ML18139A364

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Advises That Responses to IE Bulletins 79-06 & 79-06A, Revision 1,were Found Acceptable.Branch Evaluation Encl
ML18139A364
Person / Time
Site: Surry  
Issue date: 05/28/1980
From: Varga S
Office of Nuclear Reactor Regulation
To: Ferguson J
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
References
IEB-79-06, IEB-79-6, NUDOCS 8006250292
Download: ML18139A364 (16)


Text

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  • DlJCKET FILE 5(f J a-CJ UNITED STATES*

NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20555 May 28, 1980 Docket Nos. 50-280, 281 Mr. J. H. Ferguson Executive Vice President-Power Virginia Electric & Power Company P. 0. Box 26666 Richmond, VA 23261

Dear Mr. Ferguson:

SUBJECT:

NRC STAFF EVALUATION OF VEPCO RESPONSES TO IE BULLETINS 79-06 AND 79-06A, REVISION 1, FOR SURRY POWER STATION, UNIT NOS. 1 & 2

. We'have reviewed the information provided by your letters dated April 26 and

  • June 26, 1979, in response to IE Bulletins 79-0GA and 79-06A, Revision 1, for Surry Power Station, Unit Nos. 1 & 2.

The enclosure provides our evaluation of your responses with respect to their specificity, completeness, and responsiveness to the bulletins.

In this regard, we have found that you have taken appropriate actions to meet the requirements of IE Bulleti~s 79-0GA and 79-06A, Revision 1.

It should be noted that the staff review of the Three Mile Island, Unit 2 a,ccident is continuing.

Consequently, other corrective actions may be required at a later date.

For example, IE Bulletin 79-06C was issued on July 26, 1979, requiring new considerations for operation of the reactor cool ant pumps fo 11 owing an accident.

Our reviews of the Westinghouse Owners 1

Group response to Items 2 and 3 of Bulletin 79-0GC (Westinghouse reports WCAP-9584 and WCAP-9600, respectively) are documented in NUREG"-0623 and NUREG-0611, respectively.

You will be kept informed regarding the require-ments for the Surry Power Station resulting from these reviews by separate correspondence.

Enclosure:

Evaluation of Licensee 1 s Responses to IE Bulletins 79-0GA and 79-06A, Revision 1 Sincerely,

  • .V\\];)~,

Ch. f arga,,

  • e Operating Reacto Branch #1 Division of Licensing

Mr. J. H. Ferguson Virginia Electric and Power Company cc:

Mr. Michael W. Maupin Hunton and Hi 11 i ams Post Office Box 153~

Richmond, Virginia 23213 Mr. W. L. Stewart, Manager P. o. Box 315 Surry, Virginia 23883 Swem Li bra ry College of William and Mary Williamsburg, Virginia 23185 Donald J. Burke, Resident Inspector Surry Power Station

u. s. Nuclear Regulatory Corm1ission Post Office Box 959 Williamsburg, Virginia 23185 e

May 28, 1980

INTRODUCTION EVALUATION OF LICENSEE'S RESPONSES TO IE BULLETINS 79-0GA AND 79-0GA (REVISION 1)

SURRY POWER STATION, UNIT NOS. 1 & 2 DOCKET NOS. 50-280 and 281 By letters dated April 14, and April 18, 1979, we transmitted our Office of Inspection and Enforcement (IE) Bulletins No. 79-0GA and 79-06A (Revision 1),

respectively, to Virginia Electric and Power Company (the licensee).

These bulletins specified actions to be taken by the licensee to avoid occurrence of an event similar to that which occurred on March 28, 1979, at Three Mile Island, Unit No. 2 (TMI-2).

By letter dated April 26, 1979, the licensee provided its response to the aforementioned bulletins for Surry _Power Station, Unit Nos. 1 & 2 (Surry).

The licensee supplemented its response by letter dated June 26, 1979, providing clarification and elaboration of certain of the Bulletin Action Items in response to our expressed concerns.

Our evaluation

  • of the.licensee's responses, as supplemented, is provided below.

EVALUATION In this evaluation, the paragraph numbers correspond to the bulletin action items and to the licensee's response to each action item.

1.

In Bulletin Action Item No. 1, licensees were requested to review the description of circumstances.described in Enclosure 1 of IE Bulletin 79-05 (issued to all licensees with Babcock & Wilcox (B&W)-designed plants for action, and to all other licensees for information) and the preliminary chronology of the TMI-2 accident included in Enclosure 1 to IE Bulletin 79-05A (same distribution a~ IE Bulletin 79-05).

(a) This review should be directed toward understanding:

(1) the extreme seriousness and consequences of the simultaneous blocking of both auxiliary feedwater trains at the Three Mile Island Unit 2.plant and other actions taken during the early phases of the accident; (2) the apparent operational errors which led to the eventual core damage; (3) that the potential exists, under certain accident or transient conditions, to have a water level in the pressurizer simultaneously with the reactor vessel not full of water; and (4) the necessity to systematically analyze plant conditions and parameters and take appropriate corrective action.

(b) Operational personnel should be instructed to:

(1) not override automatic action of engineered safety features unless continued operation of engineered safety features will result in unsafe plant conditions (see Section 7a.); and (2) not make operational decisions based solely on a single plant parameter indication when one or more confirmatory indications are available.

(c) All licensed operators and plant management and supervisors with operational responsibilities were to participate in this review and such participation was to be documented in plant records.

On April 22, 1979, an NRC briefing team provided a detailed review of the circumstances described in Enclosure 1 of IE Bulletin 79-05 and the preliminary chronology of the TMI-2 accident included in Enclosure 1 of IE Bulletin 79-0SA to a majority of the licensed operators and plant management.

The briefing team consisted of an IE Project Inspector, an Operator Licensing Branch (OLB/NRR) representative, and the facility Principal/Resident Inspector.

Attendance was documented and the briefing was videotaped for later presentation to any absentees at a later briefing by the NRC Principal/Resident Inspector.

The NRC briefing also provided a detailed review of Items l.a and l.b of IE Bulletin 79-06A.

We consider the NRC briefing to be an acceptable response to Bulletin Action Item No. 1.

2

2.

Action Item 2 of the Bulletin requested licensees to review actions required by operating procedures for coping with transients and accidents, with particular attention to (a) recognition of the possibility for forming voids large enough to compromise core cooling capability, (b) action required to prevent the formation of such voids, and (c) action required to enhance core cooling in the event such voids are formed.

Emphasis in (a) was placed on natural circulation capability.

In its June 26, 1979 response, the licensee stated that a chart with saturation and 50 Fahrenheit degrees subcooling curves is included in the plant emergency procedures.

Training of operators on the natural circula-tion mode of operation has been carried out and documented.

These activities represent part of the licensee's response to the requirements of Item 2.1.3.b of NUREG-0578.

The licensee also identified the instrumentation which is currently available to the _operator for recognition of void formation and to determine whether core cooling is being achieved by the natural circulation mode in the event of total loss of forced reactor coolant flow.

The licensee, as indicated by letter dated August 31, 1~79, has changed the plant emergency procedure regarding loss of reactor coolant flow to provide the operator with the indication and actions required to establish and maintain natural circulation in case that total forced reactor coolant flow is lost.

The emergency procedures dealing with a LOCA, loss of secondary coolant, and deteriorating pressure conditions were changed to incorporate the reactor coolant pump trip requirements specified by IE Bulletin 79-0GC.

The licensee revised the emergency procedure for loss of reactor coolant flow to provide the operator with guidance to enhance core cooling by natural circulation.

This procedure instructs the operator on methods to be used in feeding and bleeding the steam generators and the instruments 3

to be used to verify that core cooling by natural circulation has been established.

In addition, the licensee participated, as a member of the Westinghouse Owners Group, in the effort to develop generic guidelines for emergency procedures.

In our November 5 and December 6, 1979 letters to the Owners Group, we approved the Westinghouse generic guidelines regarding small break LOCAs for implementation by licensees with Westinghouse-designed reactors.

The Owners Group, in conjunction with Westinghouse, has also developed generic guidelines for emergency procedures regarding natural circulation.

These generic guidelines were submitted on December 28, 1979, as part of the Owners Group response to the requirements of Item 2.1.9 of NUREG-0578 regarding inadequate core cooling.

In order to satisfy NUREG-0578 requirements, the licensee should have incorporated the guidelines into the Surry procedures (small break LOCA guidelines by January 1, 1980 and inadequate core cooling guidelines by January 31, 1980).

The Office of Inspection and Enforcement will verify that acceptable gui~elines have been properly implemented.

Procedures based on these generic guidelines represent an acceptable method of complying with Bulletin Action Item No. 2.

We find that the licensee has provided an acceptable response to Bulletin Action Item No. 2.

3.

Bulletin Action Item No.3 requested that licensees with facilities that used pressurizer water level coincident with pressurizer pressure for automatic initiation of safety injection into the reactor coolant system trip the low pressurizer level setpoint bistables su~h that, when the pressurizer pressure reached the low setpoint, safety injection would be initiated regardless of the pressurizer level.

The pressurizer level bistables could be returned to their normal operating positions during the pressurizer pressure channel functional surveillance tests.

4

In its April 26 and June 26, 1979 responses, the licensee stated that the pressurizer level bistables which input to safety injection initiation would be placed in the trip mode.

Subsequently, in July 1979, operating procedures were revised to include verification that these bistables were in the trip mode before placing the plant in operation.

Procedures were changed to require operators to manually initiate safety injection when the primary system pressure was be.1 ow the actuation setpoi nt.

On September 6, 1979, we issued Amendment Nos. 52 and 51 to the Surry operating licenses.

These license amendments approved the design change to the safety injection initiation logic which the licensee had proposed.

This design change consisted of modifying the safety injection initiation system logic so that safety injection will be initiated on a two-out-of-three low pressurizer pressure condition regardless of the pressurizer level.

We consider the licensee's response to Bulletin Action Item No. 3 acceptable.

4.

Bulletin Action Item No. 4 requested that licensees review the containment isolation initia4ion design and procedures, and implement ~11 changes necessary to permit containment isolation, whether manual or automatic, of all lines whose isolation would not degrade needed safety features or cooling capability, upon automatic initiation of safety injection.

The Surry design provides for automatic initiation of containment isola-tion upon safety injection actuation, as called for in tne bulletin.

This aspect of the 1 i censee I s. response is therefore acceptab 1 e.

Containment isolation occurs in three phases.

The licensee provided a list of the lines isolated by each phase in the June 26, 1979 letter.

We have reviewed the licensee's response and find that the concerns expressed in Bulletin Action Item No. 4 have been adequately addressed.

5.

In Bulletin Action Item No. 5, licensees with facilities at which the auxiliary feedwater system is Mt automatically initiated were requested to prepare and implement immediately procedures which required the stationing of an individual (with no other assigned concurrent duties and in direct and continuous communication with the control room) to promptly 5

initiate adequate auxiliary feedwater to the steam generator(s) for those transients or accidents, the consequences of which could be limited by such action.

The auxiliary feedwater system at Surry is automatically initiated, with no operator action required in order to ensure adequate flow.

Therefore, Bulletin Action Item No. 5 does not apply to this plant.

6.

Bulletin Action Item No. 6 requested that licensees prepare and implement immediately procedures which:

(a) Identified those plant indications (such as valve discharge piping temperature, valve position indication, or valve discharge relief tank temperature or pressure indication) which plant operators could utilize to determine that the pressurizer power-operated relief valve(s) are open, and (b) Directed the plant operators to manually close the power-operated relief block valve(s) if the reactor coolant system pressure had been reduced to below the set point for normal automatic closure of the power-operated relief valve(s) and the valve(s) remained stuck in the open position.

The licensee reviewed the applicable Surry procedures and established a new emergency procedure, EP-9 entitled 11 Loss of Reactor Coolant Pressure.

11 Based on our review, we find that the licensee's response to Bulletin Action Item No. 6 is acceptable.

7.

In Bulletin Action Item No. 7, licensees were requested to review the action directed by the operating procedures and training instructions to ensure that:

(a) Operators do not override automatic actions of engineered safety features, unless continued operation of engineered safety features 6

would result in unsafe plant conditions.

For example, if continued operation of engineered safety features would threaten reactor vessel integrity, then the high pressure injection (HPI) system should be secured (as noted in b(2) below)..

(b) Operating procedures currently, or are revised to, specify that, if the (HPI) system had been automatically actuated because of a low pressure condition, it must remain in operation until either:

(1) Both. low pressure injection (LPI) pumps are in operation and flowing for 20 minutes or longer at a rate which would assure stable plant behavior, or (2) The HPI system has been in operation for 20 minutes, and all hot and cold leg temperatures are at least 50 degrees Fahrenheit below the saturation temperature for the existing RCS pressure.

If 50 degrees subcooling cannot be maintained af~er HPI cutoff, the HPI shall be react:ivated.

The degree of subcooling beyond so. degrees and the length of time HPI has been in operation shall be limited by the pressure/temperature considerations for the vessel integrity.

(c)

Operating procedures currently, or are revised to, specify that, in the event of HPI initiation with reactor coolant pumps (RCPs) operating, at least one RCP shall remain operating for two-loop plants and at least two RCPs shall remain operating for 3 or 4 loop plants, as*

  • long as the pump(s) is providing forced flow.

(d)

Operators are provided additional information and instructions to not rely upon pressurizer level indication alone, but to also examine pressurizer pressure and other plant parameter indications in evaluating plant conditions, e.g., water inventory in the reactor primary system.

7

In response to Bulletin Action Item No. 7.a, the licensee revised the applicable Surry procedures in May 1979 to prohibit overriding engineered safety features unless continued operation of engineered safety features would result in unsafe conditions.

This constitutes an acceptable response to Bulletin Action Item No. 7.a.

In response to Bulletin Action Item No. 7.b, the licensee participated in the effort by the Westinghouse Owners Group, in conjunction with Westinghouse, to develop generic guidelines for emergency procedures.

In our November 5 and December 6, 1979 letters to the Owners Group, we approved generic guidelines for emergency procedures regarding small break LOCAs for implementation by licensees with Westinghouse-designed operating plants.

These approved guidelines include the following criteria (taken from the enclosure to our letter of December 27, 1979) for termination of safety injection:

(1) The reactor coolant system pressure is greater than 2000 pounds per square inch gauge and increasing, and (2) The pressurizer water level is greater than the programmed no-load water level, and (3) The reactor coolant indicated subcooling is greater.than (insert plant-specific value, which is the sum of the errors for the temperature measurement system used and the pressure measurement system translated into temperature using the saturation tables), and (4) The water level in at least one steam generator is stable and increasing, as verified by auxi 1 i ary feedwater fl ow to that u'ni t.

Auxiliary feedwater flow to the unaffected steam generator should be greater than (a value in gallons per minute sufficient to remove decay heat after 20 minutes following reactor trip) uhtil the indicated level is returned to within the narrow range level instrument.

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Details of our evaluation of this issue are included in the report (NUREG-0611) of our generic review of Westinghouse-designed operating plants.

Our Office of Inspection and Enforcement will verify that the approved Westinghouse generic safety injection termination criteria have been properly incorporated in the Surry plant procedures.

Pending such verification, we find that the licensee's actions with regard to this bulletin action item are acceptable.

Another issue on which the Westinghouse Owners Group worked, in conjunction with Westinghouse, to achieve resolution with the staff was the matter of reactor coolant pump operation following a small break LOCA (Bulletin Action Item No. 7.c).

On July 26, 1979, IE Bulletin 79-06C superseded Action Item No. 7.c of Bulletin 79-06A.

Bulletin 79-06C required that, as a short-term action, licensees were to trip all reactor coolant pumps after an initiati_on of safety injection caused by low reactor coolant system pressure.

In its August 31, 1979 response to Bulletin 79-06C, the licensee stat~d its conformance with this requirement.

This action was to remain in effect until the results of analyses specified in Bulletin 79-06C had been used to develop new guidelines for operator action.

  • We have completed our review of the reactor coolant pump trip issue with the Owners Group.

The generic guidelines for emergency procedures regarding small break LOCAs, which we approved in our November 5 and December 6, 1979 letters to the Owners Group, contain the approved pump trip criteria for Westinghouse-designed operating plants.

Basically, they are as follows:

(1)

S-top all reactor coolant pumps after high pressure safety injection pump operation has been verified, ind when the wide range reactor pressure is at (plant-specific pressure derived from secondary system relief capacity, primary-to-secondary system pressure difference, and instrument inaccuracies).

9 j

Appropriate cautions have been included in the guidelines regarding isolation of component cooling water to _the reactor coolant pumps and maintaining seal injection flow to preclude pump damage due to inadequate cooling.

The details of our review of the pump trip issue are reported in NUREG-0623.

Pending confirmation by our Office of Inspection and Enforcement that the licensee has incorporated the pump trip criteria as specified in the approved Westinghouse generic guidelines into the Surry plant procedures, we find the licensee's response to Bulletin Action Item No. 7.c acceptable.

In response to Bulletin Action Item No. 7.d, the licensee revised Surry emergency procedure operations personnel which cautioned against over-reliance on pressurizer level indication, and recommended examination of other plant parameters in assessing water inventory and plant conditions.

In addition, the concern expressed in this bulletin action item was incorporated in the licensee's operator training program.

In its June 26, 1979 1 etter, the _licensee identified the specific p 1 ant par_ameters to be used in assessing water inventory.and plant conditions.

The licensee also stated that the applicable procedures were revised to reflect the above-mentioned considerations.

We find these actions to be an acceptable response to Bulletin Action Item No. 7.d.

8.

Bulletin Action Item No. 8 required that licensees review alignment requirements and controls for all safety-related valves necessary for proper operation of engineered safety features.

In response, the licensee stated that the required review was conducted by reviewing valve positions concurrently with the procedures that check or manipulate the valves.

In its June 26, 1979 response, the licensee added that valve lineups on safety-related systems as required by Technical Specifications are completed during plant startup.

Locked valves on safety-related systems are verified and documented with respect to their proper position.

Safety-related valves that have position indication in the control room are verified to be in their proper positions on a shift turnover check list which has been im~lemented to meet the requirements of Item 2.2.1.c of NUREG-0578, 11Shift and Relief Turnover Procedures.

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Based on our review, we find the licensee's response to Bulletin Action Item No. 8 acceptable.

9.

In Bulletin Action Item No. 9, licensees were requested to review their procedures to assure that radioactivity will not be inadvertently released from containment.

Particular emphasis was placed on the resetting of engineered safety features (ESFs) and the effects of this action on valves controlling the release of radioactivity.

In its June 26, 1979 response, the licensee listed all systems which are designed to transfer potentially radioactive fluids from containment, indicated those systems for which high radiation interlocks exist, aMd identified the means by which the operability of each system listed is assured.

Information pertaining to the resetting of ESFs and its effect on valves controlling the release of radioactivity was provided in the licensee's October 24, 1979 response to Item 2.1.4 of NUREG-0578.

In brief, once Containment Isolation has been initiated by a ~afety injection signal, the automatic isolation valves can be opened only upon manual reset of the actuating signal and deliberate remote manual operation of the individual valve.

We find that the licensee has adequately addressed the concerns expressed in Bulletin Action Item No. 9.

The staff's implementation of Item 2.1.4 of NUREG-0578 provides further assurance that the inadvertent release of radioactivity from containment upon resetting of ESFs will be precluded.

Our review of NUREG-0578 Item 2.1.4 implementation will be reported in a separate document.

10.

Action Item No. 10 of Bulletin 79-06A required that licensees review and modify, as necessary, maintenance and test procedures for safety-related systems to ens~re that they require that: (a) redundant systems are operable before a system is taken out of service, (b) systems are operable when returned to service, and (c) operators are made aware of the status of these*systems.

11

e In its June 26, 1979 supplemental response, the licensee provided additional information regarding this bulletin action item.

The Surry Technical Specifications specify the surveillance requirements that must be completed to confirm the operability of safety-related systems.

A subsystem or equipment is removed from service for preventive or corrective maintenance according to maintenance operating procedures.

When a subsystem fails or is removed from service, this event is entered in Control Room Operator and Shift Supervisor Logs to ensure that Technical Specification require-ments are met.

When maintenance has been completed, the controlling procedure ensures that testing of the subsystem/equipment is performed to determine operability.

Maintenance operating procedures will test the redundant subsystem/train before removal of a portion of the other subsystem/train if it does not isolate it from performing its safety function while testing.

The 1 i cens.ee conducted a detai 1 ed review of periodic tests to ensure the operability of a system is determined when equipment is returned to service following testing.

The transfer of information about the status of safety-related systems at shift change will be accomplished according to the requirements of It~m 2.2.1.c of NUREG-0578.

Based on our review, we find that the licensee 1 s response to Bulletin Action Item No. 10 is acceptable.

11.

Bulletin Action Item No. 11 requested licensees to review their prompt reporting procedures for NRC. notification to assure that the NRC i~

notified within one hour of the time the reactor is not in a controlled or expected condition of operation.

Further, at that time, an open, continuous communication channel shall be established and maintained with the NRC.

12

Surry has established a Standing Order to notify station management and the NRC within one hour of the time the reactor is not in a controlled or expected condition of operating.

Provisions are included for establishing and maintaining a continuous open channel of communication with the NRC using the dedicated telephone line established for this purpose.

We find the licensee 1 s action in response to Bulletin Action Item No. 11 acceptable.

12.

In Action Item No. 12, licensees were requested to review operating modes and procedures to deal with significant amounts of hydrogen gas that may be generated during a transient or other accident that would either remain inside the primary system, or be released to the containment.

In response to this bulletin action item, the licensee stated that procedures exist for removal of hydrogen gas from the containment using the two recombiners.

Periodic tests are made to demonstrate the operability of the recombiner system.

In addition, in its April 26, 1979 response, the licensee itated that prdcedures exist for removing hydrogen gas from the reactor coolant system.

Also, the Westinghouse Owners Group submitted procedures for removing nonconderisibles from the reactor coolant system in a December 28, 1979; letter.

Based on our review, we find that the licensee has provided an adequate response to Bulletin Action Item No. 12.

13.

This bulletin action item requested licensees to propose changes, as required, to those plant Technical Specifications which had to be modified as a result of implementing Bulletin Action Item Nos. 1 through 12, and to identify design changes necessary in order to effect long-term resolution of these items.

The licensee identified the one change to the Surry Technical Specifica-tions necessitated by actions required by this bulletin.

This change was required to implement two-out-of-three low-low Pressurizer Pressure Safety Injection actuation (from Bulletin Action Item No. 3).

13

We find the licensee's response to Bulletin Action Item No. 13 acceptable.

CONCLUSIONS Based on our review of the information provided by the licensee, we conclude that the licensee has correctly interpreted IE Bulletins79-06A and 79-0GA Revision 1.

The actions taken demonstrate the licensee's understanding of the concerns arising from the Three Mile Island, Unit No. 2 accident in relation to their implications on its own operations, and provide added assurance for the protection of the public health and safety during plant operation.

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