ML18136A259

From kanterella
Jump to navigation Jump to search
Forwards IE Insp Repts 50-280/79-59 & 50-281/79-78 on 790910-28.No Noncompliance Noted
ML18136A259
Person / Time
Site: Surry  Dominion icon.png
Issue date: 10/26/1979
From: Robert Lewis
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Proffitt W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
Shared Package
ML18136A260 List:
References
NUDOCS 7912050623
Download: ML18136A259 (6)


See also: IR 05000280/1979059

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA ST., N.W., SUITE 3100

ATLANTA, GEORGIA 30303

OCT 2 6 1979

cl~~~~

c£';; -o>g-o

,51'8 I

1n Reply Refer To:

RII:DJB

50-280/79-59

S0-281/79-78

Virginia Electric and Power Company

ATTN:

W. L. Proffitt

Senior Vice President, Power

P. 0. Box 26666

Richmond, VA 23261

Gentlemen:

This refers to the inspection conducted by D. J. Burke of . this office on

September 10-28, 1979, of activities authorized by NRC Operating License Nos.

DPR-32 and DPR-37 for the Surry facilities, and to the discussion of our findings

held with W. L. Stewart at the *conclusion of the inspection.

Areas examined during the inspection and our findings are discussed in the

enclosed inspection report.

Within these areas, the inspection consisted of

selective examinations of procedures and representative records, interviews with

personnel, and observations by the inspectors.

Within the scope of this inspection, no items of noncompliance were disclosed.

In accordance with Section 2.790 of the NRC's "Rules of Practice", Part 2, Title

10, Code of Federal Regulations, a copy of this letter and the enclosed inspection

report will be placed in the NRC' s Public Document Room. If this report contains

any information that you (or your contractor) believe to be proprietary, it is

necessary that you make a written application within 20 days to this office to

withhold such information from public disclosure.

Any such application must

include a full statement of the reasons on the basis of which it is claimed that

the information is proprietary, and should be prepar~d so that proprietary

information identified in the application is contained in a separate part of the

document. If we do not hear from you in this regard within the specified period,

the report will be placed in the Public Document*Room.

Should you have any questions concerning this letter, we will be glad to discuss

them with you.

Enclosure:

See Page 2

Sincerely,

z.c. I

R. C. ~ng Chief

Reactor Operations and Nuclear

Support Branch

0

r-

'-~

OCT 2 6 197S

Virginia Electric and Power Company

-2-

Enclosure:

Inspection Report Nos. 50-280/79-59,

and 50-281/79-78

cc w/encl:

W. L. Stewart, Manager

P. 0. Box 315

Surry, VA

23883

\\. '

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA ST., N.W., SUITE 3100

ATLANTA, GEORGIA 30303

Report Nos. 50-280/79-59 and 50-281/79-78

Licensee:

Virginia Electric and Power Company

Richmond, Virginia 23261

Facility Name:

Surry, Units 1 and 2

Docket Nos. 50-280 and 50-281

License Nos. DPR-32 and DPR..:37

Inspection at Surry

SUMMARY

Inspection on September 10-28, 1979

Areas Inspected

Dale Sj(gned

! 11hf/?2

Wte Signed

This routine inspection by the resident inspector involved 60 inspector-hours

onsite in the areas of plant operations and maintenance, including the Unit 2

steam generator replacement outage work, followup on previously identified items,

and plant security.

Results

Of the four areas inspected, no items of noncompliance or deviations were identified.

DETAILS

1.

Persons Contacted

Licensee Employees

2.

Virginia Electric and Power Company (VEPCO)

  • W. L. Stewart, Station Man.ager
  • J. L. Wilson, Superintendent, Operations
  • T. A. Peebles, Superintendent, Technical Services
  • R. F. Saunders, Superintendent, Maintenance

R. M. Smith, Supervisor, Health Physics

G. Kane, Operating Supervisor

  • F. L. Rentz, Resident QC Engineer
  • D. A. Ctristian, Engineering Supervisor

Other licensee employees contacted during this inspection included control

room operators, shift supervisor, QC, engineering, HP, plant maintenance,

security, engineering, and administrative personnel.

  • Attended exit interview

Management Interviews

The scope and findings were summarized on a weekly basis with those persons

indicated in Paragraph 1 above.

3.

Licensee Action on Previous Inspection Findings

Not inspected.

4.

Unresolved Items

Unresolved items were not identified during this inspection.

5.

Unit 2 Steam Generator Replacement Activities

The inspector reviewed certain U-2 SG replacement and associated activities

to verify that the activities were performed in accordance with the Steam

Generator Repair Program (SGRP) and applicable procedures.

The review included the following activities:

a.

b.

Inspection tours of the Unit 2 containment for cleanliness and

radiation control; appropriate work and radiation controls were being

implemented.

Observation of inspections and work being performed on the Unit 2 pipe

supports to satil:fy IE Bulletin 79-14.

  • .. )I

)

-2-

Within the areas inspected, no items of noncompliance or deviations were

identified.

6.

Unit 1 and 2 Operations and Maintenance

Unit 1 remains shutdown pending resolution of NRC questions regarding IE

Bulletin 79-14 (As-built piping s._y_stems verification).

The inspector

toured the Unit 1 and 2 control rooms and certai~ plant areas to verify

that the shutdown operations were in accordance with the Technical Speci-

fications and facility procedures.

Plant logs, maintenance .and records

were also reviewed.

Withi-0 the areas inspected, no items of noncompliance

were identified.

Spec~fic areas of inpsection included:

a.

In addition to verifying that a qualified ASCO solenoid operated pilot

valve (NP Series) was* installed on Unit 1 containment sump isolation

valve (TV-DA-lOOA), the inspector reviewed Design Change 79-522 testing

which verified sump isolation upon initiation of safety injection.

b.

Followup on LER 280/78-04, which addressed the temporary loss of

service water (SW) flow through charging pump intermediate seal cooler

1-SW-E-lB due to failure of the discharge gate valve.

Corrosion of

the valve stem permitted the.valve disc to drop and obstruct one train

of SW flow.

Following an engineering study (78-08), the licensee

replaced all 1 1/2 and 2 inch valves in the Unit 2 system with bronze

ball valves; Unit 1 valve replacement is scheduled to be completed

during the next major outage.

A successful hydrotest was performed on

the Unit 2 system following maintenance; however, on September 27,

1979, the inspector noted some leakage from valve 2-SW-129 flange.

-The licensee is taking corrective action on the apparent leak. Ler's

280/78~04 and 281/78-11 are closed.

c.

A walkdown of the plant high and low level liquid waste drain tank

went piping from the tanks to the process vent system, utilizing

FM-BOA and 90B prints.

No discrepancies were identified.

The inspec-

tor noted that the tanks lead open overflow piping to the local floor

drains in the auxiliary building tank rooms.

Licensee evaluation

determined that the systems which deliver liquids to the tanks would

be off-gassed and would not vent gases through the overflow lines.

d.

Review of the Unit 1 inside recirculation spray (IRS) pump and motor

testing following maintenance which included replacement of the lower

motor bearing.

After rebuilding, the IRS (1-RS-P-lA and lB) pump

motors were successfully tested at the North Anna facility for 8 and 5

hours respectively before reinstallation at Surry.

GE motors EHJ524018

(lA) and EHJ524019 (lB) were installed in Unit 1 and periodic test

e.

17.2 was performed to verify pump operability.

LER 280/79-09 remains

open pending conrrective action on Unit 2 .

Review of emergency procedures to verify that the reactor coolant

pumps are tripped upon initiation of high head safety injection caused

by low reactor coolant system pressure; the procedures have been

revised in accordance with IE Bulletin 79-0SC and 79-06C.

f.

g.

-3-

Review of Unit 1 Periodic Tests 17.1, Containment Spray System, PT

17.3, Containment Outside Recirculation Spray Pumps PT 18.1, Low Head

SI Test and Flushing of SS Piping and PT 38.8, Chemical Additon Tank

Sampling, performed between May and September, 1979, in accordance

with TS 4.5, 4.11, and 4.1.

No discrepancies were identified.

The

chemical additon tank sodium hydroxide concentration was between 19

and 22%, as required by PT ~~.8 (TS 18%).

Observation of certain anchor bolt inspections performed in Unit 1

containment in accordance with IE Bulletin 79-02.

7.

Plant Physical Protect~on

The inspector verified the following by observation:

a.

Gates and doors in protected and viatal area barriers were closed and

locked when not attended.

b.

Isolation zones described in the physical security plans were not

compromised or obstructed.

c.

Personnel were properly identified, searched, authorized, badged and

escorted as necessary for plant access control.