ML18086B366

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IE Insp Repts 50-272/82-01 & 50-311/82-01 on 820101-0208. Noncompliance Noted:Failure to Follow Radiation Protection & Implementation Procedures,Failure to Properly Approve & Issue Procedure
ML18086B366
Person / Time
Site: Salem  
Issue date: 02/24/1982
From: Greenman E, Hill W, Norrholm L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18086B364 List:
References
50-272-82-01, 50-272-82-1, 50-311-82-01, 50-311-82-1, NUDOCS 8203160505
Download: ML18086B366 (16)


See also: IR 05000272/1982001

Text

. .

~.

Report Nos.

Docket-Nos.

U. S. NUCLEAR REGULATORY COMMISSION

50-272/82-01

50-311/82-01

50...:272

50-311

DPR-70

REGION I

License Nos.

DPR-75

~~~~...---~~~~~~~

Licensee:

Public Service Electric and Gas Company

80 Park Plaza

Newark, New Jersey

07101

050272-820119

050272-820131

050272-820201

050272-820205

050311-820114

050311-820201

050311-.;820205

Facility Name:

Salem Nuclear Generating Station - Units 1 and 2

Inspection At:

Hancocks Bridge, New Jersey

8' 1982

Inspectors:

Approved By:

No. 2A,

Inspection Summary:

-@.(!z._

1 da e

~hLF1-

'Ciate

~Uk~

date

Inspections on January 1 - February 8, 1982 (Combined Report Numbers 50-272/82-01

and 50-311/82-01)

Unit 1 Areas Inspected: Routine inspections by the resident inspectors of

plant operations including tours of the facility; conformance with Technical

Specifications and operating parameters; log and record reviews; reviews of

licensee events; and followup on previous inspection items. The inspection

involved 62 inspector hours by the r~0siAent NRC inspectors.

. .

Results:

T#o~.*1te.ms.. of. nQf.l~QJJ1pU~ncE;,.we.r¢. * tclenttf.t~~' .{f,&flure *1ct~ follq\\.:t **PTOC~clures -

Paragraph 3~:. Pai'l ure *to fol low. radiati'cl'h protection procedure *:. Paragrapll * 4)

Unit 2 Areas Inspected: Routine inspections by the resident inspectors df *

plant operations including tours of the facility; conformance with Technical

Specifications and operating parameters; log and record reviews; reviews.of

licensee events; and followup on previous inspection items.

The inspection

involved 86 inspector hours by the resident and regional NRC inspectors.

Results: Three items of noncompliance were identified (Failure to follow/

implement procedures ...: Paragraphs 3, 4, and 6, failure to properly approve

and issue a procedure - Paragraph 6, failure to make a report in accordance

with 10 CFR 50.72 - Paragraph 6).

..

.

..

DETAILS

1. Persons Contacted

J. Driscoll, Assistant General Manager - Salem Operations

L. Fry, Operations Manager

J. Gallagher, Maintenance Manager

H. Midura, General Manager - Salem Operations

L. Miller, Technical Manager

J. O'Connor, Radiation Protection Engineer

F. Schnarr, Reactor Engineer

R. Silverio, Assistant to the General Manager

J. Stillman, Station QA Engineer

The inspector also interviewed other licensee personnel during the

course of the inspections including management, clerical, maintenance,

operations, performance and quality assurance personnel.

2. Status of Previous Inspection Items

lClosed) Unresolved Item (311/78-43-01)

Insulation removal during

in-service inspection of supports. The licensee uses

section IWF-1300 paragraph (e) of Article IWF-1000 of the

ASME Code as justification for not removing insulation

during support inspections. Accordingly, procedure M17B,

Coded Component and Pipe Support Visual Examination (Classes

1, 2, and 3), Revision*:7, dated January 6, 1982 states,

11Supports that are not welded to the system where the system

is insulated may be inspected without removing insulation

provided no stress is apparent. Supports that are welded to

the system shall have the insulation removed before inspection

is performed." The inspector had no further questions on

this item.

(Closed} Follow Item (272/81-19-01) Chemistry technician training.

Training procedure No. 41 Setting forth the training program

for chemistry technicians has been completed and issued on

December 2, 1981.

The inspector had no further questions on

this item.

(Closed)-- Follow Item (272/81-19-02) Training records for I&e: helpers.

  • The training records for I&C helpers have been completed,

updated and are maintained by the ,performance Department.

The inspector had no further questions on this item.

i.,*

.,

..

3

SITE

3. Shift Logs and Operating Records

a.

The inspector reviewed the following plant procedures to detennine

the licensee established requirements in this area in preparation

for a review of selected logs and records.

AP-5, Operating Practices, Revision 11, August 13, 1981;

AP-6, Incident Reports and Reportable Occurrences, Revision 7,

October 8, 1981;

AP-13, Control of Lifted Leads and Jumpers, Revision 4, February

11, 1980;

Operations Directive Manual; and,

AP-15, Safety Tagging Program, Revision 1, November 21, 1980.

b. Shift logs and operating records were reviewed to verify that:*

Control room log sheet entries are filled out and initialled;

Auxiliary log sheets are filled out and initialled;

Log entries involving abnormal conditions provide sufficient

detail to conununicate equipment status, lockout status, correc-

tion and restoration;

Log book reviews are being conducted by the staff;

Operating orders do not conflict with Technical Specification

requirements;

Incident reports detail no violation of Technical Specification

LCO or reporting requirement; and,

Logs and records were maintained in accordance with Technical

Specifications and the procedures in 3.a above.

c.

The review included examination of the following plant shift logs

and operating records and discussions with licensee personnel:

Log No. 1 - Control Room Daily Log, January 1 - February 8, 1982

Log No. 6 - Primary Plant Log, January 1 - February 8, 1982

4

Log No. 7 - Secondary Plant Log, January 1 - February 8, 1982

Log No. 8 - Unavailable Equipment Status Log, January 1 -

February 8, 1982

Night Orders, December 23, 1981 - January 6, 1982

Lifted Lead and Jumper Log - All active

Tagging Requests - All active

Nonconformance Reports for December 1981 and January 1982

d.

During the log review, the inspector identified two instances,

on January 23, 1982, in which maintenance contractor personnel

started work on the service water and safety injection systems

prior to proper isolation of the systems.

In each case, the system

was still filled and pressurized when breached.

No personnel injury

or contamination resulted in either case. Station Administrative

Procedure 15 (AP-15) requires that the supervisor in charge of the

work assure himself that the system or equipment is isolated and

the tags are in place before any work is started. The above failures

to secure this assurance contribute to noncompliance with Technical

Specification'6.8.1 (272/82-01-01).

In addition, during this period,

an attempt to clear tags on service water to containment fan coil

units was aborted by operators when the system was found not to

have been restored.

One control valve had not been reinstalled in

the system.

e.

The inspector had no further questions with respect to logs and

records reviewed.

4.

Plant Tour

a.

During the course of the inspections, the inspector made observations

and conducted multiple tours of plant areas, including the following;

(1)

Control Room (daily)

(2)

Relay Rooms

(3)

Auxiliary Building

~)

Vital Switchgear Rooms

~}

Turbine Building

..

b.

5

(6)

Yard Areas

(7)

Radwaste Building

(_8)

Penetration Areas

(9)

Control Point

(10) Site Perimeter

(11)

Fuel Handling Building

(12}

Guard House

(13)

Containment (Unit 1)

The following detenninations were made:

Monitoring instrumentation. The inspector verified that selected

instruments were functional and demonstrated parameters within

Technical Specification limits.

Valve positions. The inspector verified that selected valves were

in the position or condition required by Technical Specifications

for the applicable plant mode.

This verification included exam-

ination of control board indication and field observation of valve

positions (Charging/Safety Injection, Auxiliary Feedwater, and

Containment Spray Systems).

Radiation Controls.

The inspector verified by observation that

control point procedures and posting requirements were being

followed and that Radiation Exposure Pennits were properly employed.

Plant housekeeping conditions. The inspector observed that with

limited exceptions, housekeeping was generally acceptable.

Any

cluttered or littered areas for which maintenance was not in

progress, was brought to the attention of the plant management

or operating staff.

Fluid leaks.

No fluid leaks were observed which had not been

identified by station personnel and for which corrective action

had not been initiated, as necessary.

Piping vibration.

No excessive piping vibrations were observed

and no adverse conditions were noted .

..

6

Selected pipe hangers and seismic restraints were observed and

no adverse conditions were noted.

Equipment tagging.

The inspector selected plant components for

which valid tagging requests were in effect and verified that

the tags were in place and the equipment in the condition speci-

fied.

By frequent observation through the inspection, the inspector

verified that control room manning requirements of 10 CFR 50.54

(k} and the Technical Specifications were being met.

In addition,

the inspector observed shift turnovers to verify that continuity

of system status was maintained.

The inspector periodically

questioned shift personnel relative to plant conditions and

their knowledge of emergency procedures.

Releases.

On a sampling basis, the inspector verified that appro-

priate documentation, sampling, authorization, and monitoring

instrumentation were provided for effluent releases.

Fire protection. The inspector verified that selected fire ex-

tinguishers were accessible and inspected on schedule, that fire

alann stations were inspected on schedule, that fire alarm sta-

tions were unobstructed and that cardox systems were operable.

Technical Specifications. Through log review and direct observa-

tions during tours, the inspector verified compliance with

Technical Specifications including Limiting Conditions for

Operation (LC0

1s}. The following parameters were sampled fre-

quently:

RWST level, BAST level and temperature, containment

temperature, boration flow path, offsite power, BAST and

Accumulator chemistry.

In addition, the inspector conducted

periodic visual checks of protective instrumentation and inspec-

tion of electrical switchboards to confinn availability of safe-

guards equipment.

Security. During the course of these inspections, observations

relative to protected and vital area security were made, including

access controls, boundary integrity, search, escort, and badging.

c.

The following acceptance criteria were used for the above items:

Technical Specifications

Operation Directives Manual

Inspector Judgement

..

7

d.

During a tour of Unit 1 Containment on January 8, 1982, the inspector

identified at least three individuals inside the bioshield who were

not attired as required by Radiation Exposure Permit (REP) 0008.

The

REP required that, for entries inside the biological shield, both

caps and hoods were to be worn in addition to the standard protective

coveralls, gloves and boots.

On February 2, 1982, during a tour of

the Unit 1 Fuel Handling Building, the inspector identified one in-

dividual who was present in the posted contaminated area with no

coveralls or laboratory coat. The least restrictive Radiation Ex-

posure Permit (REP) for the area, EREP # 9901, required protective

clothing for inspection tours in contaminated areas. Adherence to

stated requirements of Radiation Exposure Permits is dictated by

station Administrative Procedure 24, Radiological Protection Program.

The above failures to comply with REP requirements contribute to

noncompliance with Technical Specification 6~11: (272/82-01-03).

e.

The inspector had no further questions relative to tours made during

this inspection.

5.

Review of Periodic and Special Reports

Upon receipt, periodic and special reports submitted by the licensee

pursuant to Technical Specifications 6.9.l and 6.9.2 were reviewed by

the inspector.

This review included the following considerations:

The report included the information required to be reported by

NRC requirements;

Test results and/or supporting information were consistent with

design predictions and performance specifications;

Planned corrective action was adequate for resolution of identi-

fied problems; and,

Determination whether any information in the report *should be

classified as an abnormal occurrence.

Within the scope of the above, the following periodic reports were re-

viewed by the inspector:

Unit 1 Monthly Operating Report - December 1981

Unit 2 Monthly Operating Report - December 1981

No unacceptable conditions were identified.

..

6. Operating Events

a.

UNIT 1

8

(1) The unit was shutdown to start the third refueling outage on January

1, 1982, and entered Mode 6 on January 11, 1982.

By January 20, 1982, the licensee had completed eddy current testing

of steam generator tubes in Steam Generators 12 and 14, with the

following results:

Steam Generate>'r 12

947 tubes tested

3 defective

2 degraded

Steam Generator 14

1551 tubes tested

8 defective 24 degraded

All defective tubes were plugged.

Both degraded tubes in Steam

Generator 12 and 9 degraded tubes in Steam Generator 14 were plugged.

The licensee has elected to plug all defective tubes with greater

than 30 % wall thinning. All indications were found in peripheral

tubes, within five rows of the edge. All indications are located at

the first, second, and/or third support loc~tions and are in the cold

leg. Licensee Event Report 272/82-02 was submitted to document the

initial findings.

The licensee plans to inspect Steam Generators 11

and 13 prior to conclusion of the outage. Additionally, the licensee

has submitted an amendment request for relief from 100 % inspection

on the basis that this problem is confined to peripheral tubes. This

item will be inspected further on receipt of the final report and

final licensing action prior to startup (272/82-01-02).

(2) By February 1, 1982, all fuel had been removed from the reactor and

fuel inspection, using a remotely-operated TV system, identified one

failed fuel pin.

On assembly C-04, pin 9 face 2, between grid straps

7 and 8, had two complete ruptures, exposing the fuel pellets, and

a circumferential crack. Visual evidence of corrosion or wear was

found at the break sites. The assembly was scheduled for discharge

during this outage and has a total burnup of 34,674 MWD/MT.

Inspec-

tion of this assembly during the previous outage had identified pin

gap closure at this location to the extent that the two adjacent

pins may have been touching. This had been judged acceptable at the

time.

Dose equivalent Iodine just prior to shutdown on December 31,

1981 was 1.68 E-2 uCi/ml.

Complete inspection of the 33 remaining

assemblies with the same burnup scheduled for re-use in the next

cycle identified no other failures.

Prompt Licensee Event Report

272/82-05 was submitted. Vendor evaluation of the failure mechanism

is continuing.

No similar gap closures were identified in reload

fuel assemblies. This event will be reviewed further when the final

licensee event report is issued *

..

(3)

(4)

9

At approximately 9:15 a.m. on February 1, a temporary connection

between the Unit 1 and Unit 2 Spent Fuel Pool Heat Exchangers

failed and spilled up to 30,000 gallons of Unit 1 Spent Fuel Pool

Water into the Unit 1 and 2 Auxiliary Buildings on elevations 84'

and 64'. To support a complete shutdown of the Unit 1 Component

Cooling System, the Spent Fuel Cooling system had been cross-

connected to the Unit 2 Spent Fuel Heat Exchanger via an 8"

diameter hard rubber hose. The hose slipped off a connection at

the Auxiliary Building dividing wall. The resulting spill dropped

level in the Spent Fuel Pool by approximately one foot.

The re-

ported maximum water level was 3" on elevation 64' before floor

drains lowered the level. Surface contamination levels to 3000

cpm were measured.

No airborne activity was found in the Auxiliary

Building. A slight increase in the plant vent monitor was noted,

resulting in a release less than 0.1 % of the instantaneous release

limit. Sixteen persons received contamination to shoes and trousers.

The most recent fuel pool gross activity was 7.2E-4 uCi/ml. Follow-

ing the hose failure, the Unit 1 Component Cooling System was re-

turned to service. Spent Fuel Pool temperature never exceeded

820F and level did not go below the 23 feet required above stored

fuel. The licensee will make a written 30-day report. The hose

installation was strengthened by the addition of another hose clamp,

for a total of three, at each fitting, specifying torque values for

clamp bolts, the addition of safety chains, and periodic surveillance

for slippage while the system was in service.

In addition, the

doors to switchgear rooms were sealed to prevent or reduce the amount

of water leaking in, should the hose fail again.

No recurrence or

slippage of the hose was identified when the system was returned to

service.

At approximately 11:00 a.m. on February 5, a health physics tech-

nician noticed lint being blown out of a dryer vent at the trailer

facility being used to launder used protective clothing.

An air

sampler was operating at the vent discharge and showed air activity

levels on the order of E-11 uCi/cc gross beta~ An area of the yard

approximately 10 feet on a side was covered with the lint discharge.

Maximum levels read with a frisker were 9000 dpm. A bypass flow-

path had developed in the discharge filter on the dryer.

The dryer

was shutdown, the area roped off and cleaned up, and the filter

replaced. Based on the potential for an unplanned release, the

licensee notified the NRC duty officer via ENS at 1:10 p.m.

The

Senior Resident Inspector was informed at 11:30 a.m. and a Radiation

Specialist already on site followed licensee actions.

No personnel

we_re contaminated.

The total postulated release was less'than 0.1

uCi. A Licensee Event Report will be submitted *.

... ,

" ...

10

Time

b.

UNIT 2

(1} Continuing problems with freezing of circulating water screens~,

required taking the generator off line at 6:55 p.m. on January 11.

The reactor remained in Mode 2.

The unit was again synchronized

at 11:14 p.m. on January 11.

l2} On January 14, 1982, Salem Unit 2 experienced a load reduction

transient which involved loss of rod control, an unseated secondary

safety valve, elevated average temperature and restoration of plant

stability without a trip. The initiating event was a reduction

in Steam Generator Feedwater Pump (SGFP} suction pressure precipi-

tated by instability in the heater drain system.

Due to several

previous trips attributed to such instability (reference NRC

Inspection Reports 50-311/81-27 and 81-29}, the licensee had

established guidelines for dealing with loss of suction pressure

and had installed a temporary alarm (set at 300 psig} to warn

operators that pressure was approaching the SGFP trip point of

215 psig. These guidelines called for bypassing the Condensate

Polishing System {CPS} and reducing turbine load in 10 % incre-

ments.

The inspector developed the following sequence of events based

on review of records, process parameter recorder charts, and

discussions with personnel.

Chart Parameters

Reactor Stm

Pzr

MWe

Power

Flow Pressure

Tavg

0104 Slight dip in heater drain pump

flow on recorder chart

0105

21 Heater Drain Tank high level 1060

0106 Intermittent, then steady, SGFP 1060

94

94

95

95

2230

2250

568

568

  • low suction pressure alann (300

psig}~ Operator initiated load

reduction by intennittently re-

ducing valve position limit.

Started manual rod insertion!

Immediate Urgent Failure Alann.

No further rod motion possible

in manual or auto. Bypassed

condensate polisher. Started

manual boration at 10 gpm.

.

.,

"*

11

Reactor Stm

Pzr

Time

Mwe

Power

Flow Pressure

Tavg

0107

SGFP suction pressure alann clears 230

92

85

2240

575

when CPS bypass valves fully open.

Terminate load reduction at 450,

load continues to drop to 230.

0108

SGFP suction pressure alann comes

240

89

74 ' 2230

582

up and.clears again. All high

steam flow alarms up.

Four steam

dump valve groups fully open,

remainder throttling.

0109 Tavg decreasing from 582, SGFP

250 89.5

74

2220

580

low suction pressure alarm.

SSS

enters control room, orders load

increase.

0110

SGFP low suction pressure alann

260

90

82

2210

578

clear.

22 and 24MS 167 (MSIV)

"open" lights out. Operator taps

11open

11 push button and "open

11

light immediately comes on.

0111

260

91

65

2210

576

0112

260

91

48

2200

574

0113 Begin increasing turbine load.

260

92

58

2200

574

Steam dump holding Tavg at 574

0114

310

91

58

2190

574

0115

350

89

58

2200

574

0116

400

86

58

2250

574

0117 Operator resets load rejection.

440

84

58

2290

574

0118 Pressure peak, full spray.

490

82

58

2340

592

Tavg peak

0119

530

80

56

.2290

590

0120 Tavg decreasing.

550

77

56

2250

589

SG pressure 1080.

23 MSL safety valve lifts

(23 MS 15 only::Oconfinned visually)

  • ,

. .

Time

0121

0122

0123

0124

0125

0126

0127

0128

0129

0130

0131

0132

0133

0134

0135

0136

0138

0145

0148

12

Mwe

560

570

Stop boration at 98 gallons

580

590

600

610

620

625

630

630

630

640

650

660

Spray demand at zero.

2PS3 spray 670

valve

11closed

11 light not lit.

Operator taps

11close

11 push button

and light illuminates.

650

Pressurizer pressure 2050 psig

(lowest) increasing. Heaters on.

Spray closed.

Request Chemistry sample.

Pressure 2140 psig increasing.

Tavg 558.

Safety still blowing

(audible).

Reactor Stm

Pzr

Power

Flow Pressure

Tavg

77

56

2240

588

77

56

2230

587

76

56

2220

586

75

56

2210

585

72

53

2205

584

71

50

2200

584

70

47

2190

583

69

44

2190

582

68

40

2180

580

67

40

2165

580

65

40

2150

578

64

40

2135

576

63

40

2120

574

60

40

2100

572

58

40

2090

570

56

40

2080

568

13

Time

0149

(appr) Pressure peaks at 2260 psig.

0150 Spray and heaters in auto.

Pressure controller in manual due

to saturation.

0210 Pressure stable

2230.

Level stable

25 %.

Tavg stable

550.

Power

46 %.

Turbine load 480 MWe.

Urgent failure alarm still up.

Safety blowing.

0225 Call to operations Manager and Asst. General Manager

0230 Cycle 23 MS 10 three times to seat 23 MS 15 ~ doesn

1t work

0300 Sample results I-131 1.4E-3Uci/ml

0330 Operations Manager on site

0521

23 MS 15 reseated by removing manual operating yoke pin

0730

Rod control restored

The inspector

1s review of this transient developed the following observa-

tions.

Technical Specification 3.2.5 establishes the following DNB related

Limiting Conditions for Operation in Mode 1; TavgS..582 degrees F,

Pressure 2!2220 psia. The accompanying ACTION Statement requires re-

storation of the parameter to within limits within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> or a reduction

to less than 5 % of rated thennal power within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

The pressure

limit is not applicable during thermal power changes in excess of 5 %/

minute.

The control room chart indicates that Tavg exceeded 582 degrees

F for a period of approximately 11 minutes, peaking at 592 degrees F.

Pressure decreased below 2220 psia on two occasions. First, for

approximately 5 minutes, dropping to 2205 psia. The second, for

approximately 22 minutes, dropping to 2065 psia.

At no time during the event were reactor protection system or emergency

safeguards system setpoints exceeded.

No automatic trip was initiated.

Control room charts indicate no significant difference in steam flow

instruments for the four steam generators during the period that valve

23 MS 15 remained unseated.

Differential pressure alarms did not

annunciate.

14

With respect to procedures, the operators employed Emergency Instruc-

tion I-4.8, Rod Control System Malfunction, which does not require

manual reactor trip on a Rod Urgent Failure alann. The procedure calls

for stabilizing the plant and boration to restore Tavg.

No limits on

Tavg are specified in this procedure. Operator action on load reduc-

tion was consistent with Operating Instruction 'I-3.4, Power Operation.

Operating Instruction III-2.3.4, Steam Dump System - Normal Operation

states that the load rejection interlock is to be reset after equilibrium

conditions are reached.

The effect of this reset is to disann the dumps

and cause all the steam dump valves to shut. At the time this was

accomplished, indicated thermal power was 84 % and turbine load was 440

MWe (38 %), based on recorder chart data.

The licensee has no procedure for dealing with an unseated or stuck open

safety valve.

If sufficient steam flow is established to trip safeguards

system limits, the emergency instructions for steam break would apply.

The guidelines for actions to be taken on receipt of a low SGFP suction

alann were contained in a procedure which had not been subject to SORC

review, nor were they issued by the Manager.

The Steam Dump operating

instruction was issued by the Manager but not SORC reviewed.

Technical Specification 6.8.1 requires procedures for activities listed

in Regulatory Guide 1.33 Appendix A.

Technical Specification 6.8.2

requires these procedures to be reviewed by SORC and issued by the

Manager.prior to implementation. Regulatory Guide 1.33 includes pro-

cedures for each safety related alarm annunciator and emergency procedures

for

110ther Expected Transients that may be Applicable.

11

Regulatory Guide

1.33 includes no requirement for steam dump operating procedures.

During this event, the saturation margin recorder was inoperable for

temperature.

The pressure margin channel was operable and displayed a

minimum margin of 375 psi during the transient.

Subsequent inspection of the safety valve found that the stem plate, on

which the manual opening yoke operates, had lost a retaining cotter pin

and had worked down the threaded stem approximately two turns. This

prevented complete seating of the valve due to interference from the

operating yoke.

All valves were subsequently inspected for clearances

and for integrity of the cotter pins.

Removal of the operating mechanism

was abandoned due to Code requirements.

Rod control was restored by replacement of a firing circuit in the control

system. Subsequent testing of the spray valve controller found no anomaly

in operation.

Review of control room charts indicates that, due to the

initial high pressure, the controller may have been in saturation and

taken some time to remove the output signal.

In addition, average temp-

erature was being reduced at a significant rate at 0135, which would

account for a pressure drop independent of spray valve operation. Based

on interviews with the operators, the valve was apparently shut at this

time but had not made up the

11close

11 limit switch. Tapping the

11close

11

push button accomplished this action.

15

10 CFR 50.72 requires that a prompt (one hour) notification be made to

NRC for any event that results in the plant not being in a controlled

or expected condition while operating or shut down.

Licensee supervisors

and management interviewed stated that they did not believe the above

situation fell in this category.

No prompt notification was made.

The licensee, based on his investigation of the transient, has provided

average temperature limits in the emergency instruction for rod control

system failure (541-581 degrees F), and has prepared instructions for

dealing with stuck open secondary safety valves.

Identified inconsis-

tencies between 10 CFR 50.72 reporting requirements and emergency plan

notification procedures are also being addressed.

A 30-day Licensee Event Report will be submitted detailing the licensee's

evaluation of the event.

Failure to prepare procedures for dealing with an open steam generator

safety valve and failure to properly issue the load reduction procedure

constitute noncompliance with Technical Specification 6.8.1 and 6.8.2

(311/82-01-01 and 311/82-01-02). Failure to report the unexpected plant*

condition to NRC constitutes noncompliance with 10 CFR 50.72 (311/82-

01-03}.

Due to the frequent protective system challenges caused by loss of feed-

water pump suction pressure over the past several months and this tran-

sient, caused by an attempt to avoid such challenge, the licensee has

initiated action to evaluate and correct the steam plant instability

which appears to be precipitating such pressure loss. These actions will

be monitored by the inspector.

The inspector had no further questions with respect to events reviewed

during this report period.

7. Maintenance Activities

The inspector observed maintenance activities on the following equipment:

a.

2C Vital Undervoltage Relay

b.

21 Overpower ~T Instrument Channel

C.

12 Component Cooling Heat Exchanger - replacement

16

These activities were observed to ascertain the following:

The work

was conducted in accordance with approved procedures, regulatory

guides, Technical Specifications, and industry codes or standards.

The following items were considered during this review; the limiting

conditions for operation were met while components or systems were

removed from service; approvals were obtained prior to initiating

the work; activities were accomplished using approved procedures and

were inspected as applicable; functional testing was performed prior

to declaring that particular component as operable; activites were

accomplished by qualified personnel; radiological controls were

implemented; and fire prevention controls were implemented.

No unacceptable conditions were identified.

8. Surveillances

The inspector observed the licensee's performance of the following

surveillance procedure:

1 PD 16.2.013 Functional Test

Intermediate Range Channel N 35, Revision 0, May 5, 1980

During the perfonnance of this test, the inspector confirmed the

following: Testing was performed in accordance with adequate procedures;

test instrumentation was calibrated; limiting conditions for operations

were met; removal and restoration of the affected components were pro-

perly accomplished; and, the test results confonned with Technical

Specification and procedural requirements and were reviewed by .personnel

other than the individual perfonning the test. Any deficiencies noted

were reviewed and resolved by the personnel of the responsible depart-

ment.

The personnel performing the surveillance activities were know-

ledgeable of the systems and the test procedures.

The inspector confirmed

that these personnel were qualified to perform the tests.

The inspector had no questions regarding the performance of surveillance

activities.

9.

Unresolved Items

10.

Areas for which more infonnation is required to determine acceptability

are considered unresolved. Unresolved items are contained in Paragraph

6.

.

Exit Interview

At periodic intervals during the course of this inspection, meetings

were held with senior facility management to discuss inspection scope

and findings.