ML18036A858

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Insp Repts 50-259/92-29,50-260/92-29 & 50-296/92-29 on 920718-0814.Violations Noted.Major Areas Inspected: Surveillance & Maint Observation,Operational Safety Verification & Verification of Plant Records
ML18036A858
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 09/02/1992
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18036A853 List:
References
50-259-92-29, 50-260-92-29, 50-296-92-29, NUDOCS 9209220150
Download: ML18036A858 (26)


See also: IR 05000259/1992029

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATL AN TA, G EO R G IA 30323

Report Nos.:

50-259/92-29,

.50-260/92-29,

and 50-296/92-29

'Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection at Browns Ferry Site near

Decatur,

Alabama

Inspector:

Inspection

Conducte

July

8

August, 14,

1992

~

~

a

on,

en>or

ss

ent

nspector

Date

cygne

Accompanied

by:

E. Christnot,

Resident

Inspector

W. Bearden,

Resident

Inspector

J.

Munday,

Resident

Inspector

Approved by:

Pa

.

e

g,

C se

R actor ProJects,

Section

4A

Division of Reactor Projects

Date

S gne

SUMMARY

Scope:

This routine resident

inspection

included surveillance

observation,

maintenance

observation,

operational

safety verification, verification of

plant records,

secondary

drawing status,

Unit 3 restart activities,

information notice 92-26,

and organization structure.

One hour of backshift coverage

was routinely worked during the work week.

Deep backshift inspections

were conducted

on July 25, August 2,

and August 9,

1992.

J

9209220150

920911

PDR

ADOCK 05000259

6

PDR

A public meeting

was held onsite

on July 27,

1992 for discussion of the

Systematic

Assessment

of Licensee

Performance

report.

The details

are in

inspection report 92-18.

Results:

Unit 2 operated

at power during this period,

paragraph

four.

A reactor trip

occurred

on July 28,

1992,

ending

89 days of continuous operation,

paragraph

four.

After a thorough review oF the tri'p, the unit was restarted

and

had

been

on line for 15 days at the end of the period.

Unit 3 recovery activities completed replacing the recirculation

system piping

and portions of the reactor water cleanup

system,

paragraph.

seven.

Other

.intergranular

stress

corrosion cracking mitigation techniques

are mechanical

stress

improvement

programs

and weld overlays.

These activities are in

progress

or being planned.

The site engineering

organization

has transitioned

to

a single organization with a Unit 3 component.

This has

increased

the

TVA

ownership of contractor design activities.

However, significant problems

were

encountered

with the drywell chiller installation

by construction contractor

personnel.

Approximately 100 field design

change

notices

were necessary

for

two design

change

notices.

One violation was identified for failure to sign onto

a hold order prior to

commencing work, paragraph

seven.

A modifications contractor

supervisor

failed to follow plant procedures.

Although, this was identified by the

licensee,

the violation is

a repeat of a previous

NCV 259,

260,

296/92-17-01.

One apparent violation was identified concerning

operator

rounds,

paragraph

five.

The licensee

conducted

an audit

and two personnel

received disciplinary

action,

The review of the licensee's

audit

and inspection

by the inspector

completed

temporary instruction TI 2515/115.

REPORT DETAILS

Persons

'Contacted

Licensee. Employees:

  • 0. Zeringue,

Vice President,

Browns Ferry Operations

  • H. McCluskey, Vice President,

Browns Ferry Restart

  • J. Scalice,

Plant Manager

  • J. Rupert,

Engineering

and Modifications Manager

  • J. Swindell, Restart

Manager

  • M. Herrell, Operations

Manager

J.

Maddox, Project, Engineer

  • H. Bajestani,

Technical

Support Manager

R. Jones,

Operations

Superintendent

A. Sorrell, Special

Programs

Manager

  • C. Crane,

Maintenance

Hanager

G. Turner, Site guality Assurance

Manager

  • R. Baron, Site Licensing Manager

P. Salas,

Compliance Supervisor

  • J. Corey, Site Radiological Control

Manager

A. Brittain, Site Security Manager

Other licensee

employees

or contractors

contacted

included licensed

reactor operators,

auxiliary operators,

craftsmen,

technicians,

.and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

P. Kellogg, Section Chief

  • C. Patterson,

Senior Resident

Inspector

  • E. Christnot,

Resident

Inspector

W. Bearden,

Resident

Inspector

J.

Hunday,

Resident

Inspector

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Surveillance Observation

(61726)

The inspectors

observed

and/or reviewed the performance of required SIs.

The inspections

included reviews o'f the SIs for technical

adequacy

and

conformance to TS, verification of test

instrument calibration,

observa-

t'

of the conduct of testing

confirmation of proper removal

from

ions

o

service

and return to service of systems,

and reviews of test data.

The

inspectors

also verified that

LCOs were met, testing

was accomplished

by

qualified personnel,

and the SIs were completed within the required

frequency.

The following SI was reviewed during this reporting period:

SI-4,9.A.1.A (C24), Diesel Generator 'C'4 Hour Run

On August 4,

1992, during completion of SI-4.9.A. I.A (C24), Diesel

Generator 'C'4 Hour Run, the

DG tripped spuriously

on reverse

power

as

the

DG was being unloaded.

The licensee

is conducting

an II of this

event.

The initial assessment

determined that

a "holding coil" in the

reverse

power relay was still in place causing the relay to remain

energized

as the

DG was unloaded.

The coil is used in high vibration

areas

to keep the reverse

power relay in place.

The holding coil was

found adjusted

out of service

on the other

seven

DGs.

The coil was

adjusted to be out of service

on the 'C'G.

The reverse

power relay is

located

in an electrical

cabinet

mounted

on

a separate

concrete

pad than

the

DG in the

DG room.

Vibration has not been

a problem in this

electrical cabinet.

The 'C'G was returned to service

on August 5,

1992.

The inspector will review the completed II which will include

extensive

review of this problem by the licensee.

No violations or deviations

were identified in the Surveillance

Observa-

tion area.

Maintenance

Observation

(62703)

Plant maintenance

activities were observed

and/or reviewed for selected

safety-related

systems

and components

to ascertain

that they were

conducted

in accordance

with requirements.

The following items were

considered

during these

reviews:

LCOs maintained,

use of approved

procedures,

functional testing and/or calibrations

were performed prior

to returning components

or systems

to service,

gC records

maintained,

activities accomplished

by qualified personnel,

use of properly

certified parts

and materials,

proper

use of clearance

procedures,

and

implementation of radiological control.s

as required.

Work documentation

(WR and

WO) were reviewed to determine

the status of

outstanding

jobs

and to assure

that priority was assigned

to safety-

related

equipment

maintenance

which might affect plant safety.

The

inspectors

observed

the following maintenance

activities during this

reporting period:

Unit 3EB Diesel

Generator

Outage

~ The

NRC inspector followed licensee activities associated

with the

scheduled

outage

on 3EB Emergency

DG.

The

DG was

removed

from

service to perform several

planned

work activities.

WO 92-53246,

which checked

the tightness of bolted connec-

tions.

This check is required six months following perfor-

mance of a six year

outage

on any diesel

generator.

e

WO 92-57723,

which replaced

the 38-2 Diesel

Fuel Transfer

pump due to high vibration.

WO 92-531,18,,which

performed

EPI-3-082-0GZ002,

Diesel

Generator

3B Redundant Start Test.

b.

The inspector

reviewed the hold order in effect on the

DG,

3-92-272,

and verified it to be adequate

for the intended

maintenance.

The inspector

observed

portions of work in progress

and the associated

work packages.

The work packages

were clear

and provided adequate

detail to support the work activity.

The

inspector verified the torque wrench being used,

I.D. number

544355,

was within it's requi) ed calibration date

and acceptable

for the intended work.

Following completion of the maintenance

the

DG was satisfactorily tested

and returned to

operable'outine

Preventative

Haintenance

An inspector

observed

work associated

with the following work

orders:

c ~

WO 92-56431,

which performed the required weekly inspection

of the

3B Control

Bay Chiller.

WO 92-49631,

which performed

EPI-O-OOO-HCCOOl,

Haintenance

and Inspection of 480

VAC and

250

VDC Hotor Control Centers.

Work was performed

on breakers for Drywell Equipment Drain

Sump

Pump

2B, Drywell Floor Drain

Sump

Pump

2B, Reactor

Building Equipment Drain

Sump

Pump

2B,

and Reactor Building,

Floor Drain Sump

Pump

2B.

The inspector

reviewed the work instructions

and determined that

the instructions

were of sufficient detail

and provided

adequate

guidance to support the intended

work activities.

Unit 2 Pre-outage

Hodifications

1.)

Hodification of Hiscellaneous

Steel

During

a routine tour of the reactor building on August 3,

1992,

the inspector

observed that

some concrete

blocks

had

been

removed

above the double doors to the reactor building

equipment

access

area.

The doors

were marked

as

an

Eg door

and pressure

boundary door.

The door was not to be left

opened without

SOS permission.

The inspector

questioned

the

SOS why the concrete

blocks were

removed

since this had

the

same effect

as leaving the doors

open.

It was determined that the concrete

blocks were

removed to

reinforce

some structural steel.

This work was

accomplished

under

DCN W17292-A.

An interim program for

seismic qualification of miscellaneous

steel

supports

was

approved for Unit 2 restart.

This work was being performed

as part of the long-term qualification.

The inspector

reviewed

WP-2211-92 which contained

a review by the

SOS.

In

this area near the reactor building elevator

and stairwell

there

are doors leading from Unit 2, from Unit I, and the

equipment

access

area to the area.

One of the doors

must

remain closed.

The inspector

concluded that adequate

controls

and review of this work activity had

been

maintained.

2.)

Scaffolding Problems

On July 31,

1992,

the inspector identified

a scaffold

incorrectly erected

in Unit 2 HPCI room.

The licensee

corrected

the scaffolding problem

and initiated II-B-92-053

to address

scaffolding problems.

The licensee

inspected all scaffo'1ding in the field and

20

scaffolds

were removed.

A comprehensive

procedure

revision

was conducted

as part of the II.

The inspector will

continue to follow these

problems with review of the II 'and

closure of IFI 260/92-21-02,

Adequacy of Scaffolding Review.

No violations or deviations

were identified in the Maintenance

Observa-

tion area.

Operational

Safety Verification (71707)

The

NRC inspectors

followed the overall plant status

and

any significant

safety matte

s related to plant operations.

Daily discussions

were held

with plant management

and various

members of the plant operating staff.

The inspectors

made routine visits to the control rooms.

Inspection

observations

included instrument readings,

setpoints

and recordings,

status of operating

systems,

status

and alignments of emergency

standby

systems,

verification of onsite

and offsite power supplies,

emergency

power sources

available for automatic operation,

the purpose of tempo-

rary tags

on equipment controls

and switches,

annunciator

alarm status,

adherence

to procedures,

adherence

to,LCOs, nuclear instruments

opera-

bility, temporary alterations

in effect, daily journals

and logs,

stack

monitor recorder traces,

and control

room manning.

This inspection

activity also included

numerous

informal discussions

with operators

and

supervisors.

General

plant tours were conducted.

Portions of the turbine buildings,

each reactor building,

and general

plant areas

were visited.

Observa-

tions included valve position

and

system alignment,

snubber

and hanger

conditions,

containment isolation alignments,

instrument readings,

housekeeping,

power supply

and breaker alignments,

radiation

and

contaminated

area controls,

tag controls

on equipment,

work activities

in progress,

and radiological protection controls.

Informal discussions

were held with selected

plant personnel

in their functional

areas

during

these tours.

Unit Status

Unit 2 tripped

on July 28,

1992,

ending

89 days of continuous

operation.

The cause of the trip is discussed

in this section.

The unit was restarted

and the generator

synchronized

to the grid

on July 30,

1992.

At the end of the report period the unit was

'on-line for

15 days.

Reactor Trip

On July 28,

1992 Unit 2 experienced

an automatic

main turbine trip

due to an indicated high water level spike

and subsequent

reactor

scram from 100 percent

power.

The spike occurred during

troubleshooting activi,ties associated

with a control relay in the

FWLC system.

Following the scram the plant was stabilized with

EHC controlling reactor pressure

and

a reactor

feed

pump

controlling water level.

Four SRV's with setpoints of 1105 psig

opened,

PCIS groups 2,3,6,

and

8 isolated,

Alternate

Rod Insertion

initiated and the 'reactor recirculation

pumps'ripped

as expected.

Additional plant equipment

responded

as expected

with the

following exceptions:

2.

The TIP probes

which were at the indexers

at the time of the

event,

automatically retracted

to the in-shield position

as

.

designed,-however

the TIP ball valves were found in the

open

position during scram recovery operations.

The local TIP

~ isolation reset

switch located

on the TIP drawer 'was

discovered

stuck depressed

in the reset position.

h

The feeder breaker for 480 volt Reactor Notor Operated

Valve

Board

2C tripped during the event.

This breaker

had

randomly tripped twice in the past

and this trip was

considered

to be

a continuation of the

same

problem.

The

breaker

was subsequently

replaced

as

a precautionary

measure.

3.

The

SRV tailpipe temperature

recorder

was found to have the

chart paper

jammed

and therefore did not record

SRV

operation.

An alternate

method

was

used to verify proper

SRV operation.

On July 27, maintenance

was to backfill the "A" channel

reactor

water level reference

leg.

The "A" channel

was indicating 2-3

inches higher than the

"B" channel

level instruments

and it was

determined that its reference

leg was not completely filled.

Prior to commencing

work Op'erations

placed the

FWLC to the

"B"

level signal to avoid any perturbations

during the backfill

process.

When this was performed

feedwater

flow decreased

resulting in

a reduction of reactor water level.

Increasing

the

demand

in manual

had

no effect and

FWLC was placed

back to the "A"

level signal

and reactor water level

was subsequently

recovered.

Technical

Support reviewed the

FWLC system

response

and schematics

and determined that the only difference

between

the "A" and "8"

level control

mode

was operating relay 6A-K7 by the level control

selector switch.

The licensee

decided to backfill the reference

leg while in the "A" level control

mode.

They then decided to

replace

the suspect

6A-K7 relay.

The relay was

removed

and

indicated level dropped

downscale

as expected

but immediately

upon

installation of the

new relay

a main turbine trip and reactor

scram occurred

as well as

a trip of all three

feedpumps.

It was

later determined that instal'/ation of the

new relay and re-

energization of the instrument loop caused

output

demand to be

.

driven to maximum in an attempt to maintain

a constant

current

output,

and in doing so resulted

in a full scale spike of the

level switches in the circuit.

To verify this the newly installed

6A-K7 relay was

removed

and re-inserted

several

times,

and signal

spiking was observed

each time.

Following the unit trip the licensee

repaired

the stuck TIP

isolation reset

switch and is investigating the procurement

and

installation of a different switch type.

A work order

was

generated

on the

SRV tailpipe temperature

recorder to investigate

and repair

as necessary.

The licensee

performed post-event

troubleshooting

on various feed4ater

control

components

to

positively identify the cause of the initial level perturbation.

The original 6A-K7 relay was tested

in the instrument

shop

and

operated

properly.

The master

FWLC and controller mode select

switch was

bench tested,and

functioned properly.

Following

reinstallation,

a functional test of the

FWLC

controller was

performed in the various operating

modes with satisfactory

results.

The event could not be recreated.

The inspector

attended

the licensee's

PORC meeting

on July 29,

1992, to review the trip.

Following

a thorough review of the trip

the reactor

was restarted

on July 29,

1992.

Drywell Leak Analysis

During previous periods of plant operation,

unexplained

increases

in drywell unidentified leakage

below the

5 gpm TS limit occurred.

The licensee

developed

a series of procedures

as

a systematic

method to determine

the source

and magnitude of unidentified

leakage

in the drywell when normal

access

is not possible.

The

procedures

developed

are

as follows:

2-TI-275A

2-TI-2758

2-TI-275C

2-TI-275D

2-TI-275 E

Drywell Leak Investigation

Temperature

Drywell Leak Investigation - Radwaste

Sumps

Drywell Leak Investigation - Primary Containment

Leak Detection

Cam,

2-RN-90-256

Drywell Leak Investigation - Chemistry

Drywell Leak Investigation

Analysis

The inspector

reviewed

each of the procedures

and concluded that

the procedures

provide

an integrated

approach

to determine

the

7

source of unidentified drywell leakage.

The procedures

contain

charts,

graphs,

physical layout sketches,

and useful historical

data from past

leakage

problems.

Each of the procedures

performs

a specific trending

and evaluation for a department

specific area

of expertise.

d.

Drywell Liner Drain

During a plant tour underneath

the torus the inspector

noted that

the drywell liner sand

cushion drain pipe

on sever'al

lines

had

rags or paper in the end of the open pipe.

The inspector also

questioned

how often the lines were checked for any leakage.

The

inspector

reviewed Generic Letter 87-05

and the licensee

response

dated

Hay 29,

I987.

In the response it was stated that the

current preventative

maintenance

and inspection activities

pertaining to this area consists of observation of the appropriate

drains'he

system engineer

provided

a logbook of periodic

wal,kdowns of the. drains.

The only moisture that

had

been

identified was from Unit I drywell.

The licensee

has identified

this as

an item for resolution prior to Unit I restart.

The paper

and tape over the

end of several

drains

was for painting in the

area.

This was

removed'o

violations or deviations

were identified in the Operational

Safety

Verification area.

h

TI 2515/115 Verification of Plant

Records

In response

to recent

NRC concerns

about falsified plant logs,

the li-

censee

conducted

a gA audit to determine if similar problems existed at

BFNP.

The

NRC issued

IN 92-30, Falsification of Plant Records,

to alert

licensees

of this potential

problem.

The licensee's

audit was conducted

during

a six week period from Harch

16 to April 27,

1992.

Sixty-four AUOs and operator

rounds

areas

were

included in the audit.

A comparison of a computer printout of security

key card entries

to operator

round logs

was conducted.

Four thousand

entrances

and exits of plant areas

were reviewed.

Some discrepancies

were identified.

Based

on the discrepancies

the licensee

reviewed re-

cords associated

with an additional six week period from January

I to

Harch

16,

1992.

Again,

some discrepancies

were identified.

The licensee

issued

a

SCAR to document

the findings and corrective

action associated

with the discrepancies

that were identified during the

audit.

Disciplinary action

was taken against

two AUOs due to the

results of the audit.

The inspectors

met with members of licensee

management

to discuss

the specific details

and audit results. 'everal

examples of deviation of TVA policy occurred

by non-licensed

operations

personnel.

The discrepancies

were

a question of whether

an adequate

entry and check of certain vital equipment

areas

had

been

made in

accordance

with established

policy.

Additional corrective actions

are

still pending which are intended to improve licensee

performance

in this

area.

These corrective actions include:

The licensee

is drafting

a new OSIL to require periodic audits

by

Operations

management

in this area.

Training for all non-licensed

personnel

on importance of operator

routines to be conducted

by each

SOS.

The licensee

has plans to implement

a new computerized

system to

take,

record,

and trend information present

on existing operator

routine sheets.

Additionally the inspector

noted that the licensee

has

had in place

an

operator

check program.

This program provides routine

observations/reviews

of performance

by operations

personnel.

This

program was started prior to Unit 2 restart.

One of the attributes

has

been monitoring the quality of routine rounds in the Unit 2 Reactor

Building and Turbine Building.

In addition to the above licensee

reviews,

NRC inspector

made

an

unannounced trip to the plant during the 2300-0700 shift on June

19,

1992, for the purpose of accompanying

the Unit 2 Reactor Building AUO on

the routine rounds.

Prior to starting the operator routine sheet

the

onduty

SOS informed the inspector that approximately

two hours

were

required for the

AUO to complete those routines.

During the period of

observation

the individual displayed excellent

knowledge concerning

the

status of operating

components

and maintenance

activities in the

building.

The

AUO was knowledgeable of existing firewatches

required in

the building and

knew the source of several

minor leaks that were

present.

The individual had

no trouble locating each of the inspection

items within the expected

period.

The operations

routine sheets

are covered in O-GOI-300-1, Operations

Routine Sheets.

TS 6.8. 1. 1 requires that written procedures

shall

be

established,

implemented,

and maintained

covering the applicable

procedures

in Appendix

A of Regulatory

Guide 1.33, Revision

2,

February

1978.

GOIs are procedures

required, in

RG 1.33.

This finding is being reviewed

as

an apparent violation of 10 CFR 50.9

concerning

completeness

and accuracy of information.

This will be

tracked

as 259,

260, 296/92-29-01,

Apparent Violation of Plant Records.

The inspector's

review in this area fulfills the inspection

requirements

for TI 2515/115

and this TI is closed.

Secondary

Drawing Status

The inspector

reviewed the post Unit 2 recovery work involved with the

updating of secondary

drawings.

Prior to the restart of Unit 2, the-

licensee

updated essential

drawings, referred to as primary/critical

drawings,

needed

to support Unit 2 operations.

Non essential

drawings,

9

referred to as normal

usage

secondary

drawings,

were to be updated prior

to the end of Unit 2 cycle

5 operations.

As of August 8,

1992,

a total of 3714 normal

us'age

secondary

drawings

had been issued,

with 957 still in process.

Of this amount,

131 were

ready,

67 were being researched,.

427 were in drafting,

227 were being

checked,

94 were being reviewed

and

11 were awaiting issue. 'F the

total of 4671 normal

usage

drawings in the. program,

the licensee

expected to have issued

4500 by the end of fiscal year 92.

Unit 3 Restart Activities

(30702)

The inspector

reviewed

and observed

the licensee's

activities involved

with the Unit 3 restart.

This included reviews of procedures,

post-job

activities,

and completed field work; observation of pre-job field work,

in-progress field work,

and

gA/gC activities;

attendance

at restart

craft level, progress

meetings,

restart

program meetings,

and

management

meetings;

and periodic discussions

with both

TVA and contractor person-

nel, skilled craftsmen,

supervisors,

managers

and executives.

a.

IGSCC Nitigation

1.)

Pipe Replacement

The replacement

of recirculation

system piping was completed

as scheduled

on August 1,

1992.

The ring header,

ten

risers,

and safe-ends

were replaced.

The

RWCU piping

replacement

is scheduled

to be completed

on August 31,

1992.

2.)

Weld Overlay

In other areas

of the recirculation

system

and

one

RHR

indication, weld overlays

were determined to be the most

feasible

method of repair.

Eight 28 inch weld overlays will

be applied to the recirculation

system

and

one

26 inch weld

overlay will be applied to the

RHR system.

GE has

been

contracted

to design

and apply the weld overlays.

This work

is tied to re-filling of the vessel

and piping system.

3.)

Nechanical

Stress

Improve'ment

Process

This process

is being used to provide

a means of mitigating

IGSCC by reducing the residual

stresses

of a weld.

The HSIP

is accomplished

by

a slight permanent contraction of the

pipe in the vicinity of the weldment.

This is accomplished

by using hydraulically activated tools.

56 welds in the

recirculation

system,

four in the

CRD system,

six in the

RHR

system,

15 in the

CS system,

and five in the

RWCU are being

treated

using HSIP.

This program is scheduled

to be

completed

on September

2,

1992.

10

The inspector

met with applicable licensee

management

and

reviewed the status *of these

programs.

These

programs

are

being conducted

in accordance

with NUREG-0313,

Rev.

2,

Technical

Report

on Haterial Selection

and Processing

Guidelines for BWR Coolant Pressure

Boundary Piping.

The

inspector

reviewed the

NUREG for discussion of the HSIP.

On

page 2.5,

two processes,

IHSI and HSIP,

are considered fully

qualified to provide

IGSCC mitigation from residual

stresses

in welds.

The inspector concluded

the repairs

and

mitigation techniques

are being performed in accordance

with

the technical

recommendations

of the

NUREG.

Pilot/Prototypical

Program

The inspector continued to monitor and review the cooling tower

activities associated

with the pilot/prototypical program.

The

inspector

documented

in report

IR 92-24,

numerous

problems

in this

area.

Oue to the difficulties encountered

in returning the

cooling towers to operable

status

the Unit 3 restart organization

cutback significantly on the resources

dedicated

to the cooling

towers.

The inspector

was informed by Unit 3 management

that the

cooling tower work was to continue

and

a new schedule

was to be

issued.

The activities reviewed

and observed

by the inspector

involved testing of cooling tower components

performed

by test

directors. in order to closeout

DCNs.

Design Activities

The inspector

reviewed the design activities associated

with the

drywell chiller installation.

The work involved numerous

AA FDCNs

generated

during the implementation of DCNs W17695

and

W17913.

The inspector

was informed that

98

FDCNs were initiated by the

constructor for disposition

by design engineering

during the

installation.

The dispositioning of a large

number of FDCNs would

require

a considerable

amount of work by design engineering.

The

inspector

was also informed that the system could

be

preoperationally

tested

before disposition of the

FDCNs

and would

not be turned over to plant operations until th'e significant

FDCNs

were dispositioned.

The inspector considered this

a weakness

in

the team approach, that the Unit 3 project managers

were attempting

to implement.

The inspector

also considered

the inadequate

tracking of the

FDCNs

as

a failure to oversee

and review

contractor activities.

This action

by the constructor

had the

potential of having

a system fully functional, not being able to

operate

due to change

paper closure,

and its final as-built

configuration being undetermined.

The inspector discussed

this

problem with licensee

management.

Construction Activities

2.)

Equipment Clearances

The inspector

reviewed the activities documented

by

IIER-B-92-05, Contractor

Employee Failure to Fully Obtain

a

Clearance

Prior to Performing Work.

The report stated that

this was the third occurrence of contractor personnel

not

receiving

a completed

clearance

issuance prior to performing

work.

The report also stated that

WP 3169-92

was revised to

include re-routing of unscheduled

lighting conduit to

facilitate installation of a horizontal tube member.

On

July 21,

1992,

a clearance

request

was submitted for this

activity.

On July 28,

1992, the contractor supervisor

was

informed that the clearance,

3-92-277,

was in-place.

After

a satisfactory

walkdown of the boundaries,

the supervisor

obtained

a copy of the clearance

sheet

but he failed to have

the clearance

assigned

to him.

The following morning, July

29,

1992,

the job was performed.

SSP 12.3,

Equipment Clearance

Procedure,

required that

clearances

be issued,

using

From SSP-139,

Clearance

Sheet,

and personnel

performing the wor k must receive authorization

from the

SOS,

and insure that the clearance

was assigned

to

the proper person.

In IR 92-17,

the inspector

documented

a

NCV 296/92-17-01,

when

on April 15,

1992,

a contractor

supervisor failed to sign onto

a clearance

for work

performed

on

a Unit 3 drywell blower.

After this event, all

of the contractor supervisors

were interviewed

and trained

in clearance

procedures.

Accordingly, this example

although

identified by the licensee

is

a repeat

and does

not meet the

criteria for a non-cited violation.

This item is identified

as violation VIO 259,

260,

296/92-29-,02,

Failure to Sign Out

a Hold Order Prior to Performing Work.

As

a result of the review of the II the inspector discovered

that

WP 3169-92

was written to install two DCNs,

numbers

W17975A,

Upgrade of the Unit 3

Rad

Con Issue Station,

and

W18019A, Install Tool

Room for Unit 3 Personnel.

The

inspector discussed

this activity of using

one

WP to install

more than

one

DCN with Unit 3 management.

The inspector

was

informed that this was not

a normal practice

and that is

usually requires

approximately six

WPs to install

a

DCN.

Drywell Chiller and Automatic Tap Changer Installation

The inspector

observed

and reviewed the construction

activities associated

with the drywell chiller installation.

The field activities observed

and reviewed involved

WPs

.

0583-92,

3103-92,

3104-92,

and 3155-92 which installed

electrical

equipment,

piping, supports,

and mechanical

equipment.

Additional observations

and reviews were

12

performed which involved

DCNs 17666A,

Stage I:

Change

Capacitor

Bank Control Logic and Setpoints,

Stage

2:

', Install Automatic Load Tap Changer

on

CSS Transformer

A,

and

17667, Install Automatic Load Tap Changer

on

CSS

Transformer

B.

Pre-Operational

Testing/Return

to Service Activities

The inspector

reviewed the pre-operational

test for DCN W17695A,

PMT 236, Drywell.Outage Cooling Pre-Operational

Test.

The test

objectives stated:

The objective of this test is to verify the capability of

the drywell outage cooling system to circulate chilled water

through the Unit 3 drywell coolers with the remainder of the

RBCCW system isolated.

and further stated:

This instruction will perform the

PMT for DCN W17695A.

This

DCN provides

supplemental

chilled water cooling for the Unit

3 Drywell via connections

to,the existing

RBCCW system.

The

drywell outage cooling system

-is intended for use only

during outages

to control high drywell ambient temperatures.

The inspector

noted during the initial walkdown of the procedure

steps

5.2.5(a)

and 5.2.5{b) required that starts of chill water

pumps

A and

B respectively

be performed.

The electrical

control

system start logic appeared

to indicate that

when the chill water

pumps were started

the applicable chiller would also start.

Discussions

with the Test Director clarified this item in that

chiller electrical

disconnects

would be used to prevent starting

of the chillers until the factory authorized representative

is

ready to perform the pre-initial startup

checks,

panel

checks,

and

initial startup

and commissioning

on the chillers in accordance

with the manufactor's

installation,

operations

and maintenance

manual.

This was to be documented

on Appendix

L of the

preoperational

test.

Section

5 of the procedure,

Test Instructions,

contained

two

subsections

which gave step

by step instructions to test

the

pump/chillers

A and

B combinations.

The procedure

in section

6

contained clearly stated test

acceptance

criteria.

The procedure

also contained

pump

and chiller performance

sheets,

and valve

checklists for initial fill line-up, pre-test line-up

and post

test line-up.

The inspector

concluded

from this review that the

pre-operational

test procedure for the drywell chiller system

was

written in accordance

with BFN pre-operational

testing

program.

0,

13

Information Notice 92-26,

Pressure

Locking of Motor Operated

Flexible

Wedge

Gate Valves

The inspector discussed

this issue with the licensee

and the possibility

of valves existing at

BFNP that are subject to hydraulic pressure

locking.

BFNP Engineering

had previously evaluated

pressure

locking/thermal

binding at

BFNP in response

to

INPO SOER 84-007

and

GE

SIL 368.

They identified the

RHR-LPCI and-Core

Spray inboard

and

outboard injection valves

as susceptible

to this phenomenum.

While

pressure

locking has not yet been

observed

at

BFNP, engineering

feels it

prudent to modify the valves to ensure satisfactory operation

in the

future.

The modification will include drilling a hole through the valve

body bridge between

the reactor vessel

side of the valve

and the bonnet

cavity.

This will vent the bonnet to the piping and prevent

pressure

locking the valves.

Furthermore,

hydrostatic testing procedures will be

revised

as applicable to include steps to drain trapped water from the

bonnets.

Additionally, operations

and maintenance will receive training

on pressure

locking and

how to recognize

and recover

from this problem.

The valves

on Unit 2 are scheduled

to be modified during the upcoming

refueling outage.

The Units I and

3 valves will be modified prior to

restart.

9.

Site Organization

(40500)

The inspector

reviewed the organizational

structure of engineering,

modifications,

and contractor interfaces.

Unit 2 engineering

and

modifications is under

a single manager.

This structure

has functioned

as

a cohesive

group with contractors

being

used

as additional

personnel

while TVA retained

ownership

and responsibility for the programs.

In

engineering,

this has

been primarily supplying additional

people.

In

modifications,

a task manager

approach

has

been

used with a

TVA manager

or supervisor

shadowing

a contractor

employee.

Over the past several

weeks

a transition to

a single site engineering

organization

under the project engineer

has occurred.

A Unit 3 restart

project engineer

component

has

been

added to the organization.

This was

done to increase

the

TVA ownership

and responsibility of Unit 3 design

activities rather than relying primarily on contractors.

The inspector

reviewed the preparations

for the Unit 2 Cycle

6 outage

and concluded

that preparations

were proceeding

in time to support the outage.

Most

of the

DCNs were issued

and over half the

WPs written.

Progress

was not

as far along for the activities performed

by Unit 3 to support

the Unit

2 outage.

This was being closely monitored

by TVA management

and with

increased

awareness

and controls executed

under the

new engineering

structure.

However,

one area of concern

was the Unit 3 modification activities.

These

are still primarily contractor controlled functions.

Significant

problems

were encountered

with the cooling tower refurbishment.

Likewise, delays

and numerous

FDCNs were encountered

with the drywell

chiller modi fications.

TVA management

was

aware of these

problems

and

continues

to assess

the organizational

structure.

Some

changes

have

14

occurred including Unit 3 contractor modifications

management

changes,

and shifting of some Unit 2 Cycle

6 outage

work from Unit 3 modification

to Unit 2 modifications.

Exit Interview (30703)

The inspection

scope

and findings were summarized

on August

14,

1991

with those

persons

indicated in paragraph

I above.

The inspectors

described

the areas

inspected

and discussed

in detail the inspection

findings listed below.

The licensee

did not identify as proprietary

any

of the material

provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the li'censee.

Item Number

Oescri tion and Reference

259,

260,

296/92-29-01

259,

260,

296/92-29-02

Apparent

VIO, Apparent Violation of Plant

Records,

paragraph

fi've.

P

VIO,,Failure to Sign Out

a Hold Orders

Prior to. Performing Work, paragraph

seven.

Licensee

management

was informed that

one TI was closed.

Acronyms

AA

AUO

BFNP

CFR

CRD

DCN

DG

EHC

EQ

FDCN

FWLC

GE

GL

GOI

GPH

HPCI

IFI

IGSCC

IHSI

II

IN

INPO

IR

LCO

LPCI

HSIP

NRC

and Initialisms

Advanced Authorized

Auxiliary Unit Operator

Browns Ferry Nuclear Plant

Code of Federal

Regulations

Control

Rod Drive

Design

Change Notice

Diesel

Generator

Electric Hydraulic Control

Environmental Qualification

Field Design

Change

Notice

Feedwater

Level Control

General Electric

Generic Letter

General

Operating Instructions

Gallons

Per Minute

High Pressure

Coolant Injection

Inspector

Followup Item

Intergranular Stress

Corrosion Cracking

Induction Heat Stress

Improvement

Incident Investigation

Information Notice

Institute of Nuclear

Power Operations

Inspection

Report

Limiting Condition for Operation

Low Pressure

Coolant Injection

Hechanical

Stress

Improvement= Program

Nuclear Regulatory

Commission

OSIL

PCIS

PORC

PHT

QA

QC

RBCCW

RHR

RWCU

SCAR

SI

SIL

SOS

SOER

SRV

SSP

TI

TIP

TS

TVA

VIO

WO

WP

WR 15

Operations

Section Instruction Letter

Primary Containment Isolation System

Plant Operations

Review Committee

Post Modification Test

Quality Assurance

Quality Control

Reactor Building Closed Cooling Water

Residual

Heat

Removal

Reactor-Mater

Cleanup

Significant Condition Adverse to Quality Report

Surveillance Instruction

Service Information Letter

Shift Operations

Supervisor

Significant Operating

Experience

Review

Safety Relief Valve

Site Standard

Practice

Technical

Instructions

Traversing

In-Core Probe

Technical Specifications

Tennessee

Valley Authority

Violation

Work Order,

Work Plan

Work Request

~O

'