ML18057B295

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Insp Rept 50-255/91-17 on 910910-20.Violation Identified Being Considered for Escalated Enforcement Action.Major Areas Inspected:Previously Identified Items,Reportable Events & Operational Safety
ML18057B295
Person / Time
Site: Palisades Entergy icon.png
Issue date: 09/30/1991
From: Jorgensen B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18057B296 List:
References
50-255-91-17, NUDOCS 9110080022
Download: ML18057B295 (6)


See also: IR 05000255/1991017

Text

      • '

U. S. NUCLEAR REGULATORY COMMISSION

REGION II I

Report No. 50-255/91017(DRP)

Docket No. 50-255

Licensee: Consumers Power Company

212 West Michigan Avenue

Jackson, MI

49201

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:

Palisades Site, Covert, MI

Inspection Conducted:

September 10 through 20, 1991

Inspectors:

E~ R. Schweibinz, Senior Project Engineer

J. R. Roto , Resident Inspector

Approved By:

2A

Inspection Summary

Date

EA: 91-126

License No. DPR-20

_9 - "30 --91

Inspection on September 10 through 20, 1991, (Rehort No. 50-255/91017(DRP))

Areas Inspected: Special safety- inspection byte senior proJect engineer

and the resident inspector of actions on previously identified items,

reportable events, and operational safety.

Results: Of the areas inspected, one apparent violation was identified

regarding the return to service of containment spray pumps (paragraph 5).

9110080022 911001

PDR

ADOCK 05000255

Q

PDR

1.

DETAILS

Persons Contacted

a.

Consumers Power Company

  • G. B. Slade, Plant General Manager
  • R. M. Rice, Plant Operations Manager
  • R. D. Orosz, Nuclear Engineering & Construction Manager
  • P. M. Donnelly, Safety & Licensing Director
  • K. M. Haas, Radiological Services Manager
  • J. L. Hanson, Operations Superintendent
  • K. E. Osborne, System Engineering Superintendent
  • M. J. Kane, Plant Operations Shift Supervisor
  • M. T. Nordin, Electrical Engineering Section Head

R. K. Moceri, System Engineer

C. S. Kozup, Technical Engineer

  • J. C. Petro, NPAD Site Supervisor

R. J. Frigo, Operations Staff Support Supervisor

  • J. L. Kuemin, Licensing Administrator
  • C. T. Hillman, Licensing Engineer
  • T. J. Palmisano, Administrative & Planning Manager

b.

Nuclear Regulatory Commission (NRC)

  • B. L. Jorgensen, Chief, Projects Section 2A
  • J. K. Heller, Senior Resident Inspector
  • J. R. Roton, Resident Inspector
  • E. R. Schweibinz, Senior Project Engineer

C. N. Orsini, Reactor Engineer (Intern)

  • Denotes those present at the Exit Interview on September 20, 1991 .

. Other members of the plant staff were also contacted during the

inspection period.

2.

Actions on Previously Identified Items (92701)

(Closed) Unresolved Item (255/91012-03):

A lack of indication of the

control power (closing coil power) for circuit breakers could lead to

unrecognized inoperability of required safety equipment.

The condition

apparently obscured inoperability of Containment Spray Pump P-54C, as

addressed in paragraph 4.

In Licensee Event Report (LER) 50-255/91-016,

August 22, 1991, the licensee committed to provide remote and local

indication of closing coil power for 2400 and 4160 volt solenoid operated

breakers. This modification is scheduled for the next refueling outage

for the safety-related breakers, and the following refueling outage for

the nonsafety-related breakers.

This item is closed.

2

... 3.

Reportable Event (92700)

The inspector reviewed the following Licensee Event Report (LER) by means

of direct observation, discussions with licensee personnel, and review of

records.

The review addressed compliance to reporting requirements and,

as applicable, that immediate corrective action and appropriate action to

prevent recurrence had been accomplished.

(Closed) LER 255/91-016 Inoperability of Containment Spray Pump P-54C

The corrective actions were reviewed and found to be acceptable.

A

corrective action that was not listed in the LER was also reviewed.

This

involved a proposed change to General Operating Procedure (GOP) 2, to test

start the containment spray pumps prior to exceeding 325°F, to ensure

operability. If the LER were to be revised, the licensee was encouraged

to include the change to GOP 2 as a corrective action.

The inoperability

of containment spray pump P-54C is addressed in paragraph 4.

This LER is

closed.

4.

Containment Spray Operability-Chronology (71707)

This inspection identified the following Technical Specifications (TS) as

applicable:

a.

TS 6.8.1 requires that written procedures shall be established,

implemented, and maintained covering the activities recommended in

Appendix

11A

11 of Regulatory Guide 1.33,

11Quality Assurance Program

Requirements," as endorsed by CPC-2A QAPD [Quality Assurance Program

Description].

Paragraph f.(4) of Appendix A to Regulatory Guide 1.33 includes

procedures for startup of safety-related PWR systems, and instructions

for energizing, startup, and changing modes of operation as appropriate,

for the containment cooling systems.

b.

Technical Specification 3.4.1 requires containment spray pumps to be

operable before reactor criticality.

c.

Technical Specification 3.4.2 permits a single containment spray

pump to be inoperable during reactor power operation, but specifies

redundant component testing and a time limit of seven days.

The operational history and related procedures for the containment

spray pumps were reviewed as they relate to unresolved item 255/91012-03,

licensee corrective action package E-PAL-91-017, and LER 255/91-016.

The following chronology was developed:

02/11 /91

Containment spray pumps P-54A, P-548, and P-54C were

verified operable via conduct of the Surveillance Test

(Q0-10) "Containment Spray Pumps Surveillance Test.

11

The final part of the test included steps to rack out

the circuit breakers and remove their control power fuses.

3

03/03/91

03/10/91

03/25/91

03/26/91

05/23/91

This is a necessary action during certain plant shutdown

modes of operation, because the containment spray system

shares some components with the shutdown cooling system.

Prior to the plant exceeding 325°F, the fuses were

reinstalled and the circuit breakers racked in.

However, pumps P-54A and P-54C were not tested with

the circuit breakers in the CONNECT position (i.e.,

the pumps were not

11bumped

11 or operated to establish

operability).

Pump P-548 was started for system

air sweeps, verifying it could be operated. All three

pumps had local indications which were believed to reflect

operable closing coil power, but (as noted in paragraph 2

above) did not.

The reactor was taken critical.

have appropriate procedures for

spray pumps to service prior to

apparent violation of TS 6.8.1,

The licensee failed to

the return of containment

critically. This is an

(255/91017-0la(DRP)).

The reactor was taken subcritical for reasons unrelated to

the containement spray system.

The containment spray pumps

were no longer required operable.

The reactor was taken critical. The containment spray pumps

were again required to be operable.

After rendering them inoperable on 02/11/91, the licensee

failed to verify that containment spray pumps P-54A and

P-54C were in an operable status until 05/22 and 05/23/91,

respectively. It was subsequently found that pump P-54C

was not operable prior to reactor criticality on 03/10/91

and 03/26/91.

This is an apparent violation of TS 3.4.1

(255/91017-0lb(DRP)).

Containment spray pump P-54C failed to start locally during

surveillance test Q0-16 despite energized lights indicating

"control power available.

11

The auxiliary operator (AO)

contacted the Shift Supervisor and was instructed to repeat

the attempt to start the pump.

The pump failed to start on

the second attempt.

The AO then checked both sets of fuses

and found them to be in good condition.

He re-installed

the fuses, and attempted another pump start.

The pump

started on the third attempt.

The licensee failed to have containment spray pump P-54C

operable between 03/10-25/91, and between 03/26/91 and

05/22/91, while the plant was in power operation.

Redundant components were not tested and the duration

exceeded seven days.

This is an apparent violation of

TS 3.4.2 (255/91017-0lc(DRP)).

4

05/23/91

06/24/91

06/25/91

06/26/91

06/27/91

06/28/91

07/09/91

07 /10/91

08/15/91

An internal corrective action document (deviation

report-PAL-91-097) was issued and reviewed.

The initial

Corrective Action Review Board (CARB) review determined

that an event report was not immediately required; further

evaluation was requested.

Past operability of pump P-54C

since reactor startup was not addressed in associated

documentation.

The evaluation was conducted and two possible causes were

listed. Either the closing coil fuses were not making up

properly, thus disabling the breaker's closing circuitry,

or local control switch (152-114) contacts may not have

adequately closed during the first two start attempts.

The most probable cause of the breaker's failure to close

was believed to be the failure of the fuses to complete the

closing circuit.

However, a Work Order was issued to

measure contact resistance of the local control switch

(152-114) and inspect associated control circuit wiring.

The event was again discussed in a CARB meeting, in the

presence of an NRC inspector. A request was made for

additional time to evaluate the root cause of the event.

The operability of pump P-54C from startup until May 23,

1991, was not discussed .

The NRC inspector discussed D-PAL-91-097 with the electrical

engineering section head and the system engineer to discuss

the control power circuit for 2400 volt circuit breakers.

The NRC Inspector obtained schematic diagrams for two types

of 4160 volt breakers.

These two schematic diagrams were

discussed with the system engineer and two shift supervisors.

The inspector also qustioned how the shift supervisors return

equipment to an operable status after the breakers have been out

of service.

They indicated the components are always start-tested.

The NRC inspector discussed the breaker issue with the Plant

Operations Manager and System Engineering Superintendent.

The inspector officially notified the licensee concerning

Unresolved Item 255/91012-03 and requested a review of how

pump operability was verified when the breakers and fuses

were reinstalled on or prior to March 3, 1991.

A CARB meeting was conducted to discuss the breaker issue and

operability of the containment spray pump.

The NRC inspector reviewed deviation reports (DRs) and work

orders issued in 1990 and 1991 for related issues.

One

event was found (D-PAL-90-194) relative to the output

circuit breaker for Emergency Diesel Generator 1-1 failing

5

to close on August 14, 1990.

in the synchronizing circuit

with the fuse holder fingers

closing coil circuit.

The problem was thought to be

but subsequently proved to be

not making contact in the

08/22/91

LER 255/91-016 was issued; see paragraph 3, above.

5.

Management Interview

The inspectors met with licensee representatives - denoted in

Paragraph 1.a - on September 20, 1991, to discuss the scope and

findings of the inspection as described in these details.

They

were informed that they could expect to be contacted concerning

an enforcement conference on these matters.

The licensee was requested to be prepared to address the following

issues at the enforcement conference:

a.

The accuracy of the findings and the bases for each of the apparent

violations.

b.

Any bases for considering Containment Spray Pump P-54C operable

between February 11 and May 23, 1991.

c.

Assuming P-54C was not operable:

(1)

Safety implications regarding P-54C alone.

(2)

Occasions, duration, and safety implications of other known

equipment inoperability in the subject period.

d.

The apparently similar inoperability of the 1-1 diesel generator

breaker in 1990 (documented on D-PAL-90-194) and whether resolution

of that problem could or should have prevented the containment spray

pump operability problem.

In addition, the likely informational content of the inspection report

with regard to documents or processes reviewed by the inspectors during

the inspection was also discussed.

The licensee did not identify any

such documents/processes as proprietary.

6