ML18038B639

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Insp Repts 50-259/96-01,50-260/96-01 & 50-296/96-01 on 951231-960203.Violations Noted.Major Areas Inspected: Operations,Including Routine Observations & Review of Unit 3 Thermal Power Above License Condition Max
ML18038B639
Person / Time
Site: Browns Ferry  
Issue date: 02/29/1996
From: Lesser M, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B637 List:
References
50-259-96-01, 50-259-96-1, 50-260-96-01, 50-260-96-1, 50-296-96-01, 50-296-96-1, NUDOCS 9603140308
Download: ML18038B639 (58)


See also: IR 05000259/1996001

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Report

Nos ~:

50-259/96-01,

50-260/96-01,

and 50-296/96-01

Licensee:

Tennessee

Valley Authority

6A 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and, 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection

Conducted:

December

31,

1995

February

3,

1996

Inspector:

nar

.

ert,

,

nidor Ress

ent

nspector

J.

Hunday,

Resident

Inspector

R. Husser,

Resident

Inspector

H. Morgan, Resident

Inspector

J. Coley, Special

Inspection

Branch,

DRS,

(paragraph

3.3)

R. Gibbs,

Maintenance

Branch,

DRS,

(paragraph

3.4)

G. HacDonald,

Maintenance

Branch,

DRS,

(paragraph

3.2)

Approved by:

ar

S.

Lesser.,

C ie

Reactor Projects

Branch

6

Division of Reactor Projects

m/z.~/9 0

ate

sgne

SUMMARY

Scope:

Inspections

were conducted

by the resident

and other inspectors

in the areas

of operations

which included routine observati'ons,

review of Unit 3 thermal

power above license condition maximum, freeze protection program,

and

verification of engineered

safeguards

system alignment;

maintenance

which

included, routine observations,

post maintenance

testing

program,

trending

and

corrective actions,

and scheduling

and planning;

engineering

which included

review of spent fuel pool cooling system

and refueling outage

core unloading

practices,

measures

to prevent'oi'sture

intrusion into safety equipment,

and

Enclosure

2

9603i40308

960229

PDR

ADQCK 05000259

8

PDR

'lN

~is

drywell air monitor setpoint determination;

plant support which included

routine security observations,

ALARA planning effectiveness,

post accident

sampling observations,

and required radiation exposure

postings.

In several

of the areas,

review of open items, including one Unit 3 post restart

Three

Mile Island item,

was also conducted.

Results:

Plant

0 erations

A violation was identified which addressed

Unit 3 operating with core thermal

power above the l.icensed condition maximum for several

hours.

Due to a

problem with a feedwater temperature

transmitter,

indicated core thermal

power

was lower than actual

power.

Operators

increased

core recirculation flow to

maintain indicated core thermal

power at the full rated value.

The condition

was identified after several

hours

when

an operator

noted irregularities

between control

room indications.

(Violation 296/96-01-01,

Core Thermal

Power

Above Licensed Condition Haximum, paragraph

2.2)

Overall implementation of the freeze protection

program was effective.

The

inspectors

noted that

some administrative

aspects

of the program were not

being rigidly implemented,

but there

was

no reduction in the cold weather

protection of safety-related

equipment.

Equipment problems

have

been

few

despite

recent

extended

periods of cold weather.

(paragraph

2.3)

Maintenance

The Post Haintenance

Test

(PHT) Program

and program implementation

were

considered

acceptable.

The

PHT process

was complex, requiring

4 procedures

for implementation.

PHT backlog

and

PHT failure rate were low.

The number of

PHT Problem Evaluation Reports

was low.

PHT activities were generally

adequate

and performed in accordance

with program procedures.

One example of

inadequate

PHT was noted in a scheduled

work order which was subsequently

returned to maintenance

planning for revision.

(paragraph

3.2)

The licensee

has

implemented effective controls for identifying, resolving,

and preventing

issues that degrade

the quality of plant operations

or safety.

The corrective action program at Browns Ferry has

been intentionally set at

a

very low threshold for reporting, evaluating,

and trending plant problem

evaluation reports in order to capture

low level events,

encourage self-

identification of conditions,

and provide effective management

oversight of

all conditi'ons in

a "window" format.

Effective senior plant management

oversight which requires

management

accountability in every area of the

corrective action program

was found to be

a strength.

One concern

was

identified associated

with the application of the Stop, Think, Act, and Review

program.

(paragraph

3.3)

Review of on-line maintenance activities concluded that the licensee

had

a

very strong

program to control the planning/scheduling

of work accomplished

on

its operating units,

which is directed at the completion of surveillance

and

maintenance

in a very aggressive

fashion, while maintaining the plants in as

safe

a condition

as possible.

Two minor discrepancies

were noted,

one

0

~ii

regarding inclusion of Individual Plant Evaluation matrix requirements

into

SSP

7,. 1,

and the other concerning the need to strengthen

the scheduling of

Preventive

Maintenance.

(paragraph'.4)

En ineerin

Review of the Unit 2 spent fuel cooling system

and core unloading practices

identified no deficiencies.

The licensee's

refueling outage practices

regarding the offloading of reactor fuel were

as described

in the Final Safety

Analysis Report.

(paragraph

4. 1)

The. licensee's

current actions to prevent moisture intrusion into

safety-.related

equipment in the intake structure

from conduits passing

through

yard areas

were considered

satisfactory.

Previously,

water

had leaked in from

cable

pul-1 points or through wall penetrations

into the intake structure in

the vicinity of safety-related

cabling.

No degradation

of the cabling was

identified and the licensee

is presently pursuing corrective actions

adequately.

(paragraph

4.2)

An unresolved

item was identified during review of an increase

in Unit 2

drywell inleakage.

The inspectors

noted that the setpoint of the drywell

continuous air monitor appeared

to conflict with statements

in the Technical

Specifications.

Information and experience

indicates that the system is

capable of performing its safety function of identifying increased

leakage

rates,

but additional

review is necessary

to ensure that Technical

Specification requirements

are being met.

(Unresolved

Item 260,296/96-01-02,

Drywell

CAN Setpoint Determination

Method, paragraph

4.3)

During a review of ALARA planning effectiveness,

the inspectors

noted that the

licensee

did not document

management

review/resolution of recommendations

included in some post job review reports.

(paragraph

5.2)

Ij

'l5

REPORT DETAILS

'Acronyms used in. this report are defined in paragraph

8.

1.0

PERSONS

CONTACTED

2.0

2.1

'Licensee

Employees:

Abney, T., Manager,

Independent

Review and Assessment

Blakley, P., Surveillanc'e Instruction Scheduler

Brazell, J., Site Security Manager

Clardy, L., Audit Manager

Coleman,

R., Radiological Controls Manager

Corey, J.,

Chemistry

and Radiol'ogical Controls Manager

  • Crane, C., Assistant

Plant Manager

Gilbert, P.,

PH Scheduler

Johnson, J., Site guality Manager

Jones,

R., Operations

Manager

Little, G., Operations

Superintendent

  • Hachon, R., Site .Vice President,

Browns Ferry

  • Haddox, J.,

Haintenance

and Hodification Manager

Parvin, J.,

CA( Supervisor

  • Pierce,

G., Technical

Support

Manager

  • Preston,

E., Plant Hanager

Rogers,

R., Maintenance/Modifications

Planning Technical

Manager

Sabados,

J.,

Chemistry Manager

Salas,

P.,

Licensing Manager

Schlessel,

J.,

Maintenance

Superintendent

Schumitsch, J., Daily Scheduling

Manager

Scott, T., Maintenance

Technical

Supervisor

Shadrick,

R.,

FME Coordinator,

Maintenance

Shriver, T., Nuclear Assurance

and Licensi'ng Manager

Thompson, J., Senior Instrument

and Control Engineer

Wages,

C., Maintenance

Program Coordinator

Wetzel, S., Acting Compliance

Licensing Manager

Wheeler, J.,

Work Week Manager

White,. D., Manager,

Reactor Safety Engineering

and Review

  • Williams, H., Engineering

and Materials Manager

  • Attended,February

2,

1996 Exit Interview

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

and chemistry/radiation

personnel.

PLANT OPERATIONS (71707,

71715,

92901,

40500)

OPERATIONS

STATUS AND OBSERVATIONS

Unit 2 and Unit 3,operated't

power during this inspection period.

On

January

21,

1996, the licensee

began final feedwater temperature

'l!

0

reduction operations

on Unit 2 by isolating the extraction

steam to the

Al, Bl, and Cl feedwater

heaters

to allow an extended

period of full

power operation.

On January

31, reactor

coastd'own

commenced

and is

expected to continue unti,l Harch 22,

when the

U2C8 refueling outage

begins.

At the close of the report period, Unit 2 was at 99X.

Operations

were routinely inspected

throughout the report period in

accordance

with the guidance

in Inspection

Hodule 71707.

In addition to

weekday monitoring,

some inspections

were conducted

on night shifts and

weekends.

Overall, control

room operators

were attentive

and

professional

in their duties.

During, one backshift control

room visit,

the inspector

observed

control rod testing in progress.

The inspector

noted that the operators

were referencing the appropriate

procedures,

keeping the

ASOS informed,

and were cautious

when changing reactivity to

increase

power back to full. rated level.

The inspector also verified

that the

SOS

was

aware of, the status of the testing

on Unit 3.

On January

9,

1996,

the inspector

noted that

one of the Unit 2 RCIC

turbine exhaust line snubbers

was leaking oil.

The indicator on the

snubber indicated that there

was very little oil remaining.

The

inspector

informed Operations

and the system engineer.

The snubber

was

subsequently

declared

inoperable,

removed,

and rebuilt.

During

disassembly,

the licensee identified that the oil was leaking from the

oil fill fitting.

During rebuild this fitting was replaced.

Following

rebuild, the snubber

was tested satisfactorily

and reinstalled

in the

system.

On January

21,

1996, the Unit I/2

B diesel

generator

auto started

unexpectedly

when the local alarm panel test pushbutton

was depressed

during testing.

The

EDG .did not tie onto the shutdown

board since

normal supply voltage

was available.

Since the cause of the auto start

was not apparent,

the

EDG was declared

inoperable until troubleshooting.

efforts were completed.

'The licensee identified that

a shorted

diode in

the annunciator .circuit caused

the energization of the start failure

auxiliary relay which caused

the auto start.

Normally the diode would

block the relay from energizing to allow testing of the annunciator

circuit.

The l.icensee

replaced

the damaged

diode

and following

successful

PHT of the

EDG declared it operable.

The licensee

reported

the

EDG start to the

NRC Operations

Center

as required.

During a routine tour of a mechanical

equipment

room in the control bay,

one of the inspectors

noted that plastic tubing had

been routed into a

ventilation duct at

an opening, which is required to be blocked

by some

Appendix

R procedures.

A piece of plexiglass is staged

to be used to

block the opening.

The hoses

are connected

to purge

pumps located -on

the control

bay chillers.

Since the hoses

were thick-walled and

appeared

to extend

wel:1 into the ductwork, the inspector questioned if

hoses

would prevent the performance of the procedure.

The

SOS

was

informed of the observation

and investigated.

Subsequently, it was

determined that the hoses

could have

been pulled out of the duct to

allow the plexiglass to block the opening.

The hoses

were relocated

so

that there is sufficient clearance

to install the plexiglass if

0

i1

required.

The issue

was discussed

with Operations

management

as

an

example of conditions which should

be questioned

by operators

during

rounds.

2.2

UNIT 3

THERMAL POWER

EXCEEDED LICENSE CONDITION MAXIMUM

On 'December

27,

1995,

feedwater temperature

transmitter

(3-TT-3-48A),

which provides

an input into the plant computer for calculations of core

thermal

power (HWt), was returned to service after repair-activities.

The feedwater temperature

is also indicated

on SPDS.

On December

28,

at 12:45 a.m.,

an operator noticed

HWt decreasing

with a steady

electrical

output

(MWe).

Upon further review, the operators

noticed

that the feedwater transmitter output,

which normally reads

375'F at

IOOX power,

was reading approximately

402 F. At 1:02 a.m.,

power was

reduced

5

MWe and the transmitter's

input to the power calculation

was

removed.

At 1: 15 a.m.,

power was reduced

another

5

MWe resulting in an

output of 1115

HWe with actual

core power of 3284

MWt.

On December

28, the inspectors

obtained

SPDS printouts

and reviewed

chart recorder traces

as well as other information in order to verify

changes

in parameters,

magnitude of change,

and time intervals.

The

incident was discussed

with Operations

and Maintenance

personnel.

During their initial review of the event,

the inspectors

noted the

following:

On December

24, the transmitter's

input to the thermal

power

calculation

was

removed .from service

due to indication swings.

On December

27,

as the transmitter

was initially returned to

service, it presented

an indication of 3'F to 4

F higher than the

other inputs

(about

379 F).

On December

27, from 4:00 p.m. to 6:52 p.m., the temperature

indication

(and input to thermal

power calculation) steadily

increased

.to 391'F,

causing

the calculated

HWt to slowly decrease.

Since

HWt indicated

was decreasing,

operators

incrementally

increased

recirculation flow to maintain

an indicated

power level

,of 100% thermal

power.

The temperature

indication remained at about

391'F. until 12:45

a.m.,

December

28,

and then

more abruptly changed

to 402'F.

The

sudden

increase

subsequently

presented

a significant drop in

indicated

HWt with little change

in

MWe output.

Operators

reduced

power shortly thereafter.

From 6:52 p.m.,

on December

27 to 12:45 a.m.,

on December

28,

actual

core power was increased

as high as

35

MWt above rated full

power of 3293

HWt.

The eight-hour shift average

was

3306

HWt

(100.4N) with an instantaneous

peak of 3328

HWt (101. 1/).

Initially, the investigation into the cause of the feedwater

temperature failure focused

on loose circuitry connections

because

lS

!I

a terminal

board lug screw was found loose.

Repair activities

included

use of an adhesive

and tightening of the screws

on this

and all similar terminals.

However, after the repair,

the

transmitter

again failed and

by the end inspection period, the

licensee

had placed the transmitter out of service.

After reviewing applicable portions of the

FSAR, the inspectors

also

reviewed the results of the

GE review of the incident to verify that no

assumptions

in the analysis of the design basis

accident

had

been

exceeded:

0

The review concluded that there

was

no adverse effect upon core

safety

and integrity.

GE stated that, in the design analysis,

there is greater

than

a

5%%d

margin to any core thermal limit. They also noted that the event

margin reduction to

4%%d was still well below design limits.

Furthermore,

analysis

performed to set core thermal limits took

into account

a

2%%d core power uncertainty.

Therefore,

GE

concluded that the overpower of about

35

HWt did not adversely

impact plant safety.

Further inspector review indicated that there

had

been

some

opportunities to identify the problem earlier

and several

factors

had

contributed to the performance of the operators

in this incident.

The

inspectors

made the following conclusions

regarding the incident:

The initial slow transmitter failure mechanism

was difficult for

the operators

to detect.

The operators

did not carefully review all available indications

of plant parameters

after reactivity changes

were initiated.

Specifically, they did not investigate

an apparent

power reduction

wi'thout corresponding

changes

in HWe output.

The computer alarms for important plant parameters

such

as

feedwater temperature

were not set at appropriate levels to alert

the operators

of this type of an equipment

problem before limits

were approached.

Information indicated that

some of the, board operators

were not

fully aware that maintenance

had recently

been

performed on, the

transmitter circuitry and there

was

no heightened sensitivity

given 'to the indication.

PER (0951914)

and

an event

human performance

analysis

also noted that

the operators

did not have

a solid model of indications expected

at

rated thermal

power.

4l

IP

As an initial response

to the event,

the licensee

has proposed

the

following corrective actions:

Reactor

Engineering will develop

a detailed

model of plant

conditions at rated thermal

power for both Unit 3 and Unit 2.

The

model will reflect current plant conditions

and is to be provided

to

BFN Operations

by the end of February,

1996.

Operations will provide the .above

model to all licensed operators

and this model will be available

as

a control

room reference

by

April, 1996.

Licensed operator requalification training program will include

training

on the detailed

model

by April, 1996

and

BFN Operations

wi.ll establish

a process for periodic updating of the model

by

Hay,

1996.

Technical

Support will evaluate

the heat balance

alarm setpoints

to verify adequate

warning of non-conservative

failures.

Setpoints

are to be changed/completed

by the

end of February,

1996.

Unit 3 Operating

License Condition 2.C(l),

Maximum Power Level states

that the licensee

is authorized to operate

the facility at steady state

reactor

power levels not in excess

of 3293

MWt.

Reactor, power,

averaged

over

an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> period

ex'ceeded this value.

This event is

a violation

and will be addressed

as Violation 296/96-01-01,

Core Thermal

Power

Above License Condition Maximum.

2.3

IMPLEMENTATION OF

FREEZE

PROTECTION

PROGRAM

On December

22,

1995,

the inspectors

toured the service water building,

intake structure,

diesel

generator buildings,

and Standby

Gas Treatment

building inspecting freeze protection

systems

as the temperature

had

been

below freezing for the previous several

days.

In the Unit I/2

diesel

generator building the inspector discovered

the portable heater

in the carbon dioxide tank room was turned

OFF.

In addition, the room

heaters

in

EDG rooms A, D,

and

3C were

OFF.

The thermostats

in the

remaining

rooms were all set differently ranging from 45 to 90 degrees

fahrenheit.

The inspector discussed

these

observations

with the

ASOS.

He noted that while the heater in the carbon dioxide tank room shoul'd-

have

been energized,

the room was'ot

so cold as to affect the operation

of the system.

The inspector

reviewed the licensee's

procedure

concerning freeze protection,

O-GOI-200-1,

Freeze

Protection

Inspection,

and noted that while the Unit 3

EDG carbon dioxide tank room heater

was

listed in this procedure

the Unit 2 tank room heater

was not.

The: ASOS

stated that the heater

would be energized

and

added to the list of items

to be verified in the procedure.

In addition,

he stated that since the

EDG rooms. were maintained

warm by convection

from the

EDG crankcase

and

jacket water heaters, it was not necessary

to use the room heaters.

Those heaters

are operated

as

needed

by building operators

.as they make

their routine rounds,

therefore the heaters

and thermostats

were not

4

i&

2.4

maintained

in a particular configuration

by plant procedures.

The

inspector

reviewed the freeze protection procedure

and considered it

adequate

to provide the necessary

protection to guard against cold

weather conditions.

Attachment

3 of this procedure is

a discrepancy

log

used to identify those

items listed in the procedure

which are in need

of maintenance.

The inspector

noted that this list of discrepancies

was

quite long, containing approximately sixty different items in need of

repair.

Although none of the .items

on the list were considered

to

require

immediate attention or affecting operability of a safety-related

system,

there were items which had

been

on the list since

September.

Step 5. 10.5 of the procedure requires that

an

ASOS review all items

on

this log every midnight shift to check the status of each

open

discrepancy.

The inspector discussed

this list with the Operations

crew

on shift and determined that the status of the items

on the list had not

been determined

for

some time.

A recent revision to the maintenance

computer software

had a'ffected the ability of the operators

to perform

the checks.

This was discussed

with the Operations

Superintendent

who

directed that this review be performed

and reinforced that thi's list be

maintained current.

A standing order was issued to provide these

instructions.

While the maintenance

of the discrepancy

log was

considered

inadequate,

the inspector could not find. a case

where it

resulted

in inadequate

freeze protection to plant equipment.

The list

generally consisted of items

such

as

damaged

door seals,

damaged

insulation,

and faulty space

heaters,

however other means of preventing

cold weather related

damage

was in place.

Toward the

end of the report

period the inspector verified that the log was being maintained current.

Subsequent

inspections

of freeze protection related

equipment identified

no additional discrepancies.

ENGINEERED SAFEGUARDS

SYSTEM VERIFICATION

During this report period the inspectors

performed

a detailed

inspection

of the Uni't 2 Core Spray system.

A walkdown of the system

was performed

to verify the system lineup was correct

and drawings accurately

reflected the as-built configuration.

Hangers

and supports

were

verified to have adequate fluid and in good working order.

Valves,

pumps,

and motors were inspected

to verify labelling was correct,

no

excessive

leakage existed,

and general

overall condition was acceptable.

Housekeeping

was verified to be acceptable

in the surrounding

area.

Instrumentation

was verified to be operable

and indicating appropriately

for system conditions.

Electrical

power was verified to be aligned for

the system in accordance

with plant procedures.

The inspector did not

identi'fy any concerns

that were not already identified by the licensee.

The

FSAR and system design

documents

were reviewed

and

compared to the

actual

system design

and operation.

The system design criteria,

BFN-50-

7075, section 3.7.1 (7), stated that the system provides

secondary

containment isolation connections

to the reactor building condensate

header, by means of locked closed valves.

The inspector noted that these

valves were not locked closed

and questioned

the licensee.

Site

engineering

subsequently

determined that the valves did not have to be

locked

and will revise the design criteria accordingly.

The inspector

OS

iS

2.5

concluded that the- Core Spray system

was properly aligned,

in good

mechanical

condition,

and capable of performing its intended function.

REVIEW OF

INPO EVALUATION REPORT

2.6

The senior resident

inspector reviewed'he final report for the

1995

INPO evaluation.

The inspector

concluded that, the report did not

include

any issues with a patential to substantially affect nuclear

safety -in the short term and thus

no specific followup NRC inspection is

necessary.

The

INPO report was, in general,

consistent with current

NRC

perceptions

of BFN performance.

OPEN

ITEMS REVIEW

2.6.1

VIO 260/94-24-02,

FAILURE TO

FOLLOW PROCEDURES

This violation addressed

four examples

regarding lack of procedural

adherence.

The licensee

responded

in correspondence

dated

December

2,

1994.

The first example involved

a failure to properly monitor reactor

water level during reactor cooldown,

as required 'by plant procedures.

At that time the licensee

was required to maintain reactor water level

indication displayed

on one of the integrated

computer

system

screens

located in the main control

room.

This. was in response

to

a problem

being experienced

with water level indication during the cooldown phase

of a reactor

shutdown in

BWR plants.

Because this requirement

was

no

longer required following the implementation of reactor vessel

level

instrumentation modifications,

the licensee's

corrective action for this

example

was to delete this requirement

from the applicable procedures.

In addition, the licensee

discussed

this event in the .monthly

SOS

meeting.

The second

example occurred

when

one of the reactor

recirculation loop temperatures

was not monitored or recorded

.as

required

by plant procedures

during reactor

cooldown.

Following the

discovery,

the appropriate

data

was recovered

from the computer files.

Corrective action for this event

was to discuss it at

an

SOS monthly

meeting

and review it with the Operators

as part of their training

program.

The third example occurred

when

SBGT system

dampers

were not

returned to their normal position following the performance of

surveillance testing.

The licensee

realigned the dampers correctly.

This example

was also discussed

at the monthly

SOS meeting.

In

addition,

the licensee

reviewed other non-Operations

surveillance

instructions to determine if the system restoration portion of the

procedure

provided adequate

guidance to ensure

proper post-test

realignment.

The review. included

563 Surveillance Instructions,

Chemistry Instructions,

and Technical

Instructions.

Sixty-six of the

procedures

required'evision

to ensure

proper.

system restoration.

The

fourth example occurred

when the licensee failed to return, a HPCI system

handswitch to the proper position following its operation,

as directed

by alarm response

procedures.

The switch was

supposed

to be used to

open

a drain valve

and then again to close the drain valve upon

completion of the draining process.

In this case,

the Operator failed

to realign the switch

as required

when the draining evolution was

completed.

Following identification of the issue,

the switch was

0

3.0

3.1

repositioned correctly.

The Operator

was counselled

and the event

was

discussed

both at the monthly

SOS meeting

and then with the Operations

shift members.

In response

to this violation and subsequent

procedural

errors,

the

l.icensee initiated

an Incident Investigation to. review operational

error

events

and develop corrective actions.

A follow-up evaluation

was

performed approximately six months after the completion of the

investigation to assess

the effect of the corrective action.

This

assessment

indicated

very. little change

regarding factors contributing

to procedural

adherence

problems.

Surveys

and interviews were completed

which indicated that the improvement

had not progressed

as far as the

licensee

had hoped.

The licensee attributes

the lack of progress

in

this area to the increased

workload associated

with the startup of

Unit 3.

Discussion with Operations

management

indicated that

a new

program to address

procedural

adherence

issues

is under development.

The inspector verified the specific corrective actions for this

violation have

been

completed.

This violation is closed.

One violation was identified in paragraph

2.2.

MAINTENANCE (62703,

92902,

40500,

61726,

92901,

37551,

92903)

MAINTENANCE AND SURVEILLANCE ROUTINE OBSERVATIONS

Maintenance activities

and surveillance tests

were observed

and/or

reviewed during the reporting period'n

accordance

with the guidance in

Inspection

Modules

62703, and. 61726

The following maintenance

and surveillance activities were reviewed

and

witnessed

during routine inspections:

WO 96-000812-00

Repair of Unit 3

PASS

Gas Return

To Suppression

Chamber

Check Valve 3-CKV-043-0163

3.2

On January

23,

1996, after

a Unit 3

PASS gas

sample

was analyzed,

(See

Paragraph

5.3) high oxygen content within the sample

was detected.

After troubleshooting activities were performed, it was determined that

the

PASS

Gas Return to the Suppression

Chamber

Check Valve, 3-CKV-043-

0163,

was intermittently preventing

gas

samples

from returning to the

PASS.

After repairs to the valve were performed,

on January

26,

1996,

the system

was returned to service

and,resampling

was, performed.

The

inspectors

concluded that the repairs were, conducted

and the system

performed satisfactori,ly.

POST

MAINTENANCE TESTING

The inspectors

performed

a review of the Post Maintenance

Testing

(PHT)

Program at Browns Ferry.

PHT tracking

and backlog were examined.

Procedures

for

PHT and

PHT, related

PERs were reviewed.

Nuclear

Assurance

audits,

maintehance

'department self assessments,

and work

order feedback

forms were reviewed for data regarding

PHT.

Work orders

'0

'lN

3.2.1

in the planning stage,

ongoing work,

and completed

work orders

were

examined for PHT adequacy.

REVIEW OF

POST

MAINTENANCE TESTING

PROGRAM

The

PMT process

was controlled

by SSPs.

The process

was complex and

required the use of the following four procedures:

SSP 6.2

Haintenance

Management

System,

SSP 6.50

Post Maintenance Testing,

SSP 8. 1

Conduct of Testing,

and

PHT-0-000-TST001

PHT Maintenance Testing

Matrix.

The required

PHT was specified

by maintenance

planning personnel

during

work order preparation

then was reviewed

by a technical

reviewer,

quality assurance

and cognizant supervisor

as appropriate

and operations

SOS prior to conducting the testing.

PHT activities which deviated

from

the guidance of PMT-O-OOO-TST001,

the

PHT Maintenance

Testing Matrix,

required Technical

Support/Maintenance

Engineer concurrence.

The

completed

PHT was reviewed

by performing department

personnel

and the on

shift SOS.

The work order tracking system

showed

a backlog of approximately

90 work

orders awaiting

PHT.

The backlog included

63 Unit

1 items with 38 items

> 6 months old.

The

PHT backlog of Unit 0

Common equipment

was

29 with

8 items

> 6 months old.

Unit 2

PHT backlog

was

24 with 6 items

> 6

months old and Unit 3

PHT backlog

was

39 with 5 items

> 6 months old.

Browns Ferry weekly, performance

data indicated that. an average of 80 to

100,corrective

maintenance

work acti.vities were completed

per week.

The

92 item

PHT backlog represented

approximately

one week of work

activities.

The inspectors

determined that the

PHT backlog

was not

excessive

indicating that most

PHTs were being performed shortly after

completion of the maintenance

activity.

r

The

BFN weekly status

reports

indicated

an average of 3 failed

PMTs per

week.

These

items represented

work which changed

from awaiting

PHT

status

back to available for work status

due to either

a problem with

the planned

PHT, or work scope

changes

or plant configuration changes.

The number of failed

PHTs was low and did not indicate

a problem, with

PHT planning.,

3.2.2

REVIEW OF CORRECTIVE ACTIONS ASSOCIATED WITH PHT ISSUES

The inspectors

reviewed the

PERs related to PHT.

From January,

1995, to

January,

1996,

eleven

PERs were identified which were related to PHT.

The eleven

PERS included

one level

B PER,

seven level

'C PERs,

and three

level

D PERs.

The

PERs were reviewed to determine root cause.

Five

PERs were due to inadequate

PHT, four PERs were due to

PHT

administrative or documentation

problems,

and two PERs were due to

PHT/plant configuration problems.

Approximately 0.2X of PHT activi'ties

resulted

in

PERs

assuming

100

PHTs performed weekly.

Noncited Violation 296/95-64-03,

Equipment

Returned to Service Without

Proper

PHT Completion,

was discussed

in

NRC Inspection

Report

11

10

50-260,296/95-64 for the

one level

B PHT PER951842.

Incident

Investigation Unit 3 Control Rod 42-39 Triple Notch Event

December

4,

1995 was performed for the level

B PER951842.

The inspectors

reviewed

the incident investigation

and determined that the root cause

evaluation

was thorough.

The short'erm

and long term corrective actions

appeared

to be focussed

on root cause resolution

and were intended to strengthen

the

PHT cl'osure process.

The inspectors

reviewed Nuclear Assurance

maintenance

audits,

maintenance

department self assessments,

and work order feedback

process

forms and determined that these evaluations

did not identify problems or

offer recommendations

for improvement to the

PHT program.

During 1994,

the licensee

conducted

an internal review of the work order process

to

identify areas for improvement.

This internal evaluation identified

some problems with PHT for the sample work orders reviewed.

The

PHT

areas for improvement identified in the licensee's,internal

assessment

included:

some

PHTs not problem related,

some

PHTs not clearly worked,

some.

PHT adequacy

marginal,

some

PHTs out of sequence

with work steps,

and

some steps

under

PHT heading

not

PMT steps.

3.2.3

VERIFICATION OF

PHT

PROGRAM EFFECTIVENESS

The inspectors

reviewed

PMT adequacy for selected

work orders

scheduled

to be performed during the week of January

8-12,

1996,

and observed

some

PHT activities in progress.

Completed, work orders

were also reviewed

for PHT adequacy

and

program

implementation.

PHT activities observed

in progress

were acceptable

and were conducted

in accordance, with the requirements

of the

PHT program

SSP procedures.

Some minor deficiencies

were noted in the review of scheduled

and

completed

work orders.

PHT for the selected

scheduled

work orders

reviewed

was acceptable

and met the

PHT

SSP requirements

except for work

order 90-022313-000.

The specified

PHT for this work order was not

adequate

for the intended

maintenance

and did not meet

PHT

SSP guidance.

The licensee

indicated that the work order was returned to maintenance

planning for revision

and that

a

PER would be written.

The review of completed

work orders

noted

some minor deficiencies

where

PHT requirements

were generic

and did not always contain

acceptance

criteria specific to the component

addressed

in the maintenance

activity.

PMT specified

was not always in accordance

with the guidance

specified in the

PHT matrix.

These minor deficiencies

were similar to

the findings of the licensee's

1994 work order improvement review

indicating that the results of that improvement effort were not fully

implemented

and effective.

Il

~IN

3.3

EFFECTIVENESS

OF

LICENSEE

CONTROLS IN IDENTIFYING, RESOLVING,

AND

PREVENTING PROBLEMS

The inspector

reviewed Nuclear Assurance

and Licensing

(NA&L) audits,

surveillances,

self assessments,

problem evaluation reports

(PERs),

procedures

and trending reports.

The inspector also attended

meetings,

and conducted

interviews with maintenance

personnel

and management

from

each group within NA&L to determine

whether the corrective action

programs

at Browns Ferry, were effective in identifying, resolving,

and

preventing

problems that degrade

the quality of plant operations

.and

safety.

The inspector's

specific area of focus

was to determine

how the

licensee's

controls

improved plant maintenance.

A detailed analysis of

NA&L audits,

monthly surveillances,

self assessments,

PERs,

and trending

reports dealing with maintenance

and issued

from April 1,

1995,

through

January

31,

1996,

was performed to assess

the licensee's ability to

identify and correct problem areas.

This review revealed that audi.ts

and assessments

were well planned,

and documentation

was excellent.

NA&L findings were in diverse

areas

and revealed that the auditors

were

knowledgeable,

experienced

and effective.

A review revealed -that the

licensee's

findings were similar to findings identified by

NRC during

the

same time period.

This indicated that the licensee

was properly

focused

on suspected

problem areas.

Evaluations

conducted

on issued

PERs were effectively derived

and documented.

Scope of the corrective

actions

were expanded to include other applicable related

systems,

equipment,

procedures,

and personnel

actions.

The inspector

attended

a

PER root cause

analysis

committee meeting to observe

the process.

Based

on discussions

among the members

the inspector concluded that the

committee

members

were knowledgeable

and capable of determining the

appropriate

root cause for the problems

addressed.

Each

member

participated

in the discussions,

diverse

views were addressed

properly

and agreement

reached.

All departments

have fully implemented

the

PER program.

As .a result

over

1400

PERs

were initiated in 1995 with over 80 percent of the total

falling in the lower threshold category.

This reflected senior

management's

goal to lower the threshold for reporting, evaluating,

and

trending plant problem evaluation reports to

a level that captured

low

level events,

encouraged

self-identification of conditions,

and provided

effective management

oversight of all conditions in

a "window" format.

Oversight of the corrective action program is implemented

by NA&L's use

of. performance

indicators

such

as:

PERs issued/closed/remaining

open;

PERs rejected;

and

PER extensions.

A review of each of the indicators

revealed that they were effectively controlled.

The inspector

also

attended daily management

review committee

(NRC) meetings to observe

the

effectiveness

of the review process.

Each

PER, regardless

of its level

of severity,

was presented

for senior

management

review.

Each

PER was

appropriately discussed

and other areas

or plant units were considered

in the corrective action.

12

To determine

how the licensee

controls were

implemented

the inspector

reviewed documents,

attended

morning maintenance

production meetings,

the plant operations

review committee

(PORC) meeting,

and the plan of

the day meetings.

The plan of the day meeting

was assessed

as

a very

effective meeting which in addition to daily planning covered the status

of many diverse subjects

which affected plant performance

and safety.

In addition, the inspector interviewed maintenance

managers,

project

coordinators,

and engineers.

Specific areas

examined

included materials

management,

foreign material exclusion,

maintenance

history to ensure

that repetitive failures would, be correctly identified,

and conduct of

maintenance

(work practice).

Each of the areas

had previously been

identified by the corrective action program or by

NRC findings to have

weaknesses.

The inspector

examined the measures

taken or in process of

being completed

and found that corrective actions in each

area

were

being aggressively

pursued.

Personnel

responsibl.e

were held directly

accountable

by the site Vice President.

This accountability required

a

bottom line status of improvements

from each organization for their "Top

Ten Issues List" (including the plant manager's

Top Ten Issue List), the

"Achieving Excellence

Program"',

"Red

and Yellow Windows", "Major Project

Issues"

and "Executive Performance

Review", using

a

12 week rolling

schedule

to establish

the specific time for each meeting.

Corrective

actions

taken in the areas identified above were very good

and should

strengthen

performance of each

area.

One area which the inspector considered

a weakness,

based

on the review

of PERs,

audits,

and assessments,

was that of work practices that dealt

with issues

such

as

human performance

and procedure

adherence.

These

items are

on Browns Ferry's

"Top Ten Issues List", and comprehensive

corrective actions

such

as making work orders

more user friendly were in

process.

However, the inspector

noted

as 'a result of attending

maintenance

production meeti'ngs,

plan of the day meetings,

reviewing

documents,

and conducting, interviews, that the licensee did not

consistently exhibit an effective

and proactive attitude towards their

"STAR (Stop, Think, Act,

& Review) Program".

The inspector noted that

although proper attention

was being directed at correcting programmatic

barriers, insufficient action

had

been taken to train individuals tasked

to perform

a specific function on how to focus his or her attention

on

properly performing that function regardless

of the situation

around

them.

The inspector interviewed

a

NASL supervisor

about this

and found

that

NASL had audited the concern

and found that,

although plant

personnel

knew what

STAR stands for, when specific situations

were

presented

to individuals

and they were

asked

how to apply

STAR to

prevent

a discrepant

condition from occurring,

the individuals could not

do so.

3.4

SCHEDULING AND PLANNING OF MAINTENANCE ACTIVITIES

This portion of,the inspection

was conducted to review the licensee's

planning

and scheduling of on-line maintenance activities.

The

inspection

included

a review of the procedures

controlling the area;

attendance

at scheduling

and plan of the day meetings;

interviews with

the Daily Scheduling

Manager,

a Work Week Manager,

and the personnel

iN

13

responsible for scheduling surveillances

and preventative

maintenance;

review of .the twelve week rolling schedule;

and review of the licensee's

matrix, which was developed to prevent the simultaneous .scheduling of

work on systems/components

critical to .the high risk scenarios

in the

licensee's

IPE.

The focus of the inspection

included

a detailed

analysis of the licensee's

Work Week Schedule

9604 issued to control the

work accomplished

during the week of January

21 - 27,

1996.

The licensee

uses

a scheduling

scheme

which employs the use of a one

year SI schedule,

a twelve week rolling schedule,

an

IPE matrix, work

week schedules,

and the plan of the day meeting to schedule

and control

the work on the three

BFN units.

The one year SI schedule

provides

a

schedule of all Technical Specification required surveil-lances for the

upcoming calendar year.

This schedule

is developed

in consideration of

the twelve week .rolling schedule,

and .is based solely on the required

surveillance

frequency in Technical Specifications,

with no

consideration of the. SI grace period or when the SI is actually

performed.

The twelve week .rolling schedule

is

a medium range

schedule,

which provides the fundamental

technical, framework for the scheduling of

work during

a twelve week period.

This schedule

(framework) is repeated

every twelve weeks.

This schedule

is designed

to maintain the plants in

as safe

a condition

as is possible,

allowing necessary

work and

surveillance to be performed

as required/needed.

The schedule

separates

plant systems

by electrical division, schedules

work on

ECCS systems

in

different work weeks,

considers

the interaction of systems

which are

shared

between

the three units,

and forces

a review of the backlog of

work on every plant system at least

every twelve weeks.

The

IPE matrix

identifies the important interactions

between

the systems for all three-

units

as addressed

in technical specifications,

and in the most

significant risk based

scenarios

in the licensee's

IPE..

The matrix

provides additional

guidance to work week managers

in the scheduling of

work, which prevents

systems

from being

removed

from service

simultaneously

which are important in the risk based evaluation of the

IPE.

The work week schedule

is the backbone of the licensee's

work

control

and scheduling

program.

The work week schedule

schedules

all

planned

work for a given work week (a period of seven days).

The

scheduling of the work for a particular work week begins

several

weeks

in advance,

and is under periodic review and revision by site scheduling

and the involved plant departments

up until the time of execution.

The

final tool used

by the licensee

to schedule

and control work is the plan

of the day meeting.

The'lan 'of the day is used to schedule

emergent

work.

Priorities are given to emergent

work which involves control

room

annunciators

or equipment in a degraded

status.

Work in these

categories

is worked

as

soon

as possible,

and other emergent

work is

prioritized for work in accordance

with, a later .work week schedule

or

during

an outage.

In order to evaluate

the effectiveness

of the licensee's

work control

and scheduling

process,

the inspector

conducted

a detailed

review of the

work scheduled

in licensee

work week 9604 ('anuary 21-27,

1996),

which

corresponded

to work week eight of the twelve week rolling schedule.

The inspector

was assisted

in this review by the work week manager

14

responsible

for that schedule.

This review consisted of a lengthy.

process

involving the evaluation of approximately

600 work items,

.involving surveillances,

preventative

maintenance

items,

and corrective

maintenance

items.

The inspector discussed

each

item on the work week

9604 schedule with the work week manager in an effort to obtain

a

complete understanding

of each work item.

In many cases

the applicable

SI,

PH or

WO was reviewed to learn the extent of work.

Each item was

then

compared to the SI schedule,

the twelve week rolling schedule

and

the

IPE matrix in order to assess

its impact

on plant safety.

This

inspection effort resulted

in the following observat'ions

and

conclusions:

The scheduling of SIs was in strict compliance with the

one year SI

schedule

and the twelve week rolling schedule,

and SIs were consistently

worked on schedule.

Several

work items (corrective maintenance

and

PHs) were noted which

were not scheduled strictly in accordance

with the twelve week rolling

schedule.

However,

in every case,

the work .did not have

any negative

impact

on plant safety.

If work was scheduled'n

deference

to the

twelve week schedule

on

an important safety

system,

the work did not

involve removal'f the syste'

'from service.

And,, i'f work was scheduled

in deference

to the twelve week schedule,

and did involve removal of the

system

from service,

the system

being worked was not important to the

safe

shutdown of the plant in the case of an event.

Scheduling of PHs was considered

to be the weakest link in the

scheduling,and

work control process,

The inspector determined that the

scheduling of. PHs involved consideration

and

use of the

25K grace

. period,

and

as

a result,

scheduling of this work. was easily postponed

during schedule

development.

Additional review of this area determined

that

PMs were accompl.ished after the late date approximately

15-20

percent of .the time.

However, it was noted that the licensee

did have

a

program in place, which,involved engineering

review for compensatory

measures

each time the late date

was missed.

This issue

was discussed

with the Daily Scheduling

Manager

and with the Site Vice President.

The

Daily Scheduling

Manager

was already

aware of the weakness

in the

scheduling of PHs,

and

was in the process

of scheduling firm completion

dates

in accordance

with the twelve week rolling schedule.

Computer

programming

problems

were hampering this effor't, but he was committed to

resolution of this issue.

When this issue

was discussed,

the Site Vice

President

confirmed that the completion of PHs

on schedule

was

considered, just as important

as completing SIs

on schedule.

Scheduling of corrective maintenance

appeared

to be adequate.

The

scheduling of emergent

work was in accordance

with the

scheme

discussed

above.

The inspector

reviewed data concerning the backlog of corrective

maintenance.

This data

showed that the backlog of on-line maintenance

work items (for Unit 2 and'ommon)

had decreased'ince

implementing the

twelve week schedule

concept

up until about August

1995 (from about

2500

items in January

1995 to about

2000 items in August 1995), but 'had

remained

about the

same

since that time.

It was also noted that when

)l~

lip

15

Unit 3 was brought

on line it only added approximately

500 items to the

on line backlog.

The inspector did not draw any specific conclusions

from this review.

3.5

., The inspector noted that all items scheduled

in a given work week were

scheduled

down to the day

and shift they were to be accomplished.

This

was discussed

with the Site Vice President,

and it was learned that the

reason for this amount of detail in the scheduling

was to improve

schedule .adherence.

The inspector

had previously reviewed data

on

schedule

adherence

and

was

aware that it was very good at about

70-80K

(i.e., work at

BFN is accomplished

on scheduled

approximately

70-80X of

the time).

The inspector

reviewed the procedure

which controls the scheduling

and

work control process,

SSP 7. 1,

Work Control, Revision

14, dated

December

21,

1994.

One weakness

was noted in this procedure

involving

requirements

regarding the implementation of the

IPE matrix.

The

inspector

noted that the procedure

did not provide any requirements

concerning

the use of this matrix in the scheduling

process.

TVA, in a

letter,

dated

December

19,

1994 committed to the incorporation of the

IPE matrices

in the scheduling

process for all

TVA plants

by the

end of

1995.

This commitment

appeared

to have. been

accomplished

at

BFN, based

on discussions, with various scheduling

personnel

and based

on

a review

of the matrix developed for this purpose.

However,

formal requirements

concerning

the use of this matrix have not been incorporated

into the

sites

scheduling

procedure.

This issue

was discussed

with the Daily

Scheduling

Manager

and the Site Vice President.

Both indicated that

action

was underway to proceduralize

the use of the matrix.

The inspectors'eview

of this area

concluded that the licensee

had

a

very strong

program to control the planning/scheduling

and control of

on-line maintenance activities,

which is directed at the completion of

surveillance

and maintenance

in a very aggressive

fashion, while

maintaining the plants in as safe

a condition

as possible.

OPEN

ITEMS REVIEW

3.5.1

VIO 259,

260, 296/94-17-01,

INSTRUMENT CALIBRATION DEFICIENCIES

This event'occurred

when licensee

personnel

did not properly update the

Preventive

Maintenance

program to reflect

a change

in the High Pressure

Coolant Injection minimum flow valve flow indicating switch unique

identification number.

The

UNID had

been revised to correct

a

discrepancy

between

the instrument label in the plant

and the equipment

computer database;

however,

the

new UNID was not added to the Preventive

Maintenance

program.

Therefore,

the flow'witch was not being

cal.ibrated.

Additionally, the setpoint for the switch was modified.

The process for changing,

a setpoint did not include

a mechanism to

ensure/verify

implementation of the changes

to the appropriate

procedures.

When this condition was identified the switch had the wrong

setpoint

and not been calibrated, for approximately

37 months.

80'

16

The licensee

responded

'in correspondence

dated August 29,

1994.

Corrective action for this violation was to revise the preventive

maintenance

procedure

and properly calibrate the affected switch.

SSP-6.3,

Preventive

Haintenance

Program,

was revis'ed to provide the

necessary

mechanism to ensure

preventive maintenance

procedures

were

updated

when UNID's were changed.

In addition,

SSP-6.8,

Instrumentation

Setpoint,

Scaling,

And Calibration Program,

was revised to require the

DCN process

be used

when. changing setpoints.

This process

includes

controls to ensure

other affected

procedures

are revised

and instruments

are recalibrated

to the .new setpoints

as necessary.

During the licensee's

review of this incident, it was identified that

other instrument setpoints

had

been revised without the .instrument

being

recalibrated

to the

new setpoint.

Upon discovery,

the licensee

performed the appropriate calibrations.

The inspector

reviewed licensee

documentation

and verified the affected calibrations

were completed

and

incorporated

into the appropriate

preventive maintenance

procedures.

Based

on completion of these corrective actions, this violation is

closed.

No violations or deviations .were identified.

4.0

4.1

ENGINEERING (37551,

92903,

40500)

REVIEW OF

SPENT

FUEL

POOL

COOLING SYSTEM AND FSAR,DESCRIPTION

OF

OUTAGE

FUEL UNLOADING PRACTICES

During this report period the inspector

performed

a detailed

walkdown of

the Unit 2 spent fuel pool cooling system using plant drawings,

applicable portions of the

FSAR,

and the system design specifications.

The inspector verified the plant drawings were accurate,

component

labelling was accurate

and physical condition of the system

was

acceptable.

Particular attention

was given to verifying that fuel pool

level instrumentation

and associated

annunciator logic power supplies

were divisionalized.

The inspector did not identify any deficiencies

not already identified by the licensee.

It was noted that the fuel pool

cooling pumps

had work requests

to repair leaking seals.

Packing

leakage

has

been

an ongoing problem with these

pumps

on all three units.

The inspector discussed

this with maintenance

personnel

and determined

that this problem has not led to

a failure of any of the pumps.

As previously stated,

the inspector

reviewed the system design basis

documents

and discussed

operating practices with the licensee

as they

pertained to core offload during refueling outages.

In the past the

licensee

has

performed

both full core

and partial core offloads.

A

partial core offload is planned for the upcoming Unit 2 cycle 8

refueling outage

scheduled

to begin in Harch,

1996.

The system design

documents

and .FSAR state that the fuel pool cooling system is capable of

removing the decay heat

from a full core offload at the

end of the fuel

cycle plus the decay heat of the spent fuel from the two previous

refuelings.

These

documents

state that the

RHR system would be required

to be operated

in parallel with the fuel pool cooling system

.in order to

IN'

17

remove this heat.

The inspector

noted that the calculations

which

determined

the 'heat

loads

and the heat

removal capability used limiting

values for fuel pool temperature,

reactor building closed cooling water

temperature,

and time after shutdown prior to fuel offload.

Discussions

with the licensee

indicated that historically the fuel pool cooling

system

has

been

able to remove the heat from a full core offload without

needing

the assistance

from the

RHR system.

The inspector

reviewed the

licensee's

procedures

applicable to the fuel pool cooling system .and

found them to contain

adequate

instruction to ensure

acceptable

pool

temperatures

are maintained.

MEASURES TO

PREVENT MOISTURE INTRUSION INTO SAFETY-REL'ATED EQUIPMENT

During routine tours over recent

months,

the inspectors

have noted water

leaking into the intake structure

through the thermolag enclosure

around

junction box 4915.

Currently, the thermolag is removed

and the box has

been

opened to address

the water intrusion issue.

This junction box

contains cabling associated

with some of the

RHRSW pumps

and is

important to safe

shutdown of the reactors.

The inspector

noted that

several

splices

are located within the enclosure.

In accordance

with

the fire protection

program,

the thermolag is

a required fire barrier.

The water leakage

has prevented

the licensee

from finishing work

activities

on the JB since

a 30 day "cure" time is required

on the

thermolag material.

Through review of .intake building access

records

and discussions

with personnel

assigned

as fire watches,

the inspector

verified that the licensee

has

been

implementing the compensatory

actions required

by the fire protection

program.

The inspector questioned

plant management

on the status of the

JB

repairs

and whether the water .leakage

issue

was being addressed

appropriately.

On January

12,

1996, the inspector

was briefed

by.

engineering

management

and discussed

the repair activities with

maintenance

personnel

at the site of the leak.

The leak into JB 4915

and the west wall of the intake structure is being pursued.

The

inspector

was provided

a copy of an onpoing general

plan to resolve the

water problems.

A drain was found in the bottom of the JB enclosure

and

was subsequently

cleaned

out so that inleakage

could flow out of the

box.

One major source of the water appears

to be from unsealed

conduit

openings

located in "Handhole

15" northwest of the intake structure.

The

handhole is open at the bottom and ground water accumulates

well above

the conduit openings.

Plans

are to instal.l moisture seals

on the

conduit openings.

On January

16, the inspector

noted that

an initial

attempt to seal

the conduits

had

been completed,

but significant water

leakage

into the JB through the conduits

(and out the cleaned

out drain

path)

was still present.

The inspector

was

aware that water intrusion problems

had occurred at

TVA nuclear sites in the past

and reviewed documentation of past

corrective actions at

BFN.

The licensee's

actions regarding

NRC

Information Notice 92-69,

Water Leakage

From Yard Area Through Conduits

Into Buildings, were reviewed.

The inspector

noted that at least

one

example of water

leakage

at

BFN due to unsealed

conduit openings

in

18

handholes

had

been

noted

and repaired.

The licensee

focused primarily

on secondary

containment

seals,

took credit for preventive maintenance

checks

performed

on manholes,

and concluded that

a review to identify

potential water leakage

paths

from yard, areas

into 'buildings containing

safety related

equipment

was not warranted.

Technical

Support personnel

conducted

a detailed

walkdown of conduits

passing

through secondary

containment

under elevation

572.5

and noted deficiencies

were corrected.

Actions in response

to

a Corrective Action Tracking Document associate'd

with water inleakage

included

a preventive

maintenance activity (BFN-0-

MISC-040) which requires

a check of plant

sump

pumps for manholes,

valve

pits,

and tunnels.

NRC review of the licensee's

actions regarding water

inleakage into manholes

was documented

in IR 94-27

and the preventive

maintenance

activity was noted.

The inspector

noted that the

hand hole

15 had recently

been

added to .the work instructions for the

PM (even

though

no

sump

pump is located in the handhole).

As, a result of the above reviews,

on January

17, the inspector discussed

with plant management

the concern that there

may be "handholes"

or other

cable "pull points" containing unsealed

conduits which may permit water

leakage into,buildings containing safety related

equipment.

The scope

of previous actions did not envelope all potential

paths.

The inspector

also questioned

the condition of the cable

and splices in JB 4915 which

had apparently

been wetted for an extended

period.

Subsequently,

after several

followup meetings with engineering

personnel,

the inspector

concluded that the vulnerability of safety

related

equipment to water intrusion from the yard was limited to

conduits/cables

routed to the intake building and the

EDG buildings.

The inspector

was provided detailed information on the routing of RHRSW

cabling

and all safety related cabling between

the turbine building and

the intake structure,

The inspector

reviewed the Fire Protection

Report

and other docketed

information and concluded that the routing was

as

described

in those

documents.

The design

and construction of the conduit

routing further limited the equipment of concern to the intake

structure.

Electrical engineering

personnel

supplied information which

supported

the conclusion that the cabling, and splices

would not be

damaged

by exposure

to water unless

such

exposure

was for years.

There

has

been. no indication of degradation

in the cabling.

Two of the inspectors

walked down the cable tray tunnel

between

the

turbine building and the intake structure.

Additionally, the pipe chase

tunnels in the turbine building were inspected.

While there

were small-

amounts of ground water intrusion in the pipe tunnels,

the water was

well below the level of safety-related

equipment

and the tunnel

sump

systems

appeared

to be functional.

In the cable tray tunnel, the

inspectors

observed that temporary repairs

had

been

performed to stop

water intrusion into the tunnel.

Since the repairs

were obviously

temporary

(pieces of wood braced

against

foam stuffed into openings),

the inspectors

questioned

plant management

about plans to permanently

repair the leaks.

Maintenance

management

subsequently

informed the

inspector that

a

DCN is being

approved to address

the problem.

hi'S

19

4.3

At the

end of this. inspection period, additional

maintenance

activities

were being completed

in an attempt to seal

the conduit openings

in

handhol'e

15.

The inspector discussed

with engineering

personnel,

the

plans to thoroughly clean out the interior of the junction box to reduce

the chance that the drain would again

become blocked.

The inspector

requested

that the cables

and splices inside the box be examined before

the box is sealed

to verify that

no damage

had occurred.

The inspector

observed

workers cleaning out the box.

The licensee is considering

available

methods of sealing .the west intake wall during .the upcoming

refueling outage.

The inspector

concluded that, while the licensee

had not been aggressive

in the past regarding the inleakage into the intake building, the

current work activities are adequately

addressing

the issues.

The

inspector

concluded that there is no current safety-related

equipment

problems

associated

with the inleakage

into the intake structure.

DRYWELL AIR MONITORING SYSTEM ALARM SETPOINT

On December

23, the licensee

noted that the Unit 2 drywell inleakage

rates

had increased slightly and that intermittent alarms

were being

received

by the containment

atmosphere

monitor.

Drywell floor drain

samples

were taken but were inconclusive in identifying the cause of the

leakage.

The licensee

developed

a plan which included increased

monitoring of the floor drain. inleakage,

drywell'tmosphere

monitoring,

and altering, the operation of various

equipment located in the drywell.

The

RCIC inboard

steam

supply valve,

2-FCV-71-2,

was backseated

in

accordance

TI-317 because it has

been the source of increased

drywell

leakage

in the past.

However, in this case, it had

no appreciable

affect

on the leakage rate.

The speed of each reactor recirculation

pump was also varied, to determine if the leakage

could

be associated

with the seals,

but no noticeable

decrease

in leakage

was noted.

Because

the leakage

was causing

the

CAN to be in constant

alarm the

alarm setpoint

was raised

corresponding

to the increased

background

rate.

The licensee

performed .this in accordance

2-TI-24, Determination

Of Hain Steam Line And .Primary Containment

Leak Detection Radiation

Monitors Alarm And Trip Setpoints.

The inspector

noted that the

indicated reading of the

CAN was approximately

2E-9 microcuries/cc

and

the alarm setpoint

was

1. 18E-8 microcuries/cc.

This results in the

setpoint

being significantly greater

than three times the average full

power reading.

Technical Specification Table 3.2.E., requires that the

setpoint for the drywell air sampling

system

be set at three times

average

background.

The'ns'pector.

was unable to determine if the method

being

used

by the licensee

to establish

the alarm setpoint

was in

accordance

with this requirement.

The inspectors

noted that the

CAHs

have alarmed in the past

when drywell inleakage

has increased

and appear

to be performing their function.

This item is addressed

as Unresolved

Item 260,296/96-01-02,

Drywell

CAM. Setpoint Determination

Method,

pending

NRC review of the licensee's

alarm setpoint

procedure

and its

compliance with the Technical Specification.

20

4.4

REVIEW OF

OPEN

ITEHS

4.4.1

(CLOSED)

VIO 260/94-01-06,

APPENDIX R DESIGN

ERRORS

The first example resulted

from a licensee

determination that in fire

area

16 and fire zone 2-4,

power supply cables for redundant

RWCU valves

were not adequately

protected .nor separated

as required

by 10 CFR 50

Appendix R.

A second

example

concerned

cables

associated

with the

1D

Raw Cooling Water

pump which were not adequately

separated

from the

4Kv

Shutdown

Board A. It was determined that,a fault in the

Raw Cooling

Water

pump could propagate

to the shutdown

board

and

damage other

equipment required during

an Appendix

R event.

The licensee

responded

in correspondence

dated April 13,

1994.

Upon discovery of these

conditions,

the licensee initiated firewatch coverage

in the affected

areas.

Long term correcti.ve actions for the first example

include the

modification of the

RWCU system to install

an additional valve which

will isolate

upon detecting

a high coolant temperature

downstream of the

non-regenative

heat exchangers.

This will preclude

damage to the low

pressure

RWCU piping and subsequent

loss of reactor inventory.

DCN

W27992A is the controlling document for this modification which is

scheduled

to be installed during the upcoming cycle 8 refueling outage.

The inspectors

reviewed this modification, which was installed

on

Unit 3 prior to restart,

and found that it satisfied the concerns

identified in the violation.

The Appendix

R Safe

Shutdown

program

has

been modified for Unit 3 and will be similarly revised to incorporate

the Unit 2 modification.

Long term corrective actions for the second

example

included the installation of isolation fuses to isolate the

faulted cable

from the shutdown

board,

thus pres'erving the shutdown

board for use

by Appendix

R equipment.

This modification was installed

by

DCN T28107A.

The inspector

reviewed the applicable plant drawing

and'erified

it had

been appropriately revised to include the

new fuses.

The inspector verified the proper size fuses

were installed in the field

and were properly labelled.

Based

on this inspection, this violation is

closed.

4.4.2

(CLOSED) THI '296/II.F.2.4,

INSTRUHENTATION FOR DETECTION OF

INADE(UATE

CORE

COOLING

This THI item addressed

the need for additional instrumentation/controls

to supplement/take

the place of existing instrumentation to provide

an,

unambiguous

indication of inadequate

core cooling.

This was performed

by replacing reactor water level sensing lines, installing Rosemount

analog transmitters

and analog trip units.

The design

changes

performed

on Unit 3 were essentially

a duplication of those

performed for the

recovery of Unit 2.

This item remained

open following the restart of

Unit 3 in order that final post modification testing could be performed

on the subject instrumentation.

(A partial

review of this item had been

performed during the recovery effort and was documented

in IR 95-16).

The licensee

performed this testing,

in accordance

with 3-TI-149

(Reactor Water Level Heasurement),

during the power ascension

of Unit 3.

This inspection effort focused

on the review of the TI-149 results.

The

inspector's

review of the testing results

indicated that the reactor

21

water level instrumentation

accurately

tracked the reactor water level

from low power conditions

up to and including rated

power.

Based

on

this review, this item is closed for Unit 3.

No violations or deviations

were identified.

5.0

5.1

5.2

PLANT SUPPORT

(71750)

ROUTINE SECURITY OBSERVATIONS;

WALKDOWN OF

PROTECTED

AREA FENCE

The inspectors

performed

a walkdown of the protected

area fence.

The

fence

was verified to be in good .condition with no holes in the fence

fabric nor any loose fence posts.

However, the inspectors

noted that

the northern portion of,the protected

area

fence line, due to

construction

work in the area,

was in need of ground strapping repair.

One section of intrusion monitoring was also out of service for ground

repair.

It was the inspector's

understanding

that such repairs

are

scheduled

to be completed

in the near-term.

The inspectors verified the

appropriate

compensatory

action

was taken

and the area

adequately

protected.

The inspectors

observed

personnel

and packages

entering the

protected

area

and verified they were searched

either by special

purpose

detectors

or physical

patdown.

ALARA POST-JOB

REPORTS

On November 29,

1995, during

a routine walkdown of the refuel'ing floor,

an inspector observed, removal of items from the Unit 3 Spent

Fuel

Pool

(SFP).

One item removed

was

a vacuum hose which had

been

used to remove

cavity debris during drain-down for vessel

reassembly.

Some debris

included stellite/cobalt particles

found from control rod ball bearing

replacement

work. Initial plans included;

removal of the hose

from the

SFP,

placement of the assembly into plastic bags, further placement

in a

transfer cart,

and final transport of the

hose to

a shielded

box located

at the Unit

1 end of the refuel floor.

After the hose

was removed,

water was,drained

and the hose

was bagged.

Initial survey readings of

about

2 R/hr contact

(0.5 R/hr whole body) were observed;

however,

during transport,

more whter drained out of the assembly

and into the

bag

and dose rates

increased

to about

12 R/hr contact

(3 R/hr whole

body).

The hose

was quickly placed into the shielded

box; however,

rates

continued to increase

and readings

outside the box read

about

6

R/hr contact

(2 R/hr whole body).

An on-the-spot decision

was

made

by

the job. coordinator to remove the hose

from the box and immediately

place it back into the:SFP.

The inspector

noted that

ALARA post-job

"lessons

learned."

included considerations

for better shielding

and

better anticipation of expected

doses

outside of shielded containers.

As

a follow-up to the above observations,

an inspector also reviewed

PER

¹951852A.

On December

8,

1995, during

2A

RWCU pump work, maintenance

personnel

encountered

contamination/radiation

levels higher than

previously experi'enced.

Thr'ee individuals were contaminated

and

one

exceeded

his administratively, permissible, dose.

In explanations

detailing the issues, it was explained that the transport cart used to

22

ferry the

pump from the

pump room to the decon

chamber

was inadequate

because little shielding

was built into the cart.

The inspectors

noted

that there

was

a statement

that "this deficiency (had)

been

noted

on

previous post-job reports but (was) never rectified".

From their review of the

ALARA post-job reports,

the inspectors

concluded that it was not clear that the licensee

was using information

provided by the workers.

The inspectors

noted that workers

had

made

apparently

reasonable

recommendations

for dose reduction but it was not

clear that management

had reviewed the information for application to

future jobs.

The above described specific issues

were discussed

with

management

as examples of how better

ALARA post-job "lessons

learned"

follow-up may have helped to reduce

exposures.

Management

acknowledged

that improved use of such information may have

been beneficial

and

immediately reviewed the specific issues of concern

and initiated

changes

to improve the timeliness of post job reviews.

5.3

POST-ACCIDENT SAMPLING SYSTEM (PASS)

ACTIVITIES (UNIT 3)

On January

23,

1996,

an inspector

observed

PASS gas sampling activities.

BFN technical

personnel

performed this activity in accordance

with 3-TI-

331,

Post Accident Sampling Procedure,

Revision

1, Appendix D,

PASS

Gas

Atmosphere

Sampling.

The inspector noted the following:

Throughout

PASS panel

setup

and sampling activities,

many

"individual steps"

consisted of both conditional

phrases

&

substeps,

which is inconsistent with the guidelines of SSP 2.2,

Writing Procedures.

For example

Step 7.2.3 stated:

"Ensure the LI(UID PRESSURE

INDR, 3-PI-043-7661,

is reading less

than

150 psig.

If the pressure

reading is elevated,

THEN STOP .the

PASS setup,

NOTIFY. the Chemistry Shift Supervisor

and the Shift

Operations

Supervisor,

and

SUBMIT appropriate priority work

request.

(Sampling

may continue with Shift Operations

Supervisor

approval.)"

Step 7.2.9,

presented

information which confused the technicians:

"IF there

has

been

a PCIS Group

6 isolation,

THEN N/A Step 7.2. 10,

CONTACT the Unit Operator,

and

RE(VEST the following valve

operations

(handswitches

are located

on Panels 9-54 and 9-55).

Otherwise,

N/A this step."

PASS panel labeling consists of both "old" and

"new" system

numbering labels which could confuse,

rather than help, the

technicians

in determining which valve, or which controller,

should

be operated.

The Unit 3

PASS panel

has the

same green color,, label,ing

and

overall lay-out as Unit 2. This presents

a potential for wrong

unit/system operation

which would be conceivable

in accident

situations.

<<i

4

al,

ijg;i

23

TI-331 calls for good communications with control

board operators.

This can

be accomplished

by use of either in-plant telephones

or

radios.

,However,

due to high noise levels in the area,

both

telephones

and radios

may prove to be difficult to 'use for clear

communications.

The Unit 3

PASS panel

does not have

a nearby

telephone

and both Unit 2 and Unit 3 panels lack adequate

sound

insulation ("Hear-Here" ) booths

near the panels.

During a previously observed

PASS sampling activity (IR 50-296/95-16),

a

NRC inspector

had noted several

deficiencies.

Improvement

was

observed

in the recent

sampl'e.

The following compares

issues

found in

1995

and recently observed activities:

Februar

1995 Issue

Januar

1996 Activities

Over looked procedure

steps result in

in an incorrect flowpath.

Detector calibration stickers

had incorrect calibration dates.

Questions

on whether or not

radiation meters energized/operating.

Technician's

local procedure

did not

match remote (operation's)

procedure.

No requirement within instruction to

secure

PASS line-up after sample.

No procedure

steps

were missed

and

the flowpath selected

was correct.

Labeling was noted

as correct.

Indicators functioned

as designed.

Local procedure

was identical to

the remote procedure.

TI-331 called for correct alignment

and technicians

returned line-up to

"as found" condition.

Insufficient questioning attitude

on the part of the workers involved

in the activity.

An adequate

questioning attitude

was

observed

by the inspector.

The sample

was subsequently

analyzed;

however,

due to an apparent

PASS

check valve problem,

(See

paragraph

3. 1 of this report).

High oxygen

levels were detected

and the sample results

were unsatisfactory.

On

January

26,

1996,

using procedure

TI-331, another

sample

was collected

and analyzed.

and satisfactory results

were obtained.

The inspector

concluded that

PASS procedure,

3-TI-331, while adequate for

obtaining/analyzing

gas

samples,

could

be improved.

The technicians

and

job foreman

appeared

knowledgeable with procedure

contents

and

methodologies for obtaining samples

and the inspector

found these

activities to be satisfactory.

5.4

RADIOLOGICAL CONTROLS;

REQUIRED POSTINGS

UNITS 1,

2 AND 3

On January

29,

1996,

an inspector,

during routine plant walkdowns,

examined various field postings for their compliance with BFN procedure

RCI-1. I, Standardized

Radiological

Postings,

BFN procedure

RCI-17.,

Control of High Radiation Areas

and Very High Radiation Areas,

and

Vt'N,

10 CFR 20 requirements.

The inspector noted the following:

Unit 2, East

RHR Heat Exchanger

Bay - A "High Radiological

Area"

sign is posted;

however,

the posting did not display probable

area

dose rates.

Unit 2, Pressure

Suppression

Chamber Water Tank Area

Same

comments

as East

RHR Heat Exchanger

Bay.

Unit 2,

East

and West scram discharge

volume cage

areas

and

walkways

A "Radiation Area" sign is posted:

however,

the posting

did not address

probable

area

dose rates.

Units 1,

2 and

3 Refueling Floor - Some areas of the refueling

floor, which clearly contain radioactive material,

are marked

"Radiological Area"; i.e.,

area

around

Vessel

Head Lifting Device

and storage barrels located at the Unit

1 end of the refuel floor.

However., similar areas; i.e., the Unit

1 pit area which contains

radioactive material, is simply marked "Radioactive Material

Area".

The inspector

found that the plant postings

were in compliance with

guidance

contained within the licensee

procedures

and

10 CFR 20.

Overall, plant radiological .postings

are adequate

and meet regulatory

requirements.

No violations or deviations

were identified.

6.0

Review of UFSAR Commitments

A recent discovery of a licensee

operating their facility in a manner

contrary to the Updated Final Safety Analysis Report

(UFSAR) description

highlighted the need for a special

focused review that compares

plant

practices,

procedures

and/or parameters

to the

UFSAR descriptions.

During

a portion of the inspection period (February 1-3,

1996) the

inspectors

reviewed the applicable sections of the

UFSAR that related to

the inspection

areas

discussed

in this report.

7.0

EXIT

The inspection

scope

and findings were summarized

on February

2,

1996,

by L. Wert with those

persons

indicated in paragraph l.

Interim exits-

were conducted

on January

12,

1996 and February

1,

1996.

The inspectors

described

the areas

inspected

and discussed

in detail the inspection

results.

A listing of inspection findings is provided.

During one of

the interim exits,

the issue involving the

STAR Program

was discussed

with senior plant management,

and the inspectors

were informed that when

the

STAR Program

was initially started

at Browns Ferry, strong

emphasis

was stressed

on its use.

However, since that time the emphasis

has not

been stressed

as effectively as it could have been.

Proprietary

<0

25

information is not contained

in this report.

Dissenting

comments

were

not received

from the licensee.

Item Number

VIO 296/96-01-01

Status

Open

Descri tion and Reference

Core Thermal

Power Above

Licensed Condition Maximum,

paragraph

2.2

URI 260/96-01-02

Open

Drywell

CAM Setpoint

Determination

Method,

paragraph

4.3

VIO 260/94-24-02

Closed

Failure To Follow Procedures,

paragraph

2.6.1

. VIO 259,

260, 296/94-17-01

Closed

Instrument

Cal ibrati on

Deficiencies,

paragraph

3.5. 1

VIO 260/94-01;06

Closed

Appendix

R Design Errors,

paragraph

4.4. 1

THI 296/II.F-.2.4

Cl osed

Instrumentation for Detection

of Inadequate

Core Cooling,

paragraph

4.4.2

8.0

ACRONYHS

ALARA

ASOS

BFN

BWR

CAN

CAQ

CFR

CR

DCN

ECCS

EDG

FHE

FSAR

GE

HPCI

INPO

IPE

IR

JB

HWe

HWt

NA&L

NRC

As Low As Reasonably

Ach'ievable

Assistant .Shift Operations

Supervisor

Browns Ferry Nuclear Plant

Boiling Water Reactor

Continuous Air Monitor

Condition Adverse to Quality

Code of Federal

Regulations

Control

Room

Design

Change Notice

Emergency

Core Cooling System

Emergency Diesel

Generator

Foreign Material Exclusion

Final Safety Analysis Report

General

Electric

High Pressure

Coolant Injection

Institute for Nuclear

Power Operations

Individual Plant Evaluation

Inspection

Report

Junction

Box

Megawatts-Electrical

Megawatts-Thermal

Nuclear Assurance

and Licensing

Nuclear Regulatory

Commission

VN'<lf

PASS

PDR:

PER

PM

'PMT

R/hr

RCIC

RHR'HRSW

RWCU

SBGT

SF.P

SI

SPDS

'SOS

SSP

STAR

T,I

TS'VA.

UNID

URI

V,IO

WO 26

Post Accident Sampling System

Public Document

Room

Problem~Evaluation

Report

Preventive .Maintenance

Post Modification Testing

REM per hour

.Reactor

Core Isolation Cooling

Residual

Heat

Removal.

Residual

Heat. Removal Service Water

Reactor 'Water

Cleanup

Standby

Gas Treatment

Spent

Fuel

Pool'urveillance Instruction

Safety

Parameter.

Display System

Shift Operation. Supervisor

Site Standard

Practices

Stop, Think, Act, and Review

Technical

Instruction

Technical Specifications

Tennessee

Valley Authority

Unique Equipment Identification

Unresolved

Item

Violation .

Work Order

cN