ML18059B196

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Insp Rept 50-255/94-12 on 940701-0819.One non-cited Violation Noted.Major Areas Inspected:Corrective Actions from Previous Insp Findings,Operational Safety Verification, Safety Feature Systems,Onsite Event Followup & Security
ML18059B196
Person / Time
Site: Palisades Entergy icon.png
Issue date: 09/08/1994
From: Kropp W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18059B195 List:
References
50-255-94-12, NUDOCS 9409210068
Download: ML18059B196 (21)


See also: IR 05000255/1994012

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I II

Report No~ 50-255/94012(DRP).

.Docket No. 50-255

Licens~e: Consumers Power Company

212 West Michigan Avenue

Jackson, MI

49201

License Nos. DPR-20

Facility* Name:

Palisades Nuclear Generating Facility

Inspection At:

Palisades Site, Covert, Michigan

Inspection Conducted:

July 1 through August 19, 1994

. Inspectors:

M. E. Parker

D. G. Passehl

R. L. Hague

J. F. Schapker

C. N. Orsini

K. Salehi

  • . Approved By:

f

Sect ion 2A .

Inspection Summary

Inspection from July 1 through August 19,

1994~ Report No. 50-255/94012CDRP)

Areas Inspected:

Routine, unannounced safety inspection by resident and

regional inspectors of actions on previous inspection findings, operational

safety verification, engineered safety feature systems, onsite event

follow-up~ current material conditiorr, housekeeping and plant:,cleanliness~

~adiological controls, security, safety assessment/quality verification,

maintenance, surveillance, engineering and technical support, and dry ~ask

. storage of spent fuel.

Results: Within the 12 areas inspected, no cited violations or deviatioris

were identified.

One noncited violation.was identified (paragraph 7).

The following is a summary of the licensee's performance during this

inspection period:

Plant Operations

The licensee's performance in this area was adequate.

The plant operated at

essentially full power since startup on June 18, 1994 .

~~9210068 940908

. G

ADOCK 0500025 5

PDR

..

. ( ..

..

.

.

The licensee's resp6nse to a July 27, 1994, firemain rupture was mixed ..

Operatbrs quickly recognized the situation and deenergized the fire water

pumps to prevent more extensive soil washout and damage to other structures in

the vicinity.

Fire suppression capability wasreturned within a- reasonable

time after as~essing the conseq~ences. of the event.

However, areas requiring

continuous firewatches due to inoperable fire suppression capability were not

adequately established.

The insp~ttor found the lic~nsee's procedures ~nd*

training in thi~ regard were lacking.

The licensee's response to an August 9, 1994,:ov~rflow of wa~er from the valve

pit adjacent to the Primary System Storage Tank and the Utility Water Storage

Tank was good.

Operators and health physics personnel took immediate steps to

identify and isolate the leak.

There was an adverse trend in Chargin.g Pump P-55A availability due to material*

condition deficiencies. *Several times during the past summer the pump has

been inoperable, causing an increased out-of-service time to necessitate

  • repairs.
  • rhe licensee's actions on monitoring and evaluating Dose Equivalent Iodine

were satisfactory.

The current average monthly activity level is

approximately 0.045 microcuries per milliliter. The licensee has secured the

services of two tontra~tors in its "fuel integrity working group," that meets

regularly to review and discuss the data.

Safety Assessment/Quality Verification

Consumers Power Company's Management.and Safety Review Committee {MSRC) for

the Big Rock Point and Palisades nuclear plants met on June 29, 1994.

The

members met to discuss recent plant ope,rations, outages, internal assessment

findings, program changes, and future schedules.

Issues were discussed based

on plant tours, interviews, and discussions with various licensee personnel ..

The MSRC made several positive 6bservations and suggestions for improvement at

the meeting.

Maintenance and Surveillance

The licensee's performance in this area was adequate .. *The licensee continued

to experience problems with the ~ain Generator Voltage Regulator Firing .

Circuit.

Altho~gh work to disable the west firing circuit module trip was

effective, there have -been other spurious alarms associated with the ma-in

generator control-circuits showing that equipment problems still exist.

Engineering and Technical Support*

The licensee's performance .in this area was adequate.

The inspectors met with

licensee representatives working the alternate spent fuel pool cooling

project. The licensee appears to ha~e adequate measure~ in place to assure a

successful completion of the prbject. *

  • .*

2

Dry Cask Storage Of Spent Fuel

The licensee's performance in this area was adequate.

was issued for failing to provide double verification

analysis of the boron concentration of the spent fuel

cask loading.

A noncited violation

for sampling and ..

pool water during dry

On July 28, 1994, the licensee identified three minor iridications o~ the

multi~assembly scaled basket (MSB) #4 ihat were nbt identified d~ring the

original review of the radiographs.

The licen~ee subsequently performed an

oper~bility evaluation and determined that the MSB #4 was operable. This

determination was based upon testing performed on the MSB prior to it being

placed into service on the storage pad.

The licensee was in the process of*

completing a more detailed operability assessment that includes a fracture

analysis .. The licensee is making plans to unload the MSB.

Dose rates higher than expected were identified on Ventilated Concrete Casks_

(VCC) #3 and #4 after loading.

The highest dose rate for VCC #3 was 60

mrem/hr (0.6 mSv/hr), and for VSC #4 was 56 mrem/hr (0.56 mSv/hr).

The

licensee followed the required actions of the license, which included

verifying the correct fuel* loading and performing an analysis to demonstrate

compliance with 10 CFR Part 20 and 10 CFR Part 72 with regard to dose to the

general public. These r~quirements were completed satisfactorily.

Improvements were observed duri~g loading of multi-assembly sealed basket

(MSB) #4 over the previous loading of MSB #3.

There was better prep~ration

and planning, greater control over the assigned tasks, enhanced communication,

and more direct manage~ent oversight. Radiological cont~ols were effectively

implemented during loading and handling operations. Contamination control *

practices were generally gopd.

3

1.

. DETAILS

Persons Contacted

Consumers Power Company

    1. R. A. Fenech, Vice President, Nuclear Operations
  • T. J. Palmisano, Pl ant General Manage'r *

W. F. Peabody, NECO Manager (Interim)

  • R. 0. Orosz, Director, NOD Services
  • R. M. Swanson, Director, NPAO
  • 0. 0. Hice~ Nuclear Training Manager
  • s: Y. Wawro, Acting Operations Manager
  1. Or W. Rogers, Safety & Licensing Director

R. B.

Kasper~ Maintenance Manager

  • R. C. Miller, System Engineering Manager
  1. K. M. Haas, Radi6logical Services M~nager

C. R .. ~itt, Administrative Manager

  • J. C. Griggs, Human Resource Director
  • H. A. Heavin, Controller

M. A. Savage, Corporate Communications

  • 0. G. Malone, Shift Operations Superintendent~

0. J. Malone, Radiological Services Supervisor

  • T. P. Neal , *Heal th *Physics Support Superintendent

. #R. A. Vincent, Licensing Administrator

  1. J. Decker, General NOT Supervisor
    1. 0. Fadel, NECO Engineering Program Manager

'*

  1. M. Ferens, NECO Ory Fuel Storage Procurement Manager
  1. S. Maclean,. NECO Ory Fuel Storage Engineer - ';

,--~*

  1. J, Nordby, NECO Welding Engineer *
  • *'. *
    1. J. Pomaranski, NECO Construction Manager
    1. R. Smedley, Licensing Staff Engineer
  1. 0. Zeigler, NOT Fi~ld Services Supervisor.

Nuclear Regulatory Commission*

  • W. J. Kropp, Reactor Projects Section Chief
    1. M. E. Parker, Senior Resident Inspector
  • D. G. Passehl, Resident *inspector
  1. C. Haughney, .Branch Chief, NMSS
  1. S. O'Connor, Team Leader, NMSS
  1. J. ~mith, Reactor Inspector, Riii
  • Denote~ those* attending the exit interview conducted on August 19,

1994.

  1. Denotes those attending the exit interview c~nducted on August 3, 199t ....

The inspectors also had discussions with other licensee employees,

including members of the technical and engineering staffs, reactor and

auxiliary operators, shift engineers and electrical, mechanical and

instrument maintenance personnel, and contract security personnel.

4

.* .. :*****

2.

Action on Previous Inspection Findings {92701)

a..

{Closed) Inspection F6llowup Item 255/91009~01CDRP):

Mainte~anc~

personnel used an uncontrolled copy of a vendor manual during a

maintenance activity to disassemble and clean a raw water

  • strainer.

No Notice of Violation was issued:.because this was

considered an addition~l example of ~ violation issued in

Inspection Report 255/91006{0RSS) involving use of uncontrolled

vendor manuals.

Closure of this issue will be tracked under

.

violation 91006-03{0RSS}, which is still open and will be reviewed

for closeout.at a later date. This item is closed.

b.

{Closed) Inspection Followup Item 255/92006-0lCDRPl:

Concrete

spalling in auxiliary feedwater {AFW) pump room.

This item

  • concerned the licensee's evaluation of the impact of feedwater

heater E-4A settling on the integrity of the AFW pu~p room.

The

inspector's review of this issue was documented in Inspection

Report 50-255/92027{0RP).

This item is closed.

c.

<Closed) Inspection Follo~~P Item 255/92021-0lCDRPl:

Steam leaks

in vents for reheaters. This item was opened to track the

licensee's root cause determination ~nd corrective action for .

accelerated steam erosion of the vent header piping on feedwater

heaters E-6A and E-68.

The licensee's reviewdetermined ... thatthe *

tunning vent configuration was changed *during iristallation of new

E-6A/B feedwater heaters in 1990.

At that time, the vent~ were

modified to combine three 1" running vents into a single 1"

running vent. This l" running vent dis~harged into a 3" vent

header. Since the single running vent.passed the same flow, 1 to

2 percent of the steam supplied to the heaters, the velocity in.

this line was increased by a factor of three .. The running vent

entered the header at a 45° angle, which contributed to the ,.steam

cutting at the pipe wall.

The licensee has implemented several correcti~e actions that

i.ncl uded:

  • ,

The schedule 40 carbon steel vent header piping was replaced

with schedule 160 stainless steel. This increased the wall

thickness and erosion resistance of the piping.

The running vent was modified to enter the vent header albng

the centerline, thus eliminating steam cutting at the header

wall.

Operations procedures were changed to keep the running vents

closed during startup and normal power operation, and to

open the running vents once per month for a six hour purge .

of the heaters.

5

.,

The licensee has been monitoring the heaters as part of the

Thermal Performance Monitoring Program to ensure that the heat,ers

do not become air bound.

No adverse affects of the modification

and th.e procedure change have been identified by the licensee.

This item is closed.

No violations, deviations, unresol~ed, or inspection followup items were

identified iri this area.

3.

Plant Operations (71707, 93702)

The plant has operated up to 100 percent power since startup on June 18,

1994.

a.

Operational Safety Verification (71707)

The inspectors verified that the facility was being operated in

conformance with the license and regulatory requirements and that

the licensee's management control system was effective in ensuring

safe operation of the plant.

On a sampling basis, the inspectors

verified proper control room staffing and coordination of plant

activities; verified operator adherence wtth procedures and

technical specifications; mon1tored control room indications for

abnormalities; verified that electrical power was available; . .--,and

observed the frequency of plant and control room visits by station

management.

The inspectors reviewed-applicable logs and conducted

discussions with control room operators throughout the inspection

period.

The inspectors observed a number of control room shift

-turnovers.

The turnovers were conducted in a professional manner

and included log reviews, panel walkdowns, discussions of*

maintenance and surveillance activities in progress or planned,

and associated LCO time restraints, as applicable.

b.

Engineered Safety Feature lESFl Systems (71707)

During the inspection period, the inspectors selected accessible

portions of several ESF systems to verify status. Consideration

was given to the plant mode, applicable Technical Specifications

(TS), Limiting Conditions for Operation (LCO) requirements, and

other applicable requirements.

.

.

Various obser~ations, where applicable, were ~ade of hangers and

supports; housekeeping; whether freeze protection, if required,

was installed and operational; valve position and conditions;

potential ignition sources; major component labeling, lubrication,

cooling, etc.; whether instrumentation was properly installed and

functioning and significant process parameter values were

consistent with expected values; whether instrumentation was

calibrated; whether necessary support systems were operational;

and whether locally and remotely indicated breaker and valve

positions agreed.

6

"'"'*'**::

During th~ fnspection, the accessible portioris of the High

Pre~sure Safety Injection and Low Pressure Safety Injection were

-walked down.

_ The following items were identified during the walkaowns:

A pipe support on the miniflow recirculation line for high

pressure safety injection pump.P~66A was missing.

Protective grating around a floor penetration for a sensing

line for pressure transmitter PT-0306 (low pressure safety

injection pump discharg~ pressure) was lifted from the floor

and resting on the~ inch sensing line.

In response to the above items, the licensee ~valuated the

conditions and took apprbpriate ~ction.

c.

Onsite Event Follow-up (93702)

During the inspection period, the licensee experienced several

events, some of which required prompt notiffcation of the NRC

pursuant to 10 CFR 50.72.

The inspectors pursued the events -

ohsite with licensee and/or other NRC officials.

In each case,

the inspectors verified that any required notification was.:~correct

and timely.

The inspectors also verified that *the licensee

initiated prompt and appropriate actions.

The specific events

_were as follows~

Fire Main Rupture:

On July 27, 1994, the firemain system

  • ruptured underground at the south end of*the ~creen-house

.building. *The rupture caused the loss of all automatic fire

suppression ~apability throughout the plant. Jhe ltcensee-

implemented several contingency actions, such as notifying

the Covert fire department, increasing plant fire tours, and

canceling a preplanned outage on an emergency diesel

generator.

By midnight the licensee identified the location -

of the break to be just downstream of ffre water to cooling

tower isolation valve.MV~FP-176. The licensee closed the

valve thereby isolating the break. Automatic fire

suppression capability was returned sho~tly thereafter to

all areas of the plant, with the exception ot the cooling

towers and some nonessential areas.

The ruptu~e caused a buckling of the ground surface above

the failed section of pipe and washout of soil in the

vicinity of the break location. A concrete pillar

supporting the 90 inch cooling tower return line, located"

near the center of the newly-formed 12 foot diameter sink

hole, remained unaffected.

No movement of the cooling tower

support was noted to date.

The licensee has been monitoring

the line for any movement since the event occurred.

7

..

The licensee determined the probable *cause of ttie failure

was bending and twisting forces at the failure location due

to cyclic loading from heavy loads on the ground above,

  • combine.d with the more brittle nature of the pipe material

(Grade D cast iron).

Repairs include replacing the.section of~fail~d pipe with a

. stronger, more ductile pipe material, and restoring the

affected soil to proper design compaction ..

The inspector found the license~'s response to this event to.

be mixed.

The licensee's immediate response was g.ood ..

. 0-perators quickly recognized .the situation and deenergized

the fire water pumps to prevent more extensive .. soil washout

and damage to other structures in the vicinity. Fire

suppression capability was returned within a reasonable time

after assessing the consequences of the event.

However~ areas requiring ~ontinuous firewatches doe to

inoperable fire suppression capability were not adequately

established. The inspector found the licensee's procedures

and training in this regard were lacking~~ Tha weaknesses in

the licensee's procedures and training in thii area is

considered an Inspection Followup Item pending, further

review by the NRC (255/94012-01).

Overflow Of Slightly Radio~ctive Wate~ From The Utility

Water Storage Tank:

On August 9, 1994, the licens~e

discovered an overflow of water from the valv~ pit adjacent

to the Primary System Storage Tank and the Utility Water

Storage Tank, T-90 and T-91 respectively. Subsequerit

evaluation determined that the water was coming from.tank

T-91, which receives distillate from the .dirty waste

evaporator. Health Physics took immediate action to rope

off the area and obtain soil sa~ples. Soil samples around

the tank where the overflow occurred indi~ated low levels of

activity. The licensee has removed some contaminated soil*

and is.continuing to perform a more detailed radiation

survey to determine the extent of contamination.

Once the

valve pit was pumped down, the licensee was able to

determine that the leak was on a recirculation line.jn the.

valve pit.

In additi~n, the licensee retracted the following telephone

notifications made earlier. to the NRC:

Control Room Heating. Cooling~ and Ventilation CHVAC) System

Failed To Meet Design Basis Flow Requirements:

On May 22,

1994, a non-emergency 4-hou,r report was made based on the *

results of the service water flow test for the control room

HVAC coolers. The report stated that the flow required to

8

* ..

support the service water temperature analyzed upper limit

of 81.5 degrees F at 46 gpm was not met during the testing.

The test results showed flows through HVAC condensing units

VC-10 at 45 gpm, and VC-11 at 44 gpm;

The condition was*

reported.per 10 CFR 50.72(b)(2)(iii) and under 10 CFR

50.72(b)(2)(i).

.

.

After further reviews, the licensee deter~ined that the*

plant would not have exceeded the design basis, andthe

control room HVAC coolets would have been able to perform

their design basis function.

This was based on the s~rvice

water fl ow data and the 1 ake temperature dl,lri ng the 1 ate

fall and winter time period when the low flow condition

existed concurrent with the unit at power.

The 1 icensee had November temperature data that showed the .

lake water temperature at approximately 50 degrees F.

Therefore, ample margin existed in the service water

temperature to make up for the apparent 1-2 gpm drop in

service water flow.

Emergency Diesel Generator (EOG) Potential Overload:

On

April 27, 1994, a non-emergen~y 4-hour report ~as made when

the licensee found that the potential eiisted for the EOG to

exceed the two hour rating if emergency sa f eguards.,,system

pumps were all operating at run-out conditions concu~rent

with a Loss of Cotilant Accident with a Loss of Offsite Power

and only one EOG operating.

The condition was reported per

10 CFR 50.72(b)(2)(iii)(D).

The licensee. subsequently determined that the inputs for the

time to initiate manual loading of a hydrogen recombiner and

.a second battery charger were not realistic. The licensee

concluded that there would be 30 minutes into the event *

befote the hydrogen recombiner was put in operation and the

second battery charger would not be energized until after

one hour into the event.

W~th this information the EOG loadirig calculation w~s

revised and resulted in a total load within the two hour

rating.

  • d.

Current Material Condition (71707}

The inspectors performed general plant as well as selected system

and component walkdowns to assess the general and specific

material condition of the plant, to verify that work requests had

been initiated for identif;ed equipment problems, and to evaluate

housekeeping.

Walkdowns included an assessment of the buildings,

components, and systems for proper identification and tagging,

accessibility, fire and .security door integrity, scaffolding,

radiological ~ontrols, and any unusual conditions. Unusual

9

.*

conditions included but were not limited to water, oil, or other

liquids on the floor or equipment; indications of l~akage through

ceiling, walls, or floors; loose insulation; cofrosion; excessive

noise; unusual temperatures; and abnormal ventilation and

lighting ..

.

.

'

.

Material tondition this inspection period was generally good,

b~t

some areas warrant continued attention, including Charging Pump

P-55A.

The inspector noted an increase in equipment problems

associated with P-55A over the past few months. *The licensee has

been unable to obtain an acceptable seal package for the pump .

. The pump has leaked excessively several times during the past.few

months necessitating repairs and challenging the TS LCO.

There have been other problems with the pump as revealed by a

re~iew of control room logs.

The inspector reviewed the control

room logs for the past three months and noted in the past two

months alone the pump ran for ~nly 15, 16, and 11 days,

respectively, before being declared ~noperable for repacking.

Historically, the pump would run for approximately two months

before repacking became necessary. Other noted deficiencies

throughout the period included:

Loss of automatic speed control;

Pieces of RTV sealant floating in the plunger well

a~ea; *

Unexplained b~nging hoises in the fluid drive section near

the pump discharg~;

Clattering of the discharge check~valve.

Although some of the problems, such as the short life of the

packing, appear to be design related; other problems were due to

questionable maintenan~e work practices that led to maintenance

rework-.

Involvement by engineering was satisfactory. The

inspectoi found the system engineer appropriately involved with

resolution of the design discrepancies.

The material condition of

Charging Pump P-55A is considered an Unresolved Item pending

further review by the NRC and licensee (255/94012-02} .

  • . M

Considering the previous problems with the material condition of

the charging pumps, the licensee has agreed to respond to this

Unresolved Item within 60 days of receipt of this letter .. The

response should address what actions the licensee plans to take to

improve the material condition of the charging pump and to reduce

the.out-of-service time and potential challenge to the T.S. LCO.

e .. *Housekeeping and Plant Cleanli~ess (71707}

The inspectors monitored the status of housekeeping and plant

cleanliness for fire protection and protection of safety-related

10

. .

f.

equipment from intrusion of foreign matter~ :* .. No significant

concerns were identified this inspection period .

Radiological Controls (71707)

The inspectors verified that -personnel

were~;.fol lowing heal th

physics procedures for dosimetry, protective clothing; frisking,

post~ng, etc., and randomly examined radiation protection

instrumentation for use, operability, and c~libration.

The inspectors reviewed the licensee's current action on Dose

Equivalent Iodine (DEi).

Dose equivalent iodine values .. are,.us.ed

as an indicator of failed fuel.

The current average monthly

activity level is. approximately 0.045 mitrocuries per milliliter.

The TS have an upper limit of 1.00 microcuries per milliliter

before plant shutdown is required.

The current DEi value has placed the plant in the second of fouf

"Action Le~els" (0.03 < DEi < 0.12) per plant procedure COP-1,

"Primary Coolant System Chemistry." At t~is_ level the licensee is

required to increaseprimary coolant sampling frequency to daily,

and to evaluate the efficiency of the Chemical Volume and Control

System demineralizers.

The iicensee has performed these actions

in addition to several others, including review of .chemt.stry*data

by outside contractors, NWT and Siemens Power Corporation.

The

two contractors-are members of th~ licensee's "fuel integrity

working group," that meet reg~larly to review and discuss the

data.

.

The current position of the group is that there is between one and

three leaking fuel rods in the core, likely in a second cycle "N"

fuel assembly.

The inspectors found that the licensee is taking appropriate

actions to track and evaluate the data. * The group has predicted

that based on current trends, the DEi activity level should be

about 0.08 microcuries per milliliter at the end of this cycle.

g.

Security (71707)

. Each week during routine activities or tours, the inspectors

monitored the licensee's security program to ensure that observed

actions were being implemented according to the approved security

plan.

The inspectors noted that persons within the protected area

displayed proper photo-identification badges and those individuals

requiring escorts were properly escorted. The inspectors also*

verified that checked vital areas were locked and alarmed.

Additionally, the inspectors also observed that pe~sonnel and

packages entering the protected area were searched by appropriate

equipment or by hand.

. 11

No violations, deviations, unresolved, .or inspection followup items were

identified in this area.

4.

Safety Assessment/Quality Verification {40500 and. 92700)

Consumers Power Company's Management and Safety Rev*iew Committee {MSRC)

    • for the Big Rock Point and Palisades nuclear plants met on June 29,

19.94.

The members met to discuss recent pl ant oper.ati.ons, outages,

internal assessment findings, program changes, and future schedules.

Issues were discussed based on plant tours, interviews,.and discussions

with various licensee personnel.

The MSRC made several positive

obser~ations and suggestions f6r impro~ement.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

5.

Maintenance/Surveillance {62703 and 61726)

a.

Maintenance Activities (62703) .

Routinely, station mainten~nce activities w~re observed and/or

reviewed to ascertain that they were conducted in accordance ... with

approved.procedures, regulatory guides and industry codes or

standards, and in conformance with technical sp~cifi~ations.

The following items ~ere also considered during this review:

LCOs

were met while components or systems were removed from service;

, approvals were obtained prior to initiating' the work; functional

testing and/or calibrations were perfor~ed prior to returning

  • components or systems to service; quality control records were*

maintained; and activities were accomplished by qualified.

personnel.

The inspectors were concerned with the large number (approximately

1800) of outstanding non-outage corrective maintenance work orders

in the licens~e's backlog.

The licensee was aware of the issue

and has begun steps to address.the issue.

The inspectors will

continue to follow the licensee's progress in resolving the

backlog.

Portions of the following maintenance activities were observed or

reviewed:

Work ~nstruction WI-24413037-02:

Disable Main Generator *

Voltage Regulator Firing Circuit Module Trip: Workers used

the work instruction and Temporary Modification TM-94-072 to

disable the west firing circuit module trip in the main

  • generator's voltage regulator to avoid an unanticipated

turbine/reactor trip. The work was performed by electrical

maintenance personnel with support from system engineering.

The quality of support for this job appeared good.

The

12

.

    • .:;

.

.

licensee had extensive vendor input and held discussions

with other nuclear utilities that had experiented similar

problems.

The job was performed satisfactorily.

However, there have been other spurious alarms associated*

with the main generator control circuits that indicate

    • equipment problems still exist. The licen~ee appears to

have taken appropriate followup actions, includi~g

continuous monitoring ~f suspect component~. .

Work Orders 24412845. 24411704. 24413113. 2441-3114.

24413145. and 24413782: Addresses various Charging Pump

P-55A deficiencies which is further discussed in paragraph

3.d of this report.

  • Work Order 24413584:

Repair fir~ main rupture which is

further discussed in paragraph 3.c of thi~ report~ *

Work Order 24413217 and 24413262:

Resolve TI-0122HA, "A"

.Hot Leg Temperat~re Indication Fluctuations

Work Order 24410670:

Load and Transport Multi~Assembly

Sealed Basket {MSB) No. 3

Work Order 24410664:

Load and Transport Multi-Assembly

Sealed Basket {MSB) No. 4

  • Work Order 24413278:. Lower High Temperature Alarm Setpoint.

Per.Temporary Modification 94-069 From 175 to 147 Degrees F

on Primary Coolant Pump P-50D

  • Work Order 24412785:

Erect Masonry Block Wall,around:.fuel

Oil Transfer Pumps PISA and Pl8B for Seiche Protection

b.

Surveillance Activities {61726)

During the inspection period, the inspectors observed TS required

surveil 1 ance testing and verified that testing was p.erformed in *

accordance with adequate procedures, that test instrumentation was

calibrated, that results conformed with technical specifications

and procedure requirements and were reviewed, and that any

deficiencies identified during the testing were properly resolved.

The inspectors also witnessed or reviewed portions of the

following surveillances:

M0-7A-2. "Emergency Diesel Generator 1-2 CK-68))" Rev.31

FPSP-M0-1. "Fire Suppression System Valve Alignment." Rev.6

MI~6. "Ar~a Monitor Operational Check." Rev.I

13

No Violations, deviations, unresolved, of inspectio~'followup items were

identified in this area.

  • 6.

Engineering and Technical Support {37700)

7.

The inspectors met with licensee representatives working the alternate

spent fuel pool cooling project.

The purpose of the project w~s to

upgrade the material condition of components {Valves, piping, etc.)

.associated with the spent fuel pool cooling systems and component

cooling water cooling systems during the next refueling outage in 1995.

The discussions centered on the system design and layout, design

contingencies, and preriminary work plan.

The licensee appears to have adequate measures in place to assure a

succe~sful completion of the project.

The alternate cooling system is

scheduled to be in effect for about thirty days when there would be

minimal heat load in the spent fuel pool.

The 'portions of the system

that were in safety related areas of the plant would meet seismic

requirements, materials would be certified to appr6priate standards

where appropriate, and a backup class lE power supply would be

available.

Procedures were in place to o~erate and maintain the system

during normal and off-normal conditions.

The inspectors will continue to periodically monitor the licensee~.s

progress on this project.

No violati6ns, deviat~~ns, unresol~ed, or inspection followup items were

identified in this area.

Dry Cask Storage of Spent Fuel (83750, 37700)

The inspectors monitored the licensee's loading -0f ~pent fuel assemblies*

from the spent fuel pool fuel storage racks to the dry cas*k 'MSBs.

This

inspection covered loading of two dry casks, Nos. 3 and 4.

Dry Cask No.

3 was loaded on June 20, 1994, and Dry Cask No.4 was loaded on July 11, *

1994.

Although overall the loadings were performed successfully,

several weaknesses were observed with loading of MSB No.3, whereas

loading of MSB 4 was greatly improved.

a.

Background

The licensee contracted with Pacific Sierra ~uclear Corporation

{PSN) to design and construct a dry cask spent fuel storage

facility to be partially constructed onsite for long term

temporary storage of spent fuel.

The licensee has documented a 10

CFR 50.59 evaluation as required by 10 CFR 72.212 (Subpart K),

showing that use of the general license for storage of spent fuel

at the power reactor site will not involve an unreviewed safety

q~estion or Technical Specification (TS) change.

The PSN cask design consists of a steel m~lti-assembly sealed

basket (MSB) which holds 24 spent fuel assemblies {sealed) and a

14

.*:*

steel clad ventilated concrete cask {VCC) which provides

biological shielding and MSB protection.

The PSN cask design has** been granted a Certificate ot' Compl hnce

{C of C) by the NRC.

This inspection was conducted using the

.

specifications, standards, codes, and commitments described in the

licensee's design certification.

b.

Radiological and Fuel Handling Observations For MSB No. 3

The inspectors observed radiological practices and monitored the

loading of 15 spent fuel assemblies from the spent fuel pool to

MSB 3 on June 20, 1994.

Radiological controls were generally

good.- In the area of fuel handling,, there were several concerns

identified due to poor preparation and a lack of ownership by.

operations personnel;

Radiolrigical control.s during loading ot MSBJ were effectiv~ly

implemented during loading and handling operations. Contamination

control practices were generally good.

There were some problems

with personnel walking pastcoritaminated area boundaries without

the proper protective clothing. This was caused when the boundary

was moved as the multi-assembly transfer cask (MTC) and MSBwere

1 ifted. from the fue 1 poo 1 to the cask wash down pit;**.:. The' 1-icensee

indicated that the posting criteria would be reviewed .for the job

. to determine if a more effective means could be implemented for

  • future cask 16ading operations..

During reviews of fuel handling operations for the loading of MSB

No. 3 on June 20, 1994, the inspectors identified the following

concerns:

The spent fuel pool boron was not sampled in accordance with

the C of C requirements. A violation was issued {paragraph

7.c);

Operators worked up to 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> to accomplish the activity

in a high temperature and high humidity environment. This

increased the likelihood for error;

Communications and video recording gear were not properly

prestaged prior to loading fuel, causing unnecessary delays;.

A hose used to fi 1 ter spent fue 1 poo 1 water was found to

interfere with movement of the fuel handling machine and had

to be re-located, causing extra effort to control

contamination and unnecessary delays;

Some contamination boundary postings were i neons pi cuous as .

described above.

15

These* concerns were discussed with the licensee. During

subsequent loading of MSB No. 4 on July 11,

1994~ the inspectors

  • did not identify any similar concerns. *The inspectors noted_ that

the lit~nse~:took extensive measures to addr~ss these concerns,

including dedicating a senior reactor operator to be in overall

contrbl of fuel loading activities. The inspectors considered the

licensee's actions to correct the above concerns noted during the.**

loading of MSB No. 3 ~s effective.

c.

Violation For Inadequate Boron Sampling of the Spent Fuel Pool

The C of C for dry cask fabrication and loading required the *

licensee to sample and analyze the boron contentration of the

spent fuel pool water within four (4) h~urs of setting the first

fuel assembly in th~ MSB.

The require~ent mandated double

verification for sampling and a~alysis. Specifically, double

verification required two independent technicians take samples and

perform independent analyses. Contrary to this requirement,

during loading of MSB N6. 3, the li~ensee identified that ~

routine sample was taken and analyzed by only one technician.

Although the licensee took three separate .-.samples between 2: 05

p.m. and 7:17 p.m. (the time of the first~fuel assembly loading),

the samples were not taken by two persons and were not *

independently analyzed.

,

A potential contributor to this problem was that Chemistry

Department personnel were unaware of the requirement.

This

requirement should have been provided by the Operations

.

Department, who had the overall responsibility of loading MSB 3.

The first sample taken at 2:05 p.m. was*a**routine sample reported

by Chemistry to the Control Room.

Procedure FHS0-17,

"Multi-Assembly Basket Loading Procedure," Section 3' *. 3, did not

require double verification~ therefore, this sample should not

have been used to meet the C of C requirement:

In fact, norie of

the three boron samples met the C of C requirements for

independent verification.

On the following day, d~ring the review

of sampling records and procedure requirements, the licensee

iden.tified this problem and initiated condition*-,report

C-PAL-94-0409.

10 CFR 72.210 requires the licensee to comply with the

requirements specified in the C of C pertaining to storage of

spent fuel assemblies.

Further, 10 CFR 72~212(b)(2)(i) requires

that conditions set forth in the C of C must be met prior to ~ /

  • loading fuel.

Not meeting the specific requirement for double

verification during the sampling of the SFP, as delineated in the

In

considering the violation, the enforcement discretion criteria

specified in 10 CFR Part 2, Appendix C, Section VII(B)(2) was

  • considered.

16

d.

This violation will not be subject to enforcement *action because*

...

the licensee's efforts in i dent i fyi ng and correcting the vi o lati"on

met the above enforcement criterfa. Corrective actions included .

revising the governing procedure for dry cask loading with

adequate cautions concerning double verification.

In addition,

  • the licensee counseled responsible department\\personnel and other

involved individuals. Double verification of .the boron was

performed during t'he loading of MSB No. 4.

Adequate .checks exist

to preclude reoccurrence during subsequent cask loadings.

Fuel Handling Observations During Loading of MSB No. 4

  • The loading of-MSB 4 was performed on July 11, 1994, with.

significant improvement from MSB 3 loadi~g activities.

The *

inspectors* observed loading of 24 fuel

a~semblies into MSB 4. The

improve~ents reduced the overall length of the activity to less*

than a third of the time consumed during the prior cask loading.

These changes reflected better pre~araiion and planning, greater.

control over the assigned tasks, enhanced communication,. and more

di re ct management oversight. Proper ownership of this acnv*ity

was evident from its start to its completion_

Various steps were

preplanned and were properly ~oordinated.

e.

Welding Inspection

The NRC inspector observed the welding* of the seal lid and

structural lid of the MSB Nos. 3 and 4.

The following was

verified:

The essential welding variables were controlled i~

accordance with the applic~ble welding procedure

.

specifications (WPS FC-LID revision 4 (FCAW)

and;SM~L1D

revision 2 (SMAW)).*

The welding p~ocedure specifications and welders and welding

operators were qualified in accordance with the

specification requirements.

  • .The helium leak test was performed in accordance with the

specification requirements.

The certified material test reports for.the welding

materials were reviewed.

The welding wire and electrodes

met the requirements of the applicable American Society*of

Testing Material (ASTM) standards.

The licensee's middle management supervis1on was apparent

throughout the welding and te.sting of the MSB seal and structural

l ids.* A 11 processing observed was performed in accordance with

procedure requirements. *

17

f.

Elevated Dose Rates Found On MSB 3 and MSB 4

There were higher than expected radiation measurements when the

loaded MTC and MSB were lifted out of the spent fuel pool.

The

licensee attributed the higher reading to a new:step in their

procedure* which required draining 75 gallons of**water from the

MTC/MSB as it was being lifted. This step was added to lower the

water level in the MSB so the water would not interfere with

subsequent welding of the lid to the MSB.

This reduced the

shielding effect of the water in the MSB which was compe*nsated for

by us.ing shielding during the 1 id welding. *

When the MTC/MSB assembly was loaded into the Ventilated Concrete

Cask (VCC), further radiation dose rate surveys were required

. prior to moving the VCC to the storage pad.

The results of these

  • surveys indicated that some areas on the top of the VSC exceeded

the maximum dose rate of 50 mrem (0.5mSv/hr) prescribed by the C *

of C. The highest dose rate identified was 60 mrem/hr (0.6

mSv/hr).

The licensee followed the required actions of .the C of C

which included verifying the correct fuel Toading and performing

an analysis to demonstrate compliance with 10 CFR Part 20 and 10

CFR Pa~t.72 with regard to dose to the general public. These

requirements were completed satisfactorily. *

A further detetmination of why the observed dose ~ates exceeded

those originally predicted was also performed. This analysis**

stated that the dose rate predictions were based predominat~ly on

radiation emanating from spent fuel with a giv~n burn-up and age;

however, the licensee believed that early fuel assemblies

contained varying amounts of Cobalt (Co )-60 in* *the top hardware.

The Co-60 was produced by neutron activation of Co-59 which was a

trace element in the assembly hardware. The concentration of-.Co-59

was not controlled until recently and could vary significantly

from assembly to assembly.

Elevated dose rates were also ide~tified on VCC No. 4.

The

highest dose rate was 56 mrem/hr (0.56 mSv/hr). A NRC Region III

radiation specialist was sent to the site to make confirmatory

surveys on VCC No. 3.

In addition, the results for VCC No. 4 were

reviewed.

The results of these surveys wer~ in agreement with

those of the licensee.

The shielding analysis for the cask

assumed a uniform plane source of 50 mrem/hr{.5 mSv/hr) emanating

from the top of th~ cask.

A 29 point survey performed *on the top*

of VCC 3 showed an average dose rate of 28.9 mrem/hr {.29 mSv/hr).

Similar results were obtained for VCC 4; ther~fore, the dose to

the public from VCC No. 3 and No. 4 was enveloped by the original

shiel~ing analysis.

In July 1994, the NRC's Office of Nuclear Material Safety and .*

Safeguards conducted an audit of manufacturing activities of the

cask vendor, Sierra Nuclear.

The results of this inspectibn are

documented in Inspection Report 94207. Several quality assurance

18

issues were identified involving manufacture of the fifth through

the ninth casks.

As a result of these-concerns, the licensee

elected to perform a re-review of fabrication documents associated

with the four casks previously loaded.

-

O~ July 28, 1994, during a re-review of the radio~raphs for the*

multi-assembly sealed basket (MSB), the licensee identified three

indications on MSB No. 4 that were ncit.identified in the origi~al

~eview of radiographs. *The indicati6ns were characterized as

follows:

1) 3/4 inch linear longitudinal indication off center

line of weld,

2) 5/16 inch traverse linear indication off center

of weld, and 3) 3/8 inch linear longitudinal indication .on edge .. of

weld.

Upon di~covery of the indications, the licensee subsequently

  • performed an operability evaluation and determined that the MSB

No.4 was operable. Thts determination was based upon testing

performed on the MSB prior to being placed into service on the

.*

stor~ge pad.

The testing consisted of a hydro pressure test and

vacuum drying with 30 minutes hold times. :Based* upon the above

testing the licensee concluded that a thru-wall crack did not

exist.

In addition, no fatigue loading exists and, therefore,

there .are no forces present to propagate the present indications.

The 1 iCensee is working with the cask manufacturer, ~*Sierra *Nuc1'e*ar * *

Cqrporaticin, to perform a detailed finite analysis to assure

continued interim operability ts not affected.

(See paragraph 9.a

for additional information.)

The licensee is developing plans to return MSB No. 4 to the spent

fuel pool area where.the fuel will be unloaded and re-lbaded into

  • another cask.

One non-cited violation was identified in this area.

No deviations,

unresolved, or inspection followup items were identified.

8.

Report Review

During the inspection period, the inspectors r~viewed.the licensee's~

monthly operating report for June and July 1994.

The inspectors

confirmed that the information provided met the reporting requirements

of TS 6.9.1.C and Regulatory Guide 1.16, "Reporting of Operating

information."

No violations, deviations, unresolved, or inspection followup items"were-:

identified in this area.

8.

Unresolved Items

Unresolved items are matters which require more information in order to

ascertain whether it is an acceptable item, an open item, a deviation or

. a violation.

One unresolved Items was disclosed during this inspection

is discussed in paragraph 3.d.

19

...

9.

Inspection Follow-up Items

In~pector follow-up items are matters which have been discussed with the.*

licensee, which will be reviewed by the inspector, and which involve

some.action on the part of the NRC or licensee rir both.

~one Inspection

Follow-up Item disclosed during the inspection is discussed in paragraph

3.c.

10. * Meetings and Other Activities

a.

Management Meetings {30702)

A meeting was held between the licensee and the NRC at the

Palisades Site on August 3, 1994, to discuss Consumers Power

Company's {CPC's) Fabrication Validation Plan to verify

acceptability of the multi-assembly se~led baskets {MSB) .f6r the.

VSC-24 dry spent fuel storage system that were presently onsite~

CPC personnel briefed NRC on the Validation Plan, the

implementation of the Plan on MSB No.

6~, lssues identified. during

the validation process, and resolution of the issues.

The

briefing consisted of background information leading to the need

for the Validation Plan, results from reviews of material

deficiencies on MSB Nos. 6, 7, and 8, and results *from CPC*'vendor *

surveillance/audits.

Implementation of the Validation Plan was

not complete as bf the date of the briefing.

The need f6r the Plan w~s identified through results of a Quality*

Assurance {QA) inspection conducted by NRC and audits conducted by

.utilities of the MSB fabricator, Sierra Nuclear Corporation {SNC).

From this information, CPC determined that there was a need to

conduct this validation program.

CPC created a checklist/matrix to document the verification of

certain critical dimensions, weld quality and weld material

traceability, the existence of certified material test reports,

the use of approved suppliers, and other quality attributes in the

fabricati~n of MSB Nos. 1 through 10.

In addition, CPC set up a radiographic film reader to all-0~ NRC to

review radiographs of the MSBs.

Approximately half of the *

radiographs for MSB No. 4 were reviewed by NRC.

Based on the information presented during the briefing to NRC, and

providing that the implementation of the Fabrication Validation

Plan is completed satisfactorily, NRC concluded that CPC will be

able to verify that the MSBs will perform as designed.

b.

Exit Interview {30703)

The inspectors met with the licensee representatives denoted in

paragraph 1 during the inspection period and at the conclusion of

20

..

the inspection on August 19, 1994.

The inspectors summarized the

scope and results of the inspection and discussed the likely

content of this inspection report.* The licensee acknowledged the

information and did not indicate that any of the informatiori

disclosed. during the inspection could be considered proprietary in

nature.

21