ML18057A939

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Insp Rept 50-255/90-25 on 900919-910418.No Violations Cited. Major Areas Inspected:Activities Re Replacement of Steam Generators,Including Engineering,Field Implementation & Testing Activities
ML18057A939
Person / Time
Site: Palisades 
Issue date: 05/24/1991
From: James Gavula, Jeffrey Jacobson, James Smith
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18057A938 List:
References
50-255-90-25, NUDOCS 9106040174
Download: ML18057A939 (38)


See also: IR 05000255/1990025

Text

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. I

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. U.S. NUCLEAR REGULATORY COMMISSION

REGION I I I

Report No:

50-255/90025(DRS)

Docket No:

50-255

. License No:

DPR-20

Licensee:

Consumers Power Company

1945 West Parnall Road

Jackson, MI 49201

Facility Name:. Palisades Nuclear Generating Plant

Inspection At:

Palisades Site, Covert, MI 49043

Inspection Cond

1uct1. S ptember 19, 1990, through April 18, 1991

r011t

~

Team LeadetJ~-* )t Ja obs on . *

.

rf~.Jcff~~

Insp~ctorL ,.J: A. 'blvul a ~ fov

Approved

.

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J. f.i Smith.

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P. V.

Lougge~;d

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R. A. Langstaff

  • ~:UC/312~ /q

By:

D.

~- Danielsoh, Chief

Materials and Processes Section

Inspection Summary

stt.'1~1

Date

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Date

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Date

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Date

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Date

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Date

Inspection on September 19, 1990, through April 18, 1991, (Report No:

50-255/90025(DRS)).

Areas Inspected:

Announced team inspection of activities related to

replacement of the steam generators .. Areas inspected include engine~ring,

field implementation*, and testing activities (73756, 92700, 37700,. 37701);

Results: Three apparent violations were identified; multiple examples of

inadequate design control (Paragraphs 2.a and 5); failure to follow procedures

(Paragraphs 2.a and 5); and insufficient corrective actions (Paragraphs 2.a

and 5).

No Notice of Violation is being issued at this time pending further

evaluation by the NRC .

  • ~11(>6040174

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910524

05000255

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The following strength was noted during this inspection:

0

The

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Scheduling, planning, and coordination of outage activities were

considered excellent.

following weaknesses were noted during this inspection:

Mechanical contractor (Townsend & Bottum) welding procedures were not

sufficiently detailed to control the welding process.

Corrective actions taken to improve implementation of piping design

controls were not effective in the areas examined.

Procedural improvements in.the piping design areas did not reflect FSAR

commitments.

Although technical audits identified nonconformances in implementation

of Bechtel's design controls, effective corrective actions to prevent

recurrence did not occur .

2

TABLE OF CONTENTS

. SECTION

Executive Summary

i

1. O

Piersons Contacted ......... ~ ......... ~ .............. ' ... ~...... I

2.0 * Licen~ee Action on Previous Inspection Finding~ .............. 1

3.0

Review of Licensee Event Reports *..... ~~ ................ ~ .... 7

4.0

Steam Generator Replacement Project Implementation ........... 7

. 5.0

Design Engineering ........................................... * 13

6.0

Testing Activities ....... ~ .................................... 27

7.0

Unresolved Items ..........*............................ ;~ .... 32

a*. 0

Open Items . ................................................... 3-2

9.0

Exit Interview ............

    • .................................... 32

. *

Executive Summary

This report ~ocuments the NRC inspection of the design, implementation and

test activities associated with the Palisades Steam Generator Replacement

Project (SGRP).

Palisades' planning efforts for the SGRP began several years

ago with_ subsequent design activities starting in early 1990, field-

implementation during mid to late 1990, and start-u~ tests during early 1991.

Although the steam generators were replaced with nearly identical units,

extensive modifications were required to the containment structure and

attached piping systems.

Various portions of these changes along with

modificatitins to other safety related plant equipment were reviewed during the

course of this team inspection.

_Previous NRC inspections at Palisades have identified numerous examples where

the design controls for the modification process did not perform as required. *

This weakness had been both recognized and ~cknowledged by the plant and

extensive efforts had recently been undertaken to improve this- area.

The

prob 1 ems as characterized by the previous inspect i ans were not -SO much a 1 ack

of design controls as much as poor performance of the controlling process.

While the recent improvement efforts appear to have further enhanced the

process controls, the results of this inspection indicate the performance

problems still exist.

As with the previous inspections, very few problems were noted during the

field implementation of the modifications.

In this respect, the SGRP was

considered successful with construction activities being well planned and

coordinated. Except-for the problems with the reactor coolant pipe welding

and containment liner plate welding, there were no major field implementation

setbacks.

-

Similarly, however, design control deficiencies continued to be identified in

the calculations used as a basis for the field implementation.

While the

majority of these deficiencies did not result in hardware changes and were not

of great safety significance individually, the number and nature of the design

errors was significant, was indicative that the design control process was

still not performing well, a_nd had the potential to produce significant

reductions in safety margins. Although several of the deficiencies could be

classified as documentation problems, they have an effect on the accuracy and

adequacy of existing analyses when used for modifications.

Previous NRC

inspections have noted similar deficiencies which resulted in a loss of

confidence in design basis information and subsequent extensive

reverification. This inspection again identified instances where design basis

calculations were assumed to be correct without careful verification of their

application.

For example, original seismic response spectra were utilized for

the revised piping design specification without regard to inconsistencies with

current Final Safety Analysis Report (FSAR) commitments .

  • .

. '

I.

DETAILS

Persons Contacted

Consumers Power Company (CPCol

  • D. P. Hoffman, Vice President, Nuclear
  • .*D. W. Joos, Vice President, Energy Supply Services
  • R. D. Orosz, Nuclear Engineering and Construction Manager

~ *W. Clark, Engineering and Construction Manager

  • G. B. Slade, General Manager
  • J. G. Lewis, Assistant Project Manager
  • J. L. Kuemin, Licensing*Engineer

J. C. Nordby,- Welding Engineer

  • W. L. Roberts, Licensing Engineer

T. Fouty, Senior Nuclear Operations Analyst

M. Vanek, Level II, Ultrasonics Examiner

Bechtel Construction

M. Charney, Field Services Manager

R. Steffy, Project Manager

H. Kaiser, Mechanical Engineer

E. Brueckner, Welding Engineer

G. Finnam, QC Welding Engineer

U.S. Nuclear Regulatory Commission CNRC)

  • H. J. Miller, Director, DRS
  • T. 0. Martin, Deputy Director, DRS
  • D. H. Danielson, thief, M&PS

. *B. E. Holian, Project Manager, NRR

  • J. K. Heller, Senior Resident Inspector

J. A. Hopkins, Resident Inspector

The NRC inspectors also contacted other licensee and contractor

  • personnel during the inspection.
  • Denotes thos~ attending the exit meeting on April 18, 1991.

2.

Licensee Action on Previous Inspection Findings (92702)

a.

(Closed) Unresolved Item (255/89007-05): *Questionable design

control practices regarding branch connection welds on Auxiliary

Feedwater bypass piping.

Full penetration welds as required by

design, were shown as fillet welds on the installation documents.

The licensee responded to this issue in a letter to the NRC dated

. December 18, 1989. According to the response, the only method to

verify full penetration for the welds in question was to employ

remote boroscopic examination. This would, according to their

response, require disassembly of adjacent valves to gain access to

the inside of the pipe and would be performed for the four branch

connectio~ welds no later than the 1990 refueling outage.

The

I

,*

licensee's above corrective actions were tracked under Event

Report E-PAL-89-030P which proposed to verify full penetration

welds for the branch connection. A reference to the licensee's

response letter was included in the Event Report's proposed

corrective action.

During this inspection, the NRC inspectrir asked to see the visual

ex~mination report documenting the v~rification of the welds in

question.

The licensee provided a one page document which was

used to close out the corrective actions for the above event

report .. The document discussed the_circumstances surrounding the

installation of the welds and concluded that full penetration

welds were installed as required. This conclusion was based on

reviews tif the available documentation as well as discussions with *

the job supervisor. Consequently, the visual ~erification as

committed to in the original response, ~as not performed.

The NRC inspector's review of this document disclosed several

inconsistencies in the licen~ee's logic. It was stated that the

connection was initially tack welded then had root passes

performed which, the licensee claimed, would not have been done

unless it was a full penetration weld.

The NRC inspector pointed

out that all of the fillet welds in this modification also showed

these same attributes in the weld sheets and therefore their logic

was fl awed ..

Once the incohsistency was presented, the licensee agreed to

radiograph the four connections in question to potentially provide

a basis for their position. The result~ of the radiographs were

documerited in a CPCo Deviation Report which identified weld No. 14

on Drawing 24804972-01-0 as having incomplete penetration and weld

No.* 1 on Drawing 24804973-01-0 as having incomplete penetration

  • and/or slag inclusions;

Based qn the above discussion this Unresolved Item was considered

closed.

Instead this item was considered an example of a

violation of .10 CFR 50, Appendix B; Criteria III, in that design

control measures failed to assure that design requirements wefe

correctly translated into drawings or instructions (255/90025-

0lA).

In addition, since the licensee failed to identify the deficient

conditions and chose to close the event report item without

adquate bases, this was considered an example of an apparent

violation of 10 CFR 50, Appendix B, Criteria XVI, in that

.

corrective action measures failed to promptly identify and correct

a condition adverse to quality (255/90025~02A).

Furthermore, the licensee's corrective action program stated that

if the corrective actions taken differ from the.proposed actions

specified by the Plant Review Committee (PRC), the Event Report

shall be returned to the PRC for concurrence. This process was

2

a.

. *

not followed when, instead of verifying that the welds were full

penetration as described in their response, th~ item was closed

using reviews and discussion~. This was considered an example of

an apparent violation of 10 CFR 50, Appendix B, Criteria V, in

that the procedure for corrective actions was not followed

(255/90025-03A).

.

.

The licensee subsequently issued work requests to repair the two

welds in question prior to the end of the outage.

b.

(Closed) Open Item (255/89007-04):

Inconsistency between the

codes of construction specified in the FSAR and the implementing

procedure.

c.

The license~'s response to the NRC, dated August 10, 1989, stated

that the Palisades staff would complete a reconciliation of all

piping codes of construction to the latest edition of ANSI 831.1,

"Power Piping" and would revise the Updated Final Safety Analysts

Report (UFSAR) to identify applicable codes and standards.

Revision 11 to Palisades UFSAR, dated December 18, 1990, included

a paragraph stating that the code of record for new and existing

piping was changed to ANSI 831.1 (1973) Power Piping Code with

Summer of 1973 Addenda.

This item is considered closed*.

However, during the NRC inspectcir's review of the licensee's code*

reconciliation document, the.licensee ~tated that the

incorporation of th~ "0.75 i" factor for piping stress

jntensification was previously adopted without including any of

the Code related requirements.

It stated that the previous UFSAR

design criteria contained one factor out of the-new Paragraph

  • 104. 8 of the Summer 1973 Addenda and none of the re 1 ated

requirements in Paragraph 119.6~4, Figure 119.6.4(8), Table D-1,

Table D-2 or Figure D-1.

When this problem was discussed with licensee representatives, it

was stated that the stress intensification issue was discussed in

an April 1980 meeting between the NRC and CPCo and found to be

acceptable.

Furthermore, in CPCo's submittal dated October 24,

1980; it was stated that the use of different code editions was:

found to be acceptable and reviewed in accordance with

10 CFR 50.59.

Based on the current code reconciliation document,

the acceptability of this position was questionable and

p6tentially indicated that the 50.59 review for that UFSAR change

was inadequate.

Pending a review of the licensee's action to reconcile the impact

of the improper use of the "0.75 i" fattor in all affected

analyses, t~is was considered an Unresolved_ Item (255/90025-04). *

(Closed) Violation (255/89024-01):

Design bases were not

correctly translated into desjgn documents and the design adequacy

was not sufficiently documented .

3

  • -

. **

litensee's above corrective actions were tracked urider Event

Report E-PAL-89-030P which proposed *to verify full penetration -

welds for the branch connection. A reference to the licensee's

response letter was included-in the Event Report's.proposed

corrective acti~n.

During this inspection, the NRC inspector asked to see the visual

examination report documenting the verification of the welds in

-question.

The licensee provided a one page document which was_

used to close out the corrective actions for the above event

report. The document discussed the circumstances surrounding the

installation of the welds and concluded that full penetration

welds were installed as required. This conclusion was based on

reviews of the available documentation as well as discussions with

the job supervisor. Consequently, the visual verification as

committed to in the original response, was not performed.

The NRC inspector's review of this document disclosed several

inconsistencies in the licensee's logic. It was stated that the

connection* was initially tack welded then had root passes

performed which, the.licensee claimed, would not have been done

unless it was a full penetration weld.

The NRC .inspector poin_ted

out that all of the fillet welds in this modification also showed

these same &ttributes in the weld sheets and therefore their logic

was fl awed .

. Once the inconsistency was presented, the licensee agreed to

radiograph the four connections in question to potentially provide

a basis for their position. The results of the radiographs were

documented in a CPCo Deviation Report which identified weld No. 14

on Drawing 24804972-01-0 as having incomplete _penetration and weld

No. 1 on Drawing 24804973-01-0 as having incomplete penetration

and/or slag inclusions.

Based on the above discussion this Unresolved Item was considere~

closed.

Instead this item was considered an example of a

violation 6f 10 CFR 50, Appendix B,

Crite~ia III, in that design

control measures failed to assure that design requirements were

correctly translated into drawings or instructions (255/90025-

0lA).

-

In addition, since the licensee failed to identify the -deficient

conditions and chose to close the event report item without

adquate bases, this.was considered an example of an apparent

violation of 10 CFR 50, Appendix B, Criteria XVI, in that

corrective action me.asures failed to prompt 1 y identify and correct

a condition adverse to quality (255/90025-02A).

Furthermore, the licensee's corrective action program stated that

if the corrective actions taken differ from the proposed actions

specified by the Plant Review Committee (PRC), the Event Report

shall be returned to the PRC for concurrence. This process was

2

  • -

not followed when, instead of verifying that the welds were full

pen et ration as described in their response, the item was closed .*

using reviews and discussions. This was considered an example of

an apparent violation of 10 CFR 50, Appendix 8, Criteria V, in

that the procedure for corrective actions was not followed

(255/90025-03A).

.

-

The licensee subsequently issued work requests to repair the two

welds in question prior to the end of the outage.

b.

(Closed) Open Item (255/89007-04):

Inconsistency between the

codes of construction specified in the FSAR and the implementing

c.

procedure.

The licensee's response to the NRC, dated August 10, 1989, stated

that the Palisades staff would complete a reconciliation of. all

piping codes of construction to the latest edition of ANSI 831.1,

11 Power- Piping

11 a:nd would revise the Updated Final Safety Analysis

Report (UFSAR) to identify applicable codes and standards.

Revision 11 to Palisades UFSAR, dated December 18, 1990, included

a paragraph stating that the code of record for new and existing

piping was changed to ANSI 831.1 (1973) Power Piping Code with

Summer of 1973 Addenda.

This item is considered closed.

However, during the NRC inspector's review of the licensee's code

reconci 1 i at ion document; the 1 i censee stated that the *

incorporation of the

110..75 i

11 factor for piping stress

intensification was previously adtipted without including any of

the Code related requirements.

It stated that the previous UFSAR

design criteria contained one facto~ out of the new Paragraph

104.8 of the Summer 1973 Addenda and none of the related

requirements in Paragraph 119.6.4, Figure 119.6.4(8), Table D-1, *

Table D~2 or Figure D-1.

-

When this problem was discussed with 11-censee repre$entatives, it

was ~tated that the stress i~tensification is~ue w~s disc~ssed in

~n April 1980 meeting between th~ NRC and CPCo and found to be

acceptable.

Furthermore, in CPCo's submittal dated Octobet 24, *

1980, it was stated that the use of different code editions was

found to be acceptable and reviewed in accordance ~ith

  • *

10 CFR 50.59.

Based on the current code reconciliation document,

the acceptability of this position wa~ questionable and

potentially indicated that the 50.59 review for that UFSAR change

was inadequate.

Pending a review of the licensee's action to reconcile the impact

of the improper use of the

110.75 i

11 factor in all affected

analyses, this was considered an Unresolved Item (255/90025-04].-

(Closed) Violation (255/89024-01):

Design bases were not

correctly translated into design documents and the design adequacy

was not sufficiently documented .

3

..

In their letter dated April 12, 1990, the licensee responded to

the items of noncompliance and unresolved ttems documented in NRC

Inspection Report 50-255/89024 as well as the programmatic

observations made in the December 15, 1989, *NRR Audit Team Report.

For "Corrective Actions to Prevent Recurrence" for the inspection

report'~ design control violation e~ampl~ A~2 and procedure

violation example B.3, the licensee discussed their.intention to

upgrade CPCo Specification M~195 "Requirements for the Design and

Analysis of Palisades Plant Safety Related Piping and Instrumerit

Tubing."

The revision to M-195 was further discussed in the

licensee's responses to Unresolved Items No. 4 and No. 5 in the

inspection report and to Observations No. 3, No~ 5, and No. 8 in

the NRR Audit Report.

The intent of the revision was to provide

clarifi~atio~ of how seismic response spectra were to be applied,*

increase usability, highlight the use of certain seismic ~pect~a~

include integral welded attachments in the evaluation and design

of piping supports and incorporate recent lessons learned and

experiences.

Revision 1 to CPCo's Specification M-195 was issued on May 9,

1990, with extensive changes to the document. Attachment 3 of the

specification was entitled "Original Palisades Plant Response

Spectra and Building Displacements," and consisted of a set of

tables and graphs for various elevations .in the auxiliary

building~ reactor building shell and reactor building internal

' . concrete structure. This information was generated from a s.et of

Bechtel straight-edged plots which CPCo, in their August 10,. 1989,

response to NRC Inspection Report 50~255/89007, acknowledged were

very difficult to read.

The clarity and precision of these plots

may have contributed to the following problems noted during the

NRC review of this data:

(I)

Palisades UFSAR Section 5.7.1.3, "Floor Design Response

Spectra," states that peaks at building natural frequencies

were wjdened +/- 10% to account for variations in soil and

structure material properties ..

Contrary to the above, the response spectra peak for the

first natural frequency of the containment was only widened

between 6.97% and 7.77% on five of the seven floor

elevations.

For the second natural frequency of the

containment, four of the seven floor elevations were widened

less than the prescribed 10%.

For the third natural

frequency of the containment internal structure~ the peak

was not widened at all ~or elevation 649 feet.

Thi~

insufficient widening discrepancy also applied to the

respon$e spectra for all elevations in the auxiliary

building. This ~as considered an example of an apparent

violation of 10 CFR 50, Appendix B, Criterion III in that

the design basis_* information was not correctly translated

into procedures (255/90025~018) .

4

..

(2)

Palisades UFSAR Figures 5.7-9, 5.7-IO, and 5.7-I6 give

typical floor response spectra for the containment building

at elevations 590 feet and 683 feet and for the auxiliary

building at elevation 649 feet, respectively. Zero Period

Acceleration (ZPA) values given in these figures correspond

to the acceleration values given in UFSAR Figures 5.7-7 and

5.7-I5 at the appropriate elevations~

Contrary to the above, the ZPA values given in the Tables of

Attachment 3 to Specification M-I95 were lower than the ZPA

values listed in UFSAR Figures 5.7-7 and 5.7-I5 in II of the

I3 elevations given.

The worst case was a value 20% lower

than that specified for the internal structure at elevation

649 feet. This was considered an example of an apparent

violation of IO CFR 50, Appendix B, Criterion III in that

design basis information was not correctly translated into

procedures (255/90025-0IC).

  • In addition to the above discrepancies, the following

inconsistencies in the response spectra data were ~oted by the NRC

  • inspector:

(3)

The methodology used to widen the spectra peaks at the

building natural frequencies did not appear to be

appropriate.

The acceleratiun plots used as bas~s for the

information in Attachment 3 of M-I95 showed peak broadened

spectra with sides which were not parallel to lines forming

the original spectra peaks. This has been found by the NRC

to be an unacceptable practice in the past.

(4)

For the auxiliary building, the UFSAR gives the fundamental

natural frequency of the reinforced concrete structure as

4.1 Hz in the east-west direction and 5.4 Hz in the

north-south direction. * As stated i~ the UFSAR, the results

foi each direction were enveloped to form a*single set of

results for ,the auxiliary building.

An apparent

inconsistency was noted during a review of the auxiliary

buildin~ response spectra. If these spe~tra were enveloped

for both sets of directions, it would be expected that at

least some building amplification would be seen at both

fundamental natural frequencies.

This was not the case with

the 4.1 Hz natural frequency in the east-west direction.

Comparing values, the east-west acceleration at the

fundamental frequency was a factor of 6 to 9 less than the

acceleration values at the fundamental frequency in the

north-south direction. Although the peak acceleration value

may be bounded with the existing spectia, the frequency

i

content mai not be sufficient to envelope the seismic input

for piping analyses .

5

d.

(5)

All of the original Bechtel response spectra plots for the*

containment building and auxiliary building have**

acceleration peaks occurring at 3 Hz.

However, the lines

drawn on these spectra plots to represent the bounding input

spectra did not include these peaks.

As an example, for

containment elevation 590 feet, th~ value indicated on the .

original Bechtel plot was approximately 0.6 g ~hereas the

value given in Attachment 3 of M-195 was approximately 0.4g.

For piping systems with fundamentals frequencies close to 3

Hz, the seismic response is potentially underestimated by

(6)

50%.

-

The spectra peak value.s for auxiliary building elevations

589 feet, 601 feet *and 610 feet were given as 2.650g,

2.550g, and 2.784g respectively. Since the peak *

acceleration values increase with elevation at all other

floor locatibns~ it was inconsistent for the value at

elevation 601 feet to be less than the value at elevation

589feet. While this may indicate that the peak value at

elevation 589 feet was conservatively high, this was not

intuitively obvious and some verification would be

appropriate in light of the other inconsistencies noted

above.

Pending a review of items 3, 4, 5, and 6 above by the

licensee, with written bases for the adequacy of the data

given in Attachment 3*of Specification M-195, this .was

consid~red an Unresolved- Item (255/90025-05).

(Closed) Open Item (255/90018-01):

Although used for ~scertaining*

technical specification compliance for safety injection tank

levels, the safety injection tank level switches were not

calibrated.

Upon review, the licensee discovered that the*

  • actuation level of the switches had the potential to drift as much

as two inches. Since the level switches had been set at the

technical specificatibn limits, it was possible that these limits**

may have been exceeded.

(Licensee Event Report 90-021 was

  • submitted to report the discovery_.)

However, the levels would

still have been within the recently revised 1 imits, as approved by

technical specification Amendment 136.

By revision of the

technical specification limits and modification of the low level

switches (see paragraph 6.d of this feport, facility change FC-

905) such that the switches were set two inches on the

conservative side of the technical specification limits~ potential

instrument drift was actourited for.

The licensee's commitment to

develop a setpoint methodology for instrumentation was

i~ the

process of being implemented.

However, at the time of this

inspection, the methodology had not yet been applied to these

level switches.

An I&C supervisor stated that the setpoint

methodology would be applied in the future to the level switches

a$ part of a periodic review. This item is considered closed .

  • 6

L.,

"°lj

-*

3.

Review of Licensee Event Reports CLER) (92700)

4.

a.

(Closed) LER (255/90021-LL) See Open* Item 255-90018~01, paragraph

2.d of this report. This item is considered closed.

b.

'(Closed) LER (255/900i8~LLl ."Inadequate Flow Through PCS Hot Leg

Injection Check Valves."

During performance of R0-65 "HPSI/RHPSI Check Valve Test" on

September 30, 1990, the hot leg injection (HLI) flow rates were

less than required by the acceptance criteria for full stroke

verification of the HLI check valves.

As a result of this test

failure, the licensee questioned the adequacy of the acceptance

criteria~

The licensee subsequently implemented corrective actions to ensure

that the acceptance criteria for full stroke veri fi cation reflects

the design basis requirements.' The licensee's review concluded

that the failure of the valves to full stroke was attributed to

improper application of the valve design.

Valve design

modifications were being planned by the licensee.

The NRC inspectors noted that the licensee could have avoided this

event if actions taken to address Generic Letter (GL) 89-04 had

been completed earlier.

GL 89-04 required licensees to review

their implementing pro~edures and programs and amend them as

necessary to ensure conformance with the positions stated in GL 89-04.

The licensee's review was ongoing at the time of the

event, and this procedure had not yet been evaluated.

Steam Generator Replacement Project (SGRP) Implementation (37701)

a;

Background-

Steam generator (SG) tube degradation appeared.early in the

Palisades Plant operating life. The first incidence of tube

corrosion failure occurred after less than one year of operation*

(1972). After approximately four years of operation, 1,775 tubes

out of a total 8,519 (over 20 percent) had been plugged due to

corrosion. A change in water chemistry in mid-1974 slowed the

corrosion rate down such that only 378 additional tubes were

plugged during t~e period 1976 to 1987.

However, d~ring the 16

month period beginning in December 1987, seven tube leaks resulted

in six forced outages.

A decision was made to replace the SGs in conjunction with the

plant refueling outage beginning September 15,

1990~ and

continuing through February 1991. lhe replacement SGs were

fabricated by the original equipment manufacturer, Combustion

Engineering.

7

l, .

To date, six U.S. plants (all Westinghouse design) have completed

SG replacement projects.

For those projects, the containment

equipment hatch openings were of sufficient size to accommodate

the SGs.

The Palisades replacement was unique in that the

significantly larger size of these SGs prevented removal from the

containment through.the equipment hatch. "This required that a

special construction opening, 26 feet QY 28 feet, be cut in the

containment wall.

Another unique feature of the Palisades effort was the first U.S.

application of the narrow groove welding technique developed in

. Germany.

This technique was utilized to reattach the primary

coolant piping to the SG nozzles.

b.

Procedure Review

In preparation for the SG replacement activities, the following

Bechtel procedures and safety evaluations were reviewed:

(1)

Construction Work Plans/Procedures:

WP/P NO.

TITLE

REVISION

1

Establishment, Control, and Implementation

0

of the Construction Work Plan/Procedure

Program .

2

Bechtel Site Orgahization

0

3

Indoctrination and Training

0

4

Document Control

0

5

Field Change Request/Notice

0

6

Field Sketch Preparation

0

7

Deviation Control

0

8

Field Material Requisition

0

9

Material Control

0

11

Housekeeping

0

12

Construction Safety Tagging and Clearance

0

Procedures

14

Control of Temporarily Remoyed Permanent Plant

0

Material

8

i.,_

' .. J

I

15

Maintenance of Materials and Equipment While

0

in.Storage

18

System Turnover to CPCo

0

19

Construction Test Program Requirements

0

20

Field Fabrication

0

21

Safeguards Information

0

22

Installation of Concrete Expansion Anchors

0

P-3

Piping System Cleanness During Construction

0

(2) * Welding Procedures (Automatic)

o

General Welding Standard (Narrow Gap Technique)

GWS-NC, Revision 1

o

Gener~l Welding Standard~ GWS-1, Revision 2

o

Narrow Groove Welding Procedures

o

Pl-G2 (Clad)-NGT-Ag (CVN), Revision 1

0

0

P3-G3 (Clad)-NGT-Ag (CVN), Revision .1

Pl(G2) NGT-Ag (CVN), Revision 1

o

P3(G3) NGT-Ag (CVN), Revision 1

o

Pl-T Clad-0, Revision 1

o

P3-T Clad-0, Revision 1

o

P3-G3 (Clad), Pl-G2 (Clad)-NGT-Ag (CVN), Revision 1

o

P3(G#) and Pl(G2) NGT-Ag (CVN), Revision 1

(3)

Welding Procedures (Manual)

o

Pl-A-Clad, Revision 0

o

Pl-T-Clad, Revision 0

o

P3-A-Clad, Revision 0

o

P3-T-Clad, Revision 1

0

Pl-G2 (Clad)-T (CVN), Revision 1

9

r---- --

-

I

I

0

P3-G3' (Clad)-T (CVN), Revision 1

o

Pl-A-Lh (CVN), Revision 2

.(4)

Replacement bf St~am Generators (safety evaluations)

o

Containment Construction Opening

o*

Replace 2 Inch Slowdown Piping with 4 Inch

o

Remove and Reroute Auxiliary Feedwater Piping

o

Rigging* and Transportation of Heavy Loads

All procedures and safety evaluations reviewed were found to be

well documented and to demonstrate sound technical rationale.

c.

Material Documentation

The replacement SGs were manufactured by Combustion Engineering in

Chattanooga, Tennessee, and shipped to Palisades by barge in

September 1989.

Improvements incbrporated in the riew SGs include

increased blowdown ~apacity; improved flow characteristi~s, and

optimized tube support design.

The SG shells are fabricated from

ASME SA-533, Grade A, Class 1 low alloy steel .. Th~ to~ arid bottom

heads are fabricated from ASME SA~516, Grade 7n and SA-533, Grade

B, Class 1 low alloy material respectively.

Tube ~aterial .is

Inconel

~00 (SB-163) and remains unchanged from the original SG

design.

The NRC inspector reviewed the Code Data Form (N-1} for

the SGs and traced the documentation path*back to select certified

Material Test Reports (CMTRs).

The documentation for the SG

materials was found to be traceable and in conformance with Code

requirements.

d.

Containment Opening and Heavy Lifts

The containme*nt opening was prepared by utilizing a combination* of

~ore drilling, concrete saws and specialized rope saw equipment.

During the course of initial core drilling, one of th~ horizontal

tendons used to post-tension the containment structure was

damaged.

Deviation Report No~ 90-267 was issued to disposition

. the damaged tendon which was subsequently replaced.

The NRC inspector observed a portion of the sawing effort and

removal of the 170 ton concrete block.

B6th the cutting and

lifting oper~tions were found to be perform~d_in accordance with

the approved.procedures and industry standards.

Rigging International was the responsible contractor charged with

erection of the lifti~g devices, performing the lifts, and ground

transportation of the SGs .. The NRC inspector observed portions of

the erection of the outside rigging platform and lifting device,

10

. '"'->

and the in-containment semi-gantry crane. All rigging appeared to

conform to the approved design drawings.

Review of the rigging

design was included in NRC Inspection Report 50-255/90003.

The

NRC inspector also observed portions of the SG lifts and ground

transportation. All observed SG movements were performed in

accordance with approved procedures.

The SG movements and lifts

were considered to be well coordi~ated and executed ..

e.

Wel di nq

Throughout the course of this project; the NRC inspector observed

a sample of various portions of the welding process. Observations*

included welder qualifications, weld edge preparation, fit-up,

welding, and final examination.

As previously mentioned, one of the unique features of this

project was the use of the "narrow-groove" (NG} welding technique .

. The NG welding process requires very precise weld groove prepara-

tion and highly specialized automatic welding equipment.

The

application of this process to heavy wall nuclear system *piping at

Palisades was the first of its kind in the United States. The

process had been applied in Europe with a high degree 6f success

and most recently at the Ringhals facility in Sweden.

Initial NRC

review of this process was documented in NRC Inspection Report

50-255/90003.

The NG welding procedure was based on the automatic gas tungston

arc welding (GTAW} process with; as stated above, specialized*

equipment enabling the welding torch to reach deeply into a narrow

weld groove preparation.

The NG welding process was in concert

with the ALARA concept in that the welding equipment was operated

remotely and the narrow weld-groove required significantly less

weld volume which reduced welding time.

Initial application of this process at Palisades was the welding

of the hot leg piping to the SG nozzles.

Both of these weld

joints were considered successful in that only minimal near-

surface porosity repairs were required .. At this time the cause of

the porosity was hypothesized to be a disturbance of the shielding

gas flow due to the mismatch of the outside diameters of the pipe

and SG nozzle.

Further application of this process on the cold leg connections

resulted in severe porosity defects in the completed welds.

Due

to the joint geometry, the porosity appeared as l in.ear i ndi cations

on the Code radiographs.

Skewed techni~ue radiographs were then

obtained which identified a "~all" of scattered porosity along the

fusion line. Although in-process radiography was* a topic of dis-

cussion with the NRC during early reviews of the NG weld process,

it was not utilized on this project. The licensee elected not to

perform in-process radiography due to the relative difficulty of

obtaining meaningful radiographs coupled with the history of

11

-

.

  • -

!

success with this Welding process. Since the .cause of the defects

were unknown, a decision was made to grind out the defects and

reweld the joints using the manual shielded metal-arc welding

(SMAW) process.

To date, the root cause of the NG welding defects

is unknown.

The NRC inspector reviewed the final radiographs of the reactor

coolant piping welds and main steam line modifications and found

them to meet Code acceptance criteria. In general, the overall

controls a*pplied to piping fit-ups and to activities associated *

with the NG welding process appeared excellent.

The NRC inspector reviewedBechtel NCR Nos. 14 and 15 which were

cissued to disposition ultrasonic examination (UT) indications on

the steam generator nozzles.

During clad buildup for weld prep,

welding difficulties necessitated an informational UT on the "B"

hot leg. During this examination sev~r~l areas of lack of bonding*

of the clad were identified.

As a result of this finding, all

other nozzles were examined and lack of bonding was also

identified on the "B" cold leg of "A" steam generator.

Thoµgh desirable, a 100% bond is not required for structural

  • integrity. However, to facilitate the. NG ~elding of the nozzle

joint, the affected clad was removed and restored to a desirable

conditidn.

Several other NCR's were reviewed and found to be adequately

documented and prudently dispositioned.

Per NRR letter from J. Knight to D. Dutton, NCIG, dated June 26, .

1985, licensees wishing to commit to the Visual Weld Acceptance

Criteria for Structural Welding, must document this commitment in

the form of an amendment to the FSAR. This request was docketed on

November 5, 1990.

The NRC inspector, in accordance with the above

letter, reviewed the licensee's training program and obs~rved a

portion of the training effort and found it to be acceptabl~.

The NRC inspector also reviewed a s~mple bf the mechanical

contractor's (Townsend and Bottum) welding procedures.

During

this review, several ASME Code deficiencies were noted.

While

these deficiencies ap~ear to be documentation errors, the lack of

guidance contained in the procedures is considered to be the more

significant issue.

The procedures, as written, give little or no

direction to the welder.

The CPCo welding procedures were briefly review~d and found to be

somewhat better; however, these procedures are still considered

deficient with respect to controlling the welding process.

Deficiencies in the control. of the welding process contribute to

such current issues as the undersize socket welds and branch

connection discrepancies .

12

....

5 .

')

Design Engineering (37701)

An extensive amount of piping and pipe support modifications were

required to support the SGRP.

Changes in nozzle orientations,

locations, and sizes required reanalyses of several. existing piping

systems. *Changes in seconpary chemistry design required analyses of

se~eral completely new piping systems.

In addition to modifications

associated with SGRP, changes were also made to other plant systems

which required reanalysis of piping and pipe supports.

a.

Bechtel Engineering Efforts

Modifications to piping systems associated with the SGRP ~ere

designed and analyzed by Bechtel's Gaithersburg Office. These

efforts were controlled by design criteria given in CPCo

Specification M-195, "Requirements for the Design and Analysis of

Palisades Plant Safety Related Piping and Instrument Tubing;"

Revision 1, and.by Bechtel's Specification 20557-G-OOlP, "Design

Criteria Documents for Consumers Power Company Palisades Nuclear

Plant Steam Generator Replacement Project", Revision 3.

Paragraph, 5.10.4.2, "Seismic Anchor Movements," (SAM) of M-195 *

specifies that SAMs for the original seismic criteria shall be

taken from Attachment 3 and SAMs for Code Case N-411 seismic

criteria shall be taken from Attachment 4.

For the containment

structure the SAM displacements given in Attachment 3 are lower

than the SAM displacements given in Attachment 4 by a factor of

approximately 3. Paragraph 4.4.2.4.2, "Seismic Anchor Movements,"*

of 20557-G-OOlP specified that displacements to be used were given

in Appendices D and F.

The values given .in these appendices

correspond only to the original response spectra values.

The SAM

displacements for Code Case N-411 seismic criteria were not

included in 20557-G-OOlP. * Therefore, any analysis that used the

N-411 seismic criteria, utilized the wrong SAM values.

This was considered an example of an apparent violation of

10 CFR 50, Appendix B, Criteria Ill, in that design basis

information from M-195 was not correctly translated into

Specification 20557-G-OOlP (255/90~25-0lD)~

This deficiency was corrected with the issuance of 20557-G-OOlP,

Revis'ion 4, January 21, 1991. All analyses that utilized the

incorrect N-411 SAMs were reviewed and revised if necessary.

No

modifications were required as a result of this review.

The following facility change (FC) packages, prepared by Bechtel,

were r~viewed by the NRC inspector:

13

( 1)

FC-911 Main Steam System

As part of the SGRP, *the Main Steam Piping System .was

modified to accommodate the higher nozzle location of the

steam generator. This change r~quired the installation of

an approximately 32 inch piping sptiol piece. The followi~g

documents associated with this facility change were reviewed

by the NRC inspector for comp*l i ance with NRC requirements

and licensee commitments.

(a)

Calculation No. SGRP-PDS-033, "Pipe Stress Analysis of

Steam Generator E50A Main Steam System," Revision 1,

September 6, 1990, and Revision 2, January 21, 1991. ...

The stated purpose of this calculation was to analyze

the piping in accordance with Design Criteria

20557-G~OOlP and CPCo Specification M-195.

During this review the fol1o~ing discrepancies were

noted:

l

In Revision 1, steam generator nozzle SAMs were

taken from structural elevation 649 feet. A

footnote in the calculation stated that the*

nozzle location was at elevation 676 feet 11

. inches *and that the structural movements were

used in accordance with CPCo Specification

M-195.

Specification M-195 discussed SAM

displacements for branch piping decoupled from

run piping and stated that the total seismic

displacement will be used.

By using SAM

displacements from elevation 649 feet, the

. analysis neglected the additional displacement

caused by the 28 feet difference in elevation.

This was considered an example of an apparent

violation of 10 CFR 50, Appendix B,

Criterion III, in that design verification

activities failed to assure that appropriate

design values were used in the pipe stress

analysis (255/90025-0lE) ..

Following discussions with the NRC, the licensee

revised the analysis to account for the

increased SAM displacements.

Using an

extrapolation technique, the licensee concluded

that the SAM displaiements would increase by

approximately 30%.

However, due to the flexible

nature of the main steam piping system,

reanalysis demonstrated that stresses were still

14'

within allowable limfts. This was apparently a

generic problem for any piping system attached

to the steam genetator above elevation 649 feet.

Response spectra given in Paragraph 3.7,

"Applicable Seismic In~ut;" were taken from

structural elevation 649 feet.

However, the

main steam piping is attached to the steam

generator ntizzle at elevation 676 feet 11

inches.

Paragraph 4.4.2.4.1, "Seismic Inertia,"

of Bechtel's Design Criteria 20557-G-OOlP stated

that input response spectra would be developed

by.enveloping the applicable response spectra

for all structures and elevations supporting the

piping.

This w.as an example of an *apparent violation of

10 CFR 50, Appendix B, Criteria III, in that

design verification activities failed to assure

that appropriate design values were used in the

.stress analysis (255/90025-0lF).

A meeting b~tween the licensee and NRC was held.*

on February 8, 1991, to discuss _the above issue.

The presentation given by Bechtel, on behalf of

CPCo, focused on the licensed seismic design

basis for Palisades and then went on to discuss

the main steam line seismic design.

The

presentation concluded by stating that the

response spectrum at elevation 649 *feet was

"representative" of the seismic input at the

main steam nozzle elevation 677 feet.

Although engineering principle~ dictate that

seismic acceleration will be greater at higher

elevations for certain_structural frequencies,

the licensee's presentation did not attempt to

quantify this aspect.

On this basis the

significance of the issue could not be assessed

during the meeting.* The licensee contended that

the current analysis was more conservative than

the original analysis and therefore the analysis

was appropriate.

The fundamental issue was the acceptability of*

using the structur~l model results for

elevations which were significantly higher than

the model elevations. The accuracy of the

structural model to ~redict maximum stresses in

the containment structure was not in question.

However, conservative results for maximum

stresses at the base of the structure ao not

15

  • -.

ensure conservative accelerations and

displacements at the top of the "structure", if

the structural location is not included in the

model.

Following the meeting, the NRC inspector noted

the following discrepancies in the licensee's

presentation. First, it appears that the

original main steam analysis was not performed

in accordance with the Palisades FSAR.

Paragraph 5.7.4 of the FSAR states that piping

systems spanning two or more elevations used

seismic curves closest to and higher than the

center of mass of the piping system.

Since the

highest internal structure spectra was for

elevation 649 feet and the center of mass of the

main steam piping was approximately 665 feet,

the FSAR statement was apparently not met.

Secondly, based on a review of the original

analysis, the spectrum for elevation 649 feet

wasn't even used.

Instead seismic spectra from

elevation 608 feet was used.

This second aspect

is another example of deficient I.E. Bulletin

79-14 implementation by Bechtel and will be

considered as a basis to expand the ongoing

safety related piping reverification program

(Refer to NRC Inspection Reports 50-255/89024

- and 50-255/90002).

Further discussions between the NRC and licensee

disclosed that an evaluation had been performed.

to assess the response of the main steam piping

using response spectra extrapolated up to the

677 feet elevation. This evaluation, submitted

on February 20, 1991, concluded that since the

main steam piping natural frequencies did not

correspond to the higher extrapolated spectra

peaks, the piping stresses and support loads

would not exceed allowable limits.

However, to

date the calculation has not been revised to

incorporate this aspect.

(b)

Calculation No. MSA-PD-EB1-H3, "Pipe Support Design

for Main Steam System, Steam Generator E50A, EB1-H3,"

Revision 2, January 21, 1991.

This calculation evaluated a modification to an

existing stanchion located on the lower elbow of the

. main steam riser. This integral welded attachment has

two non-standard lugs attached to the stanchion to

prevent uplift during a seismic event .

16

During this review the following discrepancies were

noted:

l

Paragraph 5.4.13.1.4, "General Requirements for

Integral Welded Attachments," of Bechtel's

Design Crite~ia 20557-G-OOlP states that "only

one-half of the lugs used shall be considered

effective," and- later states~ "when more than

half of the lugs are considered effective the

flexibility of each load path shall be evaluated

and the load distributed accordingly."

Contrary to the above, the analysis assumed that

the restraining force *would be equally

distributed between the two load paths without

considering the flexibility of each load path.

The pipe support was analyzed using a finite

element frame analysis program in which an

identital force was applied to both sides of the

supporting structure. The resulting

displacements indicated that one side of th~

structure was approximately twic~ as fle~ible-as

the other side. * Based on this, the assumption

that the force would be equally distributed was

invalid.

This was considered an example of an apparent .

. violation of 10 CFR 50, Appendix b,

Criterion III, in that design control activities

failed to appropriately verify.the adequacy of

the support design (255/90025-0lG).

Paragraph 5.7.1, "Deflection Requiremerits,

General Requirement," of CPCo's Specification

C-173(Q), Revision 1, stated that "the total

deflection of the pipe support, in the direction

of the restraint, at the point of load ... shall

not exceed 1/16 inch."

Contrary to the above, the analysis failed to

evaluate the total deflection of the pipe

support which, according to the displacements

given in the analysis, exceeded the 0.063 inch

acceptance criteria. The erroneous method used

in the analysis considered the displacement of

the lug separate from the displacement of the

structure. The total displacement of the pipe

support will be the 0.056 inch displacement from

the structure plus the 0.025 inch displacement

from the lug .

17

This was considered an example of an apparent

violation of 10 CFR 50, Appendix B,

Criterion Ill, in that

design control activities failed to

appropriately verify the adequacy of the support

design (255/90025-0lH).

~

Paragraph 5.4.17.1.1.ii of Bechtel's Design

Criteria 20557-G-OOlP, which discusses baseplate

and expansion anchor bolt design, stated that

the analysis must account for expansion anchor

bolt flexibilities.

Contrary to the above, the baseplate analysis

used ancho~ bolt stiffness values derived from

expansion anchor data, which were not applicable

to the four through-bolted one inch diameter

rods attaching the baseplate to the concrete.

This was considered an example of an apparent

violation of 10 CFR 50, Appendix B,

Criterion III, in that design control measures

failed to verify the adequacy of the design

values used in the stress analysis

(255/90025-0lI) .

(c)

Safety Review, "Main Steam System, FC-911,

Revision O," PS&L Log No. 90-0797, Re~ision O,

September 28, 1990.

This was the safety evaluation of the modification to

the Main Steam System which considered the criteria

for an unreviewed safety question as prescribed in

10 CFR 50.59.

During- this review the following discrepancy was

noted:

Paragraph 5.9.2, of CPCo's Administrative Procedure

No. 9.03A, "Facility Change for SGRP," Revision 0,

March 8, 1990, stated that "Safety evaluati.ons shall

be performed in accordance with Pali~ades

.

. Administrative Procedure 3.07, "Safety Evaluations."

Paragraph 5.2.4 of the above procedure stated that

"When ~nswering each safety review question, the

preparer shall list FSAR ... Sections reviewed as well

as those affected by the item under review~"

Contrary to the above, the safety evaluation did not

review Section 5.7.4, "Seismic Analysis of CPCo Design

Class 1 Piping," and subsequently failed to note that

18

FSAR Section.5.7.4.1 and Figure 5.7-27 were affected

by this change to the facility.

This.was considered an example of an apparent

violation of 10 CFR 50, Appendix 8, Criterion V, in

that the safety evaluation ~~s not accomplished in.

accordance with the procedure (255/90025-038).

As a result of the above, the licensee committed to

make the appropriate changes to their FSAR.

(2)

FC-893 Steam Generator Slowdown System

As .part of the SGRP, the existing 2 inch bottom blowdown

piping was completely removed and replaced with 4 inch

piping. This modification started at the generator. nozzle,

continued thrriugh modified containment penetrations, and

ended at the first containment isolation valve in each li~e.*

The changes were part of a secondary side chemistry control

improvement program and were needed to increase the capacity

of the blowdown system.

The following documents associated with this facility change

were reviewed by the NRC inspector for compliance with NRC

requirements and licensee commitments:

(a)

Calculation No. SGRP-PDS-003, "Pipe Stress An~lysis of

Steam Generator E50A Slowdown Piping Inside

Containment," Revision 5, August 21, 1990.

Section 4.2, "SIF for Branch Connections," of the

calculation provides the bases for the stress

intensification factors (SIF) used. at three welded

branch connections in the pipe stress analysis .. The

calculation concluded that an SIF of 1.0 could be

assigned using the ANSI 831.1 Code equation for branch*

connections.

However, footnotes in the Code stated

that the equation was applicable only if certain

configurational conditions were met.

Contrary to the above, the restrictions for the inner

and outer radii of the branch connection as given in

the Code equation were not specified by any

installation or fabrication document;

This was considered an example of an *apparent

violation of 10 CFR 50, Appendix 8, Criterion III, in

that design control measures failed to assure that the

design basis were correctly translated into drawings

or instructions (255/90025-0lJ).

19

. '

This deficiency potentially applied to other branch

connections designed by Bechtel since this approach

was taken from generic communications applicable to

all projects. The internal memo which discussed the

Code equation did not indicate that the 4se of the

formula had any installation *restrictions ..

Revision 6 t6 the calculation was subsequently issued

on January 30, 1991, with the SIF based on formulas

given by the manufacturer of the branch fitting.

Using this formula, the SIF was increased to 1.367;

however, there was sufficient margin in the original

design to accomodate the 37% increase at the branch

connections without exceeding_ allowable stresses.

(b)

Drawing:No. MlOl-6010, "S.G. E50A Blowdown, Pipe

Support No. H9," Revision 3, Novembe~ 10, 1990.

This was a new support for the new blowdown system

which provided vertical restraint to the piping. It

was constructed fro~ tube steel members with kickers

in the vertical and horizontal direction.

Paragraph 5.4.19.1, "Weld Design; Codes and Symbols,"

of Bechtel's Design Criteria No. 20557-G-OOlP, stated

that welds for pipe supports shall be designed* in

accordance with the American Institute of Steel

Construction (AIS.C) Manual.

Part 4 of the AISC Manual

under "Prequalified Welded Joints" states that fillet

welds for skewed T-joints are limited to a.minimum

angle of 60° and that .for angles less than 60° .the

weld is considered a part_ia_l penetration groove weld.

Contrary to the above, Field Change Notice (FCN) No.

293, December 10, 1990, changed the attachment point

of the horizontal kicker which decreased the angle

between the kicker and baseplate to *approximately 49°

without changing a portion of the field weld from a

fillet weld to a partial penetration groove weld.

The

groove weld required different qualifications for the

.welder and had different limitations regarding base

metal thickness and effective throat measurements.

This was considered an example of an apparent

violation of 10 CFR 50, Appendix B,

C~iterion III in

that design verification activities did not assure

that field changes were subject to the same design

control measures as the original .design

(255/90025-0lK) .

20

(3)

FC-894 Steam Generator Recirculation System

  • As part of the SGRP,

th~ existing 2-inch surface blowdown

piping was completely removed and replaced with 4 inch

recirculation piping. This modification started at the

generator nozzle, continued through modified containment

penetrations, and ended at the containment isolation valve

in each line. The changes were part of the secondary side

chemistry control improvement program.

The following documents associated with this facility ~hange

were reviewed by the NRC inspector for compliance with NRC

requirements and licensee commitments.

(a)

Cal~ulation No. SGRP-PDS-002~ "Pipe Stress Analysis of

Steam Generator E50B, Recirculation Piping Inside

Containment," Revision 8, January 30, .1991.

Paragraph 4.4.2.4.1, "Piping Analysis, Seismic Inertia

Loads," of Bechtel's Design Criteria No. 20557-G-OOlP

stateo that input response spectra will be developed

by enveloping the applicable response spectra for all

structures and elevations supporting the piping.

Contrary to the above, the enveloped response spectrum

did not consider accelerations at the steam generator

nozzle elevation of 661 feet but instead only used

spectral values from elevation 649 feet.

No basts or

justification was given for this discr~pancy.

This was considered an example of an apparent

violation of 10 CFR 50, Appendix B, Criterion III in

that design verification activities failed to assure

that appropriate design values were used in the stress

analysis (255/90025-0ll).

(b)

Calculation No. SGBR-PD-Hl4, "Pipe Support Design for

Steam nenerator E50B Recirculation System Support

Ml01...;6075-Hl4," Revision 2, January 30, 1991.

During as-built walkdowns, the NRC inspector noted

that this support had a significant shear cone overlap

condition between the lower bolts on the upper

baseplate and the upper bolts of the lower baseplate.

Review of the support analysis revealed that the shear

cone overlap had not been evaluated for this confirmed

calculation. This deficiency had been noted twti weeks

earlier by the CPCo technical reviewer during -the

augmented reviews of Bechtel calculations.

Paragraph 5.4.17.3.1, "Anchor Bolt Capacity Reduction

for Shear Cone Overlay," of Bechtel's Design Criteria

21

' *

J

No. 20557-G-OOlP referred to Tables 84 and 85 which

stated that if smaller spacing was used, the allowable

design capacity shall be reduced in proportion to the

ratio of the spacing provided to the required spacing. *

Contrary to the above, with an anchor bolt spacing of

5.3 inches and a required spacing of 7.5 inches for

  • 3/4 inch Hilti bolts and 6.0 inches for 1/2 inch

Drillco bolts, the stress cone overlap was not

evaluat~d in Revision 2 of the calculation.

This was considered an example of an apparent

violation of 10 CFR 50, Appendix B, Criterion III in

_that design verification activities failed to assure

the adequacy of the anchor bolt design

(255/90025-0lM).

The above calculation was subsequently revised on

March li 1991, with an evaluation of the stress cone

overla~~ The methodology used in this evaluation was *

questioned by the NRC inspector because of its

unconventional approach.

The NRC inspector questioned

how concrete could be "reserved" for the Hilti anchor

bolts and not experience any.load from the. Drill co

bolts in this reserved area.

Bechtel's response to

the question stated that the analysis methodology

complied with the requirements of ACI 349, Appendix B .

The application of the refere~ced ACI 349, Appendix B

methodology was not apparent since the document did

not discuss the "reservation" approach used by

Bechte 1 . Sect i. on B. 4. 2 *of the above reference stated

that the effective design strength of the concrete

area is limited by overlapping stress cones. Although

the concrete design strength was conservatively

1

calculated for the Drill co bolt, it was not calculated

for the Hilti bolt even though the two stress cones

6verlapped significantly. The design strength area of

the Hilti bolt was not determined using the

overlapping stress cone method prescribed in the

reference nor was the capacity reduced in accordance

with the controlling design specification.

As discussed above, the evaluation of the anchor bolt

stress cone overlap was not performed in accordanc~

with the applicable design standards.

This was considered an example of an apparent

violation of 10 CFR 50, Appendix B, Criterion III in

that design verification activities failed to assure

that the analysis used an accepted design methodology

(255/90025-0lN) .

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b .

Consumer Power Engineering Efforts

Modifications to piping systems which were not directly associated

with the SGRP were designed and analyzed by CPCo personnel. These

efforts were controlled by design criteria given in CPCo .

Specification M-195, "Requirements for the Design ~nd Analysis *Of

Palisades Plant Safety Related Piping and Instrument Tubing."

The following modifications were reviewed by the NRC inspector:

(1)

SC-90-083 Auxiliary Feedwater Turbine Replacement

This modification upgraded the turbi~e .driver for the P-8B

auxiliary feedwater pump.

The turbine casing pressure

rating was increased from 250 psig to 675 psig.

The NRC

inspector reviewed the following calculation for compliance

with_NRC requirements and licensee commitment5:

Calculation EA-SC-90-083-01, "Change K-8 Turbine to Clais II

(675 psi/6S0°F)," Revision 2, November 27, 1990. This

latest re¥ision deleted proposed changes to pipe support

EB13-H924A and changed the type of reducer on the steam

inlet pipe.

Because of dimensional differences in the

attachment flange, the 4x6 inch reducer was changed from a

concentric to an eccentric reducer.-

Paragraph 6.4.2.b, "Detailed Technical Review," of Palisades

Administrative Procedure No. 9.11, "Engineering Analyses,"

Revision 4, December 28,

1989~ stated that detailed reviews

shall verify the accuracy, completeness and adequacy of the.

  • engineering analysis.

Contrary to the above, the detailed technical review

performed for this calculation on November 27, 1990, did not

consider the effect of the additional moments caused by the

offset of the eccentric reducer nor the effect on the-SIF

for a .component which was not defined in the piping design

Code.

This was considered an example of an ~pparent violatio~ of

10 CFR 50, Appendix B, Criterion III in that the effects of

the eccentric reducer were not adequately considered d~ring

the design verification activities (255/90025-010).

Subsequent reviews by the licensee, documented in* a CPCo

Internal Memorandum from R. Jenkins to D. Bixel,

December 12, 1990, stated that the reducer change-out was

acceptable from a stress analysis perspective.

Based on

this, the significance of this deficiency is minimized .

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(2)

SC-90-032 Replacement of Valves tV-1103 and CV-1104

This modification replaced the two existing c6ntainment sump

drain isolation valves, CV-1103 and CV-1104.

The new 4 inch

valves we~e heavier than the existing valves and the piping

stress analysis was rerun to evalu~te these effects. Piping

stresses were found to be acceptable, and as expected* some

support loads increased.

The NRC inspector reviewed the pipe support calculation

No. EA-03340-HC12-Hl, Revision 3, dated May 28, 1990, for

compl~ance with NRC requirements and licensee commit~ents.

This support was a double rod hanger with a riser clamp and

had a load increase of approximately 50%.

Paragraph 5.11.5, "Rbd Hanger," of CPCo Specification C-173,

"Technical Requirements for the Analysis and Design of

Safety Related Pipe Supports," Revision 1, stated that when

double rod hangers were used on a vertical riser, the *hariger

components and supporting structure were to be designed to

take the total design load on one side.

Contrary to the above, the analysis did not evaluate the

hanger components and structure with the total design load

on one* side.

Instead the design load was divided by two and

the cbmponents were evaluated for this lesser load .

This was considered an apparent violation of 10 CFR 50,

Appendix B, Criterion III, in that design verification

activities failed to assure that an appropriate design

methodology was used in the calculation (255/90025-0lP).

Subsequent reviews performed by the licensee concluded that

as a result of the load increase, the anchor bolts on the

support exceeded al1owable loads and had to be replaced.

This additional modification was performed prior to plant

startup.

c.

. CPCo Quality Assurance Audits

Because of the extensive engineering and construction efforts

associated with the SGRP, CPCo conducted multiple QA audits of

Bechtel's work.

These audits started prior to the beginning of

the design efforts and continued through the closeout of the

construction packages. A total of four technical audits were

performed by CPCo with audit teams consisting of technical experts

from CPCo and Bechtel.

Based on the types of issue§ disclosed during these efforts, the

NRC inspector concluded that the audits were extensive in nature

and performed by competent engineers.

The details discussed in

the audit reports showed an excellent trend_toward performance

24

based inspections.

Detailed reviews done by the technical

auditors were intended to verify the accuracy and adequacy of the

engineering calculations and drawings.

The NRC inspector*

considered this a positive approach by the licensee to assess the

effectiveness of design controls and design verification

activities.

However, because of the number of discrep~ncies found during this

inspection combined with the findings and observations documented

in all four of the licensee's audits, the NRC inspector questioned

the overall effectiveness of actions taken by the licensee to

improve the design controls.

In their response to the design

control violations cited in NRC Inspection Report 50-255/89024,

the licensee acknowledged that their previous modification program

had insufficient controls and was not implemented acceptably.

While the corrective actions taken by the license.e significantly

increased the controls within the modification program, there

contin~ed to be *problems associated with effective implementation.

of these controls.

The discouraging aspect of all of this was

that even though the licensee, through their audits, had

recognized the weak program implementation at Bechtel, apparently

  • sufficient meaningful actions to correct these problems were not

taken.

In the first SGRP audit of Bechtel in December 1989, Observation

No. 1 was written for a failure to identify and correct two

calculational errors during the final checking process:

CPCo

requested that Bechtel evaluate the cir~umstances surrounding the

events which resulted in the problem and provide reasonable

assurance that this was an isolated case and not a programmatic

problem.

/

The second audit conducted in February 1990, documented six

findings and 23 observations. The audit report stated that, while

none of the findings or observations by themselves rendered any

work product completely unacceptable or useable, the number of

concerns raised by the audi.t required prompt Bechtel management

attention ..

In the third SGRP audit of Bechtel in July 1990, additional .

discrepancies were documented in which calculations were found to

be unclear, contained errors or failed to provide justification

for analytical assumptions.

The deficiency further noted that

although individually the items were not considered significant;

however, when taken collectively the conditions were considered a

failure of engineering to provide adequate attention to detail

during calculation preparation and checking.

-

In an*internal memorandum dated August 29, 1990, from CPCo's SGRP

Quality Assurance Manager to the SGRP Project Director, it was

noted that Bechtel's calculation packages appeared to suffer from

the same lack of clarity and completeness that contributed to the

25

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1179-14" situation.

He continued by stating' that the noted

concerns did not appear to have affected the technical adequacy of

the design itself. Later he stated that it appeared that

Bechtel's reviews had been ineffective, 'for whatever reason, since

the audits and SGRP reviews continued to disclose concerns.

Further, it was stated that since most of the engineering design

work was nearly completed, .it did not seem beneficial to him to

request that Bechtel institute any new reviews at that time.

Instead he recommended a final audit be performed at the end of

the *project.

The fourth SGRP audit was subsequently conducted from February 1

to February 21, 1991.

As documented in the March 25, 1991, audit

report, one finding was cited by the audit team. The finding

stated that contrary to Bechtel's quality assurance commitments,

calculations did not have adequate detail to permit a technical

review without recourse to the originator. Over 100 comments,

questions or concerns were documented in the audit team finding.

In the transmittal letter, the licensee stated that the question

of completeness and clarity of design documents was a repeat issue

from earlier audits; however, the technical adequacy of the design

product did not appear to be in question.

Paragraph 4.0 of CPCo's audit report stated:

11The finding addressed a significant number of problem~ and

questions involving most*of the calculations reviewed.

Discussion

with the Techni~al Specialists and Bechtel Engineering has

revealed that individ~ally or collectively, the content of the

finding does not jeopardize the adequacy or integrity of the

design basis. Concern is nonetheless expressed over the number ofr

problems, regardless of the degree of severity.

As the problems.

cited represent a sample, the question remains regarding the

status or quality of th~ balance of the calculations *we did not

examine..

S~RP Engineering routinely performs a technical review

similar to that done by the Technical Specialists on this audit

and have, in fact, discovered many of the same types of.problems

and discrepancies as were uncovered during the audit. Through

their comments, Bechtel has provided appropriate explanations and

corrections.

To this extent, the Audit Team is ~atisfied that the

final calculations will be of sufficient accuracy and detail and

will not request that Bechtel provide corrective action to prevent

recurrence for the finding."

Based on the above.discussions, it is apparent that Bechtel's

design control program did not produce the quality of documents

expected by CPCo or committed to in Bechtel's Quality* Assurance

Manual.

This problem was detected early in the project by audits

performed by the licensee and apparently continued throughout the

entire SGRP.

The deta i 1 ed reviews performed by the 1 i censee' s

SGRP engineering group identified and corrected the majority of

26

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6.

the deficiencies in Bechtel's calculations. These additional

reviews were needed because Bechtel's internal reviews failed to

identify discrepancies in the calculations.

The issue that these discrepancies were simply clarity and

crimpleteness problems is somewhat misleading.

If an error was

noted in a completed, reviewed Bechtel calculation and that error

did not result in a hardware problem, then this could be

considered simply as a documentation problem.

Even though this

would indicate that the design control process was not functional,

the calculation could be revised and no other corrective actions

need to be taken based on lack of significance .. If this were an

infrequent occurrence, some justification could potentially be

given; however, since this appeared to be a prevalent occurrence

in the Bechtel analyses, a programmatic breakdown in the design

corttrol process was indicated.

  • Con~u~ers Power Comp~ny Quality Assurance Program CPC-2A,

Section 16 stated that conditions adverse to quality of safety

related activities shall .be promptly identified and corrected~

Contrary to the above, corrective action measures, while promptly

identifying conditions adverse to quality in Bechtel's design

control implementation, failed to correct these conditions. This

is considered an example of an apparent violation of 10 CFR 50,

Appendix B, Criterion XVI (255/90025-02B).

The lack of sufficient corrective actions on the part of CPCo, to

correct the programmatic problems with Bechtel's design control,

is considered a significant lack of corporate management

involvement in assuring quality work at Palisades.

Testing Activities

a.

  • Inservice Testing Inspection (73756, 92700)
  • This portion of the inspection included selected sections' of the

inseryice testing of pumps and valves and activities related to.

such testing.

The NRC inspectors observed the.applicatioh of the

Valve Operation and Test Evaluation System (VOTES) to a valve

l oc-ated inside containment.

During the calibration portion of the

test, the operators detected anomalous information in the test *

data and concluded that the system could not be properly

calibrated without reinstalling a strain gage on the valve yoke.

Although the testing was not completed, the inspectors were

convinced that the operators were familiar with the equipment and

that they exercised good judgement in ter~inating a test when the

results revealed small, but reproducible anomalies.

The NRC inspectors also reviewed the details of an incident

regarding spray pump operability which occurred in February 1990.

One of three such pumps fell into the required action range of the

Inservice Testing (IST) program vibration criteria. The

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  • inspectors determined that the licensee had established the root

cause of the problem and had provided suitable corrective action .

The corrective action cited in the licensee's Event Report E-PAL-

90-0034H is considered to be capable of ~reventing a repetition of

this problem.

b.

Review of Structural Integrity Test (37700)

The structural tntegrity test (SIT) was considered a post-

modi fication test-for modification FC-914.

Its purpose was to

show that containment structural integrity was not impacted by the

SGRP a~tivities.

The NRC inspectors reviewed the licensee's procedure 20557-SIT

"Primary Reactor Containment Structural Integrity Test Procedure,"

Revision 3, as prepared by Bechtel Power Corporation.

The

inspectors had no comments on the procedure.

The NRC inspectors witnessed the containment pressurization,

including licensee hold points, and inspected the full pressure

crack-mapping activities. The inspectors reviewed the

displacement gauge data, both during the pressurization and hold

periods, and during the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> partial depressurization hold

period.

One gauge exceeded the expected maximum displacement

value.

The NRC inspectors discussed the behavior of the gauge

with the licensee during the test. The licensee'_s prelim.inary

conclusion ftir the increased displacement value was that the

containment was slightly ovoid, rather than perfectly round, and

the increase~ pressure was causing the structure to "round out.

11

This conclusion was substantiated by the behavior of the other

three gauges in the area.

No other problems were identified with

these activities.

The NRC inspectors reviewed a prel imina-ry report of the fi.nal

results.

The report concluded that the gauge discussed above was

acceptable, as the acceptance criteria was based on the average

displacement values being below the calculated maximum.

This

criterion was ~et. The inspectors had no problems with this

conclusion.

c.

Tendon* Surveillance Requirements for the Replaced Tendon (37700)

During inspection docume~ted in NRC Inspection .Report

50-255/90017, and subsequent conversations with both licensee and

Bechtel SGRP personnel, the possibility of Palisades using new

replacement tendons was discussed. Specifically, it was_ noted

that Palisades technical specifications no longer contained the

requirement for demonstrating containment tendon structural

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d.

integrity at the end of one, three, and five year intervals

following the structural integrity test, and every five years

thereafter. This subject was left for discussion in the event

that any tendons were actually replaced during the SGRP.

During

the course of the SGRP~ one tendon was damaged during the cutting

of the containment opening and had to be *replaced with.a new

cable.

In a letter from Consumers Power dated February 12, 1991, the

licensee acknowledged NRC questions in regard to tendon

inspections~ The letter stated that one vertical and two hoop

tendons from the SGRP opening, as well as one tendon which had

experienced low lift-off readings, would be examined during the

scheduled 1992 surveillance. The NRC inspectors questioned

whether the replaced tendon was one of those to be included in the

surveillance program.

During further discussions, the licensee

confirmed that the new tendon was not included in the 1992

surveillance.

It is the NRC's position that the replaced tendon should be.

included in the 1992 scheduled surveillance. This is based on the

NRC technical staff and Bechtel experience which indicates that

the majority of a new tendon's detensioning occurs during the

first year or two.

Therefore, an inspection in 1992 would show if

the replaced tendon had detensioned.

The NRC staff i~ not .

requiring that the on-going surveillance program be adjusted for a

single tendon, but does consider inclusion of this tendon in the .

1992 surveillance to be prudent.

Inclusion of this tendon into

the 1992 planned surveillance is considered an Open Item

(255/90025-06).

The NRC, in a letter from B. Holian, Palisad~s Project Manager,

NRR to G. Slade, dated November 20, 1990, reserved the final

acceptability of the containment structure until a review of the

structural integrity test was performed.

This inspection

constituted the review specified in that letter.

No violations .or deviations were identified in this area.

Review of Facility Change FC-905, Safety Injection Tank Lower

  • Level Alarm Switch Modification:

This modification altered the low level switches for the safety

injection tanks such that the switches would actuat~ at a lower

level. The change in actuation level was made to correspond to a

revised minimum l~vel incorporated into technical specification

Amendment 136. Originally, the modification set the new actuation

point at the revised technical specification minimum level.

However, due.to concerns regarding potential instrument drift of.

the level switches (see paragraph.2 of this report, Open Item 50-

255/90018-01)~ the new switch as~emblies were modified to actuate

two inches above the revised technical specification minimum level

29

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thus accqunting for potential instrument drift .

The NRC inspector reviewed the de$ign package for this

modification, the associated licensing history, and the procedure

for calibration of the safety injection tank level transmitters.

The 10 CFR 50.59 evaluations, associated *safety analyses, and

design inputs for the modification were generally found to be well

justified and documented.

However, several discrepancies were

noted during the NRC inspector's ~~views of the* following

documents:

(1)

Test Procedure T-FC-905(a)-001, "SI Tank Low Level Float

Ass~mbly," Revision 0, July 24, 1990.

(2)

One of the purposes of the test was to verify proper

operation of the newly installed low-level float assemblies.

As part of this procedure, the SI tank levels were to be

gradually raised to elev~tion 737 feet and then clear~nce of

the low-level alarm was to be verified. However,

Engineering Design Change 03 revised the level switch

actuation point by 2 inches, but the test procedure was not.

revised to account for this change.

With the elevation 737

feet specified in the procedure, the level switches would

not have actuated and the low-level alarm would not have

  • cleared as specified in the test .

10 CFR 50, Appendix B, Criterion III requires that design

control measures be applied to the delineation of test

acceptance criteria and that changes be subject to controls

commensurate with the original design.

Contrary to the above, when the ~loat design elevation was

changed, the test elevation acceptance criteria was not

.revised. This was considered an example of an apparent *

violation of 10 CFR 50, Appendix B, Criterion III

(255/90025-0lQ).

.

After the NRC inspector informed the licensee of this error,

the test procedure was promptly revised.

In this case the

significance was reduced since the error would have been

self disclosing during the test.

Calculation EA-FC-905-003, "Safety Injection Tanks (T-82)

  • Level Calibration Calculations," Revision 2, November 30,

1990.

Calculation assumption No. 2 stated that the existing

atialysis was correct. This 1978 calculation determined the

initial relationship between the differential pressure and

the SI tank level. The calculation did not account for the

effects of the weight of the pressurized nitrogen inside the

30

tanks nor the containment temperature on the differential

pressure and level relationship. Based on this, the

accuracy of the calculation was in question and the validity

  • of the assumption was suspect.

Pending the licensee's verification that the design basis

accuracy of the level. indication instrument loop had not

been exceeded by neglecting the effects of the nitrogen

weight and containment temperature, this was considered an

Unresolved Item (255/90025-07).

The significance of this issue was minimized since the

technical specification compliance was based on the level

switch actuation and not on the level indication from the

transmitter.

e.

Review of Facility Change FC-852, Addition of Second PCS Level.

f.

Indication:

This modification added a second means of reactor coolant. system

level indication. The modification provided 30 inches of level

indication centered on the hot legs for use during mid-loop

operation.

The modification added a differential pressure

transmitter which tapped into existing instrument lines. The

second means of level indication was added in response to Generic

Letter 88-17.

The NRC inspector reviewed the safety analysis, design inputs, and

installation. The 10 CFR 50.59 evaluations, associated safety

analysis, and design in~uts for the modification were found to be

well justified and documented.

No concerns were identified.

.

.

. Review of Procedure RT-70F, Primary Cool~nt System:

Procedure RT-70F was written as a technical specifications

surveillance procedure to verify leak tightness of the primary

coolant lines .. The NRC

in~pector reviewed the procedure for

adequacy as part of the post-modification testing for several

modifications.

The procedure satisfied the American Society of

Mechanical Engineers (ASME)Section XI Code requirements for a

hydrostatic test and an inservice system leak test.

No concerns

were identified .

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7.

Unresolved Items

An unresolved item is a matter about which more information is required

in order to ascertain whether it is an acceptable item, an open item, a

deviation, or a violation. The unresolved items disclosed during this

. inspection are ~iscussed in Paragraphs 2.b, 2.c, and 6.d of this report.

8.

Open I terns

Open items.are matters which have been discussed with the licensee,

which will be reviewed further by the inspector, and which involves some

action on the part of the NRC or licensee or both .. The open item

disclosed during this inspection is discussed in Paragraph 6.c of this

report.

9.

Exit Interview

The Region III inspectors met with the licensee representatives (denoted

in Paragraph 1) at the conclusion of the inspection on April 18, 1991 as

well as periodically during the course of the inspection.

The

inspectors summarized the purpose and findings of the inspection.

The

licensee representatives acknowledged this information .. The inspector

also discussed the likely informational content of the inspection ~eport

with regard to documents or processes reviewed during th~ inspection~

The licensee representatives did not identify any such

documents/processes as proprietary .

32