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LER-1979-030, /01T-0:on 791029,radiation Alarm Setpoint Component Cooling Sys Found Greater than Two Times Background.Caused by Improper Setting of Alarm Setpoint.Vent Valve Manually Isolated |
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| 2801979030R01 - NRC Website |
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NRC FORM 366 ii-'17).._
- U.S. NUCLEAR REGULATORY COMMISSION ecENSEE EVENT REPORT e
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11 210 50 61 DOCKET NUMBER 58 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
0'Tith the unit at 100% power the Radiation Alarm Setpoint for the Component Cooling
[£]TI I System was found to be greater than two times background as listed in Technical oo:TI !Specification 3.7, Table 3.7-5.
This event would have caused the surge,tank vent [ill] 1valve of the Component Cooling System not to close automatically at twice the
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!background level.
Since vent valve isolation was not required, the health and
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1safety of the general public were not affected.
[QJ]J !Technical Specification 6.6.2.a.
This event is reportable per 7
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CAUSE
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SUBCODE
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19 REPORT TYPE L!J 30 VALVE SUBCODE
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20 31 PRIME C.OMP.
REVISION NO.
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @
42 43 44 47 [III] I The initial corrective action taken was to isolate the surge tank vent valve [IJJJ I manually and determine a background radiation level.
New alarm and alert setpoints [III] I were then set on both monitors.
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DISCOVERY DISCOVERY DESCRIPTION '23,r LPJ@1...I __
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RELEASED OF RELEASE AMOUNT OF ACTIVITY~
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NUMBER Q. TYPE DESCRIPTION~
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8 80 NUMBER DESCRIPTION 41 PERSONNEL INJURIES
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9 11 12 80 LOSS OF OR DAMAGE TO FACILITY '4JI TYPE
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~ NAME m PEJEPAREB 1.L..J.
Stewart PHONE:80't 357 3184
e Attachment, Page 1 Surry Power Station, Unit 1 Docket No.: 050-0280 Report No.: LER 79-030/0lT-0 Radiation Monitor (RH-CC-105/ 106) Setpoint Alarm Improperly Set
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DESCRIPTION OF EVENT
With the unit at 100% power, the Radiation Alarm Setpoint for the Component Cooling System was found to be greater than twice background as listed in Technical Specification 3.7, Table 3.7-5.
Operating in this condition, the Component Cooling System's surge tank vent valve would not have automatically closed at twice background.
This event is contrary to Technical Specification 3.7 (Table 3.7-5) and reportable per Technical Specification 6.6.2.a.
- 2.
PROBABLE CONSEQUENCE OF EVENT:
The improper alarm setting of the Radiation Monitor for the Component Cooling System had no effect upon the health and safety of the general public.
The unit had recently obtained full power following an extensive 7 months cold shutdown, placing the relative radio-isotope inventory in the Component Cooling System at a small amount.
Therefore, the protection provided by the required response setting for vent isolation was not necessary.
- 3.
CAUSE OF EVENT
The improper setting of the alarm setpoint for the radiation monitors was due to a failure to recalibrate from full power background following an extensive period of being at cold shutdown.
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IMMEDIATE CORRECTIVE ACTION
The immediate corrective action taken was to manually isolate the Component Cooling System's surge tank vent valve and determine a new background radia-tion level.
New alarm and alert setpoints were then set on both monitors.
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SCHEDULED CORRECTIVE ACTION:
Periodic Test 26.1, Radiation Monitoring Equipment Daily Check, will be changed to require a verification of alarm and alert setpoints.
- 6.
ACTION TAKEN TO PREVENT RECURRENCE:
The same as scheduled corrective actions.
- 7.
GENERIC IMPLICATIONS:
This event possesses no generic implications.
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| 05000281/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000280/LER-1979-001, Forwards LER 79-001/01X-0 | Forwards LER 79-001/01X-0 | | | 05000280/LER-1979-001-01, /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | | | 05000281/LER-1979-001-03, /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | | | 05000281/LER-1979-002, Forwards LER 79-002/03L-0 & 79-003/03L-0 | Forwards LER 79-002/03L-0 & 79-003/03L-0 | | | 05000281/LER-1979-002-03, /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | | | 05000280/LER-1979-002-03, /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | | | 05000280/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000280/LER-1979-003-03, /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | | | 05000280/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000281/LER-1979-003-03, /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | | | 05000280/LER-1979-004, Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | | | 05000280/LER-1979-004-01, /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. 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Fuel Removed & Assemblies Rinsed.Investigation Continuing | | | 05000281/LER-1979-013, Forwards LER 79-013/01T-0 | Forwards LER 79-013/01T-0 | | | 05000281/LER-1979-013-01, /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | | | 05000280/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000280/LER-1979-013-03, /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | | | 05000280/LER-1979-014-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. 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