ML18037A629

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Insp Repts 50-259/93-39,50-260/93-39 & 50-296/93-39 on 931016-1119.Violations Noted.Major Areas Inspected: Surveillance Observation,Design Changes,Plant Modifications, Reportable Occurrences & Site Organization
ML18037A629
Person / Time
Site: Browns Ferry  
Issue date: 12/09/1993
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18037A627 List:
References
50-259-93-39, 50-260-93-39, 50-296-93-39, NUDOCS 9401040132
Download: ML18037A629 (37)


See also: IR 05000259/1993039

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 30323-0199

Report Nos.:

50-259/93-39,

50-260/93-39,

and 50-296/93-39

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Harket Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection at Browns Ferry Site near Decatur,

Alabama

Inspection

Conducted:

October

16 November

19,

1993

r

0

Inspector:

> r

ess

n

nspector

z,

v

ate

sgne

Accompanied

by:

J.

Hunday,

Resident

Inspector

R. Husser,

Resident

Inspector

G. Schnebli,

Resident

Inspector

L. Watson,

Project Engineer

Approved by:

a

.

e

Re ctor

c s, Section

4A

Division of R actor Projects

SUHHARY

a e

1gne

Scope:

This routine resident

inspection

included surveillance

observation,

maintenance

observation,

operational

safety

verification, design

changes

and plant modifications, Unit 3

restart activities, reportable

occurrences,

action

on previous

inspection findings, site organization,

and independent

safety

engineering

'group.

One hour of backshift coverage

was routinely worked during the

work week.

Deep backshift inspections

were conducted

on October

17,

30 and

November 7,

14,

18,

and

19,

1993.

9401040i32

931217

PDR

ADOCK 05000259

8

PDR

Unit two operated

continuously during this period

and was on-line

for 169 days at the 'end of the period,

paragraph

4.

A plant trip

was possibly avoided during work on the condensate

demineralizers

due to a design

change

made under the scram frequency reduction

. program.

The change modified the timing of the feed

pump

and feed

booster

pump suction trips.

Efforts such

as this have contributed

to the continuous

run time of the unit.

One violation with two examples for failure to control design

changes

was identified by an

NRC inspector,

paragraphs

5 and 6.

The first example

was for failure to adequately

review a design

change after control

room drawings were issued to reflect

identification number changes

for fuses,

handswitches,

and other.

components.

Plant operating instructions

and labeling were not

changed to agree with the drawings.

Although, the problem was

identified on system 31, air-conditioning system,

the problem is

applicable to several

other systems

being renumbered.

The

licensee's

quality assessment

of fuse labeling

came to an

erroneous

conclusion that labeling was adequate.-

The second

example involved failure to adequately

control coordination of a

design

change that modified the unit separation

boundary but the

required configuration boundaries

were not modified.

These

examples

are indication of a programmatic

problem with the

coordination of design

changes

between

engineering,

operations,

technical

support,

and other groups.

An unresolved

item was identified by an

NRC inspector for an

potentially inadequate

safe

shutdown procedure revision,

paragraph

4.

The licensee

on November 3,

1993,

made

112 changes

to the fire

protection safe

shutdown

equipment

compensatory

measures.

This

plan was approved

by the

NRC April 1,

1993.

These

changes

were

made without Commission

approval

although there is

a potential to

adversely affect the ability to achieve

and maintain safe

shutdown

in the event of a fire.

Characteristic

of these

changes

was

revising

a requirement to isolate the reactor water cleanup

system,

based

on controlling the loss of water inventory, .to

permitting the establishment

of a fire watch after seven

days.

The licensee

made these

changes after electrical

cables to the

reactor water cleanup

system isolation valves were identified as

being routed through the

same fire zone.

An inspector followup item was identified by an

NRC inspector

concerning

acceptance

criteria for the analog trip units,

paragraph

4.

There is no limit specified for the difference

between

main steam line flow differential pressure

readings.

An unresolved

item was identified by an-NRC inspector

concerning

the observation of an unfinished conduit modification, paragraph

5.

A cable

was not secured

in a cable tray as required,

a field

change notice was not incorporated into a work plan that was

closed,

and conduit covers were not installed although indicated

as completed in the work plan.

These

changes

occurred

about three

years

ago when unqualified cables

were replaced,

but has

gone

undetected until this time.

~,

Persons

Contacted

Licensee

Employees:

REPORT DETAILS

  • 0. Zeringue,

Vice President

  • R. Hachon,

Plant Manager

  • J. Rupert,

Engineering

and Modifications Manager

  • T. Shriver, Licensing

and guality Assurance

Manager

D. Nye, Recovery Manager

  • E. Preston,

Operations

Manager

  • J. Haddox,

Engineering

Manager

M. Bajestani,

Technical

Support

Manager

A. Sorrell, Chemistry

and Radiological Controls Manager

C. Crane,

Maintenance

Manager

+P. Salas,

Licensing Manager

  • R. Wells, Compliance

Manager

J.

Corey, Radiological

Control Manager

J. Brazell, Site Security Manager

Other-licensee

employees

or contractors

contacted

included licensed

reactor operators,

auxiliary operators,

craftsmen,

technicians,

'and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

2.

P. Kellogg, Section Chief

  • C. Patterson,

Senior Resident

Inspector

  • J. Munday, Resident

Inspector

  • R. Musser,

Resident

Inspector

G. Schnebli,

Resident

Inspector

L. Watson,

Project Engineer

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Surveillance Observation

(61726)

The inspectors

observed

and/or reviewed the performance of required SIs.

The inspections

included reviews of the SIs for technical

adequacy

and

conformance to TS, verification of test instrument calibration,

observations

of the conduct of testing,

confirmation of proper. removal

from service

and return to service of systems,

and reviews of test data.

The inspectors

also verified that

LCOs were met, testing

was

accomplished

by qualified personnel,

and the SIs were completed within

the required frequency.

The following SIs were reviewed-during this

reporting period:

a.

2-SI-4.7.A.3.b,

Suppression

Chamber

Reactor Building Vacuum

Breaker Cycling

b.

On October 22,

1993, the inspector

observed

the performance of 2-

SI-4.7.A.3.b,

Suppression

Chamber

Reactor Building Vacuum

Breaker Cycling.

This SI demonstrates

the operability of the two

Reactor Building to Suppression

Chamber

Vacuum Breakers

by cycling

the valves

(vacuum breakers)

and insuring that less force than the

maximum equivalent

dp specified in the

TS is utilized when

unseating

the valves.

In addition, the vacuum breakers

were

tested for freedom of motion as well as inspecting the internals

for debris

and foreign material.

Personnel

performing the testing

utilized a current revision of the SI and demonstrated

the proper

technique for independent verification.

No deficiencies

were

noted

by the inspector.

2-SI-4.5.B. I.d(II), quarterly

RHR System

Rated

Flow Test

Loop II

On October

29,

1993, the licensee

performed 2-SI-4.5.B.l.d(II),

quarterly

RHR System

Rated

Flow Test

Loop II as

a routine

surveillance required

by TS.

The surveillance

was completed

satisfactorily.

The inspector reviewed the completed

procedure

and verified the plant conditions were acceptable for performing

the test,

the acceptance

criteria were met, the test equipment

was

appropriate,

and the system

was returned to the standby lineup.

No deficiencies

were noted

by the inspector.

No violations or deviations

were identified in the Surveillance

Observation

area.

3.

Maintenance

Observation

(62703)

Plant maintenance activities were observed

and/or reviewed for selected

safety-related

systems

and components

to ascertain

that they were

conducted

in accordance

with requirements.

The following items were

considered

during these

reviews:

LCOs maintained,

use of approved

procedures,

functional testing and/or calibrations

were performed prior

to returning components

or systems

to service,

gC records maintained,

activities accomplished

by qualified personnel,

use of properly

certified parts

and materials,

proper

use of clearance

procedures,

and

implementation of radiological controls

as required.

Work documents

were reviewed to determine

the status of outstanding jobs

and to assure that priority was assigned

to safety-related

equipment

maintenance

which might affect plant safety.

The inspectors

observed

the following maintenance activity during this reporting period:

On November 9,

1993, the inspector

observed

maintenance activities

associated

with

WO 93-14450-00,

which was written to backfill the

reference

leg for the 2-LT-3-60,

an

A channel

instrument.

Operations

had previously identified that this instrument

was indicating,.

approximately

one inch higher than the instruments

in 8 channel.

The

inspector verified the prerequisites

were met and that the technicians

had the appropriate

approvals to begin work.

Operations

entered

the

applicable

LCOs and the reference

leg was backfilled without incident.

Following completion of the work, the instrument indicated approximately

one

and one-half inches lower than the

B channel.

Engineering stated

that this was expected

due to the difference in elevations

between the

condensing

pots.

The inspector will continue to follow activities in

this area.

No violations or deviations

were identified in the Maintenance

Observation

area.

Operational. Safety Verification (71707)

The

NRC inspectors

followed the overall plant status

and any significant

safety matters related to plant operations.

Daily discussions

were held

with plant management

and various

members of the plant operating staff.

The inspectors

made routine visits to the control rooms.

Inspection

observations

included instrument readings,

setpoints

and recordings,

status of operating

systems,

status

and alignments of emergency

standby

systems,

verification of onsite

and offsite power supplies,

emergency

power

sources

available for automatic operation,

the purpose of

temporary tags

on equipment controls

and switches,

annunciator

alarm

status,

adherence

to procedures,

adherence

to LCOs, nuclear instruments

operability,

te'mporary alterations

in effect, daily journals

and logs,

stack monitor recorder traces,

and control

room manning.

This

inspection activity also included numerous

informal discussions

with-

operators

and supervisors.

General

plant tours were conducted.

Portions of the turbine buildings,

each reactor building,

and general

plant areas

were visited.

Observations

included valve position

and system alignment,

snubber

and

hanger conditions,

containment isolation alignments,

instrument

readings,

housekeeping,

power supply and breaker alignments,

radiation

and contaminated

area controls,

tag controls

on equipment,

work

activities in progress,

and radiological protection controls.

Informal

discussions

were held with selected

plant personnel

in their functional

areas

during these tours.

a ~

Unit Status

b.

Unit 2 operated

continuously during this period without any

significant problem.

The unit was on-line for 169 days at the end

of the period.

Unit 2/3 Separation

Clearances

The Unit 3 electrical distribution system currently has

operational restrictions required to allow operation of Unit 2.

The restrictions

are

a result of unresolved

engineering

concerns

involving Appendix R, station blackout,

equipment qualification,

or, electrical separation/isolation

capabilities.

These

restrictions

are controlled by clearances,

caution orders,

and

operating instructions.

They, in turn, reference

the electrical

distribution system one-line drawings which use notes to restrict

breaker closure.

The inspector reviewed portions of clearances

3-

91-095,

3-91-096,

0-91-353,

and 0-91-362 which were issued to

prevent Unit

1 and

3 components

from affecting Unit 2 operation.

These clearances

contain components restricted

by engineering

holds

and other components

tagged for convenience.

This could

include entire systems that are tagged which are currently not

needed,

rather than spending

resources

to identify portions of

systems that do need to be tagged.

Boundary isolation points

tagged

by these

clearances

may be untagged for a period not

exceeding forty-five days provided it is approved

by Technical

Support,

Operations,

and if an engineering

hold exists,

by Site

Engineering.

If the component

needs to be removed from the

'learance

for a period exceeding forty-five days,

the Unit

interface drawings depicting these

components

is to be revised to

indicate the new position.

During this inspection the inspector

noted

changes

to the clearance

boundary which exceeded this time

requirement.

This was discussed

with operations

management

and

the discrepancy

was adequately

resolved.

RWCU Appendix

R Safe

Shutdown

Procedure

Concerns

On October 28,

1993,

Engineering determined that

a calculation

used erroneous

cable routing information to determine the impact

of an Appendix

R fire on the

RWCU system.

The calculation

assumed

that the

RWCU system

was unaffected to the extent that the system

could be isolated

by one of two isolation valves in the event of

an Appendix

R fire.

However, it was not recognized that the

isolation capability was not available for fires occurring in fire

zone 2-4.and fire area

16. 'uring

a review of the calculation it

was discovered that the cables to the isolation valves traverse

these

areas

and therefore the system is not assured

of being able

to be isolated

as required.

As a result of this finding,

Engineering initiated

PER 93-0145.

On October 29,

1993, roving

fire watches

were established

in fire zone 2-4 and fire area

16,

as compensatory

measures

due to this condition.

On November 2,

1993, the inspector questioned

why the licensee

did not take

compensatory

measure

A for the two valves,

as described

in the

Appendix

R SSP.

Compensatory

measure

A required that action

be

taken in accordance

with the

TS referenced for that particular

component,

which in this case,

was to isolate the system

by

shutting the two affected valves within four hours.

Additionally

on November 2,

1993,

an Engineering

walkdown verified that the

cables for the two valves in fire zone 2-4 were located adjacent

to each other

and

as such could not be relied

on during

a fire in

this area.

On November

3,

1993, the Appendix

R SSP

was revised to

allow the option of taking compensatory

measure

A or

B for the

one-hundred-twelve

items previously requiring only compensatory

measure

A.

Compensatory

measure

B requires that the Appendix

R

function of the equipment

be restored

in seven

days or an

equivalent

shutdown capability be provided,

which is typically

satisfied

by establ.ishing

a fire watch in the affected

areas.

TS 6.8. 1. 1 requires that written procedures

shall

be established,

and maintained covering the fire protection program

implementation.

In addition, license condition

14 of the Unit 2

operating license states that changes to the fire protection

program can

be made without approval of the

NRC provided the

ability to achieve

and maintain safe

shutdown is not adversely

affected

by a fire.

The

SSP revision approved

on November 3,

1993,

changed

the fire protection program in such

a way as to

potentially adversely affect the ability of the plant to achieve

and maintain safe

shutdown, without first gaining prior approval

from the

NRC.

The licensee

indicated that additional

information

was being identified on this subject

and requested

a meeting to

discuss this information.

This item is unresolved

pending the

outcome of a meeting

on the subject

and is identified as

URI

260/93-39-01.

In addition,

on November 4,

1993, the inspector

questioned

why the licensee

did not establish

a continuous fire

watch in the cable spreading

room of fire area

16 as required

by

the

SSP.

The licensee

stated that

a continuous fire watch should

be established

and corrected

the problem.

Drywell Control Air Dewpoint

Hoisture sensors

which provide

a control

room alarm upon sehsing

high moisture content in the drywell control air system

have

been

proven to be unreliable.

As a compensatory

measure,

TACF 2-93-01-

32 was written to facilitate the installation of a portable

dewpoint hygrometer

on the

2B control air receiver

tank to allow

periodic monitoring of the dewpoint temperature.

The safety

assessment

for all TACF states

that

upon receipt of the high

moisture alarm, Operations

personnel will valve in the dewpoint

hygrometer

and verify that

an acceptable

dewpoint is obtained.

The inspector questioned

two UOs and two ASOSs about the actions

to be taken

upon receipt of this alarm.

None of the operators

were aware that specific action needed to be taken in accordance

with the

TACF.

This weakness

was discussed

with operations

management

who felt it prudent to revise the

ARP to include the

appropriate

actions.

Unit Operator

Instrument

Checks

and Observations

While reviewing the Unit 2 unit operator

instrument checklist,

the

inspector noted that the main steam line flow, indicated

as

a dp

on ATUs, differed by as

much as nine psid between

steam lines.

Each

steam line has

one flow element which feeds four

transmitters.

The operator records

the dp from each

ATU and

compares

the values with the others.

When questioned

as to what

would be considered

an unacceptable

comparison,

the unit. operator

did not know.

He stated that there

was

no acceptance

criteria

assoc'i.ated

with the comparison.

This instrument

check,

performed

6

once per day to satisfy the requirements 'of TS 4.2.A, is defined

by. TS as

a qualitative determination of acceptable

operability by

observation of instrument behavior

and shall include

a comparison

with other instruments

measuring

the

same variable.

Operations

management

concluded that there

was

no requirement to define the

acceptance

criteria of an instrument

check in terms of allowable

differences

between

instruments

measuring

the

same parameter.

However, the licensee

plans

on collecting information from other

utilities concerning this and possibly revising their procedures

to better define acceptable

comparisons.

Pending resolution, this

item will be tracked

as IFI 260/93-39-02,

Acceptance Criteria For

Instrument

Comparison Surveillances.

REX System Failure

On November 2,

1993, the inspector experienced

problems with the

licensee's

REX system.

This system is

a computerized

exposure

tracking system for personnel

working under

a radiological work

permit.

The licensee

requires that personnel

have

a briefing on

the system

use prior to entry on

an

RWP.

In the morning, the

inspector entered

the

RCA on the general

access

RWP for a tour of

the reactor building.

After one hour, the inspector exited,

signing off the

RWP using the computer.

The inspector

noted that

the dose received

was zero although

one or more

HR was expected

after being in the reactor building for over an hour.

Later, in the afternoon the inspector

attempted to use the

REX

system

again for entry into the reactor building.

The computer

initially stated that entry was denied

and

a briefing was required

for entry.

A health physics technician assisted

the inspector

and

the computer indicated that

an exit entry had not been received.

The i'nspector questioned this

and noted several

rows of other

people

were in line waiting to enter the

RCA because

of similar

problems.

The inspector discussed

the systems's

apparent

problems

with a radiological controls supervisor.

Reliability of the

REX

system will be monitored

by the inspector.

Housekeeping

On November 2,

1993, during

a routine tour of the Unit 2 reactor

building the inspector

observed

several

large loose pieces of

insulation

on top of some

HVAC ducting.

The ducting was near the

overhead of this floor elevation but appeared

to be at location

for some time due to the collection of dust

and dirt around the

insulation.

On November 4,

1993, during

a routine tour of the Unit I and

2

diesel

generator

building the inspector noticed that the general

cleanliness

of the rooms

had deteriorated

somewhat.

The rooms are

normally clean.

The rooms were dusty

and

a large

number of spider

webs

had accumulated

in the area.

These

issues

were discussed

with plant management

on November

5,

1993.

Scram Reduction Efforts

On October

13,

1993, at-6:10 a.m., the Unit 2 Condensate

Demineralizer

System

bypassed

when returning demineralizer

H to

service.

This was apparently

caused

by the "E" valve on the "B"

demineralizer sticking closed

and then fully opening quickly at

the

same time the "H" demineralizer

was being placed in service.

The demineralizers

were restored to normal

and

no plant transients

were observed.

Work request

C232341

had

been previously submitted

on the "B" demineralizer for the failure of the "E" valve to

respond properly to its air signal.

The valve was subsequently

adjusted

and the work order closed out later that

same day.

Discussions with operations

personnel

indicated that had this

transient

occurred in the past it might have resulted

in a plant

trip.

However,

due to the efforts of the Scram Frequency

Reduction

Team, modifications

had

been

accomplished

to this system

that reduced

the possibility of a trip for this event.

The

recommendation

made

by the

SFRT was to stagger

the

RFPs

and the

CBPs low suction pressure trips such that all the RFP's did not

trip at the

same point'nd all the CBP's did not trip as the

same

point.

This was to be accomplished

by varying the setpoints

or

varying the time delays of the

pump trip circuitry.

By varying

one of these

parameters

a low pressure

pulse would not trip either

all the RFP's or all the CBP's.

Therefore,

loss of a single train

might allow pressure

to build back up to prevent -tripping the

other trains,

thus preventing

a loss of all feedwater.

This

modification was

implemented

by

DCN

W 16281A which was completed

in May 1991.

The inspectors

considered

the licensee's

efforts in

this area

commendable.

Cold Weather Preparation

The inspector

reviewed the licensee's

program for cold weather-

protection of equipment.

The licensee

has

an extensive

program

for identifying, establishing,

and repairing freeze protection

equipment

such

as heat tracing,

room heaters,

dampers,

and space

heaters.

Operations

completed various valve,

damper,

and door

lineups for prevention of cold weather

damage.

Maintenance

has

the responsibility of testing the equipment

and if needed

performing repairs,

and were approximately

90 percent

complete.

The freeze protection for the fire protection equipment

was

complete.

The inspector walked down various outside

areas

subject

to cold weather

damage

and verified heat tracing was established,

heaters

were operable,

and temporary protection devices

such

as

canvas

or wood shelters,

were in place.

The inspector will

continue to monitor activities in this area

as repairs

on damaged

equipment is completed.

One unresolved

item and one inspector followup item was identified in

the Operational

Safety Verification area.

Design

Changes

and Plant Modifications (37700)

Program

Review

The inspector

reviewed

changes

to the plant design

change

and

modification process.

The licensee

has replaced

BP 205,

Issue

Management,

which described

the design

issue origination process,

with BP 312,

BFN Scope Control Process.

BP 312 establishes

the PID

process.

Any nuclear

power individual can initiate a PID.

Primary

responsibilities for initial review and tracking have

been divided

between the

SNM, the

ICPN,

and the Site Controller.

The

SNN is

responsible for tracking planning items, developing

a

BFN Long

Range

Plan

and preparing

a Fiscal

Year Project List.

The

ICPM

develops

scope of work and cost benefit information.

The Site

Controller performs resource

and funding estimates.

BP 312 also establishes

two review groups,

the

SMART and the

WCT.

The

SMART performs the review for all PIDs associated

with scope

changes

and emergent

work.

The

WCT performs the review for new

work.

The PID is reviewed

by the principal manager

and system engineer

then goes to the

SMART or

WCT for disposition.

BP 312 provides

guidance

on categorizing

and ranking the items

and defines the

managers

on the

SMART and

WCT.

The inspector reviewed the MIL of open

and closed

items

and the

inactive MIL.

Packages

of selected

NIL items which were

open

or

had

been placed

on the inactive list were reviewed to determine if

the licensee

had adequate justification for the disposition of the

.item, i.e., delaying implementation or canceling the project.

The

inspector

had

no questions

on disposition of the packages.

The inspector also reviewed portions of the following procedures

which define the design review process:

SSP 9.3, Plant Modifications and Design

Change Control,

Rev.

10

SSP 9.4, Configuration Management/Control,

Rev.

1

SSP 9.5,

Design Engineering,

Rev.

0

BFEP PI 89-06,

Design

Change Control,

Rev.

9

QDCN and

SCDN Processes

During October

1993 the licensee identified that

a containment

isolation valve had

been replaced with a valve of a different,.

design

and the Appendix J test method

had not been revised to test

for stem leakage.

This issue is discussed

in paragraph

S.d.

The

valve orientation

had

been questioned

via QDCN 23603A and the

Appendix J testing error was not identified in the

QDCN review.

The inspector reviewed the

QDCN process

described

in procedures

SSP 9.3 and

BFEP PI 89-06.

'The

QDCN is used to disposition

questions

and provide clarification of existing design output

documents

including DCNs.

The inspector selected

20 of the

75

QDCNs closed in April and Hay of 1993

(end of Unit 2 Cycle

6

refueling,outage) for review.

The inspector noted that in five of

the

QDCNs generated

by organizati.ons

other than Site Engineering,

including

QDCN 23603A, the review by the System Engineer

and the

Technical

Support Superintendent

had

been

marked

as not

applicable.

Site Standard

Practice,

Plant Hodifications

and

Design

Change Control,

Rev.

10, Section 3.2.2, requires that

QDCNs

that are not originated

by Site Engineering

be reviewed

by the

Technical

Support - System Engineer

and the Technical Support

System Engineering Supervisor.

The failure to route

QDCN 23603A

to Technical

Support for review contributed to the failure to

identify the inadequate

testing configuration for leak rate

testing of containment isolation valve 2-FCV-064-20.

Technical

Support provides Appendix J reviews.

In two of the cases

reviewed,

an

FDCN had

been

changed to a

QDCN.

In these

cases,

there

does not appear to be

a review of the need to send the

QDCNs

to Technical

Support for review.

The inspector reviewed

a sample of 20 of the

63

SCDNs generated

since October

1993.

SCDNs are

used to support documentation

changes

only.

A case

where

an

SDCN has

been

used to make

changes

in plant configuration

as discussed

in paragraph six.

The

inspector

reviewed the use of the selected

SDCN to confirm that

they were used'for documentation

changes

only.

The inspector also

sampled the documents that were changed to confirm that procedures

and drawings

had

been

updated.

No problems

were identified.

Fuses

On November 5,

1993, the inspector

compared electrical

fuse

labeling in the plant against electrical

equipment fuse tabulation

drawings.

These

are primary drawings maintained in the control

room.

Because of previous

concerns

and problems with fuse

labeling the licensee's

quality assurance

organization

conducted

an assessment

of fuse labeling Assessment

Report NQA-BF-93-154,

dated

November 2,

1993.

The assessment

team concluded that the

fuse labeling program was adequate

and effectively implemented.

The problem associated

with mislabeling of SBGT fuses

discussed

in

10

the licensee's

incident investigation,

II-B-93-034 was considered

isolated.

The inspector identified several

fuse

numbers that

had

been

changed

on drawing 2-45B721-50-10

under revision,4 dated

April 3,

1993, for

DCN S19592,

but the labeling had not been

changed

in the electrical

panel

next to the fuses.

This drawing

was

a primary drawing

and

a

CCD.

The following is

an example of

the labeling problems:

Fuse

UNID

Per Drawin

2-FU3-031-7206A

2-FU3-031'-7206B

2-FU3-031-7206C

'2-FU3-031-7207D

2-FU3-031-7208E

2-FU3-031-7209F

Fuse

As

abeled

2-FU3-031-4099B1

2-FU3-031-4099B2

2-FU3-031-4099B3

2-FU3-031-4099B4

2-FU3-031-4099B5

2-FU3-031-409986

The licensee initiated

a PER-930150 that identified an additional

six fuses with labeling different than the drawing.

The inspector

conducted

an independent

review of the

DCN S19592

and concluded that numerous other numbers

were changed

in addition

to fuse numbers.

The change

was to complete the

MEL safety system

project for system 31.

This consisted of EHS loading of the (-

list, Eg-list, I-Tabs,

Valve Tabs,

and

Fuse Tabs.

Ten pages of

fuses,

handswitches,

etc.,

were changed

by this S-DCN.

The inspector

checked

two switches listed

as being changed.

2-

XSW-31-4099A1 Appendix

R SDBR ACU NORM/ENER SM was changed to 2-

XSW-031-7205.

The inspector obtained

a copy of the system panel lineup checklist

and found the checklist

had not been

changed.

In addition, the

switches located in electrical

board

room

2B were checked

and they

were still labeled

as the checklist.

This was compared to

drawings in the control

room 2-45E2749-18

and 2-45E769-18 that

had

the

new numbers.

The inspector did not sample further but concluded that the

problem was not isolated to fuses.

The problem was with anything

changed

by the

S-DCN.

The

S-DCN that required changing of

numbering of components

on plant drawings

had not been coordinated

to have operations

or others to change plant labeling

and

procedures.

The inspector

concluded this is

a programmatic

problem with

engineering

changing drawings without adequate

coordination with

other plant organizations

to insure drawings accurately reflect

the plant configuration.

The licensee

has

done

an excellent job

in the past of issuing updated

drawings to reflect plant

modifications.

The drawings are issued prior to the system being

returned to service.

However, the reverse

has not been true.

Control

room drawings

have

been

changed to change

fuse number,

handswitch

number, etc., without the corresponding

changes

being

made in the plant or procedures.

According, this is the first example of the violation concerning

design. control.

Design control requirements

are established

by 10 CFR 50 Appendix

B Criterion III, Design Control.

This violation

will be identified as 259,

260, 296/93-39-03,

Failure to Control

Design Changes.

On November

16,

1993, the inspector discussed

these

issues with

the Engineering

and Modifications manager

and Engineering

manager.

Four systems

have

been completed for the

MEL safety system

project..

These

systems

were 18, 31,

63,

and 75.

The inspector

stressed

the importance of maintaining accurate

drawings to

reflect the plant configuration.

Containment Isolation Valve Improperly Installed

As discussed

in IR 259,

260, 296/93-36,

paragraph

4c, the licensee

discovered that CIV 2-FCV-64-20 was installed

such that its shaft

seals

were outside of the test boundary of its periodic type

C

LLRT.

Another issue related to this matter

was noted

by the

inspector during the review section 5.2.3.6

(Primary Containment

Venting and

Vacuum Relief) of the

FSAR.

This section contains

a

statement

that valves

2-FCV-64-20

and

21 (Inboard Primary

Containment Isolation Valves for the Reactor Building to Torus

Vacuum Breaker

Lines) are air-operated

and actuated

by a

differential pressure

signal that is independent of electrical

power.

However, the differential pressure

transmitters.

and

solenoid valves associated

with valves

2-FCV-64-20 and

21 are

. normally energized with electrical

power.

These matters

were

still under review at the conclusion of the last inspection period

and were tracked

as Unresolved

Item 260/93-36-01,

Containment

Isolation Valve Improperly Installed.

The licensee

concluded their review of this matter by completing

Incident Investigation II-B-93-041.

The inspectors

also completed

an independent

review of the issue.

The inspectors

have concluded

that the licensee failed to include

a

10 CFR 50 Appendix J review

in the design

process

which involved the installation of

containment isolation valves.

In not performing this review, the

licensee failed to recognize the importance of valve orientation

with regards to the

LLRT required

by TS 4.7.A.2.g.

Therefore,

the

valve (2-FCV-64-20)

was installed with its shaft seals

outside of

the test

boundary of it type

C LLRT.

One of the contributing

factors in this matter was the fact that

DCN g23608A was issued

without first being reviewed

by plant technical

support.

This

DCN

involved

a question

from the licensee's

maintenance

organization

regarding the importance of flow direction when installing CIVs 2-

12

FSV-64-17,

18,

19, 20,

and 21.

The

DCN g23608A was issued

by

plant engineering without considering

Appendix 3 testing of the

valve.

The issue of Technical

Support not reviewing g-DCNs as

required

by SSP-9.3 is further discussed

in paragraph

Sb of this

report.

During the inspectors'eview

of this issue,

the inspectors

determined that

a weakness

existed in the installation

instructions provided to the craft for the valves specified in DCN

W16880A (the original

DCN written to replace

2-FCV-64-17,

18,

19,

20,

and 21).

Simple sketches

on installation instructions

were

not included in the

DCN or WP. It appears

that

a great deal of

engineering

assistance

was required during the valves

installation.

In regards

to the inspectors

concerns that

FSAR

Section 5.2.3.6 states

that valves

2-FCV-64-20 and

21 operate

independent

of electrical

power when in fact power is required to

normally operate

the valves,

the licensee is in the process

of

changing the applicable portion of FSAR Section 5.2.3.6.

The

proposed

change is as follows; one valve is air operated

and is

.,

actuated

by a differential pressure

signal;

upon loss of

electrical

power or air, the valve will fail in the open position.

This change satisfied the inspector's

concern in this area

as the

FSAR will more closely represent

actual plant conditions.

The licensee

has determined that valve 2-FCV-64-20 will be

reoriented

and tested during the next period of cold shutdown

providing the applicable

design documentation

is completed

and

materials

are available.

These

issues will continue to be tracked

= by URI 93-36-01,

pending resolution of the valve's orientation

and

testing.

Unfinished Modification

On November 2,

1993, during

a routine tour of the Unit 2 reactor

building the inspector identified some conduit that appeared

to be

an unfinished modification.

A modifications supervisor

was

contacted

and toured the area with the inspector.

On the

mezzanine

above the clean

room at the drywell entrance

there were

two conduits with missing inspection covers.

A single cable

was

in one of the conduits but the other conduit was empty.

Also, the

cable exited the conduit into a cable tray but the cable

was

dropped

down out of the cable tray.

The licensee

researched

the problem using the conduit numbers

and

found that

an

FDCN had not been incorporated into a

WP about three

years

ago.

The licensee

generated

PER

BF 930149 to resolve this

issue.

This will be tracked

as

URI 260/93-39-04,

Unfinished

Conduit Modification, pending resolution of the issue.

>f

0

~

~

13

'4f.

Reactor Water Level

Hodification'n

Hay 28,

1993, the

NRC issued Bulletin .93-03,

(Resolution of

Issues

Related to Reactor Vessel

Mater Level Instrumentation

in

BWRs), to all licensees 'operating

BWRs.

Specifically, the

bulletin deals with a generic

concern in which noncondensible

gases

could become dissolved in the reference

leg of BWR water

level instrumentation

and lead to

a false high level indication

after

a rapid depressurization

event.

In addition to several

short term compensatory

actions,

the bulletin requested

that each

licensee

implement hardware modifications necessary

to ensure

the

level instrumentation reliability for long-term operation.

This

hardware modification was to be implemented

by all licensees

in

the next cold shutdown period after July 30,

1993.

TVA responded

to the Bulletin with a letter dated July 30,

1993,

which stated that

TVA would install

a continuous fill system which

injects

CRD water to the water level instrumentation

condensing

chambers

through reference

leg piping.

Because

Browns Ferry Unit

2 has not been in a cold shutdown condition since starting

up from

the refueling outage in June

1993

and the fact that being in this

condition is

a requisite for installation of the continuous fill

system, the'odification is not yet implemented.

In preparation

of their first period of cold shutdown during the operating cycle,

the licensee

has prepared

and issued

DCN W16435C to document this

modification.

Currently, the licensee

is installing piping,

piping supports,

cabling

and conduit to the maximum extent

possible with the unit at power in order to minimize the effort

once .the unit has

reached

cold shutdown.

The licensee

anticipates

completing this work on November 23,

1993.

Once the unit reaches

cold shutdown,

current estimates

are that modification will

require

7$ days for implementation.

The inspectors

are currently

monitoring the "pre-outage"

work and anticipate monitoring the

final implementation of the modification.

One violation was identified in the design

change

area.

6.

Unit 3 Restart Activities

(30702,

37828,

61726,

62703,

71707)

The inspector

reviewed

and observed

the licensee's activities involved

with the Unit 3 restart.

This included reviews of procedures,

post-job

activities,

and completed field work; observation of pre-job field work,

in-progress field work,

and

QA/QC activities; attendance

at restart

.

craft level, progress

meetings,

restart

program meetings,

and management

meetings;

and periodic discussions

with both TVA and contractor

personnel,

skilled craftsmen,

supervisors,

managers

and executives.

a ~

Hodification of Unit Separation

Clearance

to Support Unit 3

Condenser

Hydrostatic Test

The return to service of systems

in support of Unit 3 condenser

hydrostatic test

and other activities required that

some breakers

14

be released

from an engineering

hold.

DCN S25756A revised

one-

line drawings

based

on calculations

which altered various

operational restrictions.

These restrictions

include such things

as Appendix R, station blackout,

equipment qualification,

and

electrical

cable separation/isolation

capabilities.

For example,

3B

CRD pump usage is restricted

due to a cable separation

violation and the

HPCI pump discharge

valve, 3-FCV-74-73, is

restricted

due to battery loading concerns.

The safety

assessment

for the

DCN states that the evaluation

concluded that certain

circuit breaker operating restrictions

must

be continued and/or

revised to support continued Unit 2 operation

and Unit 3 restart.

The

DCN specifically-'isted those

components

whose

use

was still

restricted.

On October

15,

1993, while verifying the proper

positioning of the components

on the list, the inspector

identified the foll'owing discrepancies:

1)

Breaker

602 on Battery Board

2 was being controlled by a

clearance

instead of a caution order.

2)

Breaker

601

on Battery Board

3 was found closed,

however it

was required to be open.

3)

Breaker

612

on Battery Board

3 was found closed

and being

controlled by a caution order,

however it was required to be

open.

After operations

management

was informed of these discrepancies

by

the inspector,

operations

personnel

walked down all of the

equipment affected

by an engineering

hold and found approximately

two pages of needed

changes

to the clearances,

caution orders,

and

Operating Instructions controlling these

components.

Discussion

with Operations

and Site Engineering

management

indicated that

these

changes

were inappropriately

made without the review of the

operations staff.

Criterion III of 10 CFR 50 Appendix B, requires

that measures

shall

be established

for the identification and

control of design interfaces

and for coordination

among

participating design organizations.

These

measures

shall include

the establishment

of procedures

among participating design

organizations for the review, approval,

release,

distribution,

and

revision of documents

involving design interfaces.

Failure to

coordinate

the issuance

of design

documents with the resulting

changes

in plant configuration is a violation of 10 CFR 50

Appendix B, Criterion III, Design Control,

and resulted

in

misconfiguration of the plant.

This will be identified as the

second

example of VIO 259,

260, 296/93-39-03,

Failure to Control

Design

Changes.

The inspector discussed

with site management

that close monitoring

of the unit separation

boundaries

was essential

as more Unit 3

systems

are tested

and returned to service.

15

b.

Design

Chan'ges

and Plant Modifications

The inspectors

review selected

Design

Change Notice packages

associated

with plant modifications to support the Unit 3 recovery

effort.

The

DCN work packages

were reviewed

and work in progress

was observed to:

ensure that the

DCN packages

were properly

reviewed

and approved

by the appropriate

organizations

in

accordance

with the licensees

administrative controls; verify the

adequacy of the

10 CFR 50.59 evaluations

performed

and that the

appropriate

FSAR revisions

were planned or completed, if

applicable;

ensure that the applicable plant operating

procedures

and design

documents

were identified and revised to reflect the

modification; verify that the modifications were reviewed

and

incorporated into the operations training program,

as applicable;.

verity that the modifications were installed in accordance

with

the work package (for those that could be physically inspected);

ensure that the modification was consistent with applicable

codes

and standards,

regulatory requirements,

and licensee

commitments;

and ensure that post modification testing requirements

were

specified

and that adequate

testing

was accomplished.

The

following DCNs were reviewed:

1)

DCN W17631,

Base Plate Installation

On October 21,

1993, during

a routine tour of the Unit 3

reactor building the inspector

observed

base plate

installation of supports.

This was being performed

under

DCN W17631.

The inspector

noted that four anchor bolts were

in place but the bolt holes were next to (about I/4 inch)

away from an existing hole.

The vacant holes were grouted

over but the sleeve

was still in place.

This in effect

appeared

to negate

the grouting since the spacing

between

the sleeves

was still below minimum spacing.

The inspector

contacted

a gA supervisor to review the installation.

In

addition the inspector reviewed

HAI 5.1 that specified the

spacing

between

anchor bolts.

Host distances

required

several

inches

between

spacing.

Initial review of this

issue

determined that

F-DCN 26899

was issued to revise

anchor bolt spacing

dimensions

because

of spacing

violations.

A different type anchor bolt penetrating

several

inches into the floor was used.

This design

strengthened

the area to be pulled out.

Additionally,

calculation

CD-f3064-922915

was revised to incorporate

the

F-DCN 26899.

The inspector reviewed the calculation

and

concluded the issue

was resolved.

2)

DCN W7731A, Electrical Separation

The inspector

reviewed the work associated

with scaffolding

in the Unit 2 reactor building spaces.

The work was being

performed under

DCN W7731A to reroute the normal

power

supply cable to 250 volt reactor

HOV Board

3C to correct

16

electrical

separation

concerns.

The cable

was

a safety

system cable but was routed in non-safety

raceways.

This

was

a Unit 3

DCN but involved work. in Unit 2 operating

spaces.

The inspector reviewed the safety

assessment

for

the

DCN and unit separ ation issues

were addressed.

TS

requirements',

secondary

containment,

and system operability

were each discussed.

Additionally, inspection of the

scaffolding in Unit 2 reactor building identified no

deficiencies.

The inspector concluded that the licensee

had

performed

a thorough

assessment

of this modification's

impact on the operating unit.

System

SPOC's

The purpose of SPOC process

is to provide

a systematic

method for

evaluating

items

and issues

which potentially affect the ability

of Unit 3 systems

and the Unit 3 portion of common

systems

to

perform as designed.

This process

determines

the status of each

item/issue

and assures

completion of those which affect system

return to operation for Unit 3 restart.

For each

system

evaluated,

the

SPOC process

may be accomplished

in two phases.

Phase

I SPOC addresses

the Restart

Test Program testing milestone

if that milestone exists for the system,

and establishes

system

status

control

by the Operations

department.

Phase II SPOC

addresses

System Return to Operation in preparation for the

declaration of system operability.

Each

phase

ensures

that open

items/issues

which potentially affect the phase

are either

completed,

or reviewed

and satisfactorily dispositioned.

The

SPOC

process

does not declare

system operability.

Rather, it is used

to support

a declaration of system operability which is made after

other requirements for operability are satisfied (e.g.,

support

systems

available;

performance of Surveillance Instructions,

etc.).

The following system

SPOC packages

were reviewed to ensure

they

complied with SSP 12.55, Unit 3 System Pre-Operability Checklist,

Revision 5.

Hinor deficiencies

were resolved with the system

engineer.

System 27,

Condenser

Circulating Water System,

Phase I.

System Testing

On November 8,

1993, the licensee

performed

a static hydrostatic

test

on the condensate

side of the main condensers.

The test

was

conducted

in accordance

with SOI-19, Flooding Hotwell for

Condenser

Tube

Leak Check.

There were no major problems

encountered;

however,

the test did identify that two condenser

tubes required plugging, seventy tubes required rerolling,

and

four tube sheet

holes required plugging because

the internal

baffle plates didn't allow for tube installation.

This was the

17

first milestone in the licensee's

efforts to return Unit 3 to

service

and it was accomplished

seven

days

ahead of schedule.

Reportable

Occurrences

(92700)

The

LERs listed below were reviewed to determine if the information

provided met

NRC requirements.

The determinations

included the

verification of compliance with TS and regulatory requirements,

and

addressed

the adequacy of the event description,

the corrective actions

taken,

the existence

of- potential generic problems,

compliance with

reporting requirements,

and the relative safety significance of each

event.

Additional in-plant reviews

and discussions

with plant

personnel,

as appropriate,

were conducted.

(CLOSED)

LER 50-296/92-006,

Inadvertent

Emergency Diesel

Generator Start

During Testing

Due To A Short Circuit.

On December 3,

1992, during the performance of the

3D

DG redundant start

test,

the

3D

DG inadvertently started

when test leads

connected

across

the autostart relay shorted.

The short occurred

when the test lead

was

pinched under

a movable handle

on the test equipment cart

and

damaged.

As corrective action the licensee

replaced

the .damaged test leads

and

secured

them in such

a fashion to reduce the potential for damage.

The

'oveable

handles

on the carts

were also removed.

Additionally, training

was provided to maintenance

personnel

on the impact of potential

degradation

of test leads.

The inspector

reviewed the training records

of the maintenance

personnel

and verified the test carts

were modified

to reduce the potential for damage to the test leads.

The inspector

considers this item closed.

Action on Previous

Inspection Findings

(92701,

92702)

a.

.

(CLOSED) Fire Protection

Weakness

Identified in IR 93-19

A weakness

was previously identified in IR 93-19 involving the

control

and timely update

requirements

of the licensee's

FPR and

the

LCO determinations for fire protection features

impacted

by

recent design

changes.

The licensee

issued

Revision

6 on

September

30,

1993, to SSP

12. 15, Fire Protection,

addr essing this

weakness.

The revision added Appendix A, Management of the Fire

- Protection

Report Volume 1, providing administrative controls for

the purpose of maintaining

and controlling the

FPR including

revising

and updating the document.

Step 5.0 of this appendix

assigns responsibility to site engineering requiring that the

FPR

be updated within 30 days after completion of a refueling outage

or earlier if deemed

necessary.

The residents

reviewed the

licensee's

corrective actions for this concern

and discussed

them

with the regional

based

inspector

and determined this issue

closed.

18

b.

(CLOSED)

URI 259,

260; 296/93-02-02,

Mislabeling of Fuses

(CLOSED)

URI 259,

260, 296/93-08-01,

Design Control Coordination

Discrepancies

(CLOSED)

URI 259,

260, 296/93-25-03,

Inoperable

SBGT Due to Fuse

Mislabeling

These

issues

are considered

closed with the issuance

of violation

259,

260,

296/93-39-03,

Failure to Control

Design

Changes.

This

violation encompasses

fuse labeling issues.

Site Organization

On November

10,

1993,

Eugene

Preston

reported

on site

as the Operations

Manager to fill the vacancy left by the resignation of Max Herrell.

On November

15,

1993,

Richard

Machon reported

on site

as the Plant

Manager replacing

John Scalice

who transferred

to Watts

Bar

as the

Operations

Vice President.

Independent

Safety Engineering

Group (40500)

The inspector

reviewed the status of the site's

ISEG.

The requirement

for an

ISEG was

a commitment under the Nuclear Performance

Plan

(Volume 3) for the restart of Browns Ferry.

The group was established

by

NUREG 0737 guidelines for multi-site utilities.

The group is

patterned after the Sequoyah plant that has the

ISEG requirement

in TS.

It is not

a TS requirement

at

BFNP.

On April 8,

1993, the licensee

submitted revision three of their N(A

plan that combined the site licensing

and quality manager into one

position.

This also placed the

ISEG under the licensing

and quality

manager on-site instead of an off-site corporate

manager.

Region II

accepted

the changes

on June

9,

1993.

The licensee

contends that the

site licensing

and quality manager

does not report to any site manager

and the independence

is maintained.

Further changes

are occurring with ISEG.

The group functions are being

incorporated into a new group called Reactor Safety Engineering

and

Review commonly called

RSER.

A procedure for this group is being

developed.

Exit Interview (30703)

The inspection

scope

and findings were summarized

on November

19,

1993,

with those

persons

indicated in paragraph

one above.

The inspectors

described

the areas

inspected

and discussed

in detail the inspection

findings listed below.

The licensee did not identify as proprietary

any

of the material

provided to or reviewed

by the inspectors

during this

inspection.

19

The Site V.P. stated that

a fire watch provided immediate detection of a

fire and the changes

to the plan,

as outlined in paragraph

4 above,

were

justified.

Item Number

Descri tion and Reference

260/93-39-01

260/93-39-02

259,

260,

296/93-39-03

URI, Inadequate

Safe

Shutdown

Procedure

Revision,

paragraph 4.c.

IFI, Acceptance Criteria For Instrument

Comparison Surveillances,

paragraph

4.e.

VIO, Inadequate

Design Control, paragraph

5.c and 6.a.

260/93-39-04

Acronyms

and Initialisms

URI, Unfinished Conduit Modification,

paragraph

5.e.

Licensee

management

was informed that

1

LER and

3 URIs were closed.

ARP

ASOS

ATU

BFEP

BFNP

BP

CBP

CCD

CFR

CIV

DCN

DG

DP

EDG

EMS

FCV

FDCN

FPR

FSAR

HPCI

HVAC

ICPM

IR

ISEG

LCO

LER

LLRT

MAI

MEL-

Annunciator Response

Procedure

Assistant Shift Operations

Supervisor

Analog Trip Units

Browns Ferry Engineering Project

Browns Ferry Nuclear

Power Plant

Business

Practice

Condensate

Booster

Pump

Configuration Control Drawing

Code of Federal

Regulations

Containment Isolation Valve

Design

Change Notice

Diesel

Generator

Differential Pressure

Emergency Diesel

Generator

Equi'pment

Management

System

Flow Control Valve

Field Design

Change Notice

Fire Protection

Report

Final Safety Analysis Report

High Pressure

Coolant Injection

Heating, Ventilation,

8 Air Conditioning

Item Coordinator Project Manager

Inspection

Report

Independent

Safety Engineering

Group

Limiting Condition for Operation

Licensee

Event Report

Local

Leak Rate Testing

Hodification Alteration Instruction

Master Equipment List

HIL

HOV

NRC

PER

PI

PID

PSID

gA

gC

RFP

RHR

RSER

RWCU

RWP

SBGT

SFRT

SI

SHH

SOI

SPAE

SPOC

SSP

SSP

TACF

TS

UO

URI

VIO

WCT

WO

WP

20

Master

Issues List

Motor Operated

Valve

Nuclear Regulatory

Commission.

Problem Evaluation Report

Project Instruction

Planning

Item Description

Pounds

Per Square

Inch Differential

guality Assurance

guality Control

Reactor

Feedwater

Pump

Residual

Heat

Removal

Reactor-'Safety

Engineering

and Review

Reactor Water Cleanup

Radiological

Work Permit

Standby

Gas Treatment

System

Scram Frequency

Reduction

Team

Surveillance Instruction

Scheduling

Methods Manager

Special

Operating Instruction

System Plant Acceptance

Evaluation

System Pre-Operability Checklist

Site Standard

Practice

Safe

Shutdown

Procedure

Temporary Alteration Control

Form

Technical Specification

Unit Operator

Unresolved

Item

Violation

Work Control

Team

Work Order

Work Permit

0