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LER-1979-024, /03L-0 on 790630:64 Fire Barrier Penetrations Not Properly Sealed in safety-related Areas.Caused by Failure to Properly Seal Penetrations During Initial Const. Work Orders Issued & Fire Watches Established |
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&a-n NAME ae____e_B_EP AR ER ll~ L. Stewart
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Surry Power Station, Unit
~Docket: No: 50-280 e
Report No: 79-024/03L-0 Event Date:
06-30--79 Title of Report:
Fire Barrier Penetration Discrepancies
1. Description of Event
During the performance of Periodic Test 24.11, it was noted that 64 of approx-imately 1800 fire barrier penetrations in safety related areas were not properly sealed, and fire watches were not established within the allotted time period.
This is contr_ary to Technical Specifications 3. 21.G.l and 3 *. 21.G. 2.a and is reportable pursuant to-Technical.Specification 6~6~2.b.4. and 6.6.2~b.3., respectively.
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Probable Consequences and Status of Redundant Systems
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The functional integrity of the fire barrier penetration seals ensures that fires will be confined or adequ~tely retarded from spreading to adjacent portions of.the facility. Establishing a'fire watch adjacent to non-functional fire barrier penetration insures prompt detection of a fire.
Because various penetrations were not properly sealed and fire watches not established, a fire in one area could have spread to other areas.of the facility prior to detection or extinguishm~nt. All other fire protection systems.remained operable*, *therefore the health,and safety *..
- of,the general* public were_ not affected. **
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Cause
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s.
The fire barrier penetrations were not properly -sealed at the time of initial construction.
Due to inadequate administrative control, fire watches were not estaolished within one hour, as required, while the discrepqncies were evaluated.
Immediate Corrective Action
Work orders to correct all discrepancies were issued immediately after completion of the procedure.
Subsequent procedure review determined*fire watches
.had not been posted as required.
Fire watches-were then posted in all safety
- - related areas where discrepancies had been not~d during the inspection 5 days prior.
Subsequent Corrective Actions All penetrations were temporarily sealed and the fire watches released.
The fire barrier penetrations will be permanently sealed in accordance with issued work orders and NFPA codes.
- 6. Actions Taken to Prevent Recurrence No further actions are considered necessary at this time.
l Generic Implications r r All fire barrier penetrations have been inspected, and the penetrations with discrepancies have been identified and are being properly sealed.
The current PT-24.11
_will be changed to preclude this situation from reoccurring. Consequently, there are
.no generic implications.
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| 05000281/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000280/LER-1979-001, Forwards LER 79-001/01X-0 | Forwards LER 79-001/01X-0 | | | 05000280/LER-1979-001-01, /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | | | 05000281/LER-1979-001-03, /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | | | 05000281/LER-1979-002, Forwards LER 79-002/03L-0 & 79-003/03L-0 | Forwards LER 79-002/03L-0 & 79-003/03L-0 | | | 05000281/LER-1979-002-03, /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | | | 05000280/LER-1979-002-03, /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | | | 05000280/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000280/LER-1979-003-03, /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | | | 05000280/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000281/LER-1979-003-03, /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | | | 05000280/LER-1979-004, Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | | | 05000280/LER-1979-004-01, /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | | | 05000281/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000281/LER-1979-004-03, /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | | | 05000280/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000281/LER-1979-005-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | | | 05000280/LER-1979-005-03, /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | | | 05000280/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000280/LER-1979-006-03, /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | | | 05000281/LER-1979-006-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | | | 05000280/LER-1979-007-03, /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | | | 05000280/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000281/LER-1979-007-03, /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | | | 05000281/LER-1979-008-03, During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | | | 05000281/LER-1979-008, Forwards Updated LER 79-008/03X-1 | Forwards Updated LER 79-008/03X-1 | | | 05000280/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000280/LER-1979-008-01, /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | | | 05000280/LER-1979-009-01, /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | | | 05000280/LER-1979-009, Forwards LER 79-009/01T-0 | Forwards LER 79-009/01T-0 | | | 05000281/LER-1979-009-03, /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | | | 05000281/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000280/LER-1979-010-03, /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | | | 05000280/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010-03, /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | | | 05000280/LER-1979-011-03, /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | | | 05000280/LER-1979-011, Forwards LER 79-011/03X-1 | Forwards LER 79-011/03X-1 | | | 05000281/LER-1979-011, Forwards LER 79-011/12T-0 | Forwards LER 79-011/12T-0 | | | 05000281/LER-1979-011-12, /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | | | 05000280/LER-1979-012-03, During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | | | 05000280/LER-1979-012, Forwards Updated LER 79-012/03X-1 | Forwards Updated LER 79-012/03X-1 | | | 05000281/LER-1979-012, Forwards LER 79-012/08T-0 | Forwards LER 79-012/08T-0 | | | 05000281/LER-1979-012-08, /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | | | 05000281/LER-1979-013, Forwards LER 79-013/01T-0 | Forwards LER 79-013/01T-0 | | | 05000281/LER-1979-013-01, /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | | | 05000280/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000280/LER-1979-013-03, /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | | | 05000280/LER-1979-014-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | | | 05000280/LER-1979-015-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | |
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