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LER-1979-008, /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const |
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LICENSEE EVENT REPORT
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!During a load study of the Unit 1 480 VAC Emergency Bus, the Architect Engineer dis-
[TITI 1coyered that an under power condition could exist for a postulated loss of coolant J
[o 14] 1accident with or with __ out the loss of off-site power.
This under power condition could J [ill] 1prevent the proper functioning of engineered safeguards equipment.
This condition j
IT.))] 1would exist until loads on the emergency bus w_ere manually shed to a point where the Io !TI !bus could be re-energized. __!!1-i~~ an~~-ent contrary to the intent of Technical Speci::-j
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[~JI] L£_~cation 3.16 and is reportable as per Technical Specification 6.6.2."A.9.
B 9 80 SYSTEM
CAUSE
CAUSE CODE CODE SUBCODE COMPONENT CODE [ill]
~_E-!J@ L~_J@ LU@ IT -1 RI A IN 1s l!J@
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9 10 12 13 18 SEQUENTIAL OCCURRENCE
@ LE R.if10 LVENT YEAR RE.PORT NO.
C0DE REPORT f ! 9 J l:=.I l 0 Io ls J
- 1/1 L..9.. L!J NUMBER 21 22 _
23 24 26 27 28 29 COMP.
SUBCODE
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19 REPORT TYPE
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30 VALVE SUBCODE L3.J@
20 l=1 31 REVISION NO.
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32 COMPONENT ACTION FUTURE EFFECT SHUTDOWN
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ATTACHMENT NPRD-4 PRIME -::;OMP.
TAi<:EN ACTION ON PLANT METHOD HOURS SUBMITTED FORfv1 SUB.
SUPPLIER MANUFACTURER LJ@jF I@)
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36 37 40 41 42 43 1 1 o 1o 1s l CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @
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\\!he under power condition developed as a result of design deficiencies during. construe:.!
OJI] ltion.
The proposed corrective ar.tion is to install an additional Category I, Class lE J [J]Ij t_80 V load cente:.: on each emergency bus.
Alternative solutions are *being investigatedj r::ITIJ I for Unit /12 switchgear.
- The health and safety of the general public were not-affecte(H [ill]
7 8
9 FACILITY STATUS
% POWER OTHER STATUS IT.TI] ~@- L.? I O.j ~J@l,_____1_-JA ____ __.
7 8
9 10 12 13 44 ACTIVITY CONTHlT
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RELEASED OF RELEt,SE AMOUNT OF ACTIVITY
NA
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10 11 44 PERSONNEL EXPOSURES r-:;:;,.
METHOD OF
['.)ISCOVERY DISCOVERY DESCRIPTION @*
Architect Engineer
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45 46 NA LOCATION OF RELEASE @
45 60 J
80 80 NUMBER
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T.YPE DESCRIPTION \\=:v IT.1TI ~O jO !l:J@jNA ------------------------_j 7
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11 12 13 SO PERSONNEL INJURIES Q
NUMBER DESCRIPTION6
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10 jO jO jt-w" NA 7
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12 ____________________________________________
80 LOSS OF OR DAMAGE TO FACILITY '431 TYPE
DESCRIPTION
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10 PUBLICITY
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ISSUEDQDESCRIPTION~
'190410 O).. 'IA [Il_E] l:~J6L ____ N_rA _______
NRC USE ONLY LJ WI 1111111 7
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- ss 69 80 W. L. Stewart NAME OF PREPARER---*----------------
PHONE:--------
804-357-318/1
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(Attachment, paw. of 2)
Surry Power Station, Units 1 & 2 Dockat Nos:
50-280/281 Report No: 79-008/0lT-0 Event Date:
3/23/79 Under Power of 480 V Emergency Bus
- 1.
Description of Event
During a load study of the Unit 1 L180 VAC emergency bus, the Architect Engineer discovered that an under power condition could exist for a postulated loss of coolant accident (LOCA) with or without loss of off-site power.
The projected maximum load following a LOCA for Emergency Bus lH.l was 1661 KVA, or 125;; of rated capacity of the 4160 to 480 VAC transformer and output line circuit breaker 14Hl.
The projected maximum
- 1oad.for bus lJl and output line *circuit breaker is 1737 KVA, or 130%
A load study of Unit !!2 480 VAC emergency bus has not been completed, but it appears a similar under power condition exists.
This event is contrary to Technical Specification 3.16 and is repor-table as per Technical Specification 6,6,2.A.9.
- 2.
Probable Consequences and Status of Redundant Systems:
The probable consequences of an under power condition would be the*
loss of vital engineered safeguards due to the tripping of the output breaker o:f the 4160 to 480 *vAc transformer.
This condition would exist until loads on the emergency bus were manually shed to a point where the bus could be re-energized.
An under power condition was projected to exist on the redundant emergency bus..
The health and safety of the public rwere not affected.
- 3.
Cause
The LOCA under power condition developed as a result of design defi-ciencies during construc.tion.
4,
Immediate Corrective Action
Unit Ill and Unit //2 were in the cold shutdown mode, and will remain in this mode until this deficiency is corrected.
- 5.
Subsequent Corrective Action:
An additfonal Class lE 480 V load center will be established for*each of the emergency buses (lH, lJ),
This will *allmv* the redistribution of sufficient load to eliminate the under power condition on each.bus, and provide the capability for future expansion.
'1, (Attachment, page 2 of 2)
Surry Power Station, Units Docket Nos:
50-280/281 Report No:
79-008/0lT-0 Event Date:
3/23/79 1 & 2*
Under Power on Lf80 V Emergency Bus (Continued)
- 5.
Subsequent Corrective Actions:
(Cont'd:)
Alternate solutions are being investigated for Unit 112 under power conditions ou 480 V emergency load center, due to room restraints and a long lead time for new equipment.
This modification will be accomplished prior to departing cold shutdown.
- 6.
Actions Taken to Prevent Recurrence:
Existing administrative and procedural controls to review any proposed change to the loading scheme of the emergency load centers will be followed.
In addition, a load study will be conducted as a part of the Emergency Bus modification to verify adequate load capability.
- 7.
Generic Implication~:
A load study is being conducted on Surry Unit #2 to determine load and possible corrective actions.
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| 05000281/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000280/LER-1979-001, Forwards LER 79-001/01X-0 | Forwards LER 79-001/01X-0 | | | 05000280/LER-1979-001-01, /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | /01X-0 on 790102:potential non-conservatism Noted in Calculations Performed in Monitoring Heat Flux Hot Channel Factor.Caused by Failure of Sys & Procedures Used for Relevant Surveillance.Input Values Adjusted | | | 05000281/LER-1979-001-03, /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | /03L-0 on 790112:personnel Batch Inner Door & Emergency Escape Manway Not Leak Tested within 72-h After Opening Because Escape Manway Safety Lock Believed Broken, Posing Hazard | | | 05000281/LER-1979-002, Forwards LER 79-002/03L-0 & 79-003/03L-0 | Forwards LER 79-002/03L-0 & 79-003/03L-0 | | | 05000281/LER-1979-002-03, /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter | | | 05000280/LER-1979-002-03, /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | /03L-0 on 790115:electrical Penetration Between Turbine Bldg & Emergency Switchgear Room Not Properly Sealed.Caused by Penetration Being Broken During Previous Implementation of Design Change | | | 05000280/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000280/LER-1979-003-03, /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | /03L-0 on 790124:error Detected in Calibr Procedures for Steam Flow Instrumentation.Caused by Error Made When Calibr Procedures Changed | | | 05000280/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000281/LER-1979-003-03, /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | /03L-0 on 790122: Following Containment Entrance Equipment Hatch Escape Airlock,Outer Door Was Not Proven Sealed within 72-h from Initial Opening.Caused by Problems in Sealing Exterior Hatch | | | 05000280/LER-1979-004, Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | Update to LER 79-004/01X-2:on 790309,A/E Notified Util of Possible Nonconservatisms in Pipe Stress Code Used to Analyze Piping Sys & of Innaccurate Valve Weights Used by Error in Pipe Stress Analysis & Valve Weight | | | 05000280/LER-1979-004-01, /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | /01X-1 on 790309:notification Received of Possible Errors in Pipe Stress Code Analyses in Some Facility Piping Sys.Inaccurate Value Weights Were Also Identified. Plants Are Shut Down Pending Evaluation | | | 05000281/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000281/LER-1979-004-03, /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | /03L-0 on 790204:setpoints of Seven Main Steam Safety Valves Not within Tech Spec Limits.Caused by Normal Setpoint Drift | | | 05000280/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000281/LER-1979-005-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203C Failed to Cycle Electrically.Caused by Slighting Bent Clutch Shaft in Valve Operation.Part Dismantled & Overhauled | | | 05000280/LER-1979-005-03, /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | /03L-0 on 790226:radiation Recorder RR-175 Stopped Printing.Caused by Gummed Gear Shaft Bushing in Print Mechanism.Bushing Was Freed & Print Mechanism Cleaned & Lubricated | | | 05000280/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000280/LER-1979-006-03, /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | /03L-0 on 790309:fire Seals in Barrier Penetration Were Removed & Not Replaced.Leak Test Not Performed on Other Seals That Had Been Reinstalled.Caused by Inadequate Administrative Control | | | 05000281/LER-1979-006-03, /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | /03L-0 on 790204:at Cold Shutdown,Valve MOV-SW-203D Failed to Operate Electrically During Functional Test.Caused by Mechanical Binding of Valve.Valve Bearing Was Replaced | | | 05000280/LER-1979-007-03, /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | /03L-0 on 790320:w/unit Shutdown,Visual Insp Resulted in Declaring One Snubber Inoperable Because of Low Fluid Level.Caused by Leakage from Reservoir Fill Fitting. Snubber Removed & Rebuilt | | | 05000280/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000281/LER-1979-007-03, /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | /03L-0 on 790205:during Functional Test,Damper 1-VS-103A Failed to Close on Train a Safety Injection Initiation.Caused by Hang Up in Brake Mechanism Holding Supply Damper Open Against Closed Spring.Damper Closed | | | 05000281/LER-1979-008-03, During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | During Surveillance Check,Found Deterioration of Piping on Low Portion of Recirculation Spray Subsystems.Caused by Chloride Stress Corrosion.Piping Replaced W/Nonsensitized Piping | | | 05000281/LER-1979-008, Forwards Updated LER 79-008/03X-1 | Forwards Updated LER 79-008/03X-1 | | | 05000280/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000280/LER-1979-008-01, /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | /01T-0 on 790323:during Load Study of 480 Volts Ac Emergency Bus,Discovered That an under-power Condition Could Exist for Postulated LOCA with or W/O Loss of Offsite Power. Caused by Design Deficiencies During Const | | | 05000280/LER-1979-009-01, /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | /01T-0 on 790412:GE Informed Util That Potential Problem Exists in Inside Recirculation Spray Pump Motors.Caused by Possible Overheating of Lower Bearing Due to Clearance Tolerances Allowed on End Shields & Shaft | | | 05000280/LER-1979-009, Forwards LER 79-009/01T-0 | Forwards LER 79-009/01T-0 | | | 05000281/LER-1979-009-03, /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | /03L-0 on 790208:while Performing Penetrant Test 39B-1,mechanic Discovered 3 Snubbers Were Not on Test.Caused by Inadvertent Omission.Change Initiated to Add 3 Snubbers to Penetrant Test 39B-1 | | | 05000281/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000280/LER-1979-010-03, /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | /03L-0 on 790323:while in Cold Shutdown, Discrepancies Found in Location & Configuration of Pipe Supports.Caused by Const Deficiencies & Util Maint.Necessary Repairs Will Be Made Prior to Startup | | | 05000280/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000281/LER-1979-010-03, /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | /03L-0 on 790306:during tests,19 of 30 Snubbers Did Not Meet Acceptance Criteria.Caused by Setting Drift & non-readjustment to Optimum Settings After Previous Satisfactory Tests.Snubbers Readjusted,Repaired or Replaced | | | 05000280/LER-1979-011-03, /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | /03X-1 on 790828:process & Ventilation Particulates & Gaseous Monitors Were W/O Power on Two Occasions.Caused by Loose Lug Connection on Power Supply Cable.Loose Connection Repaired & Plants Restored to Svc | | | 05000280/LER-1979-011, Forwards LER 79-011/03X-1 | Forwards LER 79-011/03X-1 | | | 05000281/LER-1979-011, Forwards LER 79-011/12T-0 | Forwards LER 79-011/12T-0 | | | 05000281/LER-1979-011-12, /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | /12T-0 on 790414:individual Received Excessive Dose While Inspecting Area Beneath Vessel.Caused by Elevated Radiation Levels Due to Incore Instrumentation Refueling Status.Individual Disciplined | | | 05000280/LER-1979-012-03, During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | During Shutdown Functional Test of 74 Snubbers Revealed 21 Not Meeting Design Criteria.Caused by Snubbers Not Being Readjusted to Design Conditions.Units Reset | | | 05000280/LER-1979-012, Forwards Updated LER 79-012/03X-1 | Forwards Updated LER 79-012/03X-1 | | | 05000281/LER-1979-012, Forwards LER 79-012/08T-0 | Forwards LER 79-012/08T-0 | | | 05000281/LER-1979-012-08, /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | /08T-0 on 790507:caustic Residue Discovered on 62 New Fuel Assemblies.Caused by Industrial Sabotage. Fuel Removed & Assemblies Rinsed.Investigation Continuing | | | 05000281/LER-1979-013, Forwards LER 79-013/01T-0 | Forwards LER 79-013/01T-0 | | | 05000281/LER-1979-013-01, /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | /01T-0:on 791007,MOV-SW-202B Operated Mechanically & Electrically in Apparent Reverse Manner W/Unit at Cold Shutdown.Caused by Disc Spline of Svc Water Valve Improperly Aligned to Gear Train of Motor Operator | | | 05000280/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000280/LER-1979-013-03, /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | /03L-0 on 790410:100 Gallons Released from Boron Recovery Test Tank 1-BR-TK-2B Prior to Obtaining Sample Results.Caused by Improper Valve Lineup for Tank Recirculation in Preparation for Sampling | | | 05000280/LER-1979-014-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Instrument Drift in High Alarm Setpoint.All Liquid Waste Releases Were Secured & Alarm Board Checked | | | 05000280/LER-1979-015-03, /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | /03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified | |
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