ML18038B744

From kanterella
Jump to navigation Jump to search
Insp Repts 50-259/96-06,50-260/96-06 & 50-296/96-06 on 960609-0720.Violations Noted.Major Areas Inspected: Operations,Engineering,Maintenance & Plant Support
ML18038B744
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 08/15/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B742 List:
References
50-259-96-06, 50-259-96-6, 50-260-96-06, 50-260-96-6, 50-296-96-06, 50-296-96-6, NUDOCS 9608270475
Download: ML18038B744 (80)


See also: IR 05000259/1996006

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

License

Nos:

50-259,

50-260,

50-296

DPR-33,

DRP-52,

DPR-68

Report Nos:

50-259/96-06,

50-260/96-06,

50-296/96-06

Licensee:

Tennessee

Valley Authority

Facility:

Browns Ferry Nuclear Plant, Units 1,

2

5

3

Location:

Corner of Shaw and

Browns Ferry Roads

Athens,

AL

35611

Dates:

June

9 July 20,

1996

Inspectors:

Approved by:

L. Mert, Senior Resident

Inspector

J.

Hunday,

Resident

Inspector

R. Husser,

Resident

Inspector

K. O'Donohue,

Resident

Inspector

Development

Program Participant

J.

Canady,

Resident

Inspector,

Plant Hatch

(paragraphs

Hl.4, El.3,

and Fl.l)

B. Holbrook, Senior Resident

Inspector,

Plant

Hatch (paragraph

E1.2)

D. Jones,

Senior Radiation Specialist,

DRS

(paragraphs Rl.l, R1.2, Rl.3,

R7. 1,

R 8.1)

J. Starefos,

Project Engineer,

DRP

G. HacDonald,

Reactor Inspector,

DRS

(paragraphs Hl.l, H3.1,

H7)

J. Milliams, Project Manager,

NRR

(paragraph

El. 1)

F. Wright, Senior Radiation Specialist,

DRS

(paragraphs

R1.4,

R1.5,

R2.1,

R7.2)

H. Lesser,

Chief

Reactor

Projects

Branch

6

Division of Reactor Projects

Enclosure

2

9608270475

'760815

PDR

ADOCK 05000259

8

PDR

Oi

ili

i

EXECUTIVE SUMMARY

Browns Ferry Nuclear Plant, Units 1,

2 5 3

NRC Inspection

Report 50-259/96-06,

50-260/96-06,

50-296/96-06

This integrated

inspection

included aspects

of licensee

operations,

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident

inspection including the efforts of several

resident

inspectors

from other facilities. In addition, it includes the results of

announced

inspections

by two regional radiation specialists,

a regional

reactor inspector

(maintenance),

a regional projects engineer,

and the

NRR

project Manager.

~0e

Ltto~s

~

Overall, the conduct of operations

was professional

and focused

on

safety.

Specifically, the inspectors

noted continued

good use of

annunciator

response

procedures

and control

room communications

(Section

01).

The quality of the control, room logs significantly increased

in recent

months, with more comprehensive

and detailed entries

(Section Ol).

~

.

0

Assistant Unit Operators

were professional

and thorough during plant

tours.

Overall housekeeping

conditions were satisfactory

(Section

01.2).

A non-cited violation was identified.

A Unit Supervisor identified that

a Unit 2 control rod was not correctly positioned after

a control rod

exercise test.

Corrective actions

were prompt and thorough (Section

01.3).

The inspectors identified a violation involving a disabled control

room

annunci'ator.

The annunciator is described

in the Final Safety Analysis

Report

and was disabled without a safety evaluation

(Section 03.1).

The recently initiated Operations self assessment

program

was reviewed.

The program is new and implementation of the specific checklists is

expected to improve.

The program resulted in clear promulgation of

management

expectations

and the identification of performance

issues

(Section 07).

During observation of a Standby Liquid Control system test,

the

inspectors identified that coordination

between

some of the work groups

was not strong

and that Operations

personnel

did not follow the

procedure

in sequence.

This was addressed

as

one example of a

procedural

adherence

violation (Section Ml.3).

~

~

il'

ten

ce

~

Several electrical preventive maintenance

items

and degraded grid relay

tests

were observed to be performed with good attention to detail.

Strong coordination

and communications

were also noted during those work

activities (Section Hl.l, Hl.4).

~

During observation of Standby

Gas Treatment

and Standby Liquid Control

testing,

the inspectors

identified that procedural

requirements

were not

met.

These

issues

were addressed

as two examples of a procedural

adherence

violation.

Previous

inspection reports discussed

examples of

procedural

adherence

deficiencies

associated

with maintenance

activities.

During this report period, the inspectors

noted that most

maintenance

workers demonstrated

deliberate effort toward full

procedural

compliance.

Maintenance

management

emphasized

the importance

of procedural

compliance.

Although some

improvement

was noted,

additional

progress

is needed

(Section Ml.2, H3).

~

A non-cited violation was identified associated

with a failure to

perform testing of an excess

flow check valve (Seciton H8.2).

ee in

0

The inspectors identified that

a safety evaluation

was not completed for

a planned design

change modification.

The safety analysis incorrectly

concluded that

a safety evaluation

was not required.

The modification

was not implemented.

This was addressed

as

an example of a procedural

compliance violation.

The inspectors

also identified that procedural

guidelines for determination of an unreviewed safety question did not

address all relevant design requirements

(Section El.l).

~

The inspectors identified that

a surveillance

procedure

was utilized

informally during verification of control

room emergency ventilation

system air flows (Section El.2).

~

During observation of repair activities involving an important

electrohydr aulic control system circuit and

an Emergency

Core Cooling

System instrumentation inverter,

good performance

was noted.

Coordination

between

work groups

and the pre-job briefings were

particularly strong (Section E1.3).

lant

S

ort

~

The licensee

implemented

an effective program to monitor and control

liquid and gaseous

radioactive effluents.

The projected offsite doses

from effluents were well within the limits specified in the Technical

Specifications

(TS), Offsite Dose Calculation

Manual

(ODCM), and Title

40 Code of Federal

Regulations

Part

190 (Paragraph

Rl. 1).

The licensee

complied with the sampling, analytical

and reporting

program requirements

and the radiological environmental

monitoring

i

program was effectively implemented.

The licensee's

overall performance

in the

EPA cross-check

program demonstrated

that

an effective quality

assurance

program was maintained for analysis of environmental

samples

(Paragraphs

Rl.2 and R7).

One Noncited Violation (NCV) was identified for failure to adequately

follow procedures

for receipt of radioactive material

(Paragraph

Rl.3).

~

The Radiation Protection

(RP) program was adequately

managed;

internal

and external

exposure

control programs

were effectively implemented with

all radiation exposures

within 10 CFR Part 20 limits (Paragraph

Rl.4).

Tour of licensee facilities showed generally

good radiological

housekeeping

and controls

(Paragraph

Rl.5).

Effective implementation of As Low as Reasonably

Achievable

(ALARA) dose

reduction principles, the operation of Units 2 and 3,

and reductions

in

refueling outage durations

on Unit 2 have contributed in the reduction

of site collective doses

(Paragraph

Rl.6).

Overall performance

during

a diesel driven fire pump test

was good.

However, the inspector noted

a recurring problem with the engine

heat

exchanger

has not been adequately

resolved.

Some workers did not

understand

the engine cooling water flowpath.

Subsequent

corrective

actions

by the Fire Protection

Hanager

were prompt and effective

(Section F1.2).

~i

Oi

O~

0

Re ort Details

S

mm

o

P

nt Stat

s

Unit

1 remained in a long-term layup condition with the reactor defueled.

Units

2 and

3 operated

at power during this report period.

On July 17,

1996, at 12:58 p.m., the Unit 3 Emergency

Core Cooling System

(ECCS), Division I Analog Trip Unit (ATU) inverter was declared

inoperable

following the clearing of a fuse.

The appropriate, Technical Specification

(TS) limiting conditions for operation

(LCOs) were entered

and at 5:00 p.m.

a

controlled shutdown initiated.

The licensee notified the

NRC in accordance

with 10 CFR 50.72.

The affected inverter was repaired

and declared

operable

at 5:57 p.m.

Subsequently,

the unit was returned to full rated power.

On

July 19,

power was reduced to 50 percent for condenser

waterbox cleaning,

control rod testing,

and steam valve leak repairs.

The unit was returned to

full rated

power on July 20 and operated at power for the remainder of the

reporting period.

I. 0 erations

1

01

Conduct of Operations

01.1

Gene al

Comments

71707

Using Inspection

Procedure

71707, the inspectors

conducted frequent

reviews of ongoing plant operations.

In general,

the conduct of opera-

tions was professional

and safety-conscious;

specific observations

are

detailed in the sections

below.

In particular,

the inspectors

noted

that significant improvement

was

made in the overall quality of the

Operating logs.

Previous

NRC inspections

and other assessments

noted

that the logs should

be improved.

In recent

months,

the inspectors

noted that entries

were

made

on pertinent information and the level of

detail applied to most of the entries

was significantly improved.

The

inspectors

also noted that alarm response

procedure

adherence

and

control

room communications

continued to be strong.

01.2

0 erator

Rounds

a.

Ins ection

Sco

e

71707

On several

occasions

during the report period, the inspectors

reviewed

performance of plant tours

by Operations

personnel.

The following

procedures

and attachments

were reviewed:

~

O-GOI-300-1, Operations

Routine Sheets,

Revision

37

ili

il~

~

O-GOI-300-1, Attachment 7, Unit 2 Reactor Building Tour and

Turnover Checklist

~

O-GOI-300-1, Attachment 8, Unit 2 Turbine Building Tour and

Turnover Checklist

O-GOI-300-1, Attachment 9, Unit 3 Reactor Building Tour and

Turnover Checklist

O-GOI-300-1, Attachment

10, Unit 3 Turbine Building Tour and

Turnover Checklist

~

O-GOI-300-1, Attachment

11, Units

1 and

2 Control

Bay Checklist

The inspectors

accompanied

assistant

unit operators

(AUOs) on Units

1

and

2 control

bay rounds,

Unit 3 Reactor Building rounds,

and Unit 3

Turbine Building rounds.

One of the inspectors

walked down the Unit 2

Reactor Building rounds

area after the

AUO completed the rounds for that

shift.

Observations

by the inspector included performance of the

rounds,

general

area

awareness,

and follow up actions

on items

identified during the performance of the rounds.

b.

Obse

tions

and

i din s:

Each

AUO was observed

from turnover through downloading of the rounds

information to the computer.

The following items were observed

during

the performance of 0-GOI-300-1 attachments:

The verbal turnover between

the

AUOs was informal and

unstructured.

While some

AUOs checked with control

room personnel

prior to starting the rounds,

others did not.

However, the

inspectors

did not identify any pertinent information that was not

adequately

described

in the turnovers.

Data required to be collected in the handheld

computers

and data

required

by the hard copy oF the procedure

was inconsistent.

For

instance:

Attachment

10, Unit 3 Turbine Building Tour and Turnover

Checklist calls for 250V Battery Board

6 Ground Indicator readings

during each shift. The computer did not include that requirement

for the day shift rounds.

The hard copy and the computer version

should

be identical since they are

used interchangeably.

No TS

required indications were affected.

All observed

operators

performed their rounds in a professional

manner.

Generally,

housekeeping

conditions were adequate,

except for

several oil leaks.

Oil. absorption

pads

were not changed

out

during the performance of the rounds. 'n two occasions,

the

inspector returned to particularly large oil leaks later in the

same shift and verified that the saturated oil absorption

pads

il~

0

il

C.

01.3

were replaced with fresh pads

and that the general

area

around the

equipment

was cleaned.

Conclusions

Observed

rounds

were performed adequately.

General

condition of the

units was good.

The AUOs followed through

on items identified in their

areas of responsibility during the performance of the rounds.

Adequate

communications

between the control

room and the

AUO performing the area

rounds were observed.

The licensee initiated corrective actions to

address

minor differences

between

the handheld

computer required

. parameters

and procedure

requirements.

Control

Rod Not Correctl

Re ositio ed Fol owi

od

xerc'se

est

Observations

and Findin s

At ll:30 a.m.

on June

17,

1996, the Unit 2 Unit Supervisor

noted that

control rod 58-19 was at position

46 instead of position 48.

Subsequent

investigation indicated that the rod was not returned to

position 48 after the performance of 2-SI-4.3.A.2, Control

Rod Drive

Exercise Test.

The reactor engineer

was contacted.

The rod was

returned to the correct position and Problem Evaluation Report

960792

was initiated.

One of the inspectors

reviewed Operating Instruction 85,

Control

Rod Drive, and verified that the condition did not require

actions

as

a mispositioned control rod.

The inspector reviewed the

control

room logs

and noted that the testing

was completed at 10:45 a.m.

on June

15.

Several shift turnovers

and numerous control board

walkdowns were completed after the error occurred.

Specific

verification of each control rod position is not expected

at each shift

turnover.

The inspector

noted that at least

one other rod was correctly

positioned at 46 and concluded that this may have contributed to the

issue not being identified more promptly.

Corrective actions included

counseling of the involved individuals.

Additionally, SI-4.3.A.2 was

revised to require

independent verification that control rods are

returned to correct positions after exercising.

(Previously,

the

procedure

required comparison of the rod positions

by the test

performer.)

The inspector verified that the procedure

was revised.

The

licensee attributed the cause of the incident to failure to follow

procedure.

This licensee-identified

and corrected violation is being

treated

as

a Non-Cited Violation, consistent with Section VII.B.I of the

NRC

E forcement Pol'c

.

This issue is identified as Non-Cited Violation

96-06-03,

Control

Rod Not Correctly Positioned After Testing.

il~

i

03

Operations

Procedures

and Documentation

03.1

Disabled Control

Room Annunciators

71

07

a.

I s ection

Sco

e

On June

17,

1996, the inspector reviewed the licensee's

disabled

annunciator

program.

The Unit 2 and Unit 3 disabled

annunciator

logs

were reviewed,

control

room operators

were interviewed,

and both control

rooms were walked down.

The inspector reviewed the following:

~

Operating Instruction O-OI-55, Revision

10, "Annunciator System"

~

Attachment

6 of O-OI-55, "Disabling Annunciator Input Form", dated

January ll, 1995

~

Fina'l Safety Analysis Report

(FSAR) Chapters

7.7 and 7.8

b.

Observat'o

s

and F'nd

n

s

Thirteen Unit 2 disabled

alarms

and five Unit 3 disabled

alarms

were

reviewed.

Each disabled

annunciator

window, listed in the disabled

annunciator log, was appropriately

marked

by a plastic outline to

indicate the disabled condition.

The control

room operators

were aware

of all disabled

alarms

on the assigned unit.

The compensatory

actions for the disabled

alarms

are listed as part of

Attachment

6 to OI-55.

The following was noted during the review of the

compensatory

actions:

~

Compensatory

actions

were inconsistent

between Unit 2 and 3.

Both

Unit 2 and Unit 3 had

some inputs to the annunciator for control

rod drive unit temperature

high disabled.

The Unit 2 compensatory

action stated

"Points will be monitored

on

ICS and recorder".

For

the

same annunciator,

Unit 3 compensatory

action was listed as

"none".

~

The compensatory

action, listed on Unit 2 for the disabled control

rod drive unit temperature

high annunciator,

could not be

performed for all the drives.

The stated action was that

temperatures

would be monitored

on

a recorder.

Because

several

thermocouples

were actually open circuits, there would be no input

to the recorders

or

ICS,

and the points could not be monitored.

~

A simple entry of "None" was used,

in some cases,

to indicate

no

compensatory

action would be taken without indicating why

compensatory

action

was not necessary.

Unit 2's Alarm panel

2-XA-55-4B, annunciator

window 1,

Rx Vessel

Head

Seal

Leak Off Pressure

High 2-PA-3-189,

was disabled.

The annunciator

inputs are 2-LS-3-189

and 2-PS-3-190.

2-LS-3-189 was disabled

on

~i

i

~

i

April 25,

1996

and 2-PS-3-190

was disabled

on April 30,

1996.

The

associated

Disabling Annunciator Input Forms indicated inaccurately that

the annunciator

was not required

by the

FSAR; therefore,

no safety

assessment

or safety evaluation

was completed for disabling this

annunciator.

This was incorrect since

FSAR 7.8-8 specifically describes

this alarm.

0-OI-55 provided general direction for completion of the Disabling

Annunciator Input Form.

However, the OI did not supply details

regarding expectations

of the information to include in the form.

PER 960821

was written to further address

disabling of alarms

and the

associated

safety assessments

and safety evaluations

performance.

Operations

management

indicated that revisions to OI-55 would be

evaluated.

C.

Conc usio

s

07

07.1

The documentation of compensatory

actions for disabled

annunciators

was

not strong.

One annunciator,

which is described

in the

FSAR,

was

disabled without completion of a safety evaluation.

10 CFR 50.59 {b)(l) requires

the licensee to maintain records of changes

in the facility made pursuant to that section to the extent that these

changes

constitute

changes

in the facility as described

in the safety

analysis report.

These records

must include written safety evaluations

which provide the bases for the determination that the change

does not

involve an unreviewed safety question.

Failure to perform a safety evaluation prior to disabling

Rx Vessel

Head

Seal

Leak Off Pressure

High annunciator

2-PA-3-189 is

a violation of 10 CFR 50.59 requirements

and is identified as

VIO 260/96-06-02,

Failure to

Perform

a l0 CFR 50.59 Evaluation Prior to Disabling Annunciator.

guality Assurance in Operations

0 erations Self Assessment

Pro

am

a ~

Ins ection

Sco

e

40500

71707

On June

26,

1996,

a resident inspector reviewed records

and other

information associated

with the Operations Self Assessment

Program.

The

following documents

were referenced

during the review:

Operations

Section Instruction Letter

(OSIL) 72,

Operations Self

Assessment

Process

Site Specific Procedure

12.1 {Revision 27), Conduct of Operations

Documented records

such

as completed checklists

and monthly

reports for the period February

1996 through Hay 1996

Oi

0

4I

b.

Observ t'ons

and Findin

s

The Operations Self Assessment

Process

was initiated in February

1996.

The primary intent was to provide self critical assessment

of Operations

activities.

The process

contains detailed checklists

which address

specific important activities.

The completed checklists

are reviewed

by

checklist "owners"

as well as Operations

management.

Monthly and

quarterly reports

are developed that summarize

the results of the

checklists,

incorporate Operations

performance

data from other reviews,

provide quality indicators,

and

recommend

areas that should

be

emphasized

for improvement.

The inspector noted the following:

~

The process

was still relatively new and will be revised to

improve usefulness.

~

Not all completed checklists

were signed

by the individual being

observed.

This signature is intended to indicate that feedback

was provided.

~

A quarterly report was not yet issued.

~

Several

of the checklists

were lengthy and effort was required to

accurately

complete the checklists.

Although the majority of the

reports

were not critical, indications were that personnel

were

making significant effort to properly complete the checklists at

the frequency

recommended

in the OSIL.

Approximately 100

checklists

were completed during each of the monthly periods

reviewed.

~

Checklist

CL OP.

1.7 was not yet completed.

OSIL 72 Table

2

recommends

completion monthly.

This checklist is to be completed

by Operations

management

as

an evaluation of shift management

coaching.

~

The checklists clearly promulgate

management

expectations

to the

Operations

workers.

This was

an area

noted previously as not

strong.

The inspector's

discussions

with some operators verified

that the checklists

were providing communications of expectations.

The inspector

concluded that the Operations self assessment

efforts

resulted in clear communications of management

expectations.

The

program is still new and

some refinement is expected.

The program

resulted in identification of some adverse

performance

issues

which are

currently being addressed.

For example,

PER 960726

was initiated to

address

several

events involving balance of plant components

which were

not fully positioned to their correct position.

0

il~

II. Naintenance

Nl

Conduct of Naintenance

Ml. 1

Observation of Maintenance

and Surveillance Activities

a.

s ection

Sco

e

62703

61

26

Selected

surveillance

and maintenance activities were observed to

determine if the activities were performed in accordance

with procedural

and regulatory requirements.

The inspection

scope

included observation

of surveillance activity 1-SI-4.2.A-20,

Reactor

Zone Isolation Logic

System Functional Test,

and observation of portions of the following

maintenance activities:

W096007400000

Electrical Maintenance

Troubleshoot

480

V (Volt) RHOV

Board

2A Turbine Bearing Lift Pump

W096000567000

Electrical Preventive

Maintenance

and Testing of

Alternate Feeder to 480

V Control

Bay Vent Board

B

W096005807000

Electrical Preventive

Maintenance

and Testing of Motor

Control Center

(HCC) for OffGas Building Exhaust

Fan

B

W096005805000

Electrical Preventive

Maintenance

Bridge Megger and

High Potential

Test

on 4160

V Common Board

B Auxiliary

Raw Cooling Water

Pump

1B

b.

Observations

and Findin

s

The observed

surveillance activity, 1-SI-4.2.A-20 was satisfactory.

Procedures

were verified for use

and were followed.

Work was done per

the SI and

SSP 8.1,

Conduct of Testing.

Work documents

and the SI were

actively in use

and the test

was appropriately controlled.

The pre-test

briefing was adequate

and all acceptance criteria were met except for

one damper limit switch which had

a pre-existing

open work request.

A

test deficiency was initiated for this item.

The maintenance activities observed

were required to meet the applicable

requirements

of SSP 6.2, Maintenance

Management

System

and the specific

instructions

as listed below:

W096007400000

W096000567000

EII-O-OOO-TCC106, Troubleshooting

and Configuration

Control of Electrical

Equipment

EPI-O-OOO-BKR020, Testing

and Troubleshooting of 250

VDC and 480

VAC Power Circuit Breakers

and Trip

Devices

EPI-O-OOO-BKR003,

GE Type AK-15/25 Circuit Breaker

and

Switchgear Maintenance

Oi

il~

ili

W096005807000

EPI-O-OOO-HCC001,

Maintenance

and Inspection of 480

VAC and 250

VDC MCCs

W096005805000

EPI-O-OOO-TSTOOI,

Bridge Hegger

and High Potential

Testing

on Electrical

Equipment

The maintenance activities observed

were satisfactorily performed.

Work

was accomplished

per the work documents

and the work package

instructions

were actively in use.

Drawing and procedure revisions were

verified prior to use.

Personnel

qualifications were checked for

W096000567000

and W096005807000

and the personnel

performing the wor k

were task qualified.

Personnel

were knowledgeable

on the equipment

and the procedures.

Minor

problems that occurred

were brought to supervision

and appropriately

addressed.

Measuring

and Test Equipment

(HSTE) was verified to be in

calibration.

Problems with high polarization index value were noted

on

W096005805000

and the test equipment

was checked.

Alternate test

equipment

was obtained

and the polarization index value met the

acceptance criteria of g 2.0.

The questionable

megger set

was tagged

and sent to be checked

by the calibration lab.

During the breaker trip testing portion of W096000567000

the work was

delayed

due to problems with the breaker test set.

The first test set

was not operating properly, current values

were unstable.

The second

test set obtained

was out of calibration.

A third test set

was obtained

to complete the activity.

The inspector did not observe the final

testing of this breaker.

During observation of maintenance,

the inspector

noted examples of PVC

jacketed cable potentially exuding plasticizer.

This was noted

on

cables

in trays

HB and

PU near Unit Board

2B on elevation

604 in the

Unit 2 turbine building.

The plasticizer

was not in a location where it

could impact plant equipment.

The inspector discussed

the issue with

electrical

maintenance

supervision,

and determined that, electrical

maintenance

was

aware of the issue

and

had guidance to look for this

problem in the electrical

Preventive

Maintenance

(PH) program.

The

inspector

noted blank Work Request

cards

attached

to Westinghouse

HG6

relays in the Unit

1 Auxil-iary Instrument

Room.

The licensee

determined

that the tags were to require relay inspections

in accordance

with

Problem Evaluation Report

(PER) 951697.

The licensee initiated action

to correct the tags.

Conclusions

The maintenance

and surveillance activities observed

were satisfactorily

performed in accordance

with licensee

procedures.

The minor problems

that occurred were brought to supervision

and appropriately

dispositioned.

0

Ml.2

t

db

Gas Treatment Testin

a.

I s ection

Sco

e

62703

On July 17,

1996

an inspector

performed detailed observation

of several

surveillances

on the

A train Standby

Gas Treatment

System.

The

activities observed

included overall control of surveillance testing,

the control of M&TE equipment,

and procedure

adherence.

Licensee

documents

included:

~

O-SI-4.7.8.4,

Standby

Gas Treatment

System In-place

Leak Test of

High Efficiency Particulate Air (HEPA) Filter Banks,

(Revision 7)

~

O-SI-4.7.B.5,

Standby

Gas Treatment

System In-place

Leak Test of

Charcoal

Absorber Stage,

(Revision

11)

~

O-SI-4.7.B.7,

Standby

Gas Treatment

System

Flow Rate Test,

(Revision 8)

~

O-SI-4.7.B.8,

Standby

Gas Treatment

(SBGT) Train Housing

Door

Gasket

Seal Test,

(Revision 4)

b.

Observation

and Findin s

Mechanical

maintenance

personnel

were observed

performing O-SI-4.7.B.4,

O-SI-4.7.B.5,

O-SI-4.7.B.7,

and O-SI-4.7.B.8

on

SBGT train A.

The

following was noted during the observed activities:

The coordination

between operations

and maintenance

personnel

was

adequate

and independent verification was performed correctly.

All mechanical

maintenance

personnel

involved in the surveillances

appeared

knowledgeable

and well versed

on the surveillance

activities.

e

M&TE equipment

used

was correctly marked

and within calibration.

O-SI-4.7.B.5 contained

several

steps

which were unclear.

The

surveillance instructions did not have

a step which placed the

detector toggle switch in the required test position.

O-SI-4.7.B.4,

Attachment 2, Standard Dioctyl Phthalate

(DOP)

Equipment Setup

and Operation,

did not include setup steps for the

digital detector.

The maintenance

personnel

were trained

on the

use of the digital detector

and were using notes

from the training

course to setup the detector.

When the inspector questioned

the

use of notes,

instead of the procedure,

the workers explained that

they had

been told a

PER had been written and it would be

acceptable

to use the training notes until the procedure

was

revised.

Subsequently,

the test

was halted

and then restarted

using the older and less accurate

DOP detector

because

the

surveillance

procedure

did not address

the digital

DOP detector.

0

10

~

Training was contacted

and training personnel

confirmed that there

was

a

PER written against the procedure.

While reviewing the

PER,

dated January

17,

1996, the inspector

noted that O-SI-4.7.B.4

was

listed

as requiring revision.

It is not clear why the current

procedure revision did not address

the

new equipment.

A new

PER

was written to address this issue.

c.

Conclusions

Although the surveillance instructions

were designated

as continuous

use,

there

were several

weaknesses

which inhibited step-by-step

performance.

The personnel

performing the surveillances

had sufficient

knowledge

and experience

to accomplish

most of the intended tasks with

the instructions

as written.

However, during the performance of 0-SI-

4.7.B.4 maintenance

personnel

failed to follow procedural

requirements

by using the training notes for setup of the

DOP detector instead of the

steps

provided in Attachment 2.

This issue is an example of Violation

260,296/96-06-01,

Failure to Follow Safety Related

Procedures.

M1.3

Standb

Li uid Control

S stem Testin

a.

Ins ection

Sco

e

71707

6)726

0

On June

10,

1996, at 8:00 a.m., the inspector

observed

the performance

of surveillance testing

on the Unit 3 standby liquid control

pumps.

The

activities observed

included overall control of surveillance testing,

coordination

between operations

and maintenance,

the control of -METE

equipment, first use validation of a surveillance,

and procedure

adherence.

Licensee

documents

included:

~

3-SI-4.4.1.A,

(Revision 5),

"Standby Liquid Control

(SLC)

Pump

Functional Test"

~

MCI-0-063-ACC001,

(Revision 4),

"SLC Accumulator Maintenance"

~

Drawing 3-47E854-1,

(Revision 7), "Flow Diagram Standby Liquid

Control System"

b.

Observation

and Findin

s

The surveillance

performance

required operations,

mechanical

maintenance

and electrical

maintenance

personnel.

During the inspection the

following items were noted:

Operations

did not ensure all personnel

participating in the

surveillance

attended

the pre-job brief.

Mechanical

maintenance

was not prepared to perform this

surveillance

and appeared

unfamiliar with their role in the

performance of the surveillance.

0

~

Although the surveillance

procedure called for two HKTE gauge

and

valve assemblies,

only one

H&TE gauge

and valve assembly

was used.

~

Section 7.6, of 3-SI-4.4.1.A,

was performed prior to Section 7.4.

The inspector noted that this resulted in SLC being inoperable for

a longer period than necessary.

~

The electrical

maintenance

support personnel

required for the

surveillance vibration readings

were readily available.

Two test deficiencies

noted

by operations

personnel

were

appropriately

itemized in post-test

remarks.

~

Although the first use validation comments

included requests

for

some non-intent procedure

changes,

there

was

no reference

to the

use of one or two gauge

and valve assemblies.

c.

Conclusions

Poor coordination

between operations

and mechanical

maintenance

personnel

led to the performance of Section 7.6 prior to 7.4.

This

resulted in a safety significant system being inoperable for a longer

time frame than necessary.

The surveillance

would have

been

performed

in a more timely and controlled manner

had mechanical

maintenance

personnel,

who performed the work, attended

the pre-job briefing.

After

the observations

were discussed

with Operations

management,

the licensee

performed

a case

study of this activity, identifying lessons

learned

and

ensuring the appropriate

personnel

were made

aware of these

items.

Management

expectations

regarding

performance of procedure

sections/steps

in sequence

were promulgated.

10 CFR 50, Appendix B, Criterion

V states that activities affecting

quality shall

be prescribed

by documented

instructions,

procedures,

or

drawings of a type appropriate to the circumstances

and shall

be

accomplished

in accordance

with these instructions,

procedures

or

drawings.

Site Standard

Practice 2.1, Site Procedures

Program,

states that the

each

procedure

step is performed

as written and in the exact

sequence

specified.

Failure to perform 3-SI-4.4.1.A as written and in exact

sequence

was

a violation of this requirement

and is identified as

an

example of Violation 260,296/96-06-01,

Failure to Follow Safety Related

Procedures.

il

12

De raded

Vo ta

e Rela

Ca ibr tion Testin

a ~

b.

I s ection

Sco

e

62703

The inspectors

observed portions of Surveillance Instruction (SI) 1/2-

SI-4.9.A.c(I),

"4160V Shutdown

Board A and

B Under/Degraded

Voltage Time

Delay Relay Calibration.

Only the sections

related to the phase-to-

phase

degraded

voltage relay calibration were performed.

Obse vations

and

indin

s

c ~

On July 16 the inspectors

observed

two individuals from the Customer

Group perform calibration tests for degraded

voltage relays located

on

the A and

B 4160V Shutdown Boards.

These individuals verified that the

correct relay was removed for calibration testing

by ensuring that the

labeling associated

with the relay being removed matched that specified

in 1/2-SI-4.9.A.c(I).

Additionally, a procedural

step required

a

signoff by an independent verifier after the relay was returned to its

location.

The inspectors

observed that independent verification was

performed in an appropriate

manner.

A total of six relays were

procedurally tested for calibration.

The as-found

"drop out" and

"pickup" voltages for the six relays

wer e within the acceptance

criteria

band specified

by 1/2-SI-4.9.A.c(I) and the settings

were left as found.

The inspectors verified that the appropriate

LCO was entered for the

removal of each degraded

voltage relay.

Consistency

between the

acceptance

criteria values indicated in 1/2-SI-4.9.A.c(I)

and Technical

Specification Table 4.9.A.4.C was verified.

A review of the

FSAR

related to degraded

voltage relays

(Chapter 8.5) revealed

no

discrepancies.

The data

package

was reviewed

on July 18. This review

verified the accuracy of calculations

and that recorded

values

were

within the appropriate

acceptance criteria band.

The inspectors

also

verified calibration dates for the test equipment

were current.

Conclusions

Ml.5

The degraded

voltage relays were tested for calibration according to the

instructions provided by 1/2-SI-4.9.A.c(I).

The calibration team

members

were professional

and exhibited

an excellent safety perspective.

Operations

entered

the appropriate

LCO as required.

Coordination

between

the Customer

Group personnel

and Operations

was excellent.

Overall

Conc usions

on Conduct of Maintenance

and Surveillance

Activities

Overall, the activities were performed satisfactorily.

The observed

electrical preventive maintenance

items

and degraded grid relay testing

was performed with good attention to detail.

Strong coordination

and

communications

were noted during those work activities.

During

observation of the

SBGT and

SLC system testing,

the inspector identified

that procedural

requirements

were not met.

Coordination

was not strong

during the

SLC testing.

These

issues will be addressed

as two examples

0

~,

13

H3

M3. 1

of a procedural

adherence

violation.

Previous inspection reports

discussed

examples of procedural

adherence

deficiencies

associated

with

maintenance activities.

During this report period, the inspectors

noted

that most maintenance

workers demonstrated

effort to improve procedural

compliance.

Maintenance

management

has

been

emphasizing

the importance

of procedural

compliance.

Although these

two examples

indicate that

additional progress

is needed,

some

improvement

has

been noted.

Haintenance

Procedures

and Documentation

Review of Com leted

Wor

0 ders

a ~

Ins ection

Sco

e

62703

Completed

work orders

were reviewed to determine if the completed

work

met applicable procedural

requirements

and to determine

the degree to

which the activity was documented

in the work order.

The following work

orders

were reviewed:

95002249000

96004178001

96003226000

96000079000

96005620000

95021666000.

96000079001

96002905000

96000079003

96000844000

b.

Observations

and Findin

s

c ~

The documentation

reviewed

showed that Post Maintenance Testing

(PHT)

and Foreign Materials Exclusion controls were satisfactory for the work

performed.

The inspector noted that W096004178001

did not contain

signatures

documenting

completion of the pre-evolution briefing and

verified for use.

This was not

a safety related work order.

The

initial PHT signatures

on W095002249000

were not signed prior to

starting work.

The

PHT performed for this work order was adequate

for

the work scope.

No documentation

sheets

from procedure

HCI-0-000-

TUB001, Compression Fittings Disassembly

(ALL), Inspection (All), Rework

and Reassembly,

were included in

WOs 96000079001,

and 96000079003.

The

description of actual

work completed sections of these

two non-safety

related work orders

documented that tubing connections

were

made

up snug

tight per procedure

HCI-0-000-TUB001 and tubing connection leak checks

per procedure

PMT-O-OOO-HEC001,

Leak Checks

On Tube Fittings, Threaded,

Flanged

Or Bolted Connections,

were satisfactory.

The documentation

showed that,

except for the items mentioned,

work was done according to

the procedural

requirements.

Conclusions

The level of detail of work documentation

was adequate

but not thorough.

Documentation errors

were noted

on four of the ten work orders

reviewed.

0

Cl

~

Nl

N7.1

'a ~

14

guality Assurance in Naintenance

(92902,

40500)

Rev'ew of Main Steam Relief Valve

MSRV Pilot Cartrid

e

PE

ns ection

Sco

e

40500

The inspector reviewed

PER 960377 to determine if corrective action

was

adequate.

b.

Obse vations

and Findin

s

PER 960377

was

a level

-C

PER written to document

an incorrectly oriented

NSRV pil'ot cartridge received

from Target

Rock Corporation.

The

PER

evaluation

concluded that the issue resulted

from an apparent

factory

assembly

problem.

The vendor corrected

the pilot cartridge orientation.

Vendor documentation

was reviewed to verify no valve functions would be

affected

and vendor certification was still valid.

The

PER adequately

controlled the extent of condition for the issue.

Corrective actions

for

PER 960377 were adequate.

N7.2

eview of ECCS

Room Cooler Leaka

e

PERs

a 0

ns ection

Sco

e

40500

The inspector reviewed

PERs

960653

and

960651 to determine if corrective

actions

were adequate.

b.

Obse vations

and Fn

s

PER 960653

was

a level

B PER written to document tube leakage of the

2B

RHR room cooler.

The issue

was previously identified by trend package

A920024.

The failure trend evaluation,

performed

September

17,

1992,

indicated that the leakage

was due to copper corrosion

due to continuous

chlorination chemical treatment of the Emergency

Equipment Cooling Water

(EECW) system.

The licensee

changed to a Calgon chemical

treatment

system approximately

two years

ago.

The latest failed cooler was in

service for approximately six years.

The previous cooler failure

occurred after approximately three years of service.

The inspector

reviewed corrosion rate data from system test

coupons

and

observed pictures of the Reactor Building Closed Cooling Water

(RBCCW)

heat exchanger inlet tubesheets

in 1994 and

1996,

and noted significant

reduction in heat exchanger fouling due to the

new chemical

treatment.

Visual observation of a portion of the failed cooler tubing showed

little evidence of significant corrosion.

The initial trend package

was

not conclusive.

Licensee actions to reduce

system corrosion

appeared

to

increase

cooler life.

PER 960651

was

a level

C

PER written to document

damage to a tube in the

2B Residual

Heat

Removal

(RHR) room cooler which occurred while cleaning

the cooler area which initially required repair.

The inspector

reviewed

i

15

M8

H8.1

M8.2

the

PER and corrective actions

and determined that the corrective action

was satisfactory.

Corrective actions for PERs

960651

and

960653 were

adequate.

Miscellaneous

Maintenance

and Surveillance

Issues

(92902,

92700)

C osed

LER 50-259 95001:

Emergency

Equipment Cooling Water

pump auto

started during performance of a surveillance instruction due to wrong

jumpered relay contacts

as

a result of personnel failure to perform

verification

during

a drawing and

a procedure

change.

Details of this

event were documented

in Inspection

Report 95-38.

A violation

concerning this event

was issued

and subsequently

closed in Inspection

Report 95-60.

Additional corrective actions

completed

by the licensee

that were not discussed

in those

two reports

included

a review of other

safety related drawings for similar wiring errors.

This review did not

identify any additional errors.

In addition, training on this event

was

provided to the appropriate

organizations.

Closed

LER 50-260 95006:

An excess

flow check valve was not tested

per Technical Specification requirements

due to a drawing deficiency.

On

August 14,

1995, the licensee

determined that

an instrument line excess

flow check valve,

2-ECKV-3-240A, which was part of the primary

containment

boundary,

was not tested

pursuant to Technical Specification 4.7.D.l.d.

On discovery of this condition, the licensee

isolated the

line in accordance

with the Technical Specification.

The licensee

determined that the root cause of the event

was the valve not being

documented

on the appropriate plant drawings,

which were used to

identify the primary containment

boundary.

The valve was later tested during the Unit 2, Cycle 8 refueling outage.

As additional corrective action, the licensee

ensured that other excess

flow check valves were added to the appropriate

drawings

and

surveillance

procedures.

The inspectors

determined that this event constitutes

a violation of

Technical Specifications.

This licensee identified and corrected

violation is being treated

as

a Non-Cited Violation (NCV), consistent

with Section VII.B.I of the

NRC

ENFORCEMENT POLICY.

This item is

identified as

NCV 260/96-06-04,

Excess

Flow Check Valve Not Tested

Per

Technical Specifications.

ll'

III. En ineerin

Conduct of Engineering

10

CF

50.59

Pro ra

Ins ection

Sco

e (37701)

The

NRR Project Manager conducted

an inspection of the licensee's

program implementing

10 CFR 50.59.

This regulation controls what

changes,

tests,

and experiments

can

be performed

by a licensee without

prior

NRC approval.

Changes that require prior approval

are referred to

as unreviewed safety questions

(USgs).

Changes to license requirements,

such

as technical specifications,

are controlled by 10 CFR 50.90,

50.91,

and 50.92,

and are not within the scope of this review.

The inspector reviewed procedures

used for development of Safety

Assessments

(SAs)

and Safety Evaluations

(SEs).

SSP-12. 13 provides

criteria for SAs and

SEs predominately for engineering activities,

such

as plant modification.

SSP-2.3

provides criteria for safety

assessment

of procedure

changes

and can require

a safety evaluation per SSP-12.13

if required

by the SA.

SSP-6.2 requires

a safety evaluation for certain

maintenance activities involving safety-related

or quality-related

components if instructions

are not developed

from previously-approved

materials,

or when work is performed

on plant process

equipment that is

not removed from service.

The inspector

reviewed audits

and other reviews conducted

as part of the

licensee's

quality review of the

10 CFR 50.59 program.

Recent

PERs

on

10 CFR 50.59 issues

were reviewed.

A number of recent safety

assessments

and safety evaluations

prepared

pursuant to SSP-2.3

and SSP-

12.13,

and work orders

prepared

pursuant to SSP-6.2

were also reviewed.

bservat'ons

and 'in s

The licensee's

process to determine whether

a US( is created

by a

proposed activity consists of two major activities.

First,

a safety

assessment,

or SA, is performed.

This process

screens activities to

determine if they fall within the scope of 10 CFR 50.59.

If the

SA

determines

that

10 CFR 50.59 is applicable,

then

a safety evaluation,

or

SE, is performed.

The

SE explicitly addresses

each of the criteria set

forth in 10 CFR 50.59 to determine whether

an US( exists.

During review of SSP-12.13, it was noted that accident

consequences

were

discussed

exclusively in terms of offsite dose

consequences.

This

restriction does not account for other regulatory requirements,

such

as

Loss of Coolant Accident

(LOCA) acceptance

criteria given in 10 CFR 50.46, or operator

dose restrictions of General

Design Criterion

(GDC)

19.

In addition, the procedure

does not clearly address

requirements

such station blackout

and anticipated transients

without scram.

On this

il

17

basis,

the inspector

concluded that the procedure

does not clearly

implement all regulatory requirements.

Examples of problems that could be caused

by this issue

were observed in

a safety evaluation for Design

Change Notification (DCN) 20899A, which

noted that changes

to Motor Operated

Valves

(MOVs) affected

Environmental gualification (Eg), Generic Letter (GL) 89-10,

and

10 CFR 50 Appendix

R requirements.

However, the

USA determination

only

addressed

a change in the stroke time of a valve that was described

in

the

FSAR.

The ability of components

to perform as intended for design

basis

events

could be adversely affected if criteria such

as

Eg was not

implemented.

Therefore,

the inspector

concluded that the US(

determination for thi's

DCN did not comprehensively

address all relevant

design requirements.

Another example of this issue

was noted

by the licensee's

Nuclear Safety

Review Board SA/SE subcommittee

as documented

in PER 96016,

where

a

Change

Request to Licensing Document

(CRLD) did not address

Emergency

Core Cooling

(ECCS) methodology

changes.

A similar example

was observed

in a safety evaluation which stated

accident

consequences

were not increased

since they were within bounding

main steam line break

(MSLB) results.

However, the

SE also states

other

events,

such

as loss of offsite power,

were potentially affected

by the

proposed activity.

The evaluation did not recognize that acceptance

criteria for anticipated operational

occurrences,

such

as loss of

offsite power,

can

be more limiting than for a design basis

accident,

such

as

a MSLB.

This result could be symptomatic of an emphasis

on

offsite dose

consequences,

when other criteria may be more relevant for

a given aspect of an activity.

A significant change in the quality of SAs for procedure

changes

was

observed

since

a revision was

made to SSP-2.3

in late March 1996.

The

revision deleted

requirements for a summary description explaining why a

change

was appropriate.

SAs issued prior to that revision were superior

in that it was

much easier to follow the preparer's critical thought

processes.

The licensee

recognized this problem as well, and is

considering alternatives

to improve this process.

An SA for a change to procedure 2-SI-4.10.A.I., dated

March 20,

1996,

was reviewed where

a conclusion

was drawn that the change did not

increase

the consequences

of any previously analyzed accident.

Such

a

conclusion is outside the scope of an SA.

Conclusions of this type are

properly found in SEs.

One safety assessment

was reviewed which should

have led to preparation

of a safety evaluation.

DCN T38901A was prepared to allow replacement

of the core shroud

access

hole covers

(AHC).

The

SA noted that the

new

design introduced

new core bypass

leakage for normal operations

and for

post-LOCA conditions.

The

SA concluded

no

SE was required.

However,

FSAR section 3.3 states that reactor vessel

internals "Maintain

partitions between

regions in the reactor vessel..."

and

"The reactor

~,

18

vessel

internals shall

be arranged to provide

a floodable volume."

Both

of these criteria were potentially affected

by the

new AHC installation.

One question required

by SSP-12. 13 is "Does the proposed activity affect

significantly (directly or indirectly) any information presented

in the

SAR...?"

The

SA stated that

"The replacement

AHC does not change

the

operational

performance of any reactor internals described

in the SAR."

This was

an incorrect statement,

since both the

FSAR criteria discussed

above were affected

by the change.

Further,

the

SA checklist from SSP-

12. 13 includes

an item regarding safety injection/core cooling, which

was checked

N/A.

The text of the

SA clearly stated

LOCA analyses

were

affected,

so the

SA conclusion for this item was also erroneous.

DCN

A39811A was completed to document the

10 CFR 50.59 safety evaluation

and

FSAR changes for the

AHC modification.

Although the

new design

had not been

implemented yet, the inspector

concluded

an

SE was required for this activity.

The licensee

agred with

this conclusion,

and initiated

a

PER to resolve the problem.

The

failure to follow procedures

is

a violation of 10 CFR 50, Appendix B,

Criterion

V and is addressed

as

one example of Violation 260,296/96-06-

Ol, Failure to Follow Safety Related

Procedures.

Several

recent "step-text" work orders

developed

per SSP-6.2

were

reviewed to determine whether procedural

requirements for US/

determinations

were followed.

The work orders

were not reviewed to

assess

whether the given actions

and sequence

of activities were

appropriate.

Aside from a minor documentation

problem,

no discrepancies

were identified in these

work orders.

Conclusions

A number of discrepancies

were found in the limited sample of items

examined,

including an example of a procedure violation cited

as part of

Violation 260,296/96-06-01.

While the licensee's

10 CFR 50.59 program

is generally adequate,

additional effort by the licensee

could improve

performance

in this area.

Control

Room Emer enc

Ventilation Flow Heasurements

Ins ection

Sco

e (61723)

The inspectors

reviewed licensee activities

on the Control

Room

Emergency Ventilation System which occurred

on July 5,

1996.

Reviewed

activities included surveillance

performance,

troubleshooting

and job

control.

Reviewed licensee

documents

included:

~

O-SI-4.7.E.6,

Control

Room Emergency Ventilation System

10 Hour

Operability Test,

Revision

8

O-SI-4.7.E.5.B,

Control

Room Emergency Ventilation System

Flow

Rate Test,

Revision

10

Site Standard

Practice 6.2, Haintenance

Hanagement

System

il~

0

19

Observation

and Findin

s

Operations

personnel

performed O-SI-4.7.E.6,

Control

Room Emergency

Ventilation

(CREV) System

10 Hour Operability Test,

Revision 8.

During

the test,

a flow rate below the allowed range of 2700 to 3300 cfm was

indicated

on

CREV B flow gauge 0-FI-031-7213.

This was not an

acceptance

criteria step for O-SI-4.7.E.6,

however it did cause

an

operability concern.

Because

0-FI-031-7213

had

a history of being out

of calibration, Operations

requested

the gauge to be calibrated.

Flow gauge 0-FI-031-7213

was calibrated in the

H&TE shop

and

reinstalled.

Operations

performed O-SI-4.7.E.6

a second time during

which the flow rate still indicated low.

A work request

was written to

investigate

and repair the low flow rate.

Technical

support personnel

measured

the flow by inserting

a pitot tube

directly into the duct work.

This work was completed

as minor

maintenance

without step text to supply specific direction.

The

inspectors

inquired about the level of instruction used to trouble shoot

a safety system.

Technical

support explained that they had

used

selected

steps

from O-SI-4.7.E.5.B,

Control

Room Emergency Ventilation

System

Flow Rate Test,

Revision 10.

Site Standard

Practice 6.2, Haintenance

Hanagement

System,

section 3.3.c

requires

step by step planning when other than skill of the craft steps

are required

and do not exist in pre-approved

procedures.

It allows for

a work sequence

to be created

by using various steps

from pre-approved

procedures.

The step text for a work order would include the work

sequence

steps.

Since the work was performed

as minor maintenance

rather than troubleshooting

no detailed work plan was written.

The inspectors verified that the system status

was such that the flow

rate measurements

taken

by technical

support were valid.

The proper

placement of the flow test

caps

were also verified.

Conc usions

The flow rate determination

was performed

as minor maintenance,

therefore

no instructions

were required.

An indicated low flow for the

Control

Room Emergency Ventilation System is an operability concern.

Although the flow rate

was adequate,

operability issues of safety

systems

were not determined

in a more controlled

and documented

manner.

Electro-H draulic Control

EHC

Circuit Board Problems

Ins ection

Sco

e

37551

On July 22, the inspector discussed

EHC circuit board problems with the

system engineer.

Pressure

transients

occurred

on Unit 3 on three

separate

occasions

due to a suspected

faulty 'logic card in the

'B'hannel

of the turbine speed control circuit.

A new logic card was

placed in the "B" turbine control circuit during Harch

as

a result of a

0

0

20

unit scram

on February

29.

The scram was also caused

by

EHC logic card

problems.

IR 50-259/260/296/96-03

discusses

this unit scram.

A

historical review of the

EHC system performance

revealed that the

pressure

transients

associated

with the

EHC room chillers trips did not

occur prior to the installation of the

new frequency to voltage card in

March.

The suspected

faulty turbine control logic card was replaced

on

July 25 with a tested

and properly calibrated

card from Unit l.

Observ tions

and Findin

s

Discussions

with the system engineer for the

EHC System indicated that

a

faulty frequency to voltage card in the turbine speed control circuit of

the Unit 3

EHC system

caused

reactor pressure

transients

when the

temperature

in the room increased

due to the tripping of the room

chiller units.

The pressure

transients

were the result of the control

valves receiving signals to travel in the close direction.

The Unit 3

EHC logic was duplicated

on Unit 1 for testing

and troubleshooting

purposes.

Unit

1 is not currently operating.

On July 24, the inspector observed

the performance of testing

and

troubleshooting activities

on Unit

1 using the duplicated logic of

Unit 3.

A jumper was .install'ed in the 'B'urbine speed control circuit

to defeat the logic for a loss of speed

signal that would result from

removing the logic card.

An Integrated

Computer System

(ICS) was

used

to monitor the effects of signals

going to the turbine control valves

and the intercept valves.

The logic card was

removed

and subsequently

replaced.

This removal

and replacement activity did not cause

any

substantial

perturbation in the signals.

The results of this testing

and troubleshooting

provided Technical

Support

and plant management

sufficient confidence for removing the suspected

faulty card with Unit 3

on line and replacing it with a tested

and calibrated

card from Unit 1.

The removal

and replacement

of the turbine speed control card

on Unit 3

was performed

on July 25.

Additionally, a decision

was

made

by

management

to install

a logic card associated

with the 'B'hannel

pressure

control section of the

EHC logic circuit.

This card was

removed in May as

a result of a pressure

perturbation

caused

by

EHC

logic malfunctions.

Two pre-job briefs were conducted to discuss

and

coordinate these

work activities.

One pre-job brief was held for

management

and the other for operations.

The inspectors

attended

both

of these pre-job briefs.

One inspector observed

control

room activities

and the other inspector

observed

the exchange

and installation of the

EHC logic cards.

Due to

the high risk nature of the work activity for a unit scram, .the Shift

Manager

had instructed all persons

not directly involved in the work

activity to remain at the back of the control

room.

Specific jobs were

assigned

to persons

involved in the work activity and the importance of

good communication

was stressed.

Technical

support

and instrumentation

personnel

performed the exchange of the turbine speed control card

and

installed the pressure

control card

on Unit 3 without incident.

These

activities were performed with the unit on line at

100 percent.

II

c ~

E8

21

The inspectors

performed

a review of Special

Instrument Instruction SII-

O-XX-3014, Troubleshooting

and Configuration Control of Instrumentation,

Revision

10; Site Standard

Practice

SSP-6.2,

Haintenance

Hanagement

System,

Revision

18 and the Work Order (96-009649-000) for the turbine

speed control logic card exchange.

A review of the documentation

indicated that work activities were conducted

in compliance with plant

procedures.

Co c

sions

The pre-job briefs were thorough

and personnel

leading the briefs

appeared

to be well organized

and prepared.

Hanagement's

attention to

the high risk work activity was quite evident.

The prior testing

and

troubleshooting

on the shutdown unit demonstrated

an excellent safety

attitude for preventing or minimizing unnecessary

challenges

to safety

systems.

Coordination

between operations,

technical

support

and

maintenance

was good.

Niscellaneous

Engineering

Issues

E8.1

S

R

eviews

1707

40500

A recent discovery of a licensee

operating their facility in a manner

contrary to the Final Safety Analysis Report

(FSAR) description

highlighted the need for a special

focused review that compares

plant

practices,

procedures

and/or parameters

to the

FSAR description.

While

performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the

FSAR that, related to the areas

inspected.

One inconsistency

was noted

between the wording of the

FSAR

and the plant practices,

procedures

and/or parameters

observed

by the

inspectors.

Paragraph

03.1 describes

an instance in which a control

room annunciator

described

in the

FSAR was disable without a safety

evaluation

being completed.

This issue is addressed

as

a violation.

No

other inconsistencies

were identified by the inspectors.

The licensee

is continuing

an extensive

FSAR review.

IV. Plant

Su

ort

Rl

Rl. 1

Radiological Protection

and Chemistry Controls

dioactive Eff uent Contro

Pro ram

a ~

Ins ection

Sco

e

8 750

The inspectors

reviewed the overall results of the radioactive effluent

control program

as documented

in the Annual Radioactive Effluent Release

Report for 1995.

The amounts of radioactivity released

and resulting

radiation doses for the years

1992 through

1995 were tabulated

from the

annual

reports to evaluate

long term performance of the effluent control

program.

0

22

bse vations

and Findin

s

The amounts of activity (fission and activation products, tritium, and

dissolved

and entrained

gases)

released

in liquid effluents during 1995

were generally consistent with amounts released

during 1994.

Less than

one curie of fission and activation products

was released

in liquid

effluents during 1994

and 1995, which was less

than half of the amounts

released

during the two previous years.

The amounts of activity

releases

as fission and activation gases

in gaseous

effluents

has

decreased

significantly since

1992, i.e.,

from >16000 curies in 1992 to

24 curies in 1995.

The elevated level in 1992 was due to leaking fuel in

Unit 2 and high offgas flows.

The leaking fuel was replaced

during the

1993 Unit 2 Refueling Outage

(RFO)

and the amounts of activity

subsequently

released

in the effluents decreased

sharply.

The annual

per

unit average radiation doses resulting from radioactivity in the- liquid

and gaseous

effluents released

during

1995 were less than

one percent of

their respective limits.

Selected

licensee

records

were examined to independently verify the

reported value for the amount of activity released

as fission and

activation products in liquid effluents during the fourth quarter of

1995.

The amounts of Co-60,

Cs-137,

and Na-24 listed in permits for

selected

releases

were compared to a licensee

provided tabulation of

those quantities for all releases

during that period.

The reported

sums

of those quantities

and the

sum of all fission

and activation products

were also verified.

No inconsistencies

in those data were noted

by the

inspector.

The effluent release

report indicated that there were

no abnormal

releases

during 1995

and that one liquid effluent monitor was inoperable

for greater

than

30 days.

The Unit 3 Residual

Heat

Removal Service

Water

(RHRSW) monitor (3-RM-90-134D) was inoperable

from November 3,

1995 to December

5,

1995 while the piping to the monitor was being

modified for improved efficiency.

Conclusions

Based

on the above reviews, it was concluded that the licensee

had

implemented

and maintained

an effective program to monitor and control

liquid and gaseous

radioactive effluents.

The projected offsite doses

resulting from those effluents were well within the limits specified in

the Technical Specifications

(TSs), Offsite Dose Calculation

Manual

(ODCM), and Title 40 Code of Federal

Regulations

Part

190 (40

CFR 190).

ad'olo ica

Environmenta

Monitorin

ro ram

ns ect'o

Sco

e

84750

The inspectors

reviewed the overall results of the radiological

environmental

monitoring program

as documented

in the Annual

Radiological

Environmental

Operating

Report for 1995.

23

b.

C.

Observations

and Findin

s

The inspectors

noted that, in accordance

with the

TS and

ODCH, the

report included

a description of the program,

a summary

and discussion

of the results for each

exposure

pathway,

analysis of trends

and

comparisons

with previous years

and preoperational

studies,

and

an

assessment

of the impact

on the environment resulting from plant

operations.

The report also included

a tabulation of the summarized

analytical results for the samples

collected during 1995.

From a review

of those data,

the inspector determined,

for selected

exposure

pathways,

that the sampling

and analysis

frequencies

specified in the

ODCH was

met.

The inspector also verified by direct observation that selected

sample collection sites

were located

as indicated in the

ODCH.

As

indicated in the conclusion section of the report, the radioactivity

detected

in the plant environs

was primarily the result of fallout and

natural

background radiation,

and any activity which may be present

as

a

result of plant operations

does not represent

a significant contribution

to the radiation exposure of members of the public.

Co cl sions

~

Rl. 3

Based

on the above reviews

and observations, it was concluded that the

licensee

had complied with the sampling, analytical

and reporting

program requirements

and that the radiological environmental

monitoring

program was effectively implemented.

ece'

of Radioactive Haterials

a ~

Ins ection

Sco

e

86750

b.

The inspectors

reviewed the licensee's

procedures

and selected

records

for receipt of radioactive materials.

The review included records for

receipt

and inventory of nonexempt

byproduct

and source materials

(BSN).

Observations

and Findin

s

Procedures

SSP-5.3,

SSP-10.2,

STD-10.2,

RCI-7,

and O-SI-4.8.E were

reviewed

and found to be consistent with the requirements

in 10 CFR 20,

10

CFR 30 and the

TS for receipt,

storage,. leak testing,

and inventory

of nonexempt

BSN.

Records for the three most recent inventories of

nonexempt

BSN indicated that the inventories

had

been performed at the

required frequency.

The most recent inventory change report indicated

that

a 100 millicurie Cm-244 source

(BFNP ID¹ 565)

had been

added to the

inventory on June

20,

1996.

The Air Bill for the transport of that

source indicated that the source

was shipped

from Langhorne,

Pa.

on

April 30,

1996,

but the exact date of delivery to the site was not

known.

It is assumed that the delivery date

was

on or about

Nay 2,

1996.

The source

was located

on June

20,

1996, at the inplant Nuclear

Stores

Customer, Service Center.

In accordance

with DOT requirements

the

package

containing the source

was not marked or labeled

as radioactive

material.

The packing list was stamped to indicate that the package

conformed to the conditions

and limitations specified in 49

CFR 173.422

il~

0

24

for excepted radioactive materials,

instruments,

and articles.

The

packing list, which was in a blister pack attached

to the package,

had

been folded such that the marking was not visible.

The licensee

subsequently

issued

a Problem Evaluation Report

(PER) for this issue

and

characterized

the

PER as

a level

B, which requires corrective action.

Section

7.1 of RCI-7 stipulates that the Nuclear Stores

Supervisor or

his designee

shall inspect

packages

or shipping papers to determine if

radioactive material is present

and notify the

BSM Controller when

BSM

is received.

Section 3.1

C of STD-10.2 also stipulates that responsible

receiving personnel

shall determine if a shipment contains radioactive

material,

examine the shipping documentation for packages

containing

radioactive material

and identify the contained radioisotope(s),

and

notify immediately the

BSM Custodian if the radioactive material is a

source.

TS 6. 10.2 requires that

a complete inventory of radioactive

materials in possession

shall

be maintained current at all times.

The

inspectors

determined that the licensee

had not adequately

examined the

shipping documentation

upon receipt to determine whether the package

contained radioactive material.

This

NRC identified violation is not

being cited because criteria specified in Section VII.B of the

NRC

Enforcement Policy were satisfied.

This issue is identified as

(NCV 50-

259,

260, 296/96-06-05)

onc

sions

One

NCV was identified for failure to adequately follow procedures

for

receipt of radioactive material.

Occu ational Radiation Internal

and Externa

Ex osure

Co t ol

Ins ection

Sco

e

83750

This area

was reviewed to verify personnel

radiation exposures

were

within regulatory limits and the licensee

was implementing proper

internal

and external

exposure control measures.

Observations

and Findin

s

The inspectors

reviewed current. personnel

exposure reports

and found all

internal

and external

personnel

exposures

were below regulatory limits.

Tours of the Radiation Control Areas

(RCAs) were

made to verify that

radiological

areas

were properly posted

and controlled.

Locked high

radiation areas

throughout the facilities were found properly secured.

The inspectors

reviewed selected

licensee radiation surveys

and

made

independent

radiation surveys in those

areas

to verify radiological

conditions were properly identified and posted.

The inspectors

reviewed selected

skin dose calculations resulting from

skin contaminations

in 1996.

The inspectors,

using the licensee's

procedures,

calculated the skin dose

and found that the calculations

had

been performed in accordance

with the licensee's

procedures.

All skin

doses

were well within the regulatory limits for skin dose.

No concerns

with the licensee's

skin dose methodology were identified.

i

0

25

In general,

the licensee

appeared

to be implementing effective

.radiological: controls to minimize personnel

exposures

to internal

and

external radiation sources.

No concerns with the licensee*s

internal or

external

exposure control programs

were identified.

Rl.5

o trol o

Radioactive

ateria1s

and Contaminat'o

a ~

s

ct o

Sco

e

83750

The inspectors

toured licensee facilities, examined licensee controls

for contaminated

areas

and equipment,

and discussed

controls with

Radiation Protection

(RP) personnel.

b.

Observations

and Findin s

During tours of the licensee's facilities the inspectors

found

housekeeping

was generally good.

At the time of the inspection the

licensee

was meeting the goal for contaminated

square

footage

by

averaging less than approximately

one percent of the total

RCA as

contaminated.

No uncontrolled .containers

of contaminated

or radioactive

material

were identified during the facility tours.

The licensee

reported that use of long sleeve

scrubs

and the

establishment

of clean islands within the

RCA had helped increase

worker

efficiency during the Unit 2 (U2) Re-Fueling

Outage

(RFO) 8.

The clean

islands

were clean

areas within the

RCA where workers could take breaks

and lunch, which reduced travel times to other areas

outside the

RCA.

Clean islands with whole body friskers were established

on the Refueling

Floor and the Turbine Deck.

Long sleeve

scrubs

were used with boot and

glove Protective Clothing

(PC) in the turbine bui.l'ding where

contaminated

levels were less

than 10,000 dpm/100 cm'.

Radiation

workers exiting these

areas

removed the gloves

and boots

and wore the

scrubs to a whole body frisker for personnel

contamination monitoring.

If the frisker did not identify any contamination the worker could

continue to wear the scrubs, if needed,

for additional work within the

RCA.

The licensee

reported the process

saved time in repeated

donning

of PCs

and

PC cleaning resources.

The inspectors

concluded

these

licensee

procedures

could save resources

and were not

a contamination

control problem with effective and diligent contamination monitoring

procedures.

No concerns with the processes

were identified by the

inspectors.

Licensee controls of contaminated

or radioactive materials

were found to

be adequately

implemented.

0

26

R1.6

ta'ccu

ational

Ex osure

ALARA

a.

Ins ection

Sco

e

83750

The inspectors

reviewed the status of the licensee's

collective dose for

1996

and the implementation of the

ALARA program.

b.

Observations

and Findin

s

The inspectors

reviewed the collective doses for specific

U2RF08 work

activities with ALARA personnel

and inquired about the application of

dose reduction techniques

and their results

in the outage.

The

licensee's

annual collective dose goals

are established

for Fiscal

Years

(FY) beginning October

1 each year.

A summary of collective doses for

1995

and

1996 (through July 15,

1996) is shown below.

Collective Personnel

Exposures

(Person-Rem)

Annual

Outage

Year

.Actual

Goal

Title

Actual

Goal

Duration

(Days)

1995

850

FY 895

U2RF07

424

350

54, 10/Ol/94 to ll/23/94

409

CY

Forced

4 in 1995

1996

428

FY 510

U2RFOS

241

350

32, 03/23/96 to 04/23/96

334

CY

Forced

12 in 1996

Through the first three quarters of the

1996 fiscal year, the licensee

met collective dose objectives.

The 1995 Calendar

Year

(CY) collective

dose of 409 person

rem was

one of the facility's lowest to date

and the

licensee

has

an opportunity to lower the collective dose further in

CY

1996.

Several

conditions were contributing to the licensee's

collective

dose reductions,

.including:

Shorter

RFO duration;

A good

U2 availability factor;

and

The restart of U3.

The duration of the

U2RF08 was approximately

22 days shorter than the

duration of the U2RF07.

The planned duration for the

U2RF08 was

28

days.

The actual

outage duration

was approximately

32 days.

To shorten

the length of U2RFOS the licensee

performed

some maintenance activities,

typically performed during outages,

prior to the start of the

RFO.

The

total collective dose for the outage

was approximately

241 person

rem

which included the pre-outage

work dose of 29 person

rem.

Another

reason

the collective dose for U2RF08 was

so much lower than

U2RF07 was

reduced level of Inservice Inspection (ISI) work.

The ISI work in

4l

27

U2RF07

(155 person-rem)

included

10 year ISI activities

and was greater

in scope

than the ISI activities conducted

in U2RF08

(14 person-rem);

The availability factor for Unit 2 was good, operating approximately

257

of the first 293 days of 1996

FY.

There

was

one brief shutdown of

approximately

4 days

and the 32 day

RFO during that period.

Unit 3 start-up

on November

19,

1995, effectively took the licensee

out

of an "longterm outage" that the licensee

had

been in for several

years.

Following the startup,

the availability on

U3 had also

been

good.

Unit

3 had three brief outages totaling about

8 days

and operated

approximately

236 of the

244 days following its restart.

The

U2RF08. outage

dose

was approximately

109 person-rem

below the goal.

The licensee

had over estimated

the work hours

needed to complete

27 of

the 32 tasks

having

ALARA planning activities.

Of these

27 tasks,

approximately

16 had actual

hours within 20 percent of the estimated

hours.

However,

7 (approximately

22 percent) differed from the estimate

by 40 percent or more.

These significant differences

in estimated

and

actual

hours indicated additional attention

was needed for more accurate

work estimates

necessary

in effective dose reduction planning

and'rocesses.

The inspector verified that the worker comments

and other lessons

learned

and documented

in U2RF08 ALARA Planning Reports

were receiving

management

attention.

Issues

were identified in the licensee's

corrective action program

and in ALARA/Radwaste Committee Action Items

list.

C.

Conclusions

R2

R2.1

The licensee

was effectively reducing site collective doses.

Additional

attention

and improvement in predicting the work hour estimates for

tasks

appeared

appropriate.

However,

no significant collective dose

problems

were identified during the reviews.

Facilities

and Equipment

(83750)

Continuous Air Honitors

a ~

Ins ection

Sco

e

92904

The inspectors

reviewed the status of the licensee's

Continuous Air

Nonitors.

b.

Observations

and F'ndin

s

Inspection

Report 96-05 described

a resident inspector's

observations

of

an inoperable

CAN (Continuous Air Honitor) in the Unit 2 reactor

building in Hay 1996.

Mork Request

C308169 indicated that 2-RH-90-58

failed to source

check in December

1995.

Compensatory

actions

were in

effect.

The resident

inspector discussed

the apparent

delay in

28

repairing the

CAM with radiological controls management.

PER 960618

was

initiated on the issue.

CAN 2-RN-90-58 was returned to service

on Nay

23,

1996.

The licensee's

extent of condition review conducted

on Nay

15,

1996 identified that

a total of nine

CANs were out of service.

Several

of the 'CAMs did not have scheduled

repair dates

and

some

had

been out of service for many months.

Compensatory

actions

were in

effect for the inoperable

CANs. The inspector

noted that although the

compensatory

actions

adequately

monitor the area radioactivity, there is

not an alarm function in the

CR as with the

CAMs.

A review by the

resident

inspectors

indicated that

CAN information was not relied upon

for

Emergency Operating Instruction entry conditions.

The licensee's

investigation

concluded that repairs to

CAMs with compensatory

actions

in place were not being scheduled for repairs in a timely manner.

Corrective actions

were initiated to ensure that inoperable

CANs

received the appropriate level of attention

by radiological controls

management

and scheduling

personnel.

During this report period,

two Region II senior radiation specialists

conducted additional

review of the

CANs.

The inspectors

noted that most

of the

CAMs located in Unit

1 were inoperable.

Some of the Unit

1

CAMs

had'een

installed to replace

aging CAHs'ut were not declared

operable

following their installation.

Others were installed

and declared

operational

but were removed from service.

Licensee staff subsequently

reported that there

was

no safety significance involved with the Ul CAMs

since the fuel was removed from that unit.

The inspectors

determined that three

CAMs (I-RH-90-54, 2-RN-90-51,

and

2-RH-90-59)

had problems that were not repaired for several

months.

The

inspectors

determined that the licensee

had work orders to fix various,

problems

on the three

CAMs that were inoperable for three to seven

months.

The inspectors verified that the

CAHs were not scheduled

to

receive maintenance until September,

1996.

The inspectors

discussed

maintenance activities with the Radiation Monitoring System Engineer

and

learned the system rating on Unit 2 was trending

down in FY 1996.

It

appeared

that the Radiation Monitoring System

needed

a higher priority

for preventive

and corrective maintenance.

The licensee

approved

a change to the

FSAR dated

June 6,

1996,

removing

some of the detail concerning

CAMs in FSAR section

7. 13.5.3. 1, "Air

particulate Monitoring Subsystem."

Licensee

documentation

states

that

the change

was

made to "Revise

FSAR to clarify BFN's

FSAR Commitment for

the number of CAMs associated

with Units

1 and

3 and their functional

status."

The revised description states

in part, that

CAHs are located

in the reactor turbine

and radioactive waste buildings.

Conclusion

The inspectors

determined that the licensee

was in compliance with

revised

FSAR section 7.12.5.3.1.

Although rarely needed,

CAMs can

provide one of the earliest indications of abnormal or changing airborne

and plant conditions.

The

CAHs role as

an early warning device serves

a

~,

R7

R7.1

29

useful

purpose

in the radiation control

and plant operation

programs

during abnormal

occurrences

that can not be replaced with continuous or

grab air samplers.

In general,

the inspector

found the conditions of

most

CAMs on Unit 2 and

3 satisfactory.

However, additional

maintenance

and attention

was

needed to return all of the

CAMs to fully operational

status.

The inspectors

concluded that although the inoperable

CAMs were not

receiving appropriate attention,

compensatory

actions

were in place

and

no regulatory requirements

were violated.

The licensee's

corrective

actions

appear

adequate

to address

the issue.

guality Assurance in Radiological Protection

and Chemistry Activities

I te laborator

Com arison

Pro ra

a 0

s ection

Sco

e

84750

The inspectors

reviewed the results of the licensee's

participation in

the Environmental

Protection Agency's

(EPA's) Interlaboratory

Comparison

Program

as documented

in the Annual Radiological

Environmental

Operating

Report for 1995.

b.

Obse vat'ons

and Findin

s

The inspectors

noted that the report included descriptions of the

various types of samples

analyzed

and the analyses

performed,

and

an

evaluation of the analytical results.

The

EPA provided

14 samples of

various environmental

media

and

a total of 41 analyses

were performed.

Statistical

evaluation of the program data indicated that the licensee's

analytical results

were within the

EPA control limits.

c.

Conclusions

R7.2

Based

on the licensee's

overall performance

in the

EPA cross-check

program, it was concluded that

an effective quality assurance

program

had been maintained for analysis of environmental

samples.

o ram Sel

Assessment

'a ~

s ectio

Sco

e

Title 10 CFR 20. 1101(c) requires that the licensee periodically review

the

RP program content

and implementation at least annually.

The

inspector's

review was

made to verify the performance of self assessment

activities, identify significant

RP issues

and to determine if

applicable corrective actions

were appropriately

documented

and

completed.

30

c ~

Obse vations

and Findin s

The licensee's

independent self assessment

program for the

RP program

consisted of formal audits per TS requirements,

observations

and

surveillances.

The inspector reviewed the results of self assessments

completed in the period of January

through June,

1996.

All of the

reviewed

assessments

concerning the licensee's

radiation protection

(RP)

program were conducted

by personnel

within or under the direction of the

Quality Assurance

(QA) or Licensing staff.

The assessments

made in the

RP area during this period were limited in scope

and addressed

regulatory issues,

observations,

and trends in

RP performance

as

appropriate.

Regulatory issues

were identified in, the licensee's

corrective action process for resolution.

No significant concerns with

the

RP program were identified during the assessments.

The licensee recently (July 1996) established

a self assessment

process

for the

RP staff to use in assessing

regulatory compliance

and

performance.

The program was described

in Field Operation

Implementing

Procedure

No.

20 "Radiological Control Self Assessment

Program."

The

procedure

required the development of checklists for nine

RP program

areas.

Each program area

was to have

a compliance

and performance

checklist.

The licensee

conducted

one self assessment

and it was not

documented

at the time of the inspection for the inspectors to review.

The inspectors

noted that the proposed

frequency of self assessments

appeared

adequate.

Co c usions

R8

R8.1

The inspectors

concluded the licensee

was performing periodic

assessments

of RP activities

and no adverse

trends

were identified in

those reviews.

Adverse conditions were placed into the licensee's

corrective action system for resolution.

Miscellaneous

Radiological Protection

and Chemistry Issues

(92701)

Closed

Unresolved

Item 50-259

260

296 96-001-02:

Method for

determination of drywell

CAM setpoint.

During December

1995 the

inspectors

noted that the Unit 2 Primary Containment

Leak Detection

(PCLD) Continuous Air Monitor (CAM) was in constant

alarm due to a

slight increase

in drywell leakage rate.

In accordance

with 2-TI-24,

the alarm setpoint

was increased

to correspond with the increased

background activity concentration

in the drywell.

The inspectors

noted

that the indicated drywell activity concentration

was approximately

2E-9

microcuries per cubic centimeter

(pCi/cc)

and the alarm setpoint

was

approximately 1.18E-8 pCi/cc, which was

much higher than three times

the average

background

as required

by TS Table 3.2.E.

This issue

was

deemed

an unresolved

item pending further

NRC review of the technical

justification for the method of setpoint determination.

In order to

evaluate this issue the vendor manual for the instrument

and setpoint

calculations

provided

by the licensee

were reviewed.

The vendor manual

indicates that the instrument not only has the capability of monitoring

0

il

ik

31

count rate in .units of counts per minute

(cpm) but also

has the

capability to monitor activity concentration

in units of pCi/cc when

a

fixed filter is used.

The manual further indicates that "with these

units the program automatically differentiates

the incoming count rate

to account for the cumulative buildup on the filter since it was last

changed.

Data from particulate

and Iodine channels

then

becomes

the

increase

in activity on

a filter for a given time interval,

and alarms

may be determined

on

a level of concentration

instead of a level, of

filter activity."

The licensee

provided example calculations for

setpoints

in units of concentration

(pCi/cc)

and units of count rate

(cpm).

Those calculations clearly demonstrate

that the instrument would

alarm much quicker when the instrument is monitoring concentration

rather than count rate.

Based

on these

reviews, it was determined that

the licensee's

method for detecting

an increase

in drywell leakage rate

was more conservative

than required

by TS Table 3.2.E.

This item is

closed.

Fl

Fl. 1

Conduct of Fire Protection Activities

Review of Fire Protection

Re uirements for 0 en

EDG Doo

a ~

Ins ection

Sco

e

71750

b.

The inspectors

observed

on July 22 that the fire door to the outside for

Emergency Diesel

Generator

3D was blocked

open during painting

activities within the

3D

EDG room.

Followup reviews were performed to

determine whether the door was blocked open in compliance with the Fire

Protection

Report.

Observ tions

nd Findin

s

F1.2

A copy of the completed Attachment

F Implementing

Form was obtained

from

the

SSS office. It was verified that the compensatory

actions required

by the Fire Protection

Report were taken.

The inspector questioned

the

painter providing fire watch duties

about the responsibilities of the

fire watch.

The painter responsible for providing fire watch was

familiar with the duties

and responsibilities of the fire watch.

Appropriate compensatory

measures

were taken in compliance with the Fire

.Protection

Report.

Security was posted at the door

as

a compensatory

measures

which was appropriate.

Diesel driven

ire

Pum

0 erabilit

Test

'a ~

I s ection

Sco

e

71750

61726

On June

13,

1996,

one of the resident

inspectors

observed

the monthly

operability testing of the diesel driven fire pump.

In certain fire

scenarios

and .emergencies,

this

pump could

be required to play an

important role.

The following documents

were referenced

during the

preparation,

observation,

and review:

32

~

Procedure

O-SI-4.11.B.2.a,

Diesel Driven Fire

Pump Operability

Test (Revision 20)

~

Volume

1 of the Fire Protection

Report

(The

FSAR references

this

document

as the description of the

BFN fire protection

program)

~

Controlled drawings

1-47E836-1,

1-47E850-1

and

2

Observ tions

and

indin s

The inspector verified that the positions of numerous

valves

and

controls in the vicinity of the fire pump were

as depicted

on the

drawings.

No deficiencies

were identified.

The inspector verified that the copy of the SI being

used

was the

correct revision.

One of the workers continuously referenced

the

procedure

during the test

and ensured that all steps

were completed in

order.

The equipment required for the testing

was

on hand.

The

inspector observed that the workers

seemed familiar with the test

procedure.

A hand

pump and several

drums were used to add fuel to the

diesel fuel tank before

and after the test, with care taken to prevent

spillage.

Independent verification steps

were performed properly.

Step 7.3.7.4, of the O-SI-4.11.B.2.a,

required verification that "the

diesel fire pump raw cooling water system is operating properly by

observing flow out the discharge

pipe into the reservoir"

The inspector

identified that the workers did not fully understand this step

and,

consequently,

did not correctly complete it.

Flow from the fire pump

discharge is routed through

a heat exchanger to remove heat from the

engine coolant

and then is discharged

into the reservoir (canal) via a

small pipe.

The workers observed that the fire pump discharge

was

flowing into the canal

instead of looking at the engine

raw cooling

water discharge

pipe.

When the diesel

was secured

at the conclusion of the test,

engine

coolant leaked out of the cap

on the top of the heat exchanger.

The

workers indicated that this had occurred during previous tests.

When

the

pump is secured,

cooling water flow through the heat exchanger

is

lost and the coolant expands

out the heat

exchanger

cap to the floor.

The inspector questioned

the cause of the problem,

what level of coolant

is necessary

for the heat exchanger to function,

and whether coolant

level

had decreased

below that level.

The inspector noted that the

procedure did not require checks of engine coolant level before or after

operation of the pump.

The fire protection group manager

reviewed the issue including contact

with the diesel

vendor.

The cause of the problem was determined to be

that the cap

on the heat exchanger

was broken

and, consequently,

was not

holding in the coolant.

The cap was replaced.

Subsequently,

the

pump

was operated

and

no coolant flowed out of the heat exchanger

when the

engine

was secured.

Information indicated that the level

was not

decreased

below the minimum required for operability of the

pump.

il~

il

33

The fire protection group manager

intends to revise procedures

to

address

the heat exchanger

water level issues.

He stated that training

would be held to inform workers of the engine cooling water flowpath.

The inspector

concluded that overall control of the testing

was good.

The testing

met the requirements

of Section 9.4. 11.8.2.a of Volume

1 of

the Fire Protection

Report.

Procedural

steps

were followed in sequence.

The activities associated

with adding fuel were performed with an

emphasis

on safety

and spill prevention.

Although the heat exchanger

coolant loss issue

was not resolved effectively in the past,

the fire

protection manager

was responsive

on this occasion

and promptly

initiated corrective actions regarding

both deficiencies.

F8

Niscellaneous

Fire Protection

Issues

F8.1

tenance of Fire Protectio

Doors

a.

ns ection

Sco

e

62703

64704

The inspectors

reviewed

some aspects

of maintenance

and testing

associated

with fire protection doors to verify that the activities were

being performed with proper controls

and qualified personnel.

In recent

months,

the licensee

has

been vigorously pursuing correction of fire

impairments

which require compensatory

actions.

Haintenance

of the fire

doors is being transferred

from a craft worker group to the Fire

Protection

Group.

The following documents

were referenced

during the

preparation

and. inspection:

Fire Protection Report,

Volume 1, Fire Protection

Plan

and Fire

Hazards Analysis (Revision 6)

Procedure

0-SI-4. 11.G.2,

Semiannual

Fire Door Inspection

(Revision

18)

Hechanical

Preventive Instruction HPI-0-260-DRS001,

Inspection

and

Haintenance of Doors.

Site Specific Procedure

(SSP) 6.2, Haintenance

Hanagement

System

(Revision

18)

~

Site Specific Procedure

3.2,

Augmented

gA Program

b.

Obse vations

and

indin s

The inspectors

determined that the licensee's

documentation clearly

indicated the classification of the fire doors

and the listed

classifications

met the requirements

of the controlling procedures.

The

inspectors

concluded that many of maintenance activities performed

on

fire doors could be categorized

as minor maintenance

as described

in SSP

Ib

34

C.

3.2'.

Nore extensive

maintenance

on doors,

such

as replacement,

is

required to be performed

by task trained maintenance

craftsman.

The inspectors

discussed

the overall status of .fire doors

and details of

several

ongoing door repairs with the fire protection manager.

He

stated'hat

all repairs to fire doors were currently being performed

by

a dedicated

mechanical

maintenance

craftsman with fire group personnel

assisting.

The intent is that the craftsman train the fire group

personnel

in maintenance

of the doors

and eventually door repairs will

be the responsibility of the fire protection group.

The .manager

explained that detailed task qualification training is being developed

for the fire group. workers.

Procedures will be revised to permit the

fire group workers to perform limited work on the doors

as deficiencies

were identified.

The manager stated that fire protection group workers

will not perform repairs to fire doors until they are formally qualified

to complete

such repairs.

The inspectors

reviewed maintenance

department

records

and determined

the specific task qualifications .associated

with fire door

repair/testing.

The inspectors

then verified that the dedicated

mechanical

maintenance

worker had completed those task qualifications.

Discussions

with workers indicated'hat

the craftsman is considered

"an

expert"

on door repairs at

BFN.

The inspectors

reviewed the licensee's

actions to address

several

recent

test deficiencies

which had

been generated

due to recurring problems

on

several fire doors.

The inspectors

noted that the .required

administrative actions

were being rigorously completed.

For example,

failures of fire doors to close/latch

properly during daily checks

were

noted in the applicable SI, addressed

as test deficiencies,

and work

requests

were initiated.

The problems

were tracked to closure

by

"attachment

F" forms

(Volume

2 of the

FPR, Fire Protection

System/Equipment

Removal

From Service)

which was also

used to ensure

compensatory

actions

were implemented for the deficient doors.

The

inspectors

also reviewed the work orders for several fire doors which

were scheduled

to be replaced

and verified that the appropriate

worker

task qualifications were listed in the work orders.

Conclusions

The inspectors

concluded that fire door maintenance

and testing

activities of fire doors were being adequately controlled.

V. Nana

ement Neetin

s

X1

Exit Neeting

Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on July 19,

1996.

The licensee

acknowledged

the findings presented.

ik

0

0

35

The inspectors

asked the licensee

whether

any mater'ials

examined during the

inspection

should

be considered

proprietary.

No proprietary information was

identified.

Licensee

PARTIAL LIST OF

PERSONS

CONTACTED

J.

Corey, Radiation

and Chemistry Manager

C. Crane, Assistant

Plant Manager

R. Jones,

Operations

Manager

R. Machon, Site Vice President,

Browns Ferry

E. Preston,

Plant Manager

P. Salas,

Licensing Manager

T. Shriver,

Nuclear

Assurance

and Licensing Manager

H. Williams, Engineering

and Materials Manager

IP 37700:

IP 40500:

IP 61726:

IP 62703:

IP 71707:

IP 83750:

IP 92700:

IP 92901:

IP 92902:

IP 92903:

IP 92904:

IP 93702:

IP 84750

IP 86750

IP 92701

INSPECTION

PROCEDURES

USED

Design

Changes

and Modifications

Effectiveness of Licensee Controls in Identifying, Resolving,

and

Preventing

Problems

Surveillance

Maintenance

Observation

Plant Operations

Occupational

Exposure

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

Followup - Operations

Followup - Engineering

Followup Maintenance

Followup Plant Support

Prompt Onsite

Response

to Events at Operating

Power Reactors

Radioactive

Waste Treatment,

and Effluent and Environmental

Monitoring

Solid Radioactive

Waste

Management

and Transportation of

Radioactive Materials

Followup

il

~0ened

36

ITEHS OPENED,

CLOSED,

AND DISCUSSED

Status

Desc

tio

and

e e

e ce

VIO

VIO

NCV

NCV

NCV

~Cosed

260,296/96-06-01

Open

260/96-06-02

260/96-06-03

260/96-06-04

259,260,296/

96-06-05

Failure to Follow Safety Related

Procedures

(paragraphs

Hl.2, Hl.3

and El.l)

Failure to Perform

a

10 CFR 50.59

Evaluation Prior to Disabling

Annunciator (paragraph

03.1)

Opened

and

Return Control

Rod Not Correctly

Closed

Positioned After Testing

(paragraph

01.3)

Opened

and

Excess

Flow Check Valve Not Tested

Closed

per Technical Specifications

(paragraph

H8.2)

Opened

and

Failure to Follow Procedure for

Closed

Receipt of Radioactive Haterials

(paragraph

R1.3)

LER

LER

URI

Item Number

259/95001

260/95006

Status

Closed

Closed

50-259,260,296/

Closed

96-01-02

Descri tion and

Re e ence

EECW Pump Auto Started

(paragraph

H8.1)

An Excess

Flow Check Valve was not

Tested

Per Technical Specifications

(paragraph

H8.2)

Drywell

CAH Setpoint

(paragraph

R8.1)

il~

il'l,