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LER-1979-032, /01T-0:on 791109,notified by Westinghouse of Possible Nonconservative Feature Re Fuel Rod Burst in App K LOCA Analysis.Earlier Clad Burst Caused by Reduction in Heatup Rate.Facility Has Sufficient Margin in Model |
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NRC FORM 366 (7-77).,
U.S. NUCLEAR REGULATORY COMMISSION e
LICENSEE EVENT REPORT e 60NTROLBLOCK: l~--.-.JL-...L-.--L~~l~Ll__,IG) 1 6
(PLEASE PRINT OR TYPE ALL REQUIRED li\\lFORMATION)
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LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T [BJ]
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EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PP.OBABLE CONSEQUENCES@
I During a recent reanalysis by Westinghouse, a non-conservative feature con] d exist in the Appendix K LOCA analysis with respect to the calculation related to fue]
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rod burst.
The fuel clad burst curve is dependent on the clad heatup 'rate prior ta [Im burst and a reduction in heatup* rat~ (<25°F/second) causes earlier clad burst.
This event is reportable in accordance with Technical Specification 6.6.2.a.8. The health_~
safety of the general public were not affected by this event.
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SYSTEM CODE IR 1c I@
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\\:..!..) REPORT 17 j9 I NUMBER 21 22
CAUSE
CAUSE CODE SUBCODE COMPONENT CODE
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20 31 ACTION FUTURE EFFECT SHUTDOWN r::;;,.
ATTACHMENT NPRD-4 PRIME COMP.
SUPPLIER REVISION NO.
l_QJ 32 COMPONENT MANUFACTURER 80 TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM SUB.
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43 44 47 j Heatup rate prior to burst was determined from most recent LOCA/ECCS analysis.
It was ITIIJ I determined that Surry has sufficient margin in the model to allow opera ti on wi tbout a I
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FACILITY STATUS
% POW::R OTHER STATUS
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DISCOVERY DISCOVERY DESCRIPTION ~
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45 46 80 LOCATION OF RELEASE @
NA 45 80 NUMBER.
TYPE
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9 11 12 13 80 PERSONNEL INJURIES fJ NUMBER DESCRIPTION 41
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9 11 12 80 LOSS OF OR DAMAGE TO FACI LJTY '43' TYPE
DESCRIPTION
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9 10 80 PUBLICITY 36 NRC USE ONLY ISS.VEDQ DESCRIPTION 4-5 l")I 9}
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ATTACHMENT:
Page 1 of 2 SURRY POWER STATION DOCKET NO:
50-280 REPORT NO:
79-032/0lT-0 EVENT DATE: 11/9/79 TITLE OF EVENT:
Fuel Rod Burst Analysis
- 1.
DESCRIPTION OF EVENT
On November 9, 1979, VEPCO was notified of an unreviewed safety question by Westinghouse Electric Corporation.
The unreviewed safety question con-cerned a potential non-conservative feature of the Westinghouse ECCS large break evaluation model which could affect the peak clad temperature calcu-lated for the LOCA transient.
The event is reportable in accordance with Te.chnical Specification 6. 6. 2. a. 8.
- 2.
PROBABLE CONSEQUENCES/STATUS OF REDUNDANT SYSTEMS The Westinghouse evaluation revealed that heatup rates could be< 25°F/second.
During the LOCA transient, the fuel clad burst curve establishes the time of clad burs and (since the clad temperature.and the pressure differential across the clad are changing throughout the LOCA transient) the post-burst conditions of the clad. It was determined that sufficient margin existed in the analysis such that the health and safety of the public were not affected.
- 3.
CAUSE
The potential non-conservative feature of the Westinghouse large break ECCS evaluation utilized a model which uses a curve that represents fuel clad burst conditions for clad heatup rates of> 25°F/second.
The fuel clad burst curve is dependent on the clad heatup rate prior to burst and a reduction in heatup rate causes earlier clad burst.
A shift in clad burst time can affect the peak clad temperature (PCT) calculated for the LOCA transient.
- 4.
It1MEDIATE CORRECTLVE ACTIONS Since the cuu.rent Surry LOCA-ECCS analyses exhibited heatup rates less than 25°F/sec., a specific reanalysis was performed to ascertain the effect on PCT £or the Surry Unit 1 analysis. It was determined that sufficient margin existed to the PCT limit of 2200°F for Surry Unit 1 to offset the small effect of using a more appropriate burst curve.
- 5.
SCHEDULED CORRECTIVE ACTION Westinghouse determined that Surry has margin available in the model to allow operation without a reduction in FQ.
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ATTACHMENT:
SURRY POWER DOCKET NO:
REPORT NO:
e Page 2 of 2 STATION, UNIT 1 50-280 79-032/0lT-O TITLE OF EVENT:
Fuel Rod Burst Analysis
- 6.
ACTION TAKEN TO PREVENT RECURRENCE Since the Westinghouse LOCA/ECCS evaluation for Surry has been completed, no further action is required to prevent recurrence.
- 7.
GENERIC IMPLICATIONS This event was a Westinghouse identified generic item.
However, since Surry Unit 2 is not currently operating, a re-evaluation has not been performed.
A re-evaluation of the Surry Unit 2 will be performed prior to Unit 2 startup.
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| 05000281/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000280/LER-1979-001, Forwards LER 79-001/01X-0 | Forwards LER 79-001/01X-0 | | | 05000280/LER-1979-001-01, /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | | | 05000281/LER-1979-001-03, /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | | | 05000281/LER-1979-002, Forwards LER 79-002/03L-0 & 79-003/03L-0 | Forwards LER 79-002/03L-0 & 79-003/03L-0 | | | 05000281/LER-1979-002-03, /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | | | 05000280/LER-1979-002-03, /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | | | 05000280/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000280/LER-1979-003-03, /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | | | 05000280/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000281/LER-1979-003-03, /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | | | 05000280/LER-1979-004, Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | | | 05000280/LER-1979-004-01, /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | | | 05000281/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000281/LER-1979-004-03, /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | | | 05000280/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000281/LER-1979-005-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | | | 05000280/LER-1979-005-03, /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | | | 05000280/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000280/LER-1979-006-03, /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | | | 05000281/LER-1979-006-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | | | 05000280/LER-1979-007-03, /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | | | 05000280/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000281/LER-1979-007-03, /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | | | 05000281/LER-1979-008-03, During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | | | 05000281/LER-1979-008, Forwards Updated LER 79-008/03X-1 | Forwards Updated LER 79-008/03X-1 | | | 05000280/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000280/LER-1979-008-01, /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | | | 05000280/LER-1979-009-01, /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | | | 05000280/LER-1979-009, Forwards LER 79-009/01T-0 | Forwards LER 79-009/01T-0 | | | 05000281/LER-1979-009-03, /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | | | 05000281/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000280/LER-1979-010-03, /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | | | 05000280/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010-03, /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | | | 05000280/LER-1979-011-03, /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | | | 05000280/LER-1979-011, Forwards LER 79-011/03X-1 | Forwards LER 79-011/03X-1 | | | 05000281/LER-1979-011, Forwards LER 79-011/12T-0 | Forwards LER 79-011/12T-0 | | | 05000281/LER-1979-011-12, /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | | | 05000280/LER-1979-012-03, During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | | | 05000280/LER-1979-012, Forwards Updated LER 79-012/03X-1 | Forwards Updated LER 79-012/03X-1 | | | 05000281/LER-1979-012, Forwards LER 79-012/08T-0 | Forwards LER 79-012/08T-0 | | | 05000281/LER-1979-012-08, /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | | | 05000281/LER-1979-013, Forwards LER 79-013/01T-0 | Forwards LER 79-013/01T-0 | | | 05000281/LER-1979-013-01, /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | | | 05000280/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000280/LER-1979-013-03, /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | | | 05000280/LER-1979-014-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | | | 05000280/LER-1979-015-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | |
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