ML18139A746

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LER 80-046/03L-0:on 800809,during Startup Operations, Containment Vacuum Sys Steam Ejector Was Placed in Svc W/O Obtaining Containment Gaseous Release Form.Caused by Personnel Error
ML18139A746
Person / Time
Site: Surry Dominion icon.png
Issue date: 09/08/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A744 List:
References
LER-80-046-03L-02, LER-80-46-3L-2, NUDOCS 8009150278
Download: ML18139A746 (2)


Text

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7:, REPORT DATE 80 J0 6C: 61 DOCKl:i NUMBER 6c 69 EVENi DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

I During start-up of Unit One the Containment Vacuum System Steam Ejector was placed in service without obtaining a containment gaseous release form. This is a violation of Technical Specification 6.4.D and is reportable in accordance with Tech. Spec. 6.

~ I 6.2.b.(2). The release did not exceed the limits of the Technical Specifications therefore

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the health and safety of the public were not affected.

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. ATTACHMENT 1 e SURRY POWER STATION, UNIT 1 DOCKET NO: 50*-280 REPORT NO: 80-046/03L-O EVENT DATE: 08-09-80 TITLE OF EVENT: UNAUTHORIZED HOGGING OPERATION

1. Description of Event:

During start-up of unit one the Containment Vacuum System Steam Ejector was placed in service without obtaining a containment gaseous release form. This is a violation of Technical Specification 6.4.D and is reportable in accordance with Technical Specificat~on 6.6.2.b.(2).

2. Probable Consequences and Status of Redundant Equipment:

A valid gaseous waste discharge form for purging operations was in effect at the time of the hogging operation. The ejector was secured at 13 psia and health physics obtained a sample for analysis.

The release did not exceed the Technical Specification limits.

Therefore the health and safety of the public were not affected.

3. Cause:

Operator error

4. Immediate Corrective Action:

Terminated Steam Ejector Operation

5. Subsequent Corrective Action:

None required

6. Action Taken to Prevent Recurrence:

Instructions will be provided to the operating staff to insure the appropri-ate documentation is accomplished when hogging the containment.

7. Generic Implications:

None