ML18058B290

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Insp Rept 50-255/92-26 on 921123-24.Violation Noted.Major Areas Inspected:Configuration Control Project Implementation,Status & Corrective Actions
ML18058B290
Person / Time
Site: Palisades Entergy icon.png
Issue date: 12/15/1992
From: Burgess B, Yin I
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18058B285 List:
References
50-255-92-26, NUDOCS 9212220040
Download: ML18058B290 (8)


See also: IR 05000255/1992026

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Report No.

50-255/92026(DRS)

Docket No.

50-255

Licensee:

Consumers Power Company

1945 West Parnall Road

Jackson, MI 49201

License No. DPR-20

Facility Name: *palisades Nuclear Generating Plant

Inspection At:

Palisades site, covert, MI 49043

Inspection Conducted:

November

.ft_fk--

23-24, 1992

Inspector:

/Isa Yi.!1/.

I

Approved By:

Bruce L.-Burgess Chief

Operational Programs Section

Inspection Summary

Inspection on November 23-24. 1992 (Report No. 50-255/92026CDRS))

Areas Inspected:

Routine, announced inspection of licensee

configuration control project (CCP) implementation, stat~s, and

  • corrective actions.

Results:

The CCP was implemented in accordance with the

licensee's schedule.

The Writer's Guide for the Design Basis

Document incorporated all of the past concerns raised by the

inspector.

The inspection identified that some of the

significant, safety-related CCP findings were not evaluated in

a timely manner.

One violation was issued regarding a lack of

measures to ensure that changes to procedures are controlled and

of good quality (Paragraph 6.b).

9212220040 921215 -

PDR

ADDCK 05000255

G

PDR

1.

2.

3.

DETAILS

Persons Contacted

Consumers Power Company CCPl

R. D. Orosz, Nuclear Engineering and Construction Manager

T. J. Palmisano, Operations Manager

T. A. Buczwinski, Engineering Program Manager

P. M. Donnelly, Plant Safety and Licensing Director

J. Kuemin, Licensing Administrator

B. L. Harshe, Supervisory Engineer

R. A. Vincent, Plant Safety Engineering Administrator

J. Blewett, Project Engineer

V. A. Meineke, Staff Engineer

u. s. Nuclear Regulatory Commission

J. Heller, Senior Eesident Inspector

Introduction

This was the third inspection of CP's Configuration Control

Project (CCP).

The CCP which consisted of a Design Basis

Documentation (DBD) program and a Safety system Design

Confirmation (SSDC) program.

The first inspection was

conducted in March through May 1990, and the findings were

documented in Inspection Report (IR) 50-255/90010.

The

second inspection was conducted in April and May 1991, and

reported in IR 50-255/91010.

The purpose of these

inspections was to followup on the results of Consumer Power

Company's CCP program that resulted from the issuance of

CAL-RIII-86-002 on May 21, 1986.

The scope of this

inspection included a review of CCP completion status,

assessment of the program, and followup of the licensee's

corrective measures for the safety issues identified by the

CCP process.

CCP Scope and Implementation

Phase I

In 1986 the licensee responded to NRC concerns

raised during a safety system functional inspection

conducted on the high pressure safety injection system;

by

conducting an operational readiness review for the auxiliary

f eedwater system.

Evaluation and testing were extended to

other plant systems.

These activities were documented in a

Phase I Preliminary Assessment Report, dated August 12,

1987 *

2

Phase II

The scope was developed in 1987, and the work was scheduled

for completion before the end of 1992.

The status of the

DBDs and SSDCs was as follows:

~-~<,:i~- 111'.

Mechanical Systems

Component cooling water, service water and control room

HVAC were completed, and containment spray was

scheduled for completion in December, 1992.

Nuclear Steam Supply Systems

All CE supplied systems including the reactor coolant,

reactor protection, high pressure safety injection, low

pressure safety injection, control rod drive, and

chemical and volume control were completed.

Electrical Systems

All systems with Emergency Diesel Generator and DC

power supplies were completed.

With the exception of

emergency lighting and pressurizer heater emergency

power, all systems with AC power supplies were

completed.

The licensee also completed the 345 KV

switchyard DBD.

The remaining AC power and a grid

stability study will be completed in December 1992.

Except for containment spray and control room HVAC,

scheduled for 1993, all SSDCs for Phase II work were

completed.

No SSDCs were planned for the 345 KV switchyard,

grid stability, and emergency lighting.

The SSDC for

pressurizer heater power was included in the ~400.V design

confirmation study.

The inspector concluded that the scope of the licensee's

review was extensive, and would meet the corporate

completion schedule discussed previously with the NRC

(second quarter of 1993).

Phase III

Phase III DBD development and SSDC reviews

included containment heat removal, electric and I&C

separation and isolation, auxiliary building HVAC, main

steam, feedwater, condensate, fire protection, radwaste, and

spent fuel cooling.

The work was scheduled and funded for

1993 to 1996.

3

4.

DBD Writer's Guide

During this inspection, the inspector reviewed the revised

procedure, "Writer's Guide for Preparation of system Design

Basis Documents," Revision 4, dated September 1992, and

determined that the licensee had appropriately addressed

previous NRC comments.

5.

Resolution of CCP Findings

a.

Significance of Finding

The licensee classified each CCP identified discrepancy

into three categories:

Category I for minor problems,

Category II for issues where additional information was

needed to determine significance, and Category III for

major problems.

Category III discrepancies were

addressed through the formal corrective action system.

In accordance with the licensee program, all

discrepancies were evaluated for operability concerns

prior to assigning a Category.

During the April 1990 NRC inspection, the inspector

observed a large number of Category !Is, and questioned

the licensee's timeliness for determining safety

significance.

During May 1991 inspection, the number

of Category !Is were significantly reduced.

During the

present inspection, the inspector identified 155 open

category !Is issued since June 1989.

The licensee

stated that they had developed and implemented an

evaluation system in February 1991.

This system was

based largely on engineering judgement to assess the

importance of all the category !Is as follows:

Priority I -

A design document that supported or

defined technical specification (TS) safety

limits, LCOs, limiting system setpoints or

surveillance requirements.

These documents

demonstrated that T.S. addressed system, structure

or component (SSC) performed their safety

function.~

Priority II - A design document that defined the

controlling parameters or provided support for

demonstrating the functionality of a SSC not

addressed in TS, but supports a system addressed

in TS, such as heating ventilation and air

conditioning (HVAC).

4

Priority III, IV, and V - Design documents for

SSC's with less importance.

The licensee records showed the following Priority I's,

and II's still open.

System Review and Revision

CCW

DBD

Rev. 1

eves

DBD

Rev. o

RPS

DBD

Rev. 0

Emergency Power Systems

DBD Rev. 0

Emergency Power Systems

DBD

Rev. 1

Station Power Systems

DBD Rev. 0

station Power systems

DBD

Rev. 1

2400 V AC

SSDC

Rev. 0

No. of Open Priority

I's and II's

3 !I's since April 1991

2 II's since October

1991

2 I's, and 1 II since

Sept. 1992

1 I since Feb. 1992,

and 4 !Is

since Oct. 1991

8 II's since July 1992

2 !I's since December

1990

1 II since May 1991

4 !I's since February

1991

A total of 28 I's and II's

The inspector again expressed a concern about the

timeliness of resolving potentially important safety

related CCP findings.

The licensee stated that their

present program allowed one year to address Priority Is

and !Is *. However, after-reviewing the data compiled by

the inspector, the licensee agreed that the s*i tuation

was unacceptable.

The licensee committed to revise

Administration Procedure 13.01 to require the

engineering staff, assigned to the CCP, to initiate

resolution for Priority Is and IIs shortly after

identification.

This measure would ensure that

Category II items could be re-classified to Category I

or III within a four to six month period.

b.

Licensee Closeout of Category III Discrepancies

There were 28 Category III discrepancies identified in

the CCP reviews.

Deviation Reports (DRs) were written

for all these findings and were forwarded to various

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  • P

licensee departments for resolution.

The inspector

observed that ten DRs remained open.

All ten open DRs

had multiple issues or parts, and were partially

resolved.

The inspector considered licensee control of

these DRs to be acceptable.

6.

Review of Licensee DR Closeouts

The inspector reviewed the following completed DRs issued as

a result of CCW DBD reviews and document compilation.

Each

DR was closed after engineering evaluation and corrective

action:

a.

D-PAL-91-084

The DR documented that component cooling water to high

pressure safety injection, low pressure safety

injection and containment spray pump seal cooling inlet

and discharge solenoid valve safety injection signal

(SIS) relays did not have proper physical separation

inside the main control room panels.

The issue was

identified in April 1991, and_ closed in May 1991.

The inspector reviewed the engineering evaluation to

accept the as found condition, and had no adverse

comments.

b.

D-PAL-89-032

The inspector's review of this DR identified that the

licensee's administrative procedures were not

sufficient to control facility changes based on DBD

results.

Chronology of Events:

l}

1970:

Licensee identified that the procured

component cooling water heat exchangers were

significantly under-sized.

2)

September 10. 1979:

TS amendment 51 section

3.3.2.d stated "One shutdown heat exchanger and

one component cooling water heat exchanger may be

inoperable for a period of no more -than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />."

3)

Pre-February 1989:

Standard Operating Procedure

(SOP} 16, for the component cooling water system

(CCW), allowed, during normal plant operation, one

CCW heat exchanger to be out of service for up to

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

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4)

January 1989:

The DBD program confirmed that both

CCW heat exchangers were under-sized.

The DBD

concluded -

(1) both CCWHXs were needed during

power operations for primary system heat load

removal and (2) at system flow rates greater than

8000 gpm tube damage would occur due to flow

induced vibration (see IR 50-255/90010,

paragraph 4.c).

5)

January 1989:

DR issued on the subject

recommending that SOP-16 and Technical

Specifications be revised to require both CCWHSs

be inservice when reactor coolant is greater than

3250 F.

6)

January 1989:

SOP-16, revision 6 issued requiring

both CCWHSs to be in service with reactor coolant

temperature above 3250F.

7)

No Technical specification change was ever

proposed.

8)

November 1992:

SOP-16, revision 8 issued to

delete the requirement for both CCWHXs to be in

service above 3250F *

The licensee explained that the deletion of the

requirement in SOP-16 resulted from a Training

Department discovery in November 1991 that it

conflicted with TS 3.3.2.d.

The operations department,

after receiving the deviation report, discussed the

matter with the licensing department, but failed to

perform a detailed review of the CCW DBD and

communicate with the appropriate DBD engineer.

The

lack of technical information, and the fact that a

10 CFR 50.59 safety evaluation was not required for the

1989 SOP-16 revision contributed to the decision by the

licensee to delete the requirement.

The deletion of the CCWHX requirement from SOP-16

allowed the plant to be operated in accordance with the

Technical Specifications.

Operation of CCW per the

requirements of the Technical Specifications would

allow removal of one CCWHX for up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

With

one CCWHX inservice at full power, the ccw system would

be configured in such a way that serious degradation or

damage would occur to the heat exchanger potentially

rendering ccw inoperable.

Based on review of this

event, it was evident that the licensee had not

established sufficient administrative measures to

control changes to procedures to maintain procedural

quality, including the results of DBD reviews.

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10 CFR 50, Appendix B, Criterion VI, requires that

measures be established to control the issuance of

documents, such as instructions, procedures and

drawings, including changes, which prescribe all

actions affecting quality.

The failure of the licensee

to establish sufficient administrative controls to

ensure that changes to station operating procedures

(SOP-16) include the necessary actions to maintain

quality is considered a violation of 10 CFR 50,

Appendix B, Criterion VI.

7.

Exit Meeting

The inspector met with licensee representatives (denoted in

Paragraph 1) on November 24, 1992, at the site and

summarized the purpose, scope, and findings of the

inspection.

The inspector discussed likely informational

content of the inspection report with regard to documents or

processes reviewed by the inspector during the inspection.

The licensee did not identify any such documents or

processes as proprietary .

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