ML18096B143

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Monthly Operating Rept for Nov 1992 for Salem Generating Station,Unit 1
ML18096B143
Person / Time
Site: Salem 
Issue date: 11/30/1992
From: Fest J, Polizzi V, Shedlock M
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9212160065
Download: ML18096B143 (13)


Text

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Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station December 10, 1992 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Dear Sir:

MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of November 1992 are being sent to you.

RH:pc Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Safety Related Maintenance 10CFR50.59 Evaluations Operating Summary Refueling Information Sincerely yours,

,y0r94rp~

General Manager Salem Operations cc:

Mr. Thomas T. Martin Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19046 Enclosures 8-l-7.R4 The En~w:1\\/ P.cnn!a..

921130

~5A 21 *gg~~ 05000272 PDR*

R 95-2189 ( 1 OM) 12-89

AVERAGE DAILY UNIT POWER LEVEL Docket No.:

50-272 Unit Name:

Salem #1 Date:

12/10/92 Completed by:

Mark Shedlock Telephone:

339-2122 Month NOVEMBER 1992 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET)

(MWe-NET) 1 0

17 1114 2

124 18 1114 3

179 19 1106 4

843 20 1125 5

1078 21 1114 6

1121 22 1113 7

1119 23 1113 8

1116 24 1125 9

1124 25 1094 10 1109 26 1099 11 1109 27 1118 12 1108 28 1123 13 1108 29 1113 14 1091 30 1115 15 1107 31 16 1115 P. 8.1-7 Rl

OPERATING DATA REPORT Docket No:

50-272 Date:

12/10/92 Completed by:

Mark Shedlock Telephone:

339-2122 Operating Status

1.

Unit Name Salem No. 1 Notes

2.

Reporting Period November 1992

3.

Licensed Thermal Power (MWt) 3411

4.

Nameplate Rating (Gross MWe) 1170

5.

Design Electrical Rating (Net MWe) 1115

6.

Maximum Dependable Capacity(Gross MWe) 1149

7.

Maximum Dependable Capacity (Net MWe) 1106

8.

If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason NA

9.

Power Level to Which Restricted, if any (Net MWe)

N/A

10. Reasons for Restrictions, if any ~~~~~~-=N""-=A:.-~~~~~~~~~~~
11. Hours in Reporting Period
12. No. of Hrs. Rx. was Critical
13. Reactor Reserve Shutdown Hrs.
14. Hours Generator On-Line
15. Unit Reserve Shutdown Hours
16. Gross Thermal Energy Generated (MWH)
17. Gross Elec. Energy Generated (MWH)
18. Net Elec. ~nergy Gen. (MWH)
19. Unit Service Factor
20. Unit Availability Factor
21. Unit Capacity Factor (using MDC Net)
22. Unit Capacity Factor (using DER Net)
23. Unit Forced Outage Rate This Month 720 720 0

693.5 0

2231620.8 751810 719986 96.3 96.3 90.4 89.7 3.7 Year to Date 8040 4864.7 0

4459.7 0

14609736.0 4867050 4625513 55.5 55.5 52.0 51.6 25.4 Cumulative 135193 88465.0 0

85507.7 0

270106881. 2 89671680 85402086 63.2 63.2 57.1 56.7 21.5

24. Shutdowns scheduled over next 6 months (type, date and duration of each)

None

25. If shutdown at end of Report Period, Estimated Date of Startup:

NA 8-l-7.R2

NO.

DATE 0036 11/01/92 0044 11/03/92 1

F:

Forced S:

Scheduled UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH NOVEMBER 1992 METHOD OF SHUTTING LICENSE DURATION DOWN EVENT SYSTEM TYPE1 (HOURS)

REASON 2 REACTOR REPORT #

CODE4 F

23.3 A

4 CH F

3.2 B

9 cc 2

3 Reason A-Equipment Failure (explain)

B-Maintenance or Test C-Refuel ing D-Requlatory Restriction E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain)

Method:

1-Manual 2-Manual Scram 3-Automatic Scram 4-Continuation of Previous Outage 5-Load Reduction 9-0ther COMPONENT CODE5 DOCKET NO.: _,5:..:0:....*-=2"-'72=-----

UNIT NAME:

Salem #1 DATE:

12/10/92 COMPLETED BY:

Mark Shedlock TELEPHONE:

339-2122 CAUSE AND CORRECTIVE ACTION TO PREVENT RECURRENCE VAL VEX 12BF19 PACKING LEAK TURBIN TURBINE TRIP TESTING 4

Exhibit G - Instructions for Preparation of Data Entry Sheets for Licensee Event Report CLER) File (NUREG-0161) 5 Exhibit 1 - Same Source

SAFETY RELATED MAINTENANCE MONTH: -

NOVEMBER 1992 DOCKET NO:

UNIT NAME:

50-272 SALEM 1 WO NO UNIT 920825164 900828109 1

911004121 1

920916227 1

921007171 1

921013096 1

921019112 1

921019116 1

921031115 1

921104105 1

DATE:

COMPLETED BY:

TELEPHONE:

DECEMBER 10, 1992 J. FEST (609)339-2904 EQUIPMENT IDENTIFICATION HAGAN SUMMATOR FAILURE DESCRIPTION:

HAGAN SUMMATOR S/N # M0-124 DEFECTIVE -

REWORK 14 REACTOR COOLANT PUMP FAILURE DESCRIPTION:

14 RCP NO. 3 SEAL LEAKING -

DISASSEMBLE AND INSPECT AND/OR REPLACE 1R46 RADIATION MONITOR FAILURE DESCRIPTION:

1R46 CABINET FANS BAD -

REPLACE VALVE 12SW387 FAILURE DESCRIPTION:

REPAIR DOWNSTREAM SPOOL 1-SW-P-1108 1R41 RADIATION MONITOR FAILURE DESCRIPTION:

APD VENT FAN NOT WORKING -

REPLACE VALVE 11SW127 FAILURE DESCRIPTION:

11SW127 EXCEEDED STROKE TIME -

INVESTIGATE AND CORRECT VALVE 1SW185 FAILURE DESCRIPTION:

1SW185 FAILED STROKE TIME -

INVESTIGATE AND CORRECT VALVE 11SW122 FAILURE DESCRIPTION:

11SW122 FAILED STROKE TIME -

INVESTIGATE AND CORRECT MAIN STEAMLINE RADIATION MONITOR FAILURE DESCRIPTION:

MONITOR RECORDER READS HIGH -

INVESTIGATE VALVE 12SW129 FAILURE DESCRIPTION:

12SW129 EXCEEDED STROKE TIME -

INVESTIGATE AND CORRECT

.SAFETY RELATED MAINTENANCE MONTH: -

NOVEMBER 1992 DOCKET NO:

UNIT NAME:

50-272 SALEM 1 (cont'd)

WO NO UNIT 921104175 1

921122096 1

921124055 1

921124079 1

DATE:

COMPLETED BY:

TELEPHONE:

DECEMBER 10, 1992 J. FEST (609)339-2904 EQUIPMENT IDENTIFICATION 12CV160 -

12 eve BAT INLET FAILURE DESCRIPTION:

REPLACE FAILED LOCAL PRESSURE GAGES 12 STEAM GENERATOR LEVEL FAILURE DESCRIPTION:

12 S/G LEVEL CHANNEL 3 INDICATING LOW -

INVESTIGATE AND CORRECT 12 STEAM GENERATOR LEVEL FAILURE DESCRIPTION:

12 S/G LEVEL CHANNEL 1 IS 3% OUT INVESTIGATE AND CORRECT 11 STEAM GENERATOR LEVEL FAILURE DESCRIPTION:

11 S/G LEVEL APPROACHING OOS -

INVESTIGATE AND CORRECT

NOVEMBER 1992 DOCKET NO:

UNIT NAME:

DATE:

COMPLETED BY:

TELEPHONE:

50-272 SALEM 1 DECEMBER 10, 1992 J. FEST (609)339-2904 The following iteins were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59.

The Station Operations Review Committee has reviewed and concurs with these evaluations.

ITEM

SUMMARY

A.

Design Change Packages (DCPs) lEC-3157 Pkg 2 lSC-2267 Pkg 4 "Chemical Waste Discharge Line" -

This change adds a new Chemical Waste Discharge line from the Turbine Building to the Non-Rad Basin.

This line will run above ground over the walkway between the Turbine Building southwest corner and the B Building north wall.

It then runs along the north and west B Building walls to a point opposite the Non-Rad Basin.

The line then drops underground to transverse the roadway between the B Building and the basin.

At the basin this new line will dump into the basin separately from the existing line and will also connect to the existing bypass to the clarifiers.

In the Turbine Building, on elevation 88', this line connects to the existing Chemical Waste line from the Salem Units 1 and 2 Condensate Polishing High Conductivity sumps* and also the Hope Creek Demineralized Water Makeup System.

This allows the existing underground Chemical Waste line to provide dedicated service for the Salem Demineralized Water Makeup System Chemical Waste Tank.

Isolation valves are provided at elevation 88 1 so that either line can be used for all services if required.

This DCP will also remove the existing acid and caustic storage tank level bubblers from the storage tanks and from the area on elevation 100 where the new discharge line will penetrate the building wall at an existing wall opening.

The operation of the Demineralized Water Make Up and Condensate Polishing Systems are not addressed in the Technical Specifications.

Therefore, there is no reduction in the margin of safety as defined in the basis for any Technical Specification.

(SORC 92-114)

"SEC Circuit -

Service Water Pump Start Test switch Installation" Rev. 1 -

The purpose of this change is to provide a permanently mounted key lock test switch in the 14 service water pump

'!OCFR50.59 EVALUATIONS MONTH: -

NOVEMBER 1992 (cont'd)

ITEM lEC-3105 Pkg 1 DOCKET NO:

UNIT NAME:

DATE:

COMPLETED BY:

TELEPHONE:

SUMMARY

50-272 SALEM 1 DECEMBER 10, 1992 J. FEST (609)339-2904 circuit breaker cubicle.

The switch will be installed in the service water pump SEC circuitry, and when placed in the "Test" position, will ensure that two service water pumps are available to provide flow to the plant (Minimum Safeguards Requirement) powered from different vital busses during performance of SP(0)4.0.5-P-SW (14-16),

Full Flow Test Surveillance, with an SEC Mode Operation.

This modification will also eliminate the current practice of lifting a lead in the SEC cabinet during performance of SP(0)4.0.5-P-SW (14-16), and provide an added degree of personnel safety.

Since the installation of a key lock test switch does not affect the subject Technical Specification Requirement, the margin of safety as defined in the Basis of the Technical Specifications is not reduced.

(SORC 92-115)

"Rad Waste Panel 104 Modifications" Rev.1 -

The purpose of this change is to modify Rad Waste Panel 104 and associated instruments and equipment.

Work will include upgrading of instrument loops with new components, physical repair of Panel 104, removal of equipment no longer needed, and a functional verification of each instrument loop.

The instruments being replaced include indicating switches which are used to monitor administratively controlled evolutions within the Liquid Radwaste, Gaseous Waste, and eves Systems. The replacement components are similar in fit and function to the existing instruments except that,the Helicoid indicating switches do not permit indication beyond the setpoint values. The switches have "control tabs" on the setpoint indicators which lock in the alarm value but prevent the indicating needle from passing the setpoint indicator.

Process values beyond the setpoint will not be shown to the operator.

The purpose of this revision of the DCP is to authorize revision of OD-36 to ensure that daily checks of instrument setpoint locations will occur. The new method of indication has been analyzed and no unresolved safety question is involved.

(SORC 92-116)

NOVEMBER 1992 (cont'd)

ITEM DOCKET NO:

UNIT NAME:

DATE:

COMPLETED BY:

TELEPHONE:

SUMMARY

50-272 SALEM 1 DECEMBER 10, 1992 J. FEST (609)339-2904


~------------------

lEA-01034 Pkg 1 lEE-0011 Pkg 1 "Reclassification of Liquid Radwaste Piping Between 1WL91 and 1WL385 11 The purpose of the design change is to reclassify the piping classified SP53B (Nuclear Class III, Seismic Class III) between valve numbers 1WL91 and 1WL385 to SP53P (non-Nuclear, Seismic Class III). The working and design pressure and temperature of both specs are the same, as are the material requirements.

This piping was originally conservatively classified as safety-related because the criteria for classification at the time of construction had not been finalized. The relevant guidelines are those of Reg. Guide 1.143.

The Technical Specifications refer to the treatment of the effluent prior to release to an unrestricted area.

If the system is not operating or leaks into the Auxiliary Building, no radioactive effluent will be released without being treated.

Therefore, the margin of safety

~or any of the Technical Specifications will not be reduced.

(SORC 92-117)

"Traveling Screen Blowdown*i -

This engineering change installs three 2 11 stainless steel blowdown lines, associated shutoff valves and supports from the three fish spray wash headers located in No.

13B traveling screen in the Circulating Water Intake Structure.

The nozzles of the traveling screen fish spray wash headers frequently clog with silt and grass which restricts or totally blocks water spray.

Currently, the nozzles must be unplugged manually by unscrewing and clearing each nozzle individually.

This process requires a traveling screen outage and maintenance personnel to climb onto and into the traveling screens which requires approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to complete.

Opening the shutoff valve will flush out the debris and silt from the spray headers, thus clearing the spray nozzles.

The water will be discharged back into the bay.

There is no reduction in the margin of safety as defined in the basis for any Technical Specification.

(SORC 92-118)

-10CFR50. 59 EVALUATIONS MONTH: -

NOVEMBER 1992 (cont'd)

ITEM DOCKET NO:

UNIT NAME:

DATE:

COMPLETED BY:

TELEPHONE:

SUMMARY

50-272 SALEM 1 DECEMBER 10, 1992 J. FEST (609)339-2904 B.

Procedures and Revisions NC.NA-AP.ZZ-0048(Q)

Sl.OP-SO.BR-OOOl(Z)

"Station Performance Monitoring Program" Rev. 1 -

The purpose of this change is as follows: 1) Adds a requirement for the System Engineered to initiate a design change request for selected component problems, 2) Adds responsibilities relative to component monitoring (Section 3.7).

Reference:

1991 INPO report, 3) Adds a requirement to consider adding circulate system components that have experienced failures (two or more times within an 18 month period) to the program in elimination of the failures would increase the reliability of the related system, 4) Adds a requirement for the responsible system Engineer to initiate appropriate corrective action(s) for excessive component failures and if none are required, so indicate, 5) Deletes former Section 5.7, ASME Section XI Component Testing Effectiveness, and Unplanned Capability Loss Factor to Definitions.

The revision to the procedure does not change the intent of the administrative controls for performance monitoring.

The overall program has been enhanced by adding responsibilities relative to component monitoring as committed to in response to the 1991 INPO assessment of Salem and providing industry operating experience feedback to the Technical Departments.

This revision cannot reduce the margin of safety as defined in the basis of any Technical Specification.

(SORC 92-115)

"Boric Acid Evaporator Operations" Rev. o - The purpose of this procedure is to provide direction for the operation of the Boric Acid Evaporator.

This new procedure allows for transfer of the Boric Acid Evaporator bottom to the CVCS Holdup Tank or the Boric Acid Tank.

The intent of the UFSAR was to ensure that the evaporator bottoms were sampled prior to discharge to the eves HUT or the Boric Acid Tank. The UFSAR implies allowance for sampling without transfer to the concentrates holding tank because it mentions the existence of a sample connection at the discharge of the boric acid concentrates' pump.

This procedure places procedural controls on boron concentration of the

'10CFR50. !59 EVALUATIONS MONTH: -

NOVEMBER 1992 (cont'd)

ITEM NC.NA-AP.ZZ-0036(Q)

DOCKET NO:

UNIT NAME:

DATE:

COMPLETED BY:

TELEPHONE:

SUMMARY

50-272 SALEM 1 DECEMBER 10, 1992 J. FEST (609)339-2904 bottom concentrates that are discharged to the CVCS HUT and/or the Boric Acid Tanks.

The boron recovery system is not used for accident mitigation, therefore, this procedure does not reduce the margin of safety as defined in the basis for any Technical Specification.

(SORC 92-116)

"Control of Information System and Computer Resources" Rev. 1 -

The purpose of this revision is as follows: 1) This revision meets the biennial review requirements of NC.NA-AP.ZZ-0032(Q), 2)

This revision clarifies when an Information Systems Request is required, 3) Changes have been made to address user responsibilities, 4) A software policy has been addressed, 5) Section on "System Usage" had been moved to NC.NA-AP.ZZ-0064(Q), Software Quality Assurance.

The Technical Specifications do not address Information Systems or Computer Resources, therefore the margin of safety for the basis of any Technical Specification is not reduced.

(SORC 92-118)

SALEM UNIT NO. 1 SALEM GENERATING STATION MONTHLY OPERATING

SUMMARY

UNIT 1 NOVEMBER 1992 The Unit began the period shutdown for repairs to 12BF19 and various other leaks on the Service Water, Heater Drain and Main Steam systems.

A startup was* commenced on November 1, 1992, and the Unit was restored to full power on November 5, 1992.

The Unit continued to operate at essentially full power throughout the remainder of the period.

'REFUELil(G INFORMATION MONTH: -

NOVEMBER 1992 MONTH NOVEMBER 1992 DOCKET NO:

UNIT NAME:

DATE:

COMPLETED BY:

TELEPHONE:

1.

Refueling information has changed from last month:

YES NO X

2.

Scheduled date for next refueling:

OCTOBER 2, 1993 50-272 SALEM 1 DECEMBER 10, 1992 J. FEST (609)339-2904

3.

Scheduled date for restart following refueling:

DECEMBER 13, 1993

4.

a)

Will Technical Specification changes or other license amendments be required?:

YES NO NOT DETERMINED TO DATE ~-x~-

b)

Has the reload fuel design been reviewed by the Station Operating Review Committee?:

YES NO x

If no, when is it scheduled?:

5.

Scheduled date(s) for submitting proposed licensing action:

N/A

6.

Important licensing considerations associated with refueling:

7.

Number of Fuel Assemblies:

a.

Incore 193

b.

In Spent Fuel Storage 656

8.

Present licensed spent fuel storage capacity:

1170 Future spent fuel storage capacity:

1170

9.

Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:

September 2001 8-1-7.R4