1p1ng design did not include provisions for venting the line

prior to placing it in service.

  • 1~86-36; missed testing requirements on containment recircula-

tion spray heat exchangers after pressure retaining rubber

gaskets were installed without provision to perform Type B

containment testing.

2-86-14; inside and outside containment sump trip valves had

excessive leakage due to erosion of globe type trip valves.

They were replaced by ball type valves which should prove to be

an improved design.

1-87-01; -PORVs were declared inoperable due to excessive stroke

times caused by undersized air supply lines to the valve

operators.

The air lines will

be replaced with larger

components.

In particular, LERs 1-86-07, 1-86-32, and 1-86-36 reflect avoidable

design change errors. The other LERs, with the exception of 1-86-11,

reflect problems associated with the original plant design.

The

bolting

material

problems described in

LER 1-86-07

suggests

inadequate material specification for the 1979

design change

requiring stud rep 1 acement in borated water systems.

LERs 1-86-32

and 1-86-36 were caused by a design change failure to anticipate

venting and testing requirements, respectively.

Of these two, only

LER 1-86-32 involved a recent design error.

For each LER, corrective

action appeared adequate. The design errors identified by these LERs

were considered neither numerous nor significant enough to suggest a

programmatic breakdown, and mostly pointed to inadequacies in the

original design or design changes incorporated more than five years

ago.

This information supports a conclusion made later in this

section that the design control program has improved since a period

of poor performance several years ago.

The following station DRs, for which design was designated as the

primary cause, were reviewed:

1-86-053

1-86-077*

1-86-083*

1-86-131

1-86-190*

1-86-328*

1-86-381*

1-86-559

1-86-586

1-87-012

1-87-074

1-87-135

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2-86-075*

2-86-259

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This sample involved approximately 60 percent of the DRs initiated

since January 1, 1987, for which design problems were determ,ned to

be the major cause.

The inspector judged the DRs denoted with an

asterisk to involve avoidable design problems.

Some of these DRs

were translated into the LERs discussed previously.

Most of the

others were mi nor in nature, such as inadequate lighting or the

retention of redundant controls.

The DR re*vi ew did not reveal any

major design control problems.

Another performance indicator used during this inspection was the

number and nature of field changes issued against a selected sample

of completed design change packages.

This effort provides informa-

tion concerning the completeness, precision, and attention-to-detail

afforded the original design effort. Although field changes are a

continuation of the design control process, excessive reliance on

them to validate the design effort brings the design organization one

step closer to actual installed errors. Excessive significant field

changes may also suggest the presence of other design errors which

are not recognizable in the field.

Field changes to the following

design change packages were reviewed:

84-34 (Unit 1) Main Steam Safety Valve Position Indication

84-40 (Unit 1) Pressurizer Instrumentation

84-58 (Unit 1) Boric Acid Transfer Piping Replacement

85-29 (Unit 1) Safety Injection System Leakage Monitoring

86-02 (Unit 2) Emergency Bus Undervoltage Relay Replacement

86-05 (Unit 1) PORV Modifications

86-06 (Unit 2) PORV Modifications

A total of 87 field changes were issued with these design packages,

an average of about 11 field changes per package.

The inspector

estimated that 54 of the 87 field changes could have been avoided

with increased management attention to the original design package.

These 54 avoidable field changes were classified in the following

categories:

Inconsistent with another field change

1

Incomplete materials list

5

No tagging instructions

3

Materials not available

3

Drawings incorrect

10

Inadequate modification procedures

12

Scope of DCP too limited

2

Testing matrix not complete

3

Configuration control problems - interference

6

Need support modification

4

Improper QC requirements

3

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Incorrect sign-off responsibility

Incorrect component designation

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The major problems appeared to be drawing errors and inadequate modi-

fication procedures.

Configuration control

problems were also

prevalent and could be indicative of ineffective or incomplete

pre-design system walkdowns.

However, taken as a whole, this field

change analysis did not reflect a design change process programmatic

breakdown; it merely suggested some minor problem areas.

The design change process management control effectiveness is

reflected in the status of back 1 ogged design changes and drawing

updates.

The design modification status is maintained in a five-year

plan that is issued annually.

The inspector reviewed the five-year

plan issued March 5, 1987, and concluded that satisfactory control is

being maintained on the completion of proposed design changes in

accordance with well-conceived priorities. For each design change a

numerical priority is established and dollar amounts are apportioned

for each of the next five years. There was no evidence that design

changes of safety concern were being unduly delayed.

The drawing update system has been upgraded recently and has practi-

cally eliminated previous drawing backlog problems.

Following a

design change package completion, certain drawings must be completed

within 15 or 90 days depending on their safety status. In 1986, out*

of 1081 committed drawings, 1058 met the applicable 15 or 90-day

requirement.

This effort exhibits on drawing update positive control

and commendable management effectiveness.

Closely related to formal design changes are temporary design changes

or temporary modifications, including jumpers.

The inspector

reviewed approximately 90 percent of the 44 outstanding temporary

modifications from a technical and administrative perspective.

All

technical issues were resolved, but some administrative problems were

noted.

In two cases (T~s 2-87-33, 2-87-29) the required engineering

reviews were not performed.

In two other cases (T_Ms 2"'.'-87-25,

2-87-29), the safety evaluation applicability was not assessed.- A

violation was not issued because the above examples did not involve a

compromise in safety, but these examples do point to a lack of

attention to detail. Other problems with the temporary modification

system were i dent ifi ed in a recent QA audit, S86-0l, Operations

Administration, issued February 12, 1987.

The findings of this audit

included the following:

SUADM-0-11, Function Bypass and Temporary Modification Control,

does not provide control_s for temporary modifications installed

for greater than three months.

As a result, required EWRs have

not been written.

SUADM-0-11 makes conflicting statements as to the review dead-

lines for SNSOC.

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The response to the findings included the assurance that SUADM-0-11

would be revised to address the.?e-issues.

The total number of

outstanding temporary modifications has trended downward from about

80 in the middle of 1986 to 44 currently.

In order to assess E&C's ability to identify and correct their own

problems, the inspector reviewed recent CTRs, the primary problem

reporting mechanism for design and modifications. ~CTRs are often a

precursor to design package field changes, an EWR, or new design

change. Their scope ranges from questions to flagrant discrepancies.

The CTRs tracked at the site are assigned to a single responsible

individual with a specific due date.* The inspector reviewed approx-

imately 200 CTRs issued since November 11, 1986.

The oldest out-

standing CTR was issued March 20, 1987, and only about 20 CTRs were

st i 11 open.

Corrective action documentation appeared adequate for

the problems identified.

Overall, the CTR system appears to be an

effective method to identify and correct problems within E&C.

The inspector reviewed ER&SA reports for the following design

changes:

86-06-2

85-30-2

86-12-2

85-11-2

86-01-1

PORV Modifications

Safety Injection Leakage Monitoring

Snubber Leak Before Break Modification

Inadequate Core Cooling System Upgrade

Emergency Bus Undervoltage Relay Replacement

The ER&SA reports address the following items:

statement of problem,

identification of quality classification, proposed resolution, fire

hazards, seismic analysis, EQ concerns, ALARA, NRC concerns, impact

on other design changes, electrical system analysis, human factors

review, inservice inspection, security issues, setpoint review, TS

review, FSAR review, design basis document review, USQD, and safety

and operational implications. This formalized checklist approach to

each design change appears effective in ensuring that major

considerations will not be overlooked.

In each case, the report

appeared well-prepared and well-conceived.

Some of the USQD evalua-

tions, required by 10 CFR 50.59, were perhaps somewhat brief in

explanations of certain conclusions.

USQD evaluations have been a

continuing concern for the licensee and significant progress has been

made over the last several years, based on conversations with the

Supervisor, IDER group (which functions as an NSRB), and comparison

between the review referenced above and the review that was performed

and is documented by NRC Inspection Report Nos. 50-280, 281/86-19.

Nevertheless, the IDER group recognizes that further improvement and

standardization is needed for safety evaluations.

A task team is

forming with the goals of revising the NOD standard by the end of

1987, and developing a company policy on 10 CFR 50.59 evaluations.

This effort, coupled with the observed improving trend, should

resolve this problem area.

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Design Change 85-21-1 documented where plant drawings and the FSAR

were updated to reflect modifications prescribed in design change 73-106, despite the fact that the work was not actually performed.

Therefore, for 13 years the p 1 ant drawings and FSAR showed check

valves, trip valves, and relief valves in CCW .piping that were not

installed.

This situation did point to a potentially serious

configuration control problem.

The licensee had accomplished several

detailed critical system walkdowns in the early .J980s but the CCW *

system was not included.

The problem was not found until a plant

survey identified it in 1985. *Apparently; this unusual scenario was

an isolated incident involving an

unauthorized drawing change

performed during the construction phase, or a mixing of as-designed

with as-built drawings.

There is no evidence that a widespread

configuration control problem exists since any similar occurrences

would have been corrected in the previously mentioned system

walkdowns or plant surveys.

The

inspector

reviewed "Report on

Safety System

Functional

Inspection, Auxiliary Feedwater System, Surry Power Station," dated

November 6, 1986, for issues pertinent to the design control area.

Many programmatic and implementation problems ~ere* discovered from

design changes to the Auxiliary Feedwater System.

Most of the

significant design control problems occurred before 1981 and involved

documentation problems, missing calculations and analyses,* missing

justification for waivers, inadequate post-modification testing, etc.

This review and the current inspection would suggest that the

licensee's design control program experienced .significant problems

around 1981 and before, but since that time, a decided improvement

trend has occurred.

Corrective action on the Auxiliary Feedwater

inspection is still pending and is being tracked on a commitment

matrix which the inspector reviewed.

The second phase of this inspection involved an in-depth review of

one recent design change.

This small-sample approach was chosen to

evaluate each design change process element to a greater depth as

well as to examine continuity between the design control program and

other.related programs (such as special processes and testing).

The inspector reviewed DC-85-30-2, entitled "Safety Injection Leakage

Monitoring/Surry, Unit 2. 11

This design change, installed during the

Fall 1986 refueling outage, entailed the installation of 3/4 inch

leakage monitoring tubing between the two check valves in the six

inch SI piping leading to the RC system cold leg.

This tubing was

installed on each of the three reactor coolant loops of Unit 2.

The

design change was initiated to simplify leakage .testing of the SI

check valves and to reduce radiation exposure of personnel, who were

previously required to disassemble the second check valve to leak

test the first check valve.

The final design specified a 3/4 inch stainless steel pipe connected

by sockolet to the six inch SI pipe.

A 3/4 inch shutoff valve was

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installed close to the six inch header. After the shutoff valve, 3/4

inch tubing was run to the cubicle within containment nearest the RC

pump, and down vertically to elevation of one foot.

At this

location, two 3/4 inch drain valves were installed in series.

To establish the DC's conformity to design base documents, the

inspector reviewed documents referenced in the following sections of

the Surry Units 1 and 2 Design Base Document's, .dated August 15, 1984:

Sl Structural-General

S4

Earthquake

EM3

Pipe Stress Analysis

EMS

Pi~e and Duct Support Analysis

MSl

Applicability of System Description to Design Criteria

MS8

Leak Testing Requirements

MS9

Vents, Drains, and Test Connections

MSlO

General Design Criteria

In particular, the following sections in the FSAR and TS were

reviewed:

FSAR

4.4

5.5

6.2

15.2.1

15.2.4

15.5.1.4

TS 3.1.*c.7.a

4.2

4.3

Tests and Inspections

Containment Tests and Inspections

Safety Injection System

Structural Design Criteria

Seismic Design

Containment Structures - Dynamic Analysis

Leakage Specifications

Reactor Coolant Computer Inspection

Reactor Coolant System Leak Tests

The base document reviews confirmed that the DCP was consistent in

intent and structure with the design bases and as-configured status

of the plant.

The only required FSAR change was to Figure 6.2-4,

where the safety injection leakage monitoring valves will be shown.

An FSAR Change Notification Form was initiated and attached to the

DCP to accomplish this rgvision.

The inspector studied various aspects of the design input and con-

curred in each case with the licensee analysis.

The quality

classification of the entire DCP was Category I, Quality Group A,

seismic.

The determination was made that materials for the modifi-

cation did not fall in the category of 10 CFR 50.49(b)(2),

environmental qualification; therefore, .electrical systems were not

affected. Precautions included in the design input for fire hazard

consideration and ALARA were included in the final design controlling

procedure (PI-U2):

This procedure appeared to be comprehensive and

complete, addressing all necessary considerations.

Of particular

note was the sign..:.off requirements for a wide spectrum of plant

personnel including HP, AN!, Loss Prevention Engineer, Station Shift

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Supervisor, Station Operations, QC, NOE, Advisory Operations, and

Station Engineering.

This multidiscipline review responsibility

offers a good checks and balances system -to reduce errors.

The

controlled copy of the completed design control procedure was

reviewed and verified to be a complete modification process record.

The procedure was independently reviewed by Engineering to ensure

that each step had been satisfactorily completed.

The

regulatory requirements for independent verification were

apparently met.

This included an overa 11 independent review of the

DCP and independent verification of certain QC hold points in the

controlling procedure.

The

DCP

review included the Reviewing

Engineer, Lead Engineer, Design Control Engineer (from NOD), and

SNSOC.

The 10 CFR 50.59 safety evaluation concluded than an unreviewed

safety question did not* exist.

This was based primarily on the

assertion that if the 3/4 inch piping were to fail during unit

operation, an insignificant amount of leakage (within the FSAR

analysis) would result. Since the leakage monitoring line would not

be involved in normal system operations, the design change would not

affect the delivery rate of water to the RC system.

Although the

safety evaluation appeared adequate and justifiable, it was brief and

probably could have expounded more on the particular consequences of

a line break on the 3/4 inch piping.

The inspector performed an in depth review of the eight field changes

made to the DCP.

The field changes generally reflected administra-

tive errors such as incorrect sign-off responsibilities, drawing

errors, or design controlling procedure errors.

Taken as a whole,

this small group of field changes reflected favorably on the

attention to detail and precision afforded the original DCP.

The

inspector verified that the provisions of each field change were

accurately translated to the design controlling procedure or

applicable drawings.

Further, the inspector performed a spot check

of plant drawings identified as requiring revision and verified that

in each case the drawings were appropriately revised.

The inspector reviewed the materials list generated by E&C to procure

material for DC-85-30-2. The materials ordered appeared to meet the

specifications of NUS-20, Class 1502, for the stainless steel piping

and shutoff valve, and NUS-9115, Class I-C~N9, for the downstream

tubing, as specified in the design input. All vendors specified were

included on the safety-related vendors list with.the exception of the

anchor bolts manufacturer.

This procurement was justified by a CQE

written by E&C.

The inspector reviewed a sample of purchase orders,

receipt inspection reports, certificates of compliance, discrepant

shipment reports, and maintenance trouble reports which were filed

with the DCP.

This documentation was consistent and supported the

materials list specifications. In particular, the original materials

list stated that all valves would be hydrostatically tested after

/


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16

receipt but was later revised to require the manufacturer to provide

certificates of conformance stating that the valves were tested to

specification MSS-SP-61.

Each valve was verified to have a certifi-

cate of conformance stating that testing to this specification was

performed.

The inspector reviewed weld testing requirements per ASME XI, Table

IWB-2500-1, and determined that the surface inspection performed was

the proper testing method.

Weld maps and inspection records were

consistent and complete.

The inspector also reviewed hydrostatic

test records for each of the three lines. A discrepancy was noted i*n

the testing for the 3/4 inch branch connection to the 6 inch SI line.

The re qui red test pressure was 2335 psi g but the . hydrostatic test

record for each of the three branch connections stated that the line

was pressurized to only 2235 psig.

The licensee was able to

demonstrate that the test was actually performed at the required

2335 psig.

The test was performed during PT-11, RC Pressure Test,

performance which established RC pressure at 2335 psig, 100 psig

above normal operating pressure. The charging pump was turned on to

perform the SI hydrostatic test. There is no pressure gauge in the

SI line so the operators had to verify flow, which implies that

pressure in the SI line had to be at least 2335 psig.

The licensee

stated that documentation would be added to the test package

explaining the error.

The jnspector verified that Periodic Test Procedure 2-PT-18.11, SI

Check Valve Leakage -

Primary Coolant System Pressure Isolation_

Valves, was revised to reflect the new method of leak testing the SI

check valves.

The overall assessment of the design control program and engineering.

is that QA effectiveness is above average. Clearly much improvement

has occurred in this area over the last several years.

Current

problems are mostly caused by lack of attention to detail as opposed

to generic or programmatic issues.

c.

Procurement Quality Assurance and Maintenance

( 1)

Procurement

Qua 1 i ty Assurance

The .Procurement Qua 1 i ty

Assurance area was inspected to eniure*that**the licensee is in

compliance with applicable NRC.requirements and licensee commit-

ments.

Additionally, the area was reviewed to determine if

adequate actions are being taken with ~endors to prevent defec-

tive material from being received on site *at Surry and North

Anna which minimizes the possibility of material being installed

in safety-related systems. The inspection included a review of:

The Virginia Power Safety-Related Vendors list, vendor audit

scheduling and schedule adherence, and a vendor audit and the

associated audit deficiency corrective action follow-up.

The

inspection also included a discussion of the use of site receipt

inspection deficiencies to influence the vendor evaluation

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17

process.

The inspector determined that the licensee was in

compliance

with

applicable

requirements and

commitments.

However, a program weakness was noted concerning the use of

receipt inspection data to influence the vendor selection and

control process. Neither the QA Engineering and Vendor Division

in Richmond nor the site QA organization have a system to

formally track vendor performance as a result of site receipt

inspections.

Data, such as an overall rejection rate for each

vendor, and details concerning the kinds of deficiencies being

encountered with each vendor, is not readily available.

Therefore, this data is not being utilized to accomp 1 i sh the

following actions which are considered to be an integral part of

an effective vendor evaluation program:

(a)

Receipt inspection data .is not used in establishing the

Virginia Power Safety-Related Vendors list.* The list is

established based on vendor audits which primarily deter-

mine if the vendor has an approved QA program meeting the

requirements of 10 CFR 50, Appendix B.

(b)

The data is not used to influence vendor audit scope or

in-process inspection by the licensee or co-ntract personnel

at the vendor's facility.

(c)

The data is not used to change purchase order requirements

to require specific vendor verification of acceptability of

attributes found to be previously deficient.

(d)

No action is taken to adjust site receipt inspection

requirements considering the vendor which is supplying the

materials.

(e)

No action is taken to formally advise vendors of rejects

and to request specific vendor corrective actions to

prevent recurrence of the deficiency.

The overall evaluation concluded that the licensee's vendor

evaluation program is average.

(2)

Maintenance - This QA assessment included a detailed review of

the maintenance area. This review was to determine maintenance

program status, review initiatives being taken to improve the

program, and determine the ability of the 1 i cen see to identify

their own problems and take adequate corrective action in

resolving those problems.

The inspection was conducted through

interviews with personnel, observation of a maintenance activity

in progress, and a review of completed maintenance work orders

and their associated maintenance procedures. The detailed scope

of this part of the assessment and conclusions reached are as

follows:

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(a)

Management Initiatives and Program Controls

Scheduling of mai ntenan*ce work by

the

WPTS

Computer

Planning System, although a relatively new system, *is

rapidly becoming a very va 1 uab 1 e management too 1 for

planning and control of maintenance.

The

system is

currently being used to generate a daily work p 1 an* (The

Plan of the Day), a ten day work schedule, and will also be

used

in

long

range maintenance and refueling outage

planning.

The*system has the capability of sorting an

entire maintenance work package in many different ways

which provides management practically any information they

may require concerning a particular package.

During the entrance meeting for this inspection, licensee

personnel gave a presentation to the inspection team which

included brief discussions of several management programs/

initiatives which are being undertaken to improve overall

performance.

The programs/i nit i at i ves which affect the

maintenance area were investigated in greater detail by the

inspector while on site.

One of these programs, Predictive

Analysis, is aimed at detecting and correcting component

failures before they actually occur.

The program consists

of three techniques/tests for arriving at the stated

purpose of the program:

Vibration analysis, oil analysis,

and motor operated valve testing (MOVATS).

Vibration

analysis is used on rotating equipment to predict bearing

failures,

component misalignments,

etc.

Oil

analysis

emp 1 oys the use of a private contractor to analyze oil

samples for foreign particulate matter.

The particulate

concentrations are tracked and trended to predict internal

component failures.

MOVATS is used to predict failures in

motor operated va 1 ves.

There is an addi ti ona 1 testing/

analysis technique to predict check valve failure.

The

licensee is just beginning to utilize this area of predic-

tive analysis.

The maintenance program at Surry now

consists of approximately 90 percent corrective maintenance

and 10 percent preventive maintenance.

The predictive

analysis program discussed above is aimed at changing this

ratio to 50/50 by the end of 1987:

Review of one of the licensee's primary trending indicators

in the maintenance area ( the tota 1 number of work orders

outstanding) concluded that little progress is being made

toward reducing the totals.

At the beginning of 1985,

there were approximately 5000 work orders outstanding.

During the middle of 1985 this

number

dropped

to

approximately 3000.

During 1986, this number stayed about

the same.

e

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19

Discussion of this area with the maintenance superintendent

led the inspector to the conclusion that a primary reason

for the lack of progress was the large amount of outage

time for both units in 1986.

(b)

Observation of Maintenance in Progress

During the assessment very 1 itt le safety related ma i nte- -

nance was being performed.

However, the inspector was able

to observe a periodic surveillance test and pump packing

adjustment on motor driven auxiliary feed pump 2-FW-P-3B.

This work was accomplished in accordance with site

procedure 2-PT-15.lB and work order number 050818.

The

test/work involved the monthly TS required checks of pump

flow, check of oil levels, oil strainer condition, oil

flow

to the bearings, temperature of the bearings,

recording of the bearing vibration analysis data, and

adjustment of pump packing.

One concern was noted during

the packing adjustment. The work order did not provide any

acceptance criteria for the packing leak rate.

Personnel

were performing the packing adjustment solely based on

their

past

experience.

Otherwise,

personne 1

were

knowledgeable of both the procedural requirements and the

equipment.

(c)

Review of Completed Maintenance Work Packages

The inspection included a detailed review of 12 completed

work order packages.

The rev; ew was conducted to verify

that maintenance of safety-related equipment is being

performed in accordance with technical requirements for the

equipment, and to assure that maintenance activities are

being properly completed and documented.

This review

determined that deficiencies exist in the licensee 1s

maintenance program.

Concerns were

raised

by

the

inspector in 11 out of the 12 work packages reviewed.

Fo 11 ow-up of these concerns with maintenance personnel

resulted in eight examples (Paragraphs 1-8) which were

collectively combined

to constitute a violation of

10 CFR 50, Appendix B, Criterion V, for failure to follow

procedure.

These items are identified as violation 280,

281/87-06-01.

1)

Work Order #45674, Containment Spray Pump Suet ion

Valve Mark #02-CS-MOV-200A,

Maintenance Procedure

  1. EMP-C-MCC-152

(Corrective

Maintenance

Procedure

for Replacement of Thermal

Overload Devices

in

Safety-Related Motor Control Centers, dated May 8,

e

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20

1986):

Paragraph 6. 3 of the maintenance procedure

required that three phase currents on the valve motor

be recorded while the valve was being cycled in the

open and in the closed direction and compared to the

full load current. Data on these measurements and the

full load current were recorded after maintenance.

Acceptance criteria in paragraph 6.3 stated that the

currents should not exceed the ful 1 1 oad current by

more than 15 percent.

The ful 1 1 oad current was

recorded as

2.1 amps;

consequently,

the maximum

current should not exceed 2.42 amps.

All three phase

currents in the open direction were recorded as

2.8 amps, which exceeded the acceptance criteria, yet

no

corrective action was

taken

concerning

the

out-of-tolerance readings.

2)

Work Order #33856, Safety Injection System Flange

Mark

  1. Ol-SI-FE-1940:

The

work

order

required

that the subject flange be disassembled, the orifice

in the flange reversed, and the flange reassembled.

This action was accomplished by maintenance personnel

without_ using the approved procedure for flange joint

make-up (MMP-C-G-201, Corrective Maintenance Procedure

for Flanged Joints in General, dated February 3, 1986).

This resulted in the bypassing of site requirements for

alignment of the flange and also the required torque

verification on the flange fasteners.

Additionally,

the flange fasteners were rep 1 aced by maintenance

personnel without authorization of the work order.

3)

Work Order #38498, Safety Injection Accumulator Drain

Valve Mark #Ol-SI-HCV-18528, Maintenance Procedure

MMP-C-G-001

(Corrective Maintenance Procedure for

valves

in

General,

dated

September 26,

1985):

Paragraph 5.5.1.8 of

the

maintenance

procedure

required that the valve be repacked using site Mainte-

nance Procedures MMP-C-G-156 ~r MMP-C-G-156.1 and that

the procedure used be attached to the work order.

This paragraph was marked

11N/N1

by

maintenance

personne 1 without authorization, the va 1 ve was not

repacked, and the applicable procedure was

not

attached to the work order.

4)

Work Order #38401, Charging Pump Reci rcul at ion Line

Isolation Valve Mark #02-CH-MOV-2373,

Maintenance

Procedure #CH-MOV-M/R (Mechani ca 1 Preventive Main-

tenance Procedure for Motor Control Centers, dated

February 28, 1985):

Page 1, Attachment 2, and para-

graph 5 .11 of the procedure* required maintenance

personnel to inspect the valve for packing 1 eakage.

The inspection noted the valve had packing leakage,

yet the

II leakage corrected 11 b 1 ock of the attachment

was annotated that the leakage was not corrected, and

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21

additionally paragraph 5.11 for adjustment of packing

if necessary was marked

11 N/A

11 *

5)

Work Order #45674, Containment Spray Pump Suction

Valve Mark #02-CS-MOV-200A,

Maintenance Procedure

  1. EMP-C-MCC-152 (Corrective Maintenance Procedure for

Replacement of Thermal Overload Devices in Safety-

Related Motor Control Centers, dated May 8, 1986):

6)

Paragraph

3.7 of the maintenance

procedure

in

part, required that the manufacturer, part number,

stock number, or purchase order number for the newly

installed thermal overload heaters be recorded on the

work order and in blanks provided below the paragraph.

This paragraph was initialed as being complete and the

data was not recorded as required.

Work Order #38498, Safety Injection Accumulator Drain

Va 1 ve Mark #Ol-SI-HCV-18528, Maintenance Procedure

MMP-C-G-001

(Corrective Maintenance Procedure for

Valves

in

General,

dated

September 26,

1985):

Paragraph 5.5.2 of the procedure required that

the torque wrench ca 1 i brat ion contra 1 number and

torque values to verify compliance with paragraph

5.5.1.12, be recorded on the Maintenance Inspection

Report, which is attachment ( 6) of the procedure.

This paragraph was initialed as being complete with

the data not having been recorded as required.

7)

Work Order #39354, Charging System Flow Control Valve

8)

Mark

  1. Ol-CH-FCV-1160,

Maintenance

Procedure

  1. MMP-C-G-001 (Corrective Maintenance Procedure for

Valves

in

general,

dated

September 26,

1985):

Paragraph 5.5.2 of the procedure required that

the torque wrench calibration control number and

torque values to verify compliance with paragraph

5.5.1.12, be recorded on the Maintenance Inspection

Report, which is attachment (6) of the procedure.

This paragraph was initialed as being complete with

the data not having been recorded as required.

Work Order 35553, Unit 1 Reactor Coolant Pump Mark

  1. Ol-RC-P-18,

Maintenance

Procedure

MMP-C-RC-009.1

(Corrective Maintenance Procedure for Reactor Coolant

Pump Sea 1 s, dated June 18, 1985):

Severa 1 paragraphs

in the procedure require the reading of dimensions.

Paragraph 4.6 requires that these readings be recorded

on

the Maintenance Inspection Report, which is

attachment (3) of the procedure.

Paragraph 4.6 was

initialed as being complete with the readings not

having been recorded as required.

9)

Severa 1 ex amp 1 es were noted where a procedura 1 step

  • should have obviously been marked

11 N/A1 1 , yet this

action was not accomplished:

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22

Examples:

a)

Work Order #47194, Mark #Ol-RH-HSS-22,

Maintenance Procedure #MMP-C-HSS-130,

Paragraphs 5.3 and 5.4

b)

Work Order #39354, Mark

  1. Ol-CH-FCV-1160, Maintenance Procedures
  1. MMP-C-G-156, Paragraph 7.2. and
  1. MMP-C-G-001, Paragraphs 5.5.1.6,

5.5.1.J and 5.5.3.

Of speci a 1 concern is the fact that a 11 of the above

completed work packages received a final review by the

maintenance foreman;

personnel

from

operations,

and

personnel from QA, yet none of these reviews were able to

detect and correct the deficiencies noted.

Six concerns, which originated out of the review of com-

pleted work packages, remained unresolved at the completion

of the assessment. These concerns were discussed in detail

with

licensee management at the exit meeting and

responsible licensee personnel were identified to obtain

resolution.

Prompt attention to these concerns during the

week of April 13, 1987, by 1 icensee personnel, the site

resident inspectors, and the regional inspector obtained

the following resolution to these concerns:

-

1)

Maintenance

procedures

require

the

cognizant

maintenance foreman to determine and record the

required torque values for various system- closure ,

fasteners. The inspector requested that the technical*

source for this information be provided for work

orders 38498, 47484 and 39354.

The source of these

requirements

was

determi~ed to

be

Maintenance

Procedures

MMP-C-G-201,

MMP.;.C-RH-015

and

MMP-C-G-001.2, respectively.

Investigation of this item determined that the

practice of requiring maintenance foremen to determine

torquing requirements by researching vendor manuals,

computer printouts and other maintenance procedures,

is very cumbersome and time consuming for the foremen.

The fact that the requirements are located in many

different references, while not resulting in incorrect

torquing for the three specific examples above, could -

result in the incorrect torque being applied.

Licensee management

should consider centralizing

torquing requirements into one procedure or requiring

maintenance engineering to provide these requirements

to the foremen, as an a 1 tern at i ve to the current

practice. This item is resolved.

  • ~ ..... , _\\ ..

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23

2)

The tradesman description of work performed on Work

Order 38401 i ndi ca_ted that he had overhauled the

Limitorque operator of valve Mark #02-CH-MOV-2373.

The work order referenced Maintenance Procedures

CM-MMP-C-MOV-178

and

CH-MDV-MR-PMS.

Procedure

CH-MDV-MR-PMS only authorized preventive maintenance

on the Li mi torque and the record copy of Procedure

CM-MMP-C-MOV-178 could not be located during the

inspection. Subsequent to the inspection the record

copy of Procedure* CM-MMP-C-MOV-178 which authorized

the work was found.

The resident inspector was

provided a copy of the completed procedure. This item

is resolved.

3)

Review of Work Order 38401 raised a concern over

whether the valve operator had been lubricated using

the correct environmentally qualified lubricant. The

note fo 11 owing paragraph 5. 9 of Procedure CH-MOV-

MR-PMS required the use of an incorrect lubricant, and

at the time the inspection was completed, the descrip-

tion of stock #0214701 (which was the lubricant used)

had not been provided to the inspector. Subsequent to

the

inspection the

record

copy

of

Procedure

CM-MMP-C-MOV-178 was found (see item #2 above).

Review of this procedure and information provided

concerning stock #0214701 determined that the correct

lubricant had been used.

Additionally, the error in

the note after* paragraph 5. 9 of Procedure CH-MOV-

MR-PMS has been corrected in the generic procedure for,

preventive maintenance of Limitorque operators.

Thi~

item is resolved.

4)

Review of Work Order 39354 indicated that the valve

packing had been replaced using Garlock packing in

lieu of the Crane packing re qui red by the vendor

drawing.

Subsequent discussion of this item with

maintenance personnel revea 1 ed that a 11 va 1 ves at

Surry are repacked using Garlock packing.

The

inspector ask to see the authorization for this

deviation.

An engineering evaluation in this area

which was performed due to this concern, indicates

that no credit was taken for packing in the original

specifications for maximum stem leakage requirements.

It further states that design stem

leakage is

contra 11 ed in most cases by stem back seats.

The

evaluation also discusses

the. design

operating

characteristics of the packing and the plant.operating

history utilizing this type of packing. Based on this

evaluation, this item is resolved.

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Review of the record copy of Work Order 35553 revealed

that the materiat-identification and control tags for

the RC pump sea 1 s- and runners which are used by the

site for material traceability, were missing from* the~

work order package.

Search of records did not produce

these tags.

However, subsequent discussion with site

personnel verified that the correct material was used.

Additionally, these component parts are not subject to

material mixing due to their size and unique configu-

ration.

This item is resolved.

During the review of Work Order 35553, a concern was

ra i sect over the 1 ubri cant and torquing requirements

for the RC pump seal closure fasteners on pump Mark

  1. 01-RC-P-lB.

The concern was that the fasteners had

been torqued to the same va 1 ues as shown on the

Westinghouse drawing utilizing a different lubricant

(Felpro N5000) in lieu of Neolube as shown on the

drawing.

Subsequent investigation determined that the

different lubricant was authorized by the licensee 1 s

response to I. E.Bulletin 82-02. As a result of the

inspector 1 s concern resolution to the issue of using

the same torque values with a different lubricant was

obtained via telecon

between

the licensee and

Westinghouse and was documented in Virginia Power

Maintenance Engineering memorandum of April 15, 1987.

This item is resolved.

This inspection noted deficiencies in the licensee 1s maintenance

program

concerning

adherence

to

procedures.

Addi ti ona 1

management attention is needed to correct this problem area.

The overall evaluation of the maintenance area is below average.

d.

Quality Assurance Department

The purpose of the inspection was to assess the effectiveness of the

Station Quality Assurance Department to prevent,

identify,

and

correct problems.

To

accomplish this,

the station 1s audit,

surveillance, inspection programs, nonconformance trending programs,

and associated reporting and overview activities were reviewed.

Interviews were conducted with responsible management personnel.

Strengths and weaknesses were identified in all areas. The overall

evaluation of the QA organization 1 s current effectiveness in these

areas was identified as average to good.

( 1) Auditing

The inspector reviewed the licensee 1 s audit schedule for 1986

and the proposed 1987 audit schedule.

In 1986, the SQAD

initiated, but did not complete, their required 17 scheduled

e

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25

Technical Specification audits.

As of January 15, 1987, four of

these audits were still in the administrative review cycle and

two were still in progress. Two of these audits have not been

issued to date. The average time taken to complete most of the

1986 scheduled audits appears excessive considering the audit

group size and experience level of the site auditors . .Excessive

time to complete audits may signify issues that may be hindering

the QA organization. These delays are not a .. good practice in*

that they promote the potential for loss of auditor independ-

ence.

The QA Manager* acknowledged thfs weakness and is placing

more emphasis on meeting schedules without a reduction in audit

quality.

In addition to performing- a cursory review of the scheduled TS

audits and the annual Operational QA Program Effectiveness audit

QA 86-03, a deta i 1 ed i ndepth review was performed on two

recently completed audits, one with findings (S86-08, Corrective

Action, issued October 10, 1986), and one without findings

(S87-03, Technical Specification Compliance, issued April 2,

1987).

These audits were found to be well planned, of suffi-

cient scope and depth to verify compliance with TS and the QA

program, and capable of determining effectiveness of the program

in the areas audited. Interview~ with the responsible auditors

and review. of audit documentation indicated sound auditing

principles were applied, findings identified a relatively

significant

problem

for

management

correction,

timely

appropriate corrective action was instituted, and follow-up

verification assured proper closeout of the findings. The

subject findings were included in the QA trend analysis process.,

Discussions with personnel and examination of the involved

auditor training and certification records indicated they were

qualified to perform audits.

The inspector accompanied auditors in the field performing an

audit-in-progress, Audit Number S87-16, Fire Protection Program.

Emphasis was initially placed on a special portion of this audit

concerning 10 CFR 50, Appendix R requirements.

The audit

preparation,

methodology

employed,* and auditor. expertise

appeared satisfactory for the area being audited. The inspector

observed that the auditors did not blindly follow a checklist

when obvious problems were apparent outside the scope of the

audit.

For example, vendor documentation (which should. have

been in the QA records vault) supporting the acceptability of

Exide batteries and battery racks was discovered in a desk

located in Vital Battery Room 28.

The circumstances that caused

the discrepancy were thoroughly investigated _and assessed.

Findings identified within the scope of the audit involving the

presence of combustible material, poor housekeeping, missing

Appendix R locker items, improper storage of a spare Appendix R

pump, fire damper identification weakness, and the lack of a

(2)

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26

surveillance procedure, were properly handled and safety hazards

were expeditiously corrected.

The audit protess appears to be adjusting to a favorable balance

between procedural review and actual work performance audits.

The licensee has strengthened their audit/surveillance program

by occasional use of vendor technical consultants as part of the

team when their expertise was -deemed necessary .. Discussions

with the Station QA Manager rev ea 1 ed that the licensee has

considered using this approach more often/ as well' as the

possible occasional use of other utility audit personnel to

provide an independent viewpoint to the audit process.

The

Virginia Power

Nuclear Operations Department Policy

Statement NODPS-QA-02 and NOD Standard on Corrective Action

(NODS-QA-01) adequately address adverse findings escalation.

During 1986, two CARs were issued to escalate audit findings.

CAR No. S86-0l was escalated to the Station Manager-QA Manager

level for resolution of unsatisfactory corrective action

proposed for issues identified in a scoping review that was

performed on IE Information Notice No. 80-21.

CAR NO. S86-02,

a 1 so handled and. reso 1 ved at that Station Manager-QA Manager

level, involved unsatisfactory corrective action concerning the

spacing and location requirements for plant smoke detectors.

Both of these issues i nvo 1 ved E&C 1 ong term so 1 ut ions that

appeared to be satisfactory and adequately handled.

Quality Control

The QC organization on site is distinctly separated into -four

different groups reporting to their own individual supervisors,

who in turn report to the Manager of QA.

These groups are O&M

E&C, NOE, and the Surveillance Inspection group.

The inspector

accompanied a *Qc inspector from the E&C QC group during his

inspection of a portion of the completed work identified in EWR

No.87-133.

This EWR was initiated to replace 3-inch water

treatment piping in Unit 2 whose wall thickness had degraded

(undersized).

The NRC inspector witnessed the QC hold point

verification of fit-up, preheat and interpass temperature checks

for weld no. 7 and the joint markings and final visual inspec-

tion of completed weld no. 6.

The* acceptance criteria

(Corporate Welding Manual PlOl, Visual Weld Inspection Guide-

lines QADIN 10.7, Weld Procedure -101, Weld Map No. EWR 87-133-

E200, R4) utilized for this piping replacement were satisfactory

for the inspection of the work activity.* Examination of the

latest listing of qualified welders ascertained. that the welder

observed working on the subject piping was qualified for the

specific weld procedure (101) used.

Likewise, examination of

the QC inspector certification and training records indicates he

was qualified to inspect the subject welds. A QA Tracking and

Trending System has been established and is primarily managed by

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the Supervisor, Quality Surveillance.

It is evident that

significant resources are being

used to generate trend

information.

This reflects positively on management's commit-

ment

to quality.

However,

discussion with knowledgeable

personnel and review of the site trending programs indicate they

are not fully developed to the point the licensee would lJke

them to be.

There are numerous programs in place to report adverse condi-

tions to management.

Some examples are, but are not limited to:

Station Deviation Reports

Work Requests

Engineering Work Requests

QC Activities Report

Nonconformance Reports

QA Audit Reports

Surveillance Audit Checklists

Construction Trouble Reports

A 1 though a 11

adverse findings are being trended in various

trending systems by various departments (QA/QC,

SES,

Site

Engineering, etc.), no one group appears to be monitoring the

various trending programs to establish overall plant-wide

trends.

The inspector also noted that station deviations are trended,

yet evaluation of the trending results apparently is not being

accomplished by SES for the SNSOC ,per Section 5.3.10 (e) of

Administration Procedure SUADM-0-12.

A *positive side to this

issue is that subsequent to this finding, the NRC inspector_

discovered Audit S86-09 (which has not been issued to date)

identified the same problem prior to NRC identification of this

issue.

Meaningful

FT&A of safety re 1 ated equipment is apparently

impossible due to an inadequate data base of information from

which to establish trends.

NRC inspector discussions with

personnel and documentation reviews revealed the Station Manager

has directed a task team to examine the existing FT&A program

and provide necessary recommendations 'lo establish a workable

program which will improve the material condition of the

station.

Examination of the QA Tracking and Trending System for open

inspection items, nonconformances, and risk releases did not

reveal

any

old outstanding

items.

It was

noted that

significant items were noted as such and corrective actions

appeared to be timely and appropriate in these areas.

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The inspector noted that in addition to routine audit/surveil-

lance/inspection programs, corporate and station management has

utilized the QA organization to assist in special station

studies, SSFis, and as task team members to improve construc-

tion, maintenance, operational, and security systems at the

station.

(3)

Licensee Event Reports (LERs)

The station has submitted 62 LERs during 1986 and a total of 5

LERs to date for 1987.

The inspector selected a random sample

of LERs to review for corrective action and determination that

problems had been thoroughly investigated, appropriate correc-

tive actions had been assigned, and that corrective action was

either closed out or was scheduled and being properly tracked.

The inspector selected LER 86-07, Rl, Failure of Bolting

Material in Valve Flanges, for detailed review.

Regarding this

reportable event, the licensee was found to have taken appro-

priate action in both the immediate notification artd the LER.

The subject LER fully developed the details of the incident that

occurred. The safety imp 1 i cations and consequences, roo*t cause

analysis, and corrective action plan implementation appear

complete and appropriate for the particular incident. Review of

Surry Power Station Deviation Trending Report dated January 1,

1986 - December 31, 1986 did not disclose any similar repetitive

problems, which substantiates the supposition that the correc-

tive action taken to prevent recurrence was effective, and that

there was no generic implications as stated in the LER.

Based

on this limited review, the identification and reporting of LERs,

appears to be thorough and complete.

(4) Associated Overview Activities

10 CFR Part 21 Reporting

QA activities subject to the prov1s1ons of 10 CFR 21 appear to

be adequately described in Surry* s Administrative Procedure

SUADM-LR-09.

During inspection of the posting requirements

specified by 10 CFR 21._6, the inspector noted that the subject

postings located on both the QA and turbine building bulletin

boards still reference procedures from the Nuclear QA Manual,

which has been deleted. Discussion with the QA Audit Supervisor

disclosed that audit finding 86-03-03 (Audit No. QA 86-03 issued

March 19, 1987) for which a response is due by April 18 ~ 1987,

is similar to the NRC identified discrepancy.

Human Performance Evaluation Systems (HPES)

The program currently has one full time coordinator assigned to

investigate personnel error-type situations and to determine the

management actions that can be taken to prevent recurrence. The

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HPES program is a positive feature which allows concerned

employees to report suspect practices or defects while remaining

anonymous without fear of reprisal.

An excellent lecture was

recently given (part of general employee training) to all

station personnel describing the HPES program and its function.

However, the inspector could find only two HPES Reporting Form

boxes on site; one was located outside the Superintendent of

Operations' Office and the other at the training center.

Neither box is conveniently located for the station worker and

none exist in the Engineering-QA Building Complex.*

6.

Licensee Action on Previously Identified Inspector Findings (92701)

(Closed) Inspector Followup Item (280, 281/86-17-01):

Revise Upper-tier

and Lower-tier Program Documents to Assure* Compliance with Nucle~r

Operations Department Standard Manual

(NODSM)

and

Station

QA/QC

Organization.

The inspector reviewed the VEPCO Topical Report update to VEP-1~5A (Serial

No.87-076, dated March 23, 1987) and the licensee's proposed TS change

(Serial No.86-366, dated July 14, 1986). This update and change concerns

reorganization of the QA organization in that the QA organization will now

report to the Senior Vice President, E&C, rather than the Senior Vice

President - Power Operations.

The inspector verified that the reporting

requirements of the QA organization are now consistent between VEPCO' s

Topical Report; Section 6 of Surry' s TS, Nuclear Operations Department

Standard

NODS-ADM-06,

Organizations,

Responsibilities,

Interfaces,

Revision O;

and the Quality Assurance Department Instruction Nuclear

(QADIN) -

Section 1, QA Organization, Revision 2.

The licensee has

,

reviewed all of its station administrative procedures against the higher-

tiered applicable NOD standards, changing any inconsistencies to agree

with the way the station operates.

The licensee has fulfilled its

commitment in this area.

(Closed) In~pector Followup Item 280, 281/86-19-01: Emergency Vent Damper

EQ Documentation.

The Environmental Qualification Maintenance List (EMQL) was revised to

include the emergency vent dampers on September 9, 1986.