05000280/LER-1980-046-03, /03L-0:on 800809,during Startup Operations, Containment Vacuum Sys Steam Ejector Was Placed in Svc W/O Obtaining Containment Gaseous Release Form.Caused by Personnel Error

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/03L-0:on 800809,during Startup Operations, Containment Vacuum Sys Steam Ejector Was Placed in Svc W/O Obtaining Containment Gaseous Release Form.Caused by Personnel Error
ML18139A746
Person / Time
Site: Surry Dominion icon.png
Issue date: 09/08/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A744 List:
References
LER-80-046-03L-02, LER-80-46-3L-2, NUDOCS 8009150278
Download: ML18139A746 (2)


LER-1980-046, /03L-0:on 800809,during Startup Operations, Containment Vacuum Sys Steam Ejector Was Placed in Svc W/O Obtaining Containment Gaseous Release Form.Caused by Personnel Error
Event date:
Report date:
2801980046R03 - NRC Website

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ATTACHMENT 1 e

SURRY POWER STATION, UNIT 1 DOCKET NO:

50*-280 REPORT NO:

80-046/03L-O EVENT DATE: 08-09-80 TITLE OF EVENT:

UNAUTHORIZED HOGGING OPERATION

1.

Description of Event

During start-up of unit one the Containment Vacuum System Steam Ejector was placed in service without obtaining a containment gaseous release form.

This is a violation of Technical Specification 6.4.D and is reportable in accordance with Technical Specificat~on 6.6.2.b.(2).

2.

Probable Consequences and Status of Redundant Equipment:

A valid gaseous waste discharge form for purging operations was in effect at the time of the hogging operation.

The ejector was secured at 13 psia and health physics obtained a sample for analysis.

The release did not exceed the Technical Specification limits.

Therefore the health and safety of the public were not affected.

3.

Cause

Operator error

4.

Immediate Corrective Action

Terminated Steam Ejector Operation

5.

Subsequent Corrective Action:

None required

6.

Action Taken to Prevent Recurrence:

Instructions will be provided to the operating staff to insure the appropri-ate documentation is accomplished when hogging the containment.

7.

Generic Implications:

None