ML18037A470

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Insp Repts 50-259/93-28,50-260/93-28 & 50-296/93-28 on 930717-0820.Violations Noted.Major Areas Inspected:Maint & Surveillance Observation,Operational Safety Verification, & Measuring & Test Equipment
ML18037A470
Person / Time
Site: Browns Ferry  
Issue date: 09/03/1993
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18037A464 List:
References
50-259-93-28, 50-260-93-28, NUDOCS 9309280186
Download: ML18037A470 (22)


See also: IR 05000259/1993028

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Report Nos.:

50-259/93-28,

50-260/93-28,

and 50-296/93-28

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection at Browns Ferry Site near Decatur,

Alabama

Inspection

Conducted:

July

17 - August 20,

1993

Inspector:

att

t

ns ect

e

en

p

or

at

1gne

Accompanied

by:

J.

Hunday,

Resident

Inspector

R. Musser,

Resident

Inspector

G. Schnebli,

Resident

Inspector

Approved by:

'a

~

Reacto

s,

Sec ion 4A

Division of

eactor Projects

SUMMARY

e

)gne

Scope:

This routine resident

inspection

included surveillance

observation,

maintenance

observation,

operational

safety

verification, measuring

and test equipment,

Unit 3 restart

activities, reportable

occurrences,

action

on previous inspection

findings,

and site organization.

One hour of backshift coverage

was routinely worked during the

work week.

Deep backshift inspections

were conducted

on

July 25,

1993,

and August 8,

1993.

9309280186

930917

PDR

ADOCK 05000259

8

PDR

2

Results:

One violation was identified by an

NRC inspector for failure to

control measuring

and test equipment,

paragraph

5.

Four examples

were identified of equipment

not being tracked

as required

by

plant procedures.

The licensee

conducted

an inventory and

identified an additional

73 items not properly tracked.

A similar

violation, 92-21-03,

was identified for failure to adequately

disposition nonconforming measuring

and test equipment.

The site

quality assurance

organization

has

had several

findings in this

area

over the past several

years but deficiencies

continue to

exist.

One violation was identified by a

NRC inspector for failure to

control transient

combustible material required

by the Fire

Protection

Program,

paragraph

4.

Six electrical

cable reels

were

moved into the Unit 2 reactor building without the required permit

and

a fire watch.

This violation is similar to

a violation in

inspection report 92-37.

One noncited violation was identified by the licensee for failure

to have

an operable radiation monitor during

a radioactive

release,

paragraph

3.

The monitor was unknowingly inoperable

because

the monitor probe

was not properly reinstalled after

a

surveillance

procedure.

The licensee

conducted

an incident

investigation of the event with comprehensive

corrective action.

REPORT DETAILS

Persons

Contacted

Licensee

Employees:

  • 0. Zeringue,

Vice President

  • J. Scalice,

Plant Manager

J. Rupert,

Engineering

and Modifications Manager

  • R. Baron, guality and Licensing Manager

D. Nye, Recovery

Manager

H.

Her rell, Operations

Manager

J.

Maddox, Engineering

Manager

  • H. Bajestani,

Technical

Support Hanager

A. Sorrell, Chemistry

and Radiological Controls Manager

C. Crane,

Maintenance

Manager

P. Salas,

Licensing Manager

  • R. Wells, Compliance

Manager

J.

Corey, Radiological

Control Manager

J. Brazell, Site Security Manager

Other licensee

employees

or contractors

contacted

included licensed

reactor operators,

auxiliary operators,

craftsmen,

technicians,

and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

P. Kellogg, Section Chief

  • C. Patterson,

Senior Resident

Inspector

  • J. Munday, Resident

Inspector

  • R. Husser,

Resident

Inspector

  • G. Schnebli,

Resident

Inspector

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Surveillance Observation

(61726)

The inspectors

observed

and/or reviewed the performance of required SIs.

The inspections

included reviews of the SIs for technical

adequacy

and

conformance to TS, verification of test instrument calibration,

observations

of the conduct of testing,

confirmation of proper removal

from service

and return to service of systems,

and reviews of test data.

The inspectors

also verified that

LCOs were met, testing

was

accomplished

by qualified personnel,

and the SIs were completed within

the required frequency.

The following SIs were reviewed during this

reporting period:

SLC Operabil ity Sur veil 1 ance

On July 19,

1993 the inspector

witnessed

portions of the

performance of 2-SI-4.4.A. 1, Standby Liquid Control Functional

Test.

This test verifies the operability of the

SLC pumps in

conformance with the requirements

specified in TS 4.4.A. 1,

4.4.B.l,

and 4.6.G.l.

The results of the surveillance

indicated

that the flow rate of pump

B fell outside the acceptable

range of

43.7 - 50.0 gpm.

The flow rate of the

pump was measured

using two

different methods,

one using

an ultrasonic flow meter

and the

other by measuring

the level decrease

over time in the tank the

pump takes suction on.

The flow meter indicated

a flow rate of

52.0

gpm while the calculated flow indicated 51.7 gpm.

The

inspector questioned

the system engineer

about the increased

capacity of the

pump since the last surveillance.

He stated that

the

pump had

been re-built during the outage

and

new baseline

data

obtained during the performance of the surveillance following the

maintenance.

He indicated that

he suspects

the capacity

had not

actually changed

since the last surveillance

but could not

positively confirm this.

Based

on positive verification of flow

by two methods

on July 19,

1993,

and

no reason to suspect

pump

degradation,

the licensee

again calculated

a new acceptable

range

for flow, 48.6

52.7

gpm.

Based

on the

new flow requirement

the

B pump was acceptable

and the SI was completed satisfactory.

The

inspector referenced

ASME Section XI Subsection

IMP-3000 and

veri'fied this method of establishing

baseline

data

was acceptable.

No other deficiencies

were noted.

Core Spray Sparger

Break Detector Surveillance

On July 19,

1993 the inspector witnessed

portions of the

performance of 2-SI-4.2.B-24(I),

Core Spray Sparger

To Reactor

Pressure

Vessel Differential Pressure

Calibration 2-PDIS-75-28.

This instruction partially satisfies

the requirements

of TS 3.2.B

and 4.2.B.

The surveillance

channel

checks points

on the gauge

with a test

gauge

as pressure

is increased

to full range

and then

again

as pressure

is decreased.

The surveillance

has

two ranges

that the points must fall within, one verifies

TS operability and

the other ensures

the point is adjusted

as close

as possible to

the center of the band

and is known as "leave

as is."

The data

taken

was within the acceptable

range to verify operability but

was not in the range to leave the instrument

as found.

Attempts

were

made to adjust the meter to within the "leave

as is" but were

unsuccessful.

Engineering

was contacted

and decided to revise the

procedure to expand the acceptable

"leave

as is" range.

The

procedure

was revised,

the instrument calibrated to within the

appropriate

tolerances,

and the surveillance

completed

satisfactorily.

The inspector

reviewed the safety analysis for

the procedure revision

as well as the vendor manual

and noted

no

discrepancies.

No other exceptions to the surveillance

were

noted.

i

No violations or deviations

were identified in the Surveillance

Observation

area.

Maintenance

Observation

(62703)

Plant maintenance activities were observed

and/or reviewed for selected

safety-related

systems

and components

to ascertain

that they were

conducted

in accordance

with requirements.

The following items were

considered

during these

reviews:

LCOs maintained,

use of approved

procedures,

functional testing and/or calibrations

were performed prior

to returning components

or systems to service,

gC records maintained,

activities accomplished

by qualified personnel,

use of properly

certified parts

and materials,

proper use of clearance

procedures,

and

implementation of radiological controls

as required.

Work documents

were reviewed to determine the status of outstanding jobs

and to assure

that priority was assigned

to safety-related

equipment

maintenance

which might affect plant safety.

The inspectors

observed

the following maintenance

activities during this reporting period:

HSIV Limit Switch Failure

On July 25,

1993, at approximately 4:55 a.m., the Unit 2 operating

shift noted that the valve position indicating lights for the

'D'utboard

HSIV were both lit.

At the time of the discovery Unit 2

was operating at

100 percent

power with steam flow being equally

distributed

among the four steam lines.

Because

steam flow in the

'D'ine was approximately the

same

as the other three

steam

lines, the operators felt assured

that 'D'utboard

MSIV was still

in the full open position.

Additionally, the operating

crew

verified that the

RPS relays associated

with the involved HSIV

were in their normal energized state

which further lended

credence

to the valve having not changed position.

A malfunctioning limit

switch was thought to be the cause of the double light indication.

The HSIVs were tested

on July 24,

1993, in accordance

with

procedure 2-SI-4.1.A-ll(I), MSIV Closure-RPS Trip Functional Test.

This test "slow closes"

each

HSIV approximately

10 percent

and

ensures

that the

RPS relays associated

with the valve de-energize

and that the valve position indicating lights demonstrate

valve

movement.

No deficiencies

were noted during this surveillance

related to valve position lights.

On July 26,

1993, the licensee

issued

WO 93-09611-00 to cycle the

'D'utboard

MSIV in accordance

with applicable portions of 2-SI-

4. 1.A-11(I).

This effort was to be performed in order to

hopefully "free up" what was thought to be

a stuck or

malfunctioning limit switch.

Prior to the performance of the

evolution, the

ASOS briefed the involved personnel

to ensure that

the evolution was thoroughly understood.

The operators

"slow

closed" the 'D'utboard

HSIV for approximately

30 seconds

(approximately equal to

10 percent closed).

As expected,

the

b.

associated

RPS relays de-energized

during the valves closure

and

re-energized

as the valve was returned to the full open position.

However, the position indicating lights never changed

state

throughout the entire evolution.

The valve's position indicating

limit switch is thought to be malfunctioning

and will be repaired

or replaced

during

a future power reduction/forced

outage.

Inoperable Liquid Radwaste Effluent Radiation Monitor

On July 13,

1993, the contents of the Floor Drain Sample

Tank were

released

to the Tennessee

River while the radiation monitor for

this release

path,

O-RM-90-130,

was inoperable.

On July 12,

1993,

the detector

was

removed from service for a setpoint

adjustment

in

accordance

with

WO 93-09182-00.

Following completion of this

work, O-SI-4.2.D. 1, Liquid Radwaste

Monitor Calibration/Functional

Test,

was performed satisfactorily

as post maintenance

testing.

Operations

declared

the monitor operable

at 0230

on July 13,

1993.

At 2200

on July 13,

1993, the floor drain sample tank was released

via this pathway;

however, following the release, it was

discovered that the detector

had not been reinstalled

in the

detector

housing during performance of the setpoint

adjustment,

as

required.

With the detector not installed in the detector

housing

the release

path would not have automatically isolated in the

event the radiation levels of the release

were to increase

to the

trip setpoint.

With the monitor out of service,

TS Table 3.2.D,

allows radwaste

discharges

to be made via this pathway,

provided

two independent

samples of the tank are analyzed in accordance

with the sampling

and analysis

program specified in the

REM and

two qualified station personnel

independently verify the release

rate calculations

and valve lineup before the discharge.

Because

the monitor was thought to be operable,

these

compensatory

actions

were not performed.

However, the release

was not unmonitored,

O-SI-4.8.A. 1-1,

Release

Procedure

Liquid Effluents,

was

performed in conjunction with the release

and serves to verify

that the

MPC limits required

by TS 3.8.A.l, are not exceeded.

Upon discovery of this condition, the detector

was reinstalled

and

the surveillance re-performed.

Failure to place the detector

back

into the detector

housing during the performance of the

surveillance is

a violation but will not be subject to enforcement

because

the licensee's

effort in identifying and correcting the

violation met the criteria specified in Section VII.B of the

Enforcement Policy.

This matter is identified as

NCV 259,

260,

296/93-28-01,

Inoperable

Radwaste Effluent Radiation Monitor.

One noncited violation was identified in the Maintenance

Observation

area.

Operational

Safety Verification (71707)

The

NRC inspectors

followed the overall plant status

and

any significant

safety matters related to plant operations.

Daily discussions

were. held

with plant management

and various

members of the plant operating staff.

The inspectors

made routine visits to the control rooms.

Inspection

observations

included instrument readings,

setpoints

and recordings,

status of operating

systems,

status

and alignments of emergency

standby

systems,

verification of onsite

and offsite power supplies,

emergency

power sources

available for automatic operation,

the purpose of

temporary tags

on equipment controls

and switches,

annunciator

alarm

status,

adherence

to procedures,

adherence

to LCOs, nuclear instruments

operability, temporary alterations

in effect, daily journals

and logs,

stack monitor recorder traces,

and control

room manning.

This

inspection activity also included

numerous

informal discussions

with

operators

and supervisors.

General

plant tours were conducted.

Portions of the turbine buildings,

each reactor building,

and general

plant areas

were visited.

Observations

included valve position

and system alignment,

snubber

and

hanger conditions,

containment isolation alignments,

instrument

readings,

housekeeping,

power supply and breaker alignments,

radiation

and contaminated

area controls,

tag controls

on equipment,

work

activities in progress,

and radiological protection controls.

Informal

discussions

were held with selected

plant personnel

in their functional

areas

during these tours.

a ~

Unit Status

b.

Unit 2 operated

continuously at power during this period without

any significant problems.

The unit was online for 78 days at the

end of the period.

Transient

Combustibles

On July 29,

1993, the inspector identified six partial reels of

electrical

cable located in the unit 2 reactor building without

the required transient

combustible permit and continuous fire

watch.

The inspector contacted

the Fire Protection

group who

posted

a continuous fire watch.

They stated

they had not been

informed that cable

was placed in the building.

The cable

was

used to implement

DCN W7728A.

TS 6.8.l.l.f, requires that written

procedures

be established,

implemented,

and maintained covering

implementation of the Fire Protection

Program.

Section

I-C of the

Fire Protection

Report Volume 2, step 5. l. 1, states

that in

critical areas,

any combustible material that is not permanently

installed shall

be designated

as

a transient

combustible.

Furthermore,

a transient

combustible permit shall

be initiated and

compensatory

measures

taken

as required.

Failure to initiate the

required transient

combustible permit and post

a continuous fire

watch is

a violation of these

requirements

and is identified as

VIO 259,

260, 296/93-28-02,

Failure To Control Transient

Combustibles.

A similar violation was issued

November 27,

1992,

in IR 92-37, for failure to adequately

control transient

combustibles.

One violation was identified in the Operational

Safety Verification

area.

Heasuring

and Test

Equipment

On July 27,

1993, the inspector

noted

an instrument cart containing

electrical test equipment left unattended

in the

1A DG room.

On July

28,

1993, the inspector noted another cart containing electrical test

equipment left unattended

in the Unit 3

DG building.

The equipment

on

both of the carts

was controlled under the Heasuring

and Test Equipment

program.

The licensee

determined

the equipment

belonged to the Customer

Group

and was

used during

DG testing.

The inspector reviewed the

H&TE

usage

logs for the equipment which indicated it had been

checked

back

into the control area.

The inspector questioned

the licensee

about

maintaining positive control of the equipment

and storing the equipment

in a suitable environment,

as required

by the

H&TE program.

Mhile the

DG buildings are not the designated

control

areas for this equipment,

the licensee

stated that occasionally it will be left there if the

equipment is to be used to test

more than

one

DG.

The licensee

moved

the equipment to the designated

control area.

The inspector

reviewed

the vendor documents

describing the environment the equipment

was to be

stored in and verified the

DG building was suitable.

Further discussion

with the licensee

concerning the environment of the storage facility

indicated that while the environmental

conditions required for each

piece of H&TE was not specifically verified they believe that no

problems exist in this area.

This is based

on the room being kept at

a

controlled temperature

and low humidity which the licensee

stated is

generally the limiting factor for storage of equipment.

The inspector

randomly selected

various

HLTE and verified this was accurate.

On August 4,

1993, the inspector

noted

a thermometer,

labelled

E10120,

being used in the plant which was under the control of the

HLTE program.

The procedure for which the thermometer

was needed,

listed this

thermometer

as well as another,

labelled

542968,

as being

used to

support the procedure.

The inspector questioned

the

H&TE issue

personnel

about the status of these

two thermometers.

E10120

was

identified in the usage

log as having been

checked

out on Hay 8,

1993,

but did not indicate

when it would be returned.

However, the inspector

was later informed that the log was wrong and that the thermometer

had

actually been lost.

The inspector

informed the

H&TE coordinator of the

location of the thermometer

and it was retrieved

and dispositioned.

The

usage

log indicated that thermometer

542968

had

been returned to the

control

area but could not be immediately located;

however, it was found

in the. control

area

some time later.

In addition, the inspector

also

noted three other instruments,

E10258,

E10595,

and

E10647,

had

been

checked

out for long term use without indicating the dates

they would be

returned.

The HLTE coordinator later informed the inspector that while

two of the instruments

were still being used,

E10595

was actually

located in the control area.

The usage

logs for these

instruments

were

also corrected

and the discrepancy dispositioned.

In addition, the

licensee

performed

an inventory of all the

H&TE and out of approximately

four thousand

items, seventy-three

could not be accounted for.

The

0

licensee

intends to generate

out-of-tolerance

investigations for these

items.

SSP-6.7,

Control of Measuring

and Test Equipment,

section 3.9, states

that

H&TE is allowed to be checked

out on

a shift by shift basis.

If

the equipment is needed for a longer period of time it can

be kept

longer but the user must provide

an expected return date

on the usage

log.

Section 3. 11 states

that the user of M&TE shall provide the work

document the equipment will be used for, the organization responsible

for the equipment,

the expected duration of use,

and information

concerning

each individual use of the equipment.

It further states

that

control of the

H&TE will be maintained while it is being used.

If the

equipment will be left unattended it must

be tagged to identify the

controlling document

and the responsible

individuals.

When the

equipment is returned,

the procedure

states that all usages

shall

be

documented

on the usage log.

Contrary to these

requirements,

electrical

H&TE was found in the plant which was left unattended

and not tagged

as

such

and

was kept for greater

than

one shift without the proper

documentation.

In addition, the usage

log identified this equipment

as

having been returned to the control area.

Four pieces of M&TE were

checked

out and kept for periods of one to three

months without the

proper documentation.

Of these four, one of the items

was also

identified as lost and

one was actually found in the control area.

The

lost H&TE was found by the inspector

and secured

by the licensee.

10 CFR 50, Appendix B, Criteria XII requires that measures

shall

be

established

to ensure that tools,

gauges,

instruments,

and other

measuring

and test devices

used in activities affecting quality are

properly controlled, calculated,

and adjusted to maintain accuracy

within specified limits.

SSP-6.7,

Control of Measuring

and Test

Equipment

implements

these

requirements.

Collectively, these

items

indicate

a lack of control of H&TE and is identified as

VIO 259,

260,

296/ 93-28-03, Failure to Control

H&TE.

Additional examples for failure to adequately

control

M&TE include,

a

QA

audit conducted

in July,

1991, which identified examples of H&TE usages

that were not logged in the usage logs.

This was documented

as

CAQR

BFSCA910168107.

In November,

1991, additional

examples

were identified

and the

CAQR was revised to include them.

In June

1992

a violation was

issued for failure to adequately disposition

M&TE found to be out of

tolerance.

Unit 3 Restart Activities

(30702,

37828,

61726,

62703,

71707)

The inspector

reviewed

and observed

the licensee's

activities involved

with the Unit 3 restart.

This included reviews of procedures,

post-job

activities,

and completed field work; observation of pre-job field work,

in-progress field work,

and

QA/QC activities; attendance

at restart

craft level, progress

meetings,

restart

program meetings,

and management

meetings;

and periodic discussions

with both TVA and contractor

personnel,

skilled craftsmen,

supervisors,

managers

and executives.

The licensee is still working on the Unit 3 Recovery Schedule

which

should

be finalized this month with a meeting scheduled

on September

7,

1993,

between licensee

and

NRC management

to discuss

the schedule

and

long range plans.

The inspectors will continue to follow the progress

of the schedule.

Currently, the work is being scheduled

and tracked

by

a Summer Semester

Schedule

which provides

a three

month look ahead for

both maintenance

and modifications.

Progress

on the three month

schedule will be used

as input to more accurately project work duration

on the long range schedule.

Construction activities continue to increase

with the completion of the

Unit 2 cycle

6 refueling outage.

Major activities in progress

include:

CRDR work in the control

room panels; fire protection systems;

seismic

upgrades;

and pipe supports.

Reportable

Occurrences

(92700)

The

LERs listed below were reviewed to determine if the information

provided met

NRC requirements.

The determinations

included the

verification of compliance with TS and regulatory requirements,

and

addressed

the adequacy of the event description,

the corrective actions

taken,

the existence of potential generic problems,

compliance with

reporting requirements,

and the relative safety significance of each

event.

Additional in-plant reviews

and discussions

with plant

personnel,

as appropriate,

were conducted.

a ~

(CLOSED)

LER 259/91-06,

Unplanned

Engineered

Safety Feature

Actuation During Maintenance Activities Due to Proximity of

Components.

On May 7,

1991,

an initiation of the

CREV system occurred

when

maintenance

personnel

performing work in panel

25-165

inadvertently

bumped relay CR-A, which is associated

with

radiation monitor 0-RM-90-259.

The bumping of the relay caused

its contacts

to close

and initiate the

CREV system

and

a high

radiation alarm in the main control

room.

In response

to this event,

the licensee

evaluated

the need for a

design

change to relocate the components

in panel

25-165

and to

provide

a cover for the

CR-A relay.

Since this matter

was

an

isolated event,

the licensee

determined that no design

change

nor

any covers would be provided for the

CR-A relay.

A second

proposed corrective action involved adding

a caution statement

to

the System Instrument Maintenance

Index, O-SIMI-31B, to inform

personnel

of the potential

ESF actuation in the event that the

relays

are

bumped.

This action was performed.

The final proposed

corrective action was that of labeling the involved relays.

This

action

was verified by the inspector.

(CLOSED)

LER 50-296/92-004,

Chemical

Release

In Unit 3 Reactor

Building Forced

An Evacuation

Of Compensatory Action Fire Watches

Leading To A Violation Of Technical Specifications.

On November 4,

1992, all compensatory fire watches,

required

by

TS, were evacuated

from the Unit 3 reactor building due to a

chemical

release.

The release

was caused

by an unexpected

exothermic reaction

from an epoxy grout compound.

Following

removal of the remaining grout and ventilating the area,

the fire

watches

were returned to their posts.

The epoxy is supplied

as

a 30 pound kit with premixed parts

and

mixing only part of the kit was not recommended

by the

manufacturer.

The craft performing the work mixed the entire kit

but put the unused portion in a closed container which prevented

heat dissipation

and caused

the release of smoke

and vapor.

The

licensee

determined

the root cause of the event to be inadequate

warning information and proper instructions

from the manufacturer.

Corrective actions

included the manufacturer of the grout

providing hands-on training to the personnel

using it.

Additionally, following this training, MNI-172, Chemical

Grouting

To Fill Voids To Rotating And Stationary

Equipment

Base Plates,

was revised to include

a precaution

concerning

epoxy grouts

and

a

requirement to contact the manufacturer for instructions for

handling when instructions

are not adequately

provided.

(CLOSED)

LER 50-259/93-003,

Engineered

Safety Feature Actuation

Caused

By A Sudden

Pressure

Relay Being Struck

By Tool.

On April 19,

1992, during the Unit 2 refueling outage,

the Athens

161

kV offsite power supply was deenergized

when

a dropped tool

, struck

a sudden

pressure

relay causing it to close.

This loss of

power initiated auto-starts

of diesel

generators

C,

D, 3A,

and 3B,

the

CREV System,

and the Standby

Gas Treatment

System.

The root

cause

was failure to provide adequate

barriers to prevent

dropped

items from contacting sensitive plant equipment.

Corrective

actions

included discussing this event with both management

and

field personnel

stressing

the importance of identifying sensitive

equipment located in the work area

and methods to avoid disturbing

them.

In addition,

SSP-9.3,

Modification and Design

Change Control,

was

revised to require

a walkdown by Operations for work occurring in

the

3C Relay

Room to ensure sensitive

equipment is adequately

protected.

The inspector questioned

the licensee

about what

controls exist to ensure

employees

other than those working on

modifications

do not disturb sensitive

equipment.

The licensee

provided

a copy of the maintenance

planners

guide which contains

information pertinent to this concern

and stated that the guide

was in the process

of being further enhanced.

In addition,

caution signs exist throughout the plant to indicate areas

containing sensitive

equipment.

10

d.

(CLOSED)

LER 260/93-05,

ESF Actuation Resulting

From a Lifted

Neutral

Lead

on

a HSIV Solenoid Circuit.

On Hay 20,

1993,

an electrician lifted a jumper and the neutral

lead of the power supply to

an ammeter for the HSIV solenoid

circuit.

The neutral

lead

was installed in series

configuration

which caused

several

Division

1 circuits to open

when the lead

was

lifted.

This resulted in a PCIS Division

1 actuation

which

controls

Group 1, 2, 3, 6,

and

8 valves.

All systems

and

components

functioned

as expected.

The licensee

determined

the

root cause for this event

was personnel

error for failing to

recognize

the impact of lifting the neutral

lead when preparing

and reviewing the work plan.

The work plan writer and the

independent

reviewer did not consider that

a procedural

precaution

for lifting the neutral

lead from the power supply was necessary

for the plant configuration at the time of the event.

The

licensee

took the following corrective actions to prevent

recurrence:

1) Work plan writers and independent

reviewers

were

trained

on the individual's responsibilities

pertaining to the

requirements

of the site standard

practice for proper review

criteria for modifications work plans

and the circumstances

of

this event;

2) the Hodifications Training Handbook was revised;

and 3) the responsible

personnel

were trained

on the need to

include necessary

precautions

in future work plans.

The

inspectors

reviewed the licensee's

corrective actions

and found

them to be adequate.

Action on Previous

Inspection Findings

(92701,

92702)

a ~

(CLOSED)

URI 260/93-18-01,

Loss of Primary Pressure

Control.

During the performance of two infrequent surveillance

procedures,

the pressure

indicator used to control pressure

was isolated.

The

NRC conducted

a human performance

study report - Browns Ferry

Unit 2 (5/ll/93) of this event.

The licensee

conducted

an

incident investigation,

ATWS/ARI/RPT Trip Due to Reactor

Overpressure,

of the event.

The inspector reviewed

each of these

reports

and concluded that the problem focused

on miscommunication

between the control

room operator

and the technician.

Procedure

enhancements

were

made to help prevent recurrence.

A digital

pressure

indicator was the primary display because

other displays

lacked the proper scales

necessary

to control pressure within the

required

band for the hydro test, 2-SI-3.3. 1.A,

ASHE Section

XI

System

Leakage Test.

However, the Harotta valve test, SI-

4.7.D. l.d-l, 2, 3, Functional Test of Instrument Line Flow Check

Valves, required the digital display be taken out of service

without written direction

on what alternative pressure

indication

to use.

The inspector

reviewed revision six of SI 4.7.D. I.d-l, 2,

3 dated

July 30,

1993

and revision three of 2-SI-3.3. 1.A dated July 16,

1993.

Procedural

steps

were

added for use of alternate

11

instrumentation to monitor vessel

pressure

when the digital

display is removed

from service with appropriate

cross reference

between the two procedures.

b.

(CLOSED) VIO 50-259,

260, 296/93-07-02,

Failure to Comply With

Radiation Protection

Procedures

This violation was identified for three specific examples of

failure to comply with radiation protection procedures.

These

examples

were identified by, the inspectors

during routine tours of

the plant during

a single day.

The first example involved an

individual handling the fuel support piece lifting tool without

being signed

on to the appropriate

RWP and without wearing

a face

shield.

The second

example dealt with an individual removing his

anti-c hood

and surgeons

cap while still within the contamination

zone.

The final example involved an individual donning

an anti-c

hood which had

been lying on

a steam line within a contamination

zone.

Corrective actions for these matters

involved issuing radiological

awareness

reports93-026

and 93-028

on the incidents.

The second

and third examples of the violation were combined into one

RAR due

to the incidents occurring within a close proximity and similar

time frame.

Secondly, all involved personnel

were counseled

on

the importance of following radiological work instructions.

In

addition, these matters

have

been incorporated into initial

radiological controls

GET and Radiological Controls

GET

retraining.

Based

on the inspector's

review of these corrective

actions, this matter is considered

closed.

9.

Site Organization

On July 27,

1993, J. Brazell, Acting Site Security Manager,

became

the

permanent Site Security Manager.

Effective July 26,

1993,

Raul

Baron, Site Manager of Nuclear Assurance

and Licensing,

became

the corporate

General

Manager of Nuclear Assurance

reporting to Hark Hedford, Vice President of Technical

Support.

John Maciejewski,

General

Manager of Nuclear Assurance will become

General

Manager of Operations

Services reporting to Dr. Hedford.

Mr.

Haciejewski will be responsible for Nuclear Training, Operations,

and

Haintenance.

10.

Exit Interview (30703)

The inspection

scope

and findings were summarized

on August 20,

1993,

with those

persons

indicated in paragraph

1 above.

The inspectors

described

the areas

inspected

and discussed

in detail the inspection

findings listed below.

The licensee

did not identify as proprietary

any

of the material

provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

tern

umber

12

esc

tio

and Refere

ce

259,

259,

259,

260, 296/93-28-01

260, 296/93-28-02

260, 296/93-28-03

NCV, Inoperable

Radwaste Effluent

Radiation Monitor, paragraph

3.

VIO, Failure to Control Transient

Combustible Material, paragraph

4.

VIO, Failure to Control

M&TE, paragraph

5.

Licensee

management

was informed that

4 LERs,

1 URI, and

1 VIO were

closed.

Acronyms

ARI

ASME

ASOS

ATWS

CAQR

CFR

CRDR

CREV

DCN

DG

ESF

GET

GPH

IR

LCO

LER

MPC

MSIV

METE

NCV

NRC

PCIS

QC

REH

RPS

RPT

RWP

SI

SIHI

SLC

SSP

TS

URI

VIO

WO

and Initialisms

Alternate

Rod Injection

American Society of Mechanical

Engineers

Assistant Shift Operations

Supervisor

Anticipated Transient Without Scram

Condition Adverse to Quality Report

Code of Federal

Regulations

Control

Room Design

Review

Control

Room Ventilation System

Design

Change Notice

Diesel

Generator

Engineered

Safety Feature

General

Employee Training

Gallons

Per Minute

Inspection

Report

Limiting Condition for Operation

Licensee

Event Report

Maximum Permissible

Concentration

Main Steam Isolation Valve

Measuring

and Test Equipment

Noncited Violation

Nuclear Regulatory

Commission

Primary Containment Isolation System

Quality Control

Radiological Effluent Manual

Reactor Protection

System

Recirculation

Pump Trip

Radiological

Work Permit

Surveillance Instruction

System Instrument Haintenance

Index

Standby Liquid Control

Site Standard

Practice

Technical Specification

Unresolved

Item

Violation

Work Order