ML18139A195

From kanterella
Jump to navigation Jump to search
IE Insp Rept 50-280/80-01 & 50-281/80-03 on 791217-800204. Noncompliance Noted:Inadequate Maint for Drain Valve Control & Inadequate Review of Substitute Gaskets Used in Maint of Pressurizer power-operated Relief Valves
ML18139A195
Person / Time
Site: Surry  
Issue date: 03/06/1980
From: Burke D, Kellogg P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18139A192 List:
References
50-280-80-01, 50-280-80-1, 50-281-80-03, 50-281-80-3, NUDOCS 8005070768
Download: ML18139A195 (10)


See also: IR 05000280/1980001

Text

  • *

-8005 070 76 0

e

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA ST., N.W., SUITE 3100

ATLANTA, GEORGIA 30303

Report Nos. 50-280/80-01 and 50-281/8003

Licensee:

Virginia Electric and Power Company

Richmond, Virginia

23261

Facility Name:

Surry Units 1 and 2

Docket Nos. 50-280 and 50-281

License Nos. DPR-32 and DPR-37

SUMMARY

Inspection on December 17, 1979 - February 4, 1980

Areas Inspected

This routine, announced inspection involved 180 inspector-hours on site in the

areas of plant operations and operating records, plant modification and main-

tenance, followup of LER's and plant security.

Results

Of the four areas inspected, no apparent items of noncompliance or deviations

were found in three areas; two apparent items of noncompliance were found in the

plant maintenance area (Infraction - inadequate maintenance procedures for valve

1-RC-107 control, and Infraction-inadequate review of substitute gaskets used

during maintenance of Unit 1 pressurizer power operated relief valves - para-

graph 6) .

  • *

DETAILS

1.

Persons Contacted

Licensee Employees

Virginia Electric and Power Company (VEPCO)

  • W. L. Stewart, Station Manager
  • J. L. Wilson, Superintendent, Operations
  • T. A. Peebles, Superintendent, Technical Services
  • R. F. Saunders, Superintendent, Maintenance

R. M. Smith, Superivsor, Health Physics

R. L. Baldwin, Supervisor, Administrative Services

G. Kane, Operating Supervisor

  • F. L. Rentz, ResidentQC Engineer

M. R. Kansler, Acting Engineering Supervisor

Other licensee employees contacted during this inspection included control

room operators, shift supervisors, QC, HP, plant maintenance, security,

engineering, chemistry, and administrative personnel.

  • Attended exit interview.

2.

Management Interviews

The scope and findings were summarized on a weekly basis with those persons

indicated in paragraph 1 above.

The items of noncompliance were discussed

and prompt licensee action was taken to resolve the specific discrepancies.

3.

Licensee Action on Previous Findings

Not inspected.

4.

Unresolved Items

5.

Unresolved items were not identified during this inspection.

Unit 1 Operations

The inspector routinely toured the Unit 1 control room and other plant

areas to verify that the plant operations were in accordance with the

Technical Specifications (TS) and facility procedures.

Plant logs, main-

tenance records, equipment and instrumentation were also reviewed.

Within

the areas inspected no items of noncompliance were identified.

Specific

areas of inspection and results included the following:

a.

The inspector reviewed and discussed with licensee and NRC personnel,

the Unit 1 "A" reactor coolant pump motor failure and subsequent

  • *

b.

c.

d.

e.

-2-

reactor trip from full power which occurred at 1:59 p.m. on December 19,

1979.

The inspector was in the control room when the differential

pressure (DP) between the "A" steam generator and the common steam

header reached 100 psi and automatically initiated Safety Injection

(SI), some 3.5 minutes after the reactor trip.

The inspector verified

that the Emergency Procedures (EP) were properly implemented and that

the Engineered Safeguards (ES) systems and components functioned as

required; the core was adequately subcooled at all times.

Since SI

was not required in this instance, the licensee has initiated an

Engineering Study to determine if the steam header to line DP setpoint

.should be increased to account for steam generator tube plugging.

The

TS 3.7 differential pressure setpoint limit is 150 psi (max.).

The

inspector verified complete NRC review and concurrence prior to Unit 1

restart on January 8, 1980.

Following the discovery of scoring or scratching on the shafts of

large bore (12") B-P hydraulic snubbers, the NRC requested that the

licensee functionally test two of the large bore snubbers which are

mounted on each reactor coolant pump.

Following review of the testing,

the NRC approved Unit 1 restart and interim operation on January 5,

1980.

The snubber reservoir levels are being checked and documented

weekly in accordance with PT 39.3; significant increases in leakage

have not been observed, although some fluid leakage is present.

The inspector observed Unit 1 restart on January 8, 1980;

the pre-

startup checklists and procedures were completed as required, and the

ECP was accurate.

The inspector verified that the steam generator

(SG) low-low level trip setpoints had been conservatively increased

from some 5% to 17% (PT 2.5) to compensate for the generic non-

conservatism identified in the accident analysis for a high energy

line break (see LER 280/79-22).

However, the reduction in the SG

level operating band or range, requires closer control of SG ievels to

prevent a reactor trip during startup. Initial criticality occurred

at 1:07 p.m.

The inspector followed up on the whole body counts (WBC) of certain

employees who worked in Unit 1 containment on December 19 and 20,

1979, following the shutdown: -The licensee identified a calculational

error in the percent maximum permissible body burden (MPBB) of iodine

131 for these employees, corrected the records, and notified the

emplpyees of the correct lower values.

The MPBB ranged from one to

several percent.

The inspector had no further questions.

The inspector noted that the Unit 1 containment particulate and gaseou~r'_..---*-----,*

.

radiation monitors (RM-159 and -160) were out of service for certain

short periods in December and January due to the condensation of

moisture in the sampled air.

The licensee sampled the containment air

...

and monitored the direct radiation monitors in the containment (RM on

manipulator crane, etc.) when RM-159 and -160 were not operable; no

significant increases in radiation levels were observed.

The licensee.

plans to insulate and/or heat trace the sampling system to reduce -

~-

condensation (Open item 280/80-01-03).

. ------ ---~--

  • -*

e

e

-3-

6.

Unit 1 Maintenance

The inspector observed and reviewed certain maintenance activities to

assure that they were conducted in accordance with established procedures

and TS requirements.

Areas inspected included the following:

a.

On January 11, 1980, the Unit 1 reactor operator temporarily placed

the excess letdown in service and noted an immediate decrease in

pressurizer level and pressure.

The level decreased from 46% to 39%

and the pressure from 2230 to some 2100 psig.

The operator immediately

isolated the excess letdown and terminated the decrease; the pressure

and level returned to normal.

Subsequent investigation determined

that valve 1-RC-107 from the primary loop drain header (which connects.

to the excess letdown heat exchanger) to the primary drains transfer

tank (PDTT) was not closed.

The valve was previously opened to 'drain

the "A" reactor coolant loop during replacement of the RCP motor, a.nd

apparently not reclosed, although certain station personnel recalled

closing the valve prior to startup.

Since the maintenance operating

procedures (MOP 5.6) for refilling the RCS loops did not contain

appropriate specific steps or instructions to cl-0se 1-RC~107, the

procedures were determined to be inadequate and contrary to Technical

Specification 6.4.A.7, which requires detailed written procedures with

appropriate check-off lists and instructions for maintenance operations

of this type (Infraction - 280/80-01-01).

b.

The inspector reviewed maintenance work performed on the Copes-Vulcan

pressurizer power operated relief valves (PORV's), PCV-1455c and

PCV-1456, which were r~built on December 28, 1979, through January 4,

1980.

The valves had been leaking slightly during previous operations,

and had indication of weeping shortly after the Unit 1 restart on

January 8, 1980.

The PORV's are currently isolated.

While reviewing

Maintenance Reports (MR) S1912041010 and S1912041011, the inspector

noted that the replacement parts used were not listed on the MR.

Review of the storekeeping records indicated that the following

gaskets were used on MR S1912041010 and MR 61912041011:

The

were

Quantity

Stock No.

2

1740493G

1

1740547G

.1

1740514G

above Flexitallic gaskets were

used on PCV-1455C:

Quantity

1

2

Stock No.

1740547G

1740514G

used on

Style

R3-3F

CG-IF

R3-15H

PCV-1456,

Style

CG-lF

R3-15H

the following

__ ,. __ _



* --~*

c.

e

e

-4-

Each PORV required two gaskets, which are stock replacement gaskets

170514G and 1740604G; these gaskets are 1500 psi (min) rated gaskets.

The R3-3F and CG-IF gaskets are rated 300 psi and 150 psi, respectively.

In addition, plant maintenance personnel told the inspector that

additional gaskets were used and not properly logged out of the store-

room.

At least two 1740850, style CG-6F (600 psi) gaskets were used,

and may have been one of the final gaskets installed in each PORV.

The use of the lower rated gaskets in the PORV's once the stock of

specified replacement gaskets was depleted, is contrary to plant

procedures for design control (QA manual, Section 3) of safety-related

components and is an infraction (280/80-01-02).

After reviewing plant

records and documentation, the inspector could not determine which

four of the above gaskets are in the PORV's.

The inspector also noted

that the licensee considers the majority of the plant gaskets to be

"off-the-shelf" type items which are not specifically identified',

accepted and tagged by the QA staff'.

The inspector is reviewing this

matter with NRC personnel (open item 280/80-01-04).

The* inspector observed additional maintenance work and testing such as

the removal and cleaning of the condensate filter screens during

operation and periodic testing of the recirculation spray pumps.

Within the areas inspected, no further items of noncompliance were

identified.

7.

Followup on BFD Relay Testing

8.

Prior to Unit 1 restart on January 8, 1980, the inspector reviewed licensee

actions taken in regard to IE Bulletin 79-25, "Failures of Westinghouse BFD

Relays in Safety-Related Systems." The inspector reviewed BFD relaty testing

performed in March of 1976 under ST-41, which verified relay drop-out times

of 25 msec or less.

Of the 89 Units 1 relays tested, three relays failed

the 25 msec test time by a few milliseconds and were replaced.

No relay

sticking or degradation has been observed since the testing.

Three new

style 5072A49 relays have been installed, but have not been tested for

overtravel.

No failure of the three relays would interfere with or affect

the engineered safeguards systems operability. All BFD relays will be

tested and/or replaced in accordance with IEB 79-25, which remains open.

Implementation of TMI-2 Lessons Learned Short-Term Recommendations (NUREG -

0578)

The licensee completed initial installation of many of the NUREG-0578

short-term recommendations (section 2) on Unit 1 prior to the January 8,

1980, restart.

Certain items such as the high range radiateion monitors

were subsequently installed as the materials became available.

Specific

items inspected included the following:

a.

Modifications to the pressurizer heater power supplies were not neces-

sary since certain heater banks were on the emergency power system.

Direct position indication of pressurizer safety and power-operated.~:


* -* -

--* - ---

.

9.

e

e

-5-

relief valves (PORV's) was accomplished by installing an acoustic

monitoring system to monitor each valve (Design change 79-S54).

In

addition to the valve tailpipe temperature monitors, the PORV's have

limit switches to monitor valve (operator) position, however environ-

mental qualification data is currently not available for these limit

switches.

The NRC will review the seismic and environmental qualifi-

cation data on the acoustic monitoring systems when available.

An

additional source of safety-grade motive power (emergency air) has

been installed on the PORV's (DC-79-S53).

b.

The Unit 1 auxiliary feedwater flow indication instrumentation was

modified by DC 79-S55 to provide each channel with power supply diversity

and physical independence.

The electrical modifications are being

reviewed by the NRC. The inspector noted that*although certain nesting

was performed after the modifications, the flow instrumentation was

not recalibrated at this time.

Since certain flow channels such as

FT-lOOA had not been calibrated since 5/12/78, the licensee stated

that the instrumentation would be calibrated during the next outage.

c.

Two core cooling monitors (saturation meters) were installed in Unit 1

to monitor RCS pressures and temperatures.

The control room instru~

mentation monitors the auctioneered high in-core T/C or loop RTD

temperature and the wide range (PI-1-402) or protection channel

(PI-1-457) pressure instrumentation pressure for subcooling.

The NRC

is reviewing the instrumentation and inputs.*

d.

Piping and systems outside containment, such as the outside recirculation

spray and low head safety injection pumps and piping, are periodically

leak tested.

e.

High range radiation monitors have been installed on the process vent,

ventilation vent, and main steam relief lines (DC 79-59), and procedures

have been developed to improve post-accident sampling capabilities

(CP-66 and 66A).

NRC review of these items is in progress.

The inspector noted that updated procedures or instructions have been

issued to operate and utilize the above new equipment.

Detailed

procedure review will be conducted at a later date.

Unit 2 SGRP

The Unit 2 steam generator replacement project was completed on December 31,

1979; testing of various Unit 2 systems is in progress.

During routine

tours of Unit 2, the inspector observed certain maintenance work and testing;

no items of noncompliance were identified.

While reviewing ETA 50006-P-4-ULC,

"Primary System Hydro and Flush", the inspector noted that the flush was

through 2-DG-78, but could not locate this valve on the P&ID FM-83B. The

licensee determined that the valve tagged 2-DG-78 is.actually 2-DG-82, and

is re tagging the valve.

.* __

v

e

e

-6-

10.

Review of Reportable Occurrences

The inspector reviewed the Reportable Occurrence (RO) reports listed below

to ascertain that NRC *reporting requirements were being met and to determine

the appropriateneess of corrective action taken and planned.

Certain

Licensee Event Reports (LER) were reviewed in greater detail to verify

corrective action and determine compliance with the Technical Specifications

and other regutatory requirements.

The review included examination of log

books, internal correspondence and records, review of SNSOC meeting minutes,

and discussions with various staff members.

Within the areas inspected, no items of noncompliance or deviations were

identified.

a.

LER 28-/79-08, concerned an apparent under power condition on the 480

VAC emergency bus that could exist during accident conditions with or

without loss of off-site power.

The condition was identified during a

load study by the AE.

Additional transformers and components were

installed and are operable in Unit 1; the Utit 2 modifications and

testing are in progress and will be reviewed prior to startup.

This

LER is closed.

b.

LER 280/79-10 identified discrepancies in the location and configuration

of certain pipe supports discovered during an investigation of the

as-built piping conditions.

The discrepancies identified have been

corrected as required by the NRC Show Cause Order of March 13, 1979,

and IE Bulletin 79-14.

Reanalysis and corrective action (if required)

continues on piping systems outside containment (e.g:

component

cooling water).

This LER is closed.

c.

LER 280/79-11 has been supplemented and the correct codes applied.

This LER is closed.

d.

LER 280/79-20 concerned the abnormal degradation of battery charger

2B2 internal power cable insulation.

The dried and cracked insulation

was determined to be the result of environmental conditions.

Reduced

air flow to the battery chargers 2Bl and 2B2 may have lead to increased

internal temperatures and teh consequent deterioration of the cable

insulation.

No insulation deterioration was noted on the stations six

similar battery chargers.

The air flow to all the battery chargers

was increased, and the units are periodically inspected.

This LER is

closed.

e.

LER 280/79-21 addressed the failure of MOV-SW-104C to fully close

during exercise.

This valve is normally open and remains open during

accident conditions; the valve operated properly after manual stroking.

This LER is closed .

f.

LER 280/79-22 concerned a non-conservatism in accident analysis:

the

steam generator level instrumentation indications would increase if a

-~--. *-** - ..... - __ ::--__ .._ ... -.:.*--*-**---*---*---**-*-~*---~- .....

e

e

-7-

rise in containment temperature decreased the reference leg water

column density.

To compensate for the temperature effects on the SG

reference leg, the low-low level trip setpoint has been increased to

15% minimum (see ~ara. 5.c).

This LER is closed.

g.

LER 280/79-23 concerned the discovery of circumferential crack indications

in the steam generator feedwater piping nozzle to reducer areas.

All

indications were repaired and inspected in accordance with IE Bulletin

79-13.

This LER is closed.

h.

LER 280/79-24 addressed the identification of 64 of the approximately

1800 plant penetration fire barriers as potentially inoperable, during

initial conduct of Periodic Test 24.11 which inspects each fire barrier.

The fire barriers were repaired as required.

This item is clos~d.

i.

LER 280/79-25 concerned a late report of RCS activity, which rose

slightly above 1.0 uci/gm for about 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after a reactor trip

from 19% power.

The LER reference to TS 6.9.1 was incorrect.

This

LER is closed.

j.

LER 280/79-27 addressed overstress in the three RTD bypass lines and

in a safety injection line inside containment.

Reanalysis and modifi-

cations were made to the lines as required.

The LER was submitted one

day late.

This LER is closed.

k.

LER 280/79-28 concerned the failure of 10 of the 209 anchor bolts

tested in accordance with IE Bulletin 79-02.

The failures were reviewed

and corrected as neces&ary.

This LER is closed.

1.

LER 280/79-30 addressed the failure to properly reset the alarm setpoints

on radiation monitors RM-CC-105&106, which monitor the component

cooling water.

Radiation monitoring equipment is now checked daily.

This LER is closed.

m.

LER 280/79-31 concerned a liquid waste release whose isotope activity

summation exceeded the radiation monitor setpoint of 1.5E-3uci/cc

without tripping.the alarm (actual summation was 1.6E-3uci/cc).

The

acutal summation is calculated since the detector is calibrated for

one* isotope and administrative control is necessary to prevent isotope

releases which the radiation monitor may not see or detect.

The

release did not exceed TS 3.11.A or 10 CFR Part 20 limits.

This LER

is closed.

n.

LER 280/79-32 addressed a Westinghouse identified non-conservatism in

the analysis which could affect the calculated peak clad temperatures.

Reanalysis for Surry 1 determined that sufficient margin existed to*

assure that the PCT limit of 2200°F was not reached.

Unit 2 will be

evaluated prior to startup and FQ reduced if necessary.

This LER is

Closed.

.*

, .......

  • , .**. 'IJ.

o.

p.

q.

r.

s.

t.

u.

v.

w.

e

e

-8-

LER 280/79-33 concerned the failure of service water valve 1-SW-107

which supplies cooling water to the charging pump seal and oil coolers;

the redundant train was operable, and the valve was immediately repaired.

Degradation of these 1.5 and 2 inch valves has been identified as a

generic problem at Surry, and all bronze ball valves are being installed;

the Unit 2 installation is complete and the Unit 1 changeout is in

progress.

This LER is closed.

LER 280/79-34 addressed a non-conservative design feature discovered

in trip valve TV-SV-102 logic which diverts SJAE discharge into contain-

ment when the SJAE radiation alarm is actuated.

A high containment

(CLS) pressure signal closes TV-SV-102 to isolate containment, however,

if the high CLS signal is reset and the radiation alarm is still

present, the valve will reopen.

The Emergency Procedures were revised

to assure TV-SV-102 is closed and will not reopen prior to resetting

CLS. This LER is closed.

LER 280/79-35 concerned a low current on heat tracing circuit 2B

(Panef 8).

The redundant circuit was operable.

A supplemental LER

has been submitted to address the generic implications of heat tracing

tape failure; corrective actions are in progress on the BAST pump

leaks and the heat tracting systems.

This LER is closed.

LER 280/79-36 addressed an error in the containment spray effectiveness

values used for containment depressurization values in accident analysis.

Until the analysis or modifications are complete, interim, more conser-

vative values for the maximum allowable service water temperatures

have been implemented.* Until 1 is operating within the revised limits,

aided by the seasonally cool weather.

This LER is closed.

LER 280/79-37 concerned a failure in the new type heat tracting tape

due to overheating.

The heat tracing.circuit was redesigned to imple-

ment more local control over each circuit.

Systematic evaluation

continues.

This LER is closed.

LER 280/79-38 addressed the inoperability of one train of the RWST

chemical addition tank discharge due to manual isolation of MOV-CS-102B;

valve MOV-CS-102A was verified operable.

This item was discussed in

IE Inspection Report 280/79-67 and is closed.

LER 280/79-39 concerned a heat tracing tape failure; the redundant

circuit was operable.

This LER is closed.

LER 280/79-40 addressed a component cooling water p1p1ng (support)

overstress condition.

Modifications were made to relieve the overstress

conditions.

This LER is closed.

LER 280/79-41 addressed the "A" RCP motor fault, the reactor trip, and

subsequent safety injectin which occurred on 12/19/79.

See para. *'S .--a_;.

of this report.

This LER is closed.

'

(

-9-

x.

LER 280/79-42 concerned an overstress condition on a component cooling

water pipe hanger; the condition was corrected.

This LER is closed.

y.

LER 280/79-43 addressed the temporary inoperability

recorder RR-175; the drive wheel string disengaged.

monitors and alarms were operable, and the recorder

LER is closed.

of radiation

The radiation

repaired.

This

In addition to the above, the inspector reviewed the licensee's October 18,

1979, response to the D. G. Eisenhut letter of 21, 1979, which requested

information on the potential for multiple equipment failures and challenges

to safety systems at PWR's.

Licensee review of trip reports and operating

reports indicated that no common mode failures occurred which prevented

operability of safety systems.

A review of periodic test (PT) procedures

determined that adequate provisions have been incorported into the PT's to

prevent challenges to.the safety-related systems; the licensee also revised

existing administrative procedures to re-emphasize the importance of avoiding

challenges to the protective features of the facility.

Some events which

might be considered multiple failures or challenges to safety systems

occurred some years ago due to inadequate procedures or personnel error;

however, the problems were revised at that time and corrective actions were

taken.

This item is closed.

6.

Plant Physical Protection

The inspector verified the following by observation:

a ..

Gates and doors in protected and vital area barriers were closed and

locked when not attended.

b.

Isolation zones described in the physical security plans were nqt

compromised or obstructed.

c.

Personnel were properly identified, searched, authorized, badged and

escorted as necessary for plant access control.

Within the areas inspected, no items of noncompliance were identified.

-

~ _;...